This is only a preview of the January 1988 issue of Silicon Chip. You can view 37 of the 96 pages in the full issue, including the advertisments. For full access, purchase the issue for $10.00 or subscribe for access to the latest issues. Articles in this series:
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When the chips are down
I didn't have much trouble deciding which story to
relate this month. It was a case of Murphy at his
best. Start at one end of the circuit and it will be
at the other end; start in the middle and you'll
move towards the wrong end. Either way, you can't
win.
The story concerns an AW AMitsubishi 63cm colour set, model
6346, one of several models based
on the ML series chassis. This is a
very recent model and, in fact, the
particular set was still under warranty, the owner having purchased
it three months earlier. He was a
new customer, having recently moved into the district, and apparently
had been directed to me as the
nearest serviceman authorised to
provide warranty service for AW A
sets.
The first contact was by phone,
initially to confirm that I could provide the service and then to find out
what was involved. I confirmed that
I could provide the service, but explained that it would be his responsibility to bring the set to me. Warranty agreements do not cover
•house calls, or the cost of transport
to or from the service department.
The · customer accepted this situation philosophically enough: "No
problem - I'll borrer me mate's
ute."
Those points clarified I made
some attempt to determine the
nature of the fault; loss of picture,
loss of colour, loss of sound or
what?
"Aw no - the picture's gone all
funny; kind of collapsed, if y'know
what I mean."
I wasn't sure whether I did or
not. The best guess was frame collapse, although the implication was
that there was still some kind of a
picture to be seen. Perhaps it was
only a partial collapse. There was
56
SILICON CHIP
obviously no point in probing further; I would just have to wait and
see.
And so it was that the "mate's
ute" eventually turned up with the
set on board, and we carried it into
the workshop. I took the opportunity to connect an antenna and
switch it on, just in case there were
any points to clarify while the
owner was still there. I suppose I
can hardly blame the owner for his
"all funny" description. The first
75mm at the top of the screen was
blank, the next 100mm showed a
reasonably linear picture, from
there to within 50mm or so of the
bottom was grossly expanded, and
the rest of the picture compressed
into that last 50mm.
It was, literally, not a pretty
picture.
Other commitments prevented
me from delving any deeper at that
stage and I put the set aside for a
day or so. When I did get around to
it I fished out the circuit and concentrated on the vertical section
(Fig.1 ).
Special Notice
These notes are being contributed by the author who, from
1950 until July this year, wrote
'The Serviceman" in another
magazine . . We feel sure that
regular readers of that series will
welcome the opportunity to continue following his adventures in
SILICON CHIP.
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Jungle IC
In fact, there wasn't a great deal
to be seen. Most of the functions
were performed inside a 48-pin
jungle type chip (IC201,
MC1310AP), including the vertical
sync separator, vertical oscillator,
ramp generator, and an amplifier
which delivered a signal at pin 16,
which was applied directly to a vertical output pair, Q451 and 452.
And that seemed to be all there was
to it.
I concentrated on the output
stage for a start. I checked the
various minor components, including two diodes, D451 and 452,
but found nothing suspicious.
Similarly, a voltage check around
the two transistors produced
figures very close to those shown on
the circuit.
The next logical step seemed to
be to get the CRO going and check
appropriata waveforms. The circuit
shows two vertical waveforms, one
at the vertical oscillator pin of the
IC (pin 20, waveform 8), and one at
the vertical output pin (pin 16,
waveform 7). I checked waveform 8
first, and this came up virtually
identical with the photograph on
the circuit.
But waveform 7 was another
matter. Even the photograph on the
circuit suggests that there is some
"mush" on the pattern and this appeared to be even more so on my
CRO. But this aside, the shape was
nothing like that on the circuit,
although the amplitude was approximately the same.
So what was happening? Was
the chip at fault and delivering a
faulty waveform to the output
stage, or was the output stage at
fault and somehow loading the chip
and distorting the waveform? Since
I had already checked the output
stage fairly thoroughly I hesitated
to blame it. On the other hand, as I
have remarked before, I am less inclined these days to suspect an IC
until all other possibilities have
seemingly been exhausted. And
there could still be something funny
about one or other of those output
transistors, which didn't show up
on my voltage check.
The transistors are each
mounted on a U-shaped aluminium
heatsink, the "U" being inverted so
that the heatsink sils above the
main board. The ends of the vertical sections are cut to provide
narrow tongues which fit into slots
in the board, then bent slightly to
hold them in place. It was
necessary to remove the heatsinks
from the board in order to gain access to the transistors, but this was
not particularly difficult.
Unfortunately, the effort seemed
to be wasted. Both transistors
tested OK, as did the two diodes,
which I tested a second time while
the transistors were out of circuit. I
also double checked the minor components (resistors and capacitors),
and the height and linearity controls, until I finally convinced
myself that there was nothing in
that part of the circuit which I
hadn't cleared.
Which seemed to put suspicion
squarely back on the chip. But still I
hesitated, trying to think of
anything I might have overlooked. I
drew a blank and was rapidly
reaching the conclusion that the
chip would have to be replaced, if
only to prove the point one way or
the other. After all, I could easily
spend several hours searching
vainly for some external fault,
which may not actually exist, and
finally be forced to change the chip
anyway.
On the other hand, if I changed
the chip now, that point would be
settled once and for all. Granted,
I'd be down the cost of a chip if I
was wrong (but one chip up in my
stock) and down by the time needed
to change the chip. Now I don't pretend to like changing chips, particularly 48-pin monsters - I don't
suppose anybody does - but I've
developed a pretty good routine and
a fair amount of skill over the
years, and can usually do the job in
about 15 minutes. That's no record,
and I know some blokes who can do
it quicker, but it's time well spent to
prove a point.
Sydney or the bush
A more practical snag was that I
didn't have such a chip in stock, so
one had to be ordered, which at
least gave me time to think while I
was awaiting delivery. In fact, this
didn't help much; I had not thought
of any other possibility by the time
the IC arrived so, muttering
something about "Sydney or the
bush", I set to with solderwick,
solder sucker and a good hot iron,
and pulled out the suspect chip.
The whole operation went
smoothly enough and I subsequently fitted the new IC, tidied
everything up, and switched on
hopefully. I don't suppose I need
spell it out; it wouldn't have been
worth writing about if it had been
as easy as all that. Suffice it to say
that the set behaved exactly as
before. I was back to square one.
So what now? Up to this pointJ
had convinced myself that I had
thought of everything before I
changed the chip. Quite obviously I
hadn't, but I was at a loss to think of
some new line of attack. I went over
the circuit again. I had proved, the
hard way, that the chip was not at
fault. I was also convinced that
there were no faulty components in
the output stage. So what did that
leave?
It was more of a growing suspicion than a sudden inspiration but I
found myself thinking more and
more about the scan coils and any
minor associated components.
Faults in scan coils are extremely
rare, but I have seen the effect of a
shorted turn, and it does some
weird things to the picture. In any
case, there was not much else left
to suspect.
Tracing out the circuit from the
vertical output stage to the scan
coils revealed the existence of
several auxiliary components,
apart from the scan coils, and I
..,..,.., ....
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1988
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Fig.1 portion of the AWA 6346 circuit showing the scan coils and associated
circuitry. The pincushion correction circuit is on PCB-PCC.
made a mental note that these
would have to be checked. But first
the coils themselves. I fished out a
shorted turns tester that I had not
had occasion to use for a long time,
unplugged the scan coils, and
checked for shorted turns. Result: a
clean bill of health; there was
nothing wrong there.
That left only a few auxiliary
components, the main ones being on
a small printed circuit board bolted
to the side of the cabinet and connected to the scan coil circuit via
flying leads and plugs and sockets.
The relevant portion of the circuit
is reproduced here to assist
readers to follow the story. The
board is designated PCB-PCC, the
"PCC" standing for Pin Cushion
Correction. It consists of a
transformer, T571, resistors R575
and 576, and capacitor C575.
Connection to the scan coils is via
two plug and socket sets; PV (Plug
Vertical) and PH (Plug Horizontal).
The vertical scan coils are connected to the vertical output stage
via pin 4 on the deflection yoke
diagram and eventually find their
way back to chassis from pin 3, via
the pincushion network, and a pair
of 8.20 resistors in parallel between "PV1" and chassis. These
resistors appear to be part of a
feedback network, and are not
shown here by reason of their
remote location.
58
SILICON CHIP
I had left the set running while I
visually checked out this section
and related it to the circuit, which
meant that the set had been running for about 15 minutes, much
longer than I had run it so far, since
I had previously turned it on only
long enough to check a few voltages
or whether the replacement chip
had achieved anything. In any case,
I had not been observing the circuitry associated with the scan
coils.
But now my attention was drawn
to R569, a 2200, 1W wirewound
resistor, mounted on the main
board, but effectively connected
between pin 3 (vertical scan coil)
and the 12V rail. I don't know what
function it serves, but I noticed it
for the simple reason that it was
running stinking hot - literally. So
hot, in fact, that it had melted the
solder connecting its pigtails to the
board.
Well, it seemed that at last I was
onto something, even if exactly
what was not clear. Looking at the
circuit again I suspected that, for
some reason, the circuit from pin 3
to chassis was incomplete, forcing
the scan current to seek a path
through R569 and the 12V rail. And
the most likely cause of this would
be failure of the two 8.20 0.25W
resistors (R462 and 464) already
mentioned.
So these were located and check-
ed - only to draw a blank; they
were spot on value and completely
free from any signs of stress. So
much for that theory. But I still had
the idea that there was a fault
somewhere in this chassis return
path and a check with the ohmmeter from pin 3 of the scan coil to
chassis confirmed that there was a
resistance of several hundred
ohms; much higher than seemed
logical.
So began a rather laborious process of checking individual connections involving the printed board
PCC and the associated plugs,
sockets and leads. In detail, PV is a
female plug, on a flying lead, which
mates with male pins, 1 and 2, on
the board. The flying leads are
crimped into the plug contacts and I
suspected that there could be trouble here. Checking this wasn't easy
because of the difficulty of ensuring
that one was making an effective
connection with the contact inside
the plug. But, after several attempts, I finally gave them a tentative all clear.
But what about the board itself,
and particularly the pins. The pins
are hollow and are mounted by inserting them in a hole in the board,
then expanding them with a flaring
tool to make a moderately strong
mechanical joint. Then, when the
board goes through the solder bath,
the flared end of the pin is soldered
to the surrounding copper pattern.
I pulled the board out and examined it closely, using a magnifying glass. As far as I could see, all
four pins were soldered perfectly to
the copper pattern. But the ohmmeter told a different story.
Measuring from pin 1 of PCC to the
surrounding copper pattern showed virtually zero resistance, but not
so pin 2. Here there was a varying
resistance of around several hundred ohms.
Significantly, even though I knew
there was a fault there, I could not
pick it visually. But a few moments
work with a hot iron, and a
somewhat lavish application of
solder and flux, removed any doubt.
In fact, I treated all four pins,
because I could no longer trust a
visual check.
TETIA CORNER
Blaupunkt (Bridge Rectifier
Chassis)
Symptom: Fuse S1242 blows
repeatedly. If the fuse is replaced
often enough, the set will eventually fail completely with a clattering
noise coming from the chassis.
Cure: D1245 (TAG 3-400) SCA
shorted or breaking down under
load. An emergency repair can be
effected by removing diodes
D1242 and D1 244 from the
bridge board. This reverts the set
to its original half-wave rectifier
design, in which state it seems to
run quite happily.
This information supplied by The
Electronics Technicians' Institute
of Australia (Tasmanian branch).
Relief and frustration
Then I switched the set on and up
came a perfect picture. I viewed the
end result with mixed feelings;
relief that I had finally cured the
fault, but also a certain amount of
anger at the frustration I had experienced, and the time I had
wasted, all because of one
miserable dry joint. Only someone
else who has been through it all will
know how I felt.
Still, that's what the game is all
about; one has to take the rough
with the smooth and, in the
ultimate, measure success by the
end result. On that basis this job
had been a complete success, even
if it had been less than satisfactory
financially. And I am still puzzled
as to how that joint could look so
good yet be so poor.
~tb.2.
ANl:>
46~
FR.ON\ AN'-f 5\G,~S
Of course, I had destroyed any
evidence in proving the point, and
there wasn't much help for that. As
I saw the joint, the solder had flowed into the hollow pin and right out
to, and over, the edge of the flared
end. It had also flowed quite freely
over the copper pattern which ran
under the flared section, and it
looked as though these two runs of
solder had mated into one.
Quite obviously they hadn't but,
short of using an electron
microscope that looks around corners, I am at a loss to suggest how it
might have been better checked.
The only real answer, I suppose, is
if in doubt, resolder it. Which I did
of course, but the "doubt" was a
long time a-coming.
And now, for a change of pace,
c..oMr>LE:'1""<=-L.'-f
r~ee-
Or s~~ss.. _.
here is a story from one of my
regular contributors, Mr J.L. of
Tasmania. It is an intriguing story
involving both technical problems
and the ingenuity in solving them,
and the frustration caused by the
replacement parts problem. This is
his story, for which he has
nominated the following appropriate title:
Sharp shooting
One thing about television servicing that appeals to me is the uncertainty principle. When a dead set
comes into the workshop I never
know what killed it, and finding out
involves a series of tests and
guesses that will, hopefully, point to
the faulty part.
This was never more clearly
shown than with a Sharp CX2020
that came in recently. Tracking
down the fault took both practical
and theoretical knowledge, plus experience, suitable test equipment
and a pile of patience.
The customer remarked that the
set failed to start up when switched
on at 7pm, although it had been
working perfectly at 5pm. There
had been no sparks or smoke, just a
total refusal to show any sign of
life. He tried the set on a known
good power point, just in case, but it
was totally dead.
As is the way with so many
customers, he felt sure that the picture tube was done for. He wasn't
really convinced when I tried to explain that if it was the tube, he
should still have sound.
When I switched it on in the
workshop, I heard the degaussing
coils go "boing" which indicated
that part of the set was working.
That characteristic degaussing
sound meant that the power lead,
mains switch and mains fuses were
all intact. I could tell this much
without even taking the back off.
But that's as far as I could go
with the back on. Next it was inside
to check the DC power supply.
Specifically, there should be about
300V on the collector of the chopper transistor (Q701) and, in this
set, 115V on its emitter. The 300V
was there, but not the 115V. Quite
obviously the chopper was not
running.
This set uses a self-oscillating
JANUARY 1988
59
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Fig.2: horizontal oscillator (IC501) and line output stage of the Sharp CX2020. Note the protective diode
incorporated in Q602.
chopper which should self-start,
then come into sync with the line
frequency as the line output stage
gets going. The pulse from the line
stage (Fig.2) is not essential to run
the chopper but, as well as its synchronising function, it is used by the
protection network to indicate the
presence of faults on the line output. No line pulse may mean a fault
and so the chopper is shut down.
So where should I start to look for
a fault in a roundabout network of
this kind.
My first line of attack is to determine if the chopper is trying to selfstart. I do this by looking at the
emitter of the chopper transistor
with the 'scope. If I'm lucky I will
see a brief flick of the trace which
indicates that the transistor is being turned on, if only for one or two
cycles. The output voltage appearing on the emitter is immediately
reflected to the protection circuit,
and if all is not right, the base drive
to the chopper is very promptly
terminated.
In this case, the flicker of the
scope trace, when it did appear,
was so brief as to be almost unnoticeable. Still, it was enough to
say that the chopper was trying,
and at this point I had to make an
60
SILICON CHIP
educated guess as to where the
troubl-e lay. It could be either a fault
in the supply itself, or a fault in the
set proper. It's a "heads or tails"
situation, but experience helps a little. Line output stage faults are
more common than power supply
faults.
In fact, faulty line output transistors are so often the cause of
stoppages that most servicemen
check that component first of all.
It's usually simple to reach the collector and measure its resistance to
chassis. If the meter shows zero
ohms, then the transistor is like the
Christmas turkey. In this case there
was no such indication and the
transistor (Q602) checked out
perfectly.
Well, sort of perfectly, because
the base-emitter junction is difficult
to check in circuit, normally showing as a short through the line drive
transformer. Still, if collectoremitter shows no sign of leakage
then it's a safe bet that the base
emitter junction is OK. Or so one
might think.
My next move was to connect the
CRO to the base of the line output
transistor to see if there was any
drive reaching this point. Again,
this was inconclusive because the
trace merely flickered, without any
evidence of a drive waveform. I
transferred the probe to the collector of the transistor, hoping to see a
similar flicker there. I already
knew that the 115V rail appeared
briefly, so if the line output transistor was being driven at all, there
should be some signs on the collector side. But there wasn't a
sausage.
Unusual failure
Up to this point I hadn't switched
on the soldering iron, but the time
had come and in a couple of
minutes I had the 2SD869 line output transistor lying naked on the
bench. And now I could really
detect the cause of the trouble. The
base emitter junction was as short
a short as any short I have ever
seen. It is an unusual failure for a
power transistor because the basecollector junction seemed undamaged, and there was no trace of
leakage between collector and
emitter.
So now I had the problem of
replacing a 2SD869. This transistor
is one of those odd animals with a
built in protection diode, used in a
number of recent vintage Japanese
sets. Replacing these can be quite a
VOOD FOR Cl-I/PS ... WOOD FOR Cl-I/PS ... WOOD FOR Cl-I/PS ... WOOD FOR CHIPS .. . WOOD FOR CHIPS ... WOOD FOR CHIPS:.. WOOD FOR C
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LM1 13H
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Geoff has managed to get hold of a limited
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While they last you can have one for
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IC SPECIALS
27C64
200nS 8kx 8 CMOS EPROM 12.5.VPP. These are
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~~~~~~
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Whatever your
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And they're only $5.99 each
CD4503/80C97 Hex
tor
CMOS
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· Tip temperatures as high as 400°C
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in a handy case (with stand for the iron) which just about fits
Porta-Sol Professional is $81.00.
PORTASOL STANDARD SOLDERING IRON
in your pocket.
Geoff
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$39.95.
P.ORTASOL TIPS
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are
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IBM and Compatible PC Users!
Save a power point - Get a rewireable IEC plug from Geoff.
It's so easy -on the back of your PC you'll fi_n d an IEC outlet
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Q:
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LM317HVH
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LM317HVK-STEEL
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LM317K-STEEL $6.60
LM3 17KC
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LM317MP
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LM317T
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LM320H-5.0
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LM320K-12
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LM320K-15
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LM320K-5.0
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LM320MP-12
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LM320MP-15
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LM320MP-5.0
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LM320T-12
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LM323K-STEEL $5.50
LM325N
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LM326H
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LM326N
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LM330T-5.0
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LM333K-STEEL $14.35
LM333T
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LM337H
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LM337HVK-STEEL
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LM337K -STEEL $9.15
LM337LZ
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LM337T
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LM338K-STEEL $13.25
LM340K -15
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LM340KC-12
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LM350K-STEEL $9.65
LM376N
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LM723CN
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LM2925T
$4.60
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LM29:l>T-8.0
LM2931CT
$3.05
LM2935T
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LM2940CT-5.0 $2.80
LM3524N
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LM76601N
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LM78L12ACH
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so.so
LM7905CK
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LM7912CK
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~~~~~- 2 5
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LM385Z-1.2
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LM399H
LM3999Z
LM349N
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$2.40
$1 .20
AUDIO AMPLIFIERS
LM380N
LM380N-B
LM381AN
LM38 1N
LM382N
LM383A T
LM384N
LM386N-1
LM387N
LM388N-1
LM389N
LM390N
LM1875T
$1.90
$1.90
$6.40
$3.95
$3.05
$4.'30
$3.50
$1.65
$2.80
$2.40
$2.40
$1.95
$8.00
INSTRUMElfTA nON
AMPLIFIERS
LM3630
LM363H-10
LM363H-500
LM725CH
$38.00
$24.00
$24.00
$9.20
OPERAnONAL
AMPLIFIERS
LM10CLH
LM10CLN
LM10CN
LM1 1CH
LM11CLH
LM11CLN
LM11CN
LM301AH
LM301AN
LM307H
LM308AH
LM308AN
LM308H
LM308N
LM310H
LM310N
LM312H
LM316H
LM318N
LM321AH
LM321H
LM324AN
LM324N
LM344H
LM346N
LM348N
$8.30
$5.95
$9.30
$9.75
$6.70
$3.30
$3.50
$1.30
S0.70
$1.95
$6.95
$5.10
$2.45
$1.00
$4.20
$4.25
$6.00
$11.20
$2.20
$28.05
$10.15
$4.70
SO.BO
$11.20
$4.75
$1.90
$2.20
SO.SO
$3.10
$1.25
$2.45
$1.05
$0.80
$0.50
$0.30
$1.60
$1.10
$1.90
$2.80
$0.55
$1.40
$0.90
$2.30
$2.25
$2.25
$2.25
TRANSISTOR ARRAYS
VOLTAGE COMPARATORS
LM306H
LM311H
LM311N
LM319N
LM339AN
LM339N
LM360N
LM360N- 14
LM361 N
LM392N
LM393N
LM710CH
LM1414N
LM3302N
LM358N
LM359N
LM709CN
LM733CH
LM733CN
LM74 1CH
LM 741CN
LM741CN-SGS
LM747CH
LM747CN
LM833N
LM1458H
LM1458N
LM:l>BON
LM3900N
LM4250CN
LM13080N
LM13600N
LM13700N
LM394CH
LM394CN
LM394H
LM395T
LM3046N
LM:ll86N
LM3146N
$5.40
$5.40
$7.40
$3.85
$1 .50
$1.15
$2.15
TEMPERATURE SENSORS
LM3351-1
LM335Z
LM35CAH
LM35CH
LM 35DZ
LM3911H-46
LM3911N
$3.15
$2.40
$12.95
$13.95
$2.60
$5.05
$2.65
SPEOAL FUNCn0N
BLOCKS
LM331AN
LM331H
LM331N
LMC669CCN
LM1812N
LM18:l>N
LM1889M
LM1893N
LM2907N
LM2907N-8
LM291 7N
LM2917N -8
LM 3909N
LM3915N
LM3916N
$9.85
$13.20
$7.60
$11 .05
$6.20
$4 .40
$5.60
$19.85
$2.35
$4.25
$4.40
$4.20
$ 1.85
$4 .25
$4 .65
COMMI.INICA nONS
ORCUITS
LM565CH
LM567CN
LMC567CN
LM 1496H
LM1496N
LM 1886N
LM:ll89N
LM3189N
LM3820N
$5.25
$1 .40
$2.35
$5.05
$2.05
$8.05
$3.95
$5.15
$3.20
nMERS
LM322N
LM555CN
LMCSSSCN
LM556CN
LM3905N
$3.05
S0.50
$1.00
$1 .10
$2.35
EXAR PRODUCTS
XR-2201 CP
XR-2202CP
XR-2200CP
XR-2204CP
XR-2206CP
XR-2209CP
XR -2211CP
XR-2240CP
XR-2243CP
XR-5533AP
XR -5534ACP
XR-558CP
XR -8038ACP
$1 .65
$1 .65
$1.65
$1 .65
$9.40
$5.20
$7.50
$3.45
$4.20
$4.15
$3.90
$3.30
$7.30
L2298 at only $4.75
8.30 to 5 Monday to Friday, 8.30 to 12 Sat.
Mail Orders add $5.00 to cover postal charges.
GEOFF WOOD ELECTRONICS P/L
All prices INCLUDE sales tax.
(02) 427 16 76
Tax exemption certificates accepted if line value
exceeds $10.00.
p~~==~[ ;:::: e:::====; 229
BURNS BAY RD.
(CORNER BEATRICE ST.)
J~"
;
BANKCARD, MASTERCARD, VISA , CHEQUES
LANE COVE WEST N.SW.
IN C IN NSW
TWX71996
P.O. BOX 671
LANE COVE N.SW. 2066
8RI~
OR CASH CHEERFULLY ACCEPTED
specialising in electronic components for the professional and hobbyist.
pain as each manufacturer seems
to have his own design and none
seem to be compatible.
Here in Tasmania we have a real
spare parts problem as all
manufacturers have withdrawn
their spare parts services to centres in Melbourne or Sydney. So our
Tasmanian customers are now faced with 10 to 20 day delays while
we order the part, then wait for the
invoice, then send the cheque, then
finally get the part. (I know - some
firms do have faster services, but
most do not and our gripe is with
the latter ones).
The only alternative for independent servicemen like myself is to
cultivate our friendships with the
manufacturers' service agents. If
they have what I require, and my
face is welcome in their workshops,
then I might be able to get the parts
needed to put my customers' sets
back into working order in a
reasonable time.
So my immediate need for a
2SD869 led me to the local Sharp
agent. When I asked his receptionist about the availability of
2SD869's, a voice from deep within
the workshop declaimed "Yer don't
need wunna them! A 2SD350 is OK
in that set." The voice was soon
joined to the jovial face of their
technician who volunteered the information that the 2SD869 was only
a 1000V transistor, and the diode
was included to catch any spikes
over that level. On the other hand, a
2SD350 was a 1500V device and to
his knowledge, none had ever failed
in these sets.
He wouldn't tell me the price of
the 2SD869, but as the 2SD350 is
about as cheap as any power transistor can be, I decided then and
there to use one in this repair. So I
soon had a 2SD350 in the chassis,
in place of the original transistor.
Pressing the power switch produced not the expected burst of
sound, but quite the opposite - absolutely nothing. This was a real
disappointment because I was convinced that the transistor had been
the only faulty part in the set.
So I had to start troubleshooting
all over again. This time the CRO on
the chopper base showed a quarter
second burst of drive waveform.
The 115V rail also showed a change
62
SILICON CHIP
- the 'scope trace at the emitter
leapt up the screen, then quickly
dropped back to the zero line. This
was a much more positive response
than the earlier flicker, but it was
no closer to restoring full operation.
Continuing my investigations, I
found that the line output transistor
now showed more enthusiasm at
switch-on, but couldn't be resolved
into actual drive. It just flickered into some kind of action, them died.
So what now? It could be (a) a faulty line oscillator chip (IC501), (b) a
dud line driver transistor (Q601), (c)
a bad line driver transformer
(T601), etc, etc. With a chain of
doubts like this, it is perhaps best to
start at the beginning.
My 'scope was not able to resolve
any trace of line drive from the
oscillator chip at switch on, but
then a quarter of a second or less is
not very long to resolve anything.
What I had to do was power up the
chip and see if it produced the right
waveform. I used a 9V battery fitted with leads and alligator clips to
apply Vee to the chip. The set uses
a 12V rail at this point, but 9V is
enough to see if things will work at
all. In this case, 9V produced a
solid train of square waves and proved the chip to be 100 % .
While the battery was connected
I was able to trace the signal up to
the base of the line driver transistor. They went no further
because the collector is powered
from the 115V rail and this wasn't
working yet. So I had to devise a
way to get voltage onto this rail.
One of the most useful pieces of
equipment in my workshop is a
Variac, a continuously variable
autotransformer. I have also built
up a simple DC power supply using
an old TV transformer, a couple of
diodes and a 350V electrolytic
capacitor. When fed from the
Variac, this supply can deliver from
about 20V up to something over
200V. (It's rather crude, but I
haven't had either the time or the
money to build a better high voltage
power supply).
For this Sharp job, I connected
the DC supply to the 115V rail and
slowly cranked up the Variac. The
9V battery was still connected, and
the IC was delivering drive pulses
to the line driver transistor.
The voltmeter monitoring the
115V rail at first indicated a rising
voltage, but it stabilised at about 5V
and went no higher. Even 100V AC
into the DC supply could produce no
more than 5V out, and the Variac
was humming ominously.
The story is nearly finished!
I took no time at all to find that
the 115V rail was shorted almost
down to chassis. Examination of the
schematic showed two components
as the likely culprits. One was
C713, a l00µF 160V electrolytic
capacitor, and the other was
ZD702, a zener diode , type
EX0074CE, connected between the
rail and chassis.
Roast dinner
The more I thought about that
zener the more dubious it looked.
Then in the parts list I found that it
was a 130V type, twice as high a
voltage as any zener I've ever seen.
I'd bet a dud fuse to a roast dinner
that it was the villain. And so it
was. Not quite a dead short, about
10 ohms, but near enough to stop
the set dead in its tracks.
The zener is only in the set as a
protection device and the set works
quite happily without it. But it is
there for safety reasons and had to
be replaced. So now came the second spare parts trauma with this
set - where do you get a 130V
zener if not from the set's maker?
Fortunately, the zener value is
not critical and I was able to
replace the faulty item with two
62V zeners in series. The set is
now, if anything, a little safer than
it was.
Getting back to the philosophy
expressed at the beginning of this
story, I find television servicing an
occupation that is intellectually
stimulating and full of interest. It is
never boring and the smile on the
face 'of the customer when he
learns that it wasn't the picture
tube after all is all the job satisfaction that I could ask for.
Alternative transistors
Thank you J.L. for a most interesting story and an insight into
the problems faced by our colleagues in more remote areas.
I have no doubt that there may be
those who would question the
wisdom of substituting the unprotected 2SD350 in place of the
original 2SD869, in spite of the
higher rating of the former .
In fact, when I showed this story
to a colleague he immediately rattled of a list of protected output transistors, which he felt could at least
be considered. These included the
2SD870, 871, 899, 900, 951, 952,
953 and 954. However, neither he
nor I would be prepared to stick our
necks out and claim that all of these
would be compatible with the
Sharp circuit.
(Incidentally, most transistors of
this general type, with built in protection diodes, also have an in-built
resistor between base and emitter.
This is not always shown on the circuit symbol and could be mistaken
for leakage. Typical value is about
400.
More to the point, of course, is
the essentially practical problem
faced by J.L. and others who live in
places remote from the manufacturers ' distributors. And even then
the expression "on back order"
crops up all too frequently.
Obviously, all is not cider and
skittles in the Apple Isle, at least as
far as spare parts are concerned.
This being so, people like J.L. have
to do the best they can with what is
available. And at least the substitution was recommended by the
manufacturer's agent who, in turn,
appeared to be basing the recommendation on practical experience.
And I'm sure that no one would
have been happier than J.L. had he
been able to fit the correct replacement but, if it's not available and a
long wait is involved what should
one do? What would you do? More
to the point, perhaps, what would I
do?
See you next month?
it
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OR MOR6 l)O~~E 10 ME POINT, W'°'~••.
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JANUARY 1988
63
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