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VCR: Very Crook Recorder
According to popular philosophy, we are supposed
to learn by our mistakes. On this basis the cynic in
me would suggest that I must be a very learned
person because, in this game, there is plenty of
room for mistakes. However, modesty for bids such
an admission.
This story concerns two General
Model VGX-510A video recorders
and two rather tricky faults which I
encountered in them. One is a fairly
routine fault, though more or less
confined to this model, while the
other may well have been a one-off.
Nevertheless, it was a Very
Crook Recorder.
But before delving into the
technical side of things, it might be
helpful to list some of the brand
names and cross company relationships which come to mind when this
model is mentioned. And it is a
rather complicated situation.
First off, the General VGX-5 lOA
is also marketed under the Palsonic
label, model VCR-5000. However,
the same deck is used in at least
five other models: the JVC
HR7200EA (for which it was
originally designed), General Electric GEV6900, Ferguson 3V29A,
Rank RV340 and some NEC models.
So we have the same deck in at
least seven different brands - a
point worth noting for future
reference.
To make things even more confusing, the General machines have
used parts from a variety of other
manufacturers. For example, while.
the VGX-5 lOA uses a JVC deck, the
more recent General VGX-540A
uses the the National NV-370 deck.
In fact, the General organisation,
having been gobbled up in some
kind of a takeover, is now known as
General Fujitsu.
Well, so much for the corporate
affairs side. Let's get back to
technicalities. Mention of the JVC
70
SILICON CHIP
7200 might remind some readers
that I dealt with a tricky problem in
one of these machines some 12 months ago, in April 1988. Reference to
those notes may help in following
this story. I should also mention
that most of these machines are
now at least five years old.
The first fault in the General
VGX-510A showed up as damaged
tape. More specifically, the tape
was crinkled along one edge usually the Jower one - but in a
few cases both edges of the tape
were affected.
The effect varied from machine
to machine. In most cases it was
minimal, probably because the
customer sought my help early, but
in some cases it caused tracking
and sound errors. In any case, it
was something which could not be
tolerated, particularly if the
machine was used to play hired
tapes.
My first attempts to cure this
This photograph of the pinch wheel
clearly shows the wear which caused
fouling of the capstan.
fault were a dismal failure. Having
never struck it before I assumed
that it was most likely a fouling problem; a build up of oxide on the
various guide posts and rollers.
And in fact, the build up was
considerable.
Unfortunately, a thorough cleanup of all these parts did little to
alleviate the problem. Next I checked the various adjustments which I
thought might have some bearing on
the problem but found nothing
suspicious. Puzzled, I put the
machine to one side while l thought
about it but before I could reach
any conclusion, a second machine
appeared on the bench with the
same problem.
Crook pinch wheel
I decided it was time to ask for
help. I rang the General service
department and put the problem to
them. The technician at the other
end didn't hesitate: "change the
pinch wheel". And that was it - he
didn't elaborate and was so positive
in his statement that I. didn't seek
elaboration. In fact, he wasn't
wrong but he'd left a lot unsaid.
Anyway, I went ahead and
ordered a stock of pinch wheels and
when they arrived attacked the
first machine. And this was when I
realised the real nature of the problem. In order to replace the pinch
wheel it is necessary to remove the
cassette carrier assembly from
above the deck proper and this
gave me a much better view of both
the pinch wheel and the associated
capstan shaft.
And that's where the real trouble
lay; on the capstan shaft. It's not
possible get a good look at this shaft
when the cassette carrier is in
place and it was now obvious that
my attempts to clean it had been
quite futile.
To tell the truth, I hadn't paid all
that much attention to it, previous
experience being that this component collects very little oxide. So a
token wipe, more or less blind, with
alcohol soaked tissue was all it had
received.
Now that I could see it properly I
realised that it was the worst case
of fouling that I had ever seen.
More to the point, it wasn't the conventional oxide fouling. There were
two black rings on the shaft, the
width of the tape apart and quite
hard. The only place this fouling
could have come from was the
pinch wheel and this was confirmed by the manner in which the
pinch wheel was worn.
So the technician had been right
but he had failed to mention the
side effect of the worn pinch wheel;
ie, the fouling on the capstan shaft.
Anyway, I fitted a new pinch
wheel and then tackled the capstan
shaft. As I said, the fouling was a
hard encrustation and while in
theory it should not have been narrower than the tape width, some of
the muck had crept into this area.
Hence the tape damage.
Getting it off wasn't easy. I
hesitated to use excessive force for
fear of damaging the capstan shaft
surface yet initially it seemed impervious to the alcohol I normally
use or the other solvents around the
shop. However, it did yield eventually and I had a nice clean
capstan again.
And that was it. The machine
behaved perfectly, with no hint of
tape damage. The second machine
also received the same treatment
a.nd it responded similarly.
Since then I have encountered
the same problem in a number of
these machines. Some came in
because of tape damage, some for
other faults but having learned my
lesson, I give them all the treatment. At the same time, I take particular care to examine all other
machines passing through the
workshop for the same fault.
Arising out of this exercise is the
conclusion that this is a very
serious problem with these machines, apparently due to the material
used in the pinch wheel. Whether
this was only a batch problem, or
whether it will continue, I cannot
say. All I do know is that every
machine of this model should be ex-
amined for this fault as a matter of
course, regardless of any other
fault.
The other point is that, so far,
this appears to be the only deck
.with this fault. A few other
machines have shown a hint of the
problem but nothing like the gross
fouling encountered on these. So
there it is - I will be keeping a
closer watch on all machines from
now on.
Fault number two
So that was fault number one
with this model. Fault number two
turned up a few months later after I
had treated several more machines
for fault number one. In fact, it was
for fault number one that this latest
machine came in and I simply took
it for granted that it would be just
another routine job and quoted the
customer accordingly.
And that's all it was initially; exactly the same fault needing exactly the same treatment. It wasn't until I had put everything back
together and given the machine a
routine test that I realised that I
still had problems. Sure, it was no
longer damaging tape but there was
a serious tracking problem wfrh
noise bars on the picture and a problem with varying sound levels.
For some reason this latter effect
seemed to be worse on tapes which
had been recorded on this machine,
rather than on pre-recorded tapes.
Even so, I wasn't particularly
worried. I imagined that a normal
setting-up routine, involving height
adjustment of the guide roller
assemblies, would be all that would
be needed. It is a fairly straightforward routine, although it is a bit fiddly and time consuming. It is
sometimes referred to as the "Interchangeability Adjustmenf''
CRO patterns
The routine is basically the same
for all machines. Some dismantling
is involved to gain access to two test
points normally located on the main
board - test points five and three
in this machine - and these are
connected to the CRO. Test point
five delivers an RF envelope pattern from the video heads while test
point three delivers a 25Hz square
wave which is used to lock the CRO
timebase. The machine is then loaded and run with a standard colour
bar tape.
Assuming correct adjustment,
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APRIL 1989
71
Envelope level is dropped at
the beginning of track.
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Fig.I: this line drawing and CRO pattern, from a
National manual, illustrate a severe tracking error.
A mirror image of this pattern may also occur.
this setup should deliver a rectangular pattern to the CRO. If it
doesn't, the height of the two guide
rollers has to be adjusted until this
is achieved. At the same time, it
may be necessary to adjust the
height and azimuth of the sound/
control head to give the best sine
wave from the audio test tone on
the tape. These adjustments tend to
interact and may need to be
repeated until both are correct.
In greater detail, the CRO pattern displays the output froin the
two heads and most importantly,
the transition point where one head
takes over from the other. In the
case of a new machine (or a new set
of heads), the output from each
head should be an almost perfect
rectangle and the transition point
should be almost invisible (Fig.2).
But if the tape is not tracking properly, or if the heads are worn, the
rectangular pattern will taper off
at one end or the other (see Fig.1).
In fact, it's possible to recognise
which guide roller should be adjusted according to whether the
taper is to the left or right.
Well, that's the theory and it
usually works out well in practice.
72
SILICON CHIP
Envelope is adjusted properly
I
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Fig.2: this diagram shows what the pattern looks
like with correct tracking, assuming that the heads
are in good condition.
The result is sometimes less than
perfect when the heads are worn
and one must then settle for the
best compromise and hope that the
end result will be acceptable. If it
isn't, a new set of heads is the only
answer.
Anyway, I went through the procedure and the CRO presented a
perfectly acceptable pattern, at
least initially. The snag was that
the machine wouldn't hold this adjustment; while one watched, the
rectangular pattern would suddenly drop at a transition point and
noise bars would appear on the
screen. I went over the procedure
again but with no more success.
Clutching at straws, I went
through the sound/control head setting up routine. Significantly, it
didn't seem to need adjustment and
in the end had no worthwhile effect
on the problem.
Well, to cut a long story short, I
went through the video head
routine about umpteen times, interspersed with checks on any
other components or adjustments
which I felt could be important. I
drew a blank all round.
In the end I had to admit that I
was going round in circles, getting
nowhere. It was time to ask for help
again. So I made another call to the
General service depa rtment. This
time I found myself talking to a
Japanese technician who seemed t0
be particularly well versed with
this machine.
He listened very carefully to my
explanation of the problem and the
steps I had taken so far, checked
whether I had done this or that, and
was finally forced to admit that I
had done all the right things. More
to the point, he couldn't think of
anything else that I could try. In
short, he wa s as puzzled as I was.
In fact, he went so far as to say
that, considering the age of the
machine, it might be more economical to write it off, rather than
chase such a difficult fault.
I did raise the matter of the guide
roller assemblies but he was most
emphatic that he had never encountered any problems with them.
As far as he was concerned, the
guide rollers simply did not give
trouble.
It's all there is
So I was back to square one. I put
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the machine aside again until I
could spare the time to really get
stuck into it. In the meantime my
thoughts kept coming back to the
guide roller assemblies; I couldn't
shake off the idea that this was all
there was left to suspect.
Eventually, I found time to set
everything up as before and repeat
the adjustment routine once again.
Initially, the results were exactly
the same. The breakthrough came
when, more or less on impulse, I applied gentle pressure with the blade
of a screwdriver to the top of the
guide roller assembly on the supply
reel side.
The result on the CRO pattern
was immediate and I found that
judicious pressure could produce
and maintain an almost perfect pat-
The Very Crook Roller which caused
the trouble . While known to be
faulty, no slackness could be detected
in the assembly.
tern. But once I withdrew the
driver, we were back to square one
again.
I wasn't sure whether this was
normal or not, so I tried the same
tactic with the guide roller on the
takeup side. The result here was
quite different. Short of applying
extreme pressure, it had virtually
no effect.
From this I assumed that there
was some slackness somewhere in
the suspect guide roller assembly.
Yet try as I might, I couldn't pinpoint it. All I had established was
that one roller responded to
pressure and the other one didn't.
The only way to prove the point was
to replace the roller.
Well, that seemed simple enough
- I thought. I turned to the manual
to find the appropriate part number
and realised that the assembly, as
such, was not listed. Each component of the assembly - there were
seven in all - was listed separately
with its own part number. Fair
enough; all I had to do was list these
numbers and ask for the complete
assembly which comprised them.
And that was the first barrier. I
rang the spare parts department,
told the assistant what I wanted
and dictated the part numbers to
him. He asked me to wait on while
he punched them into the computer,
then announced that, as far as the
computer was concerned, there
were no such part numbers.
Mentally muttering "Don't be Uncle Willie", I made the more
diplomatic suggestion that perhaps
he should check further, as the part
numbers were listed in the manual.
The upshot of this was that he pro-
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Phone: (02) 77 4 1154
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Suit bright young electronics enthusiast 19 to 24 years.
The wholesale division of Altronics
has opened sales offices in Sydney
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the following:
( 1) Is a pleasant person who gets on
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The successful applicants will be 2nd
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APillL 1989
73
may be a one-off event. Ifso, that's
fine. But the mere rarity of. the problem is itself a hazard; there is
nothing on record which will help.
Let's hope this story rectifies that.
And who knows; it might even save
a machine from being written off.
SERVICEMAN'S LOG
Foreign bodies
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H-~Ve: 'De:s~R\'8~ A VA'R\E:"'t"{
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mised to look into it and ring me
back.
And he was as good as his word,
except that the call came not from
him but from the Japanese technician I had spoken to earlier. Not
realising who I was, he started out
by explaining that they didn't keep
this assembly in stock. (I assumed
that this was a continuation of the
previously expressed idea that they
never needed to be replaced].
Then he went to enquire why I
needed this assembly. At this point I
reminded him of our previous
discussion and explained that I was
now virtually certain that a faulty
guide roller assembly was to blame.
And I gave him a detailed account
of what I had done.
My experience obviously came as
a surprise but having listened
carefully to all I had done, he seemed to be convinced that I was on the
right track. On the other hand sup74
SILICON CHIP
v,~ RECDR~S
plying a replacement was still a
problem. In the end, he said,
"Leave it with me, I'll see what I
can do". So we left it at that.
Sure enough, a couple of days
later a replacement assembly arrived in the post. I have little doubt
that it had been raided from
another machine, probably one
written off for some other reason.
I lost no time in fitting the new
assembly and going through the
whole setting up procedure again.
And to my immense gratification, it
worked. The CRO pattern was rock
steady and the picture completely
clean. So I'd not only cured the problem, I'd proved my point and found
a new meaning for VCR: Very Crook
Roller.
I have no doubt that the technician was being perfectly honest
when he said that there was no
history of failure; which is why I
suggested at the beginning that this
And now here is something in
lighter vein. On a number of
previous occasions I have described a variety of foreign bodies that I
have fished out of malfunctioning
video recorders; parts of children's
toys, coins, matchsticks, beads and
so on. So what was there left? Read
on and see if you can top this one.
It all started with a phone call
from a lady who explained that she
had a new Panasonic (National]
video recorder which had performed perfectly for the first few months but was now giving trouble. She
was somewhat vague about the exact nature of the fault but I
gathered that it was basically a
loading problem and there was
something about a loop of tape remaining after a cassette was
unloaded.
Anyway, I suggested she bring
the machine in and we would give it
a once over. She then raised the
matter of warranty, pointing out
that, as the machine was only six
months old, she assumed it would
still be covered. I assured her that
this was so.
So, a few days later the lady
pushed the off ending machine
across the counter. It turned out to
be a Panasonic NV-G40, a very recent model featuring remote control
and digital scanner, though I'm not
quite sure what the scanner is supposed to scan; I have yet to see any
published programs featuring the
required bar pattern.
But that point aside, I was a little
concerned because this was the
first model I had encountered at
service level and I had little
technical information on hand. Fortunately, I soon realised that this
machine uses the same deck as
many earlier models; right back to
the model NV-G20 in fact.
Later that day, when things were
a bit slack, I decided to at least try
the machine and clarify the exact
nature of the fault. So I set it up on
In this case the loading had not
proceded far enough to leave a loop
of tape outside the cassette but I imagine that it was a variation of this
routine which had created a loop on
at least one occasion when the
customer used the machine. If the
loading had proceded a little further before the cassette was rejected, this could well have happened. And in view of what I subsequently found, it is quite likely that
the fault varied from time to time.
But right now, I didn't have a
clue and what I had seen didn't inspire me with a great deal of confidence. It conjured up visions of a
faulty mode select switch or
something equally complex in a
machine with which I was only
partly familiar. In any case, it looked like a job that would have to be
put aside until I had more time.
the bench and pushed in a cassette.
Initially, all seemed well; the
cassette carrier accepted the tape
and, apparently, set it down on the
deck. But then it rebelled and promptly unloaded the cassette.
Well, that was a new one on me.
Fortunately, this machine is very
easy to get at; only four screws
need be undone to release the cover
and this reveals both the deck and
the main printed board, which sit
side by side.
That done, I tried loading the
cassette again. And now I could see
that the process went as far as putting the cassette on the deck and
starting the actual tape loading
process.
In this machine the loading process differs somewhat from the
more usual arrangement. Instead of
waiting for the "play" instruction
before extracting the tape from the
cassette and wrapping it around
the drum, this machine begins extracting the tape as soon as the
cassette reaches the deck.
It doesn't go all the way. It extracts enough tape to allow it to be
loaded against the audio/control
head. The idea appears to be to provide better tape control during the
subsequent loading process, though
I have not worked out the details of
this. Anyway, this was where the
loading process baulked. It began
this first stage but before it could
complete it, the cassette was
unloaded.
Hairy legs
So I contented myself with extracting the cassette from the carrier and giving the deck assembly a
quick visual inspection. And that's
when I saw it.
It was on the deck, to the left of
the supply reel disc, hard against
the front of the machine and partly
hidden by the cassette carrier
assembly mounted above the deck.
"It" was a very large tarantula
spider and, initially, I wasn't sure
whether it was dead or alive.
This didn't worry me particularly
as tarantulas are quite harmless.
As it turned out he (or she) was very
dead and I was able to fish him (or
her) out without too much trouble.
There were also a couple of spare
legs lying around which I also
recovered.
Thus inspired I gave the rest of
TETIA TV TIP
Philips K9A
Symptom: Grotesque north/sou!h
distortion. Picture height normal 1n
the centre of the.screen but reduced to almost nothing at the sides.
Cure: Broken track between N/S
adjust trimpot R602 and the N/S
transductor. This break forces the
whole vertical scan current
through the transductor, instead of
sharing it with the adjustment
network.
the deck a thorough inspection,
removing the cover above the head
drum in the process. This would
have been done anyway, since I
make it a policy to give all tape-path
components a routine clean
regardless of the main fault. I also
wanted to make sure there were no
more beasties involved.
There weren't as it turned out
but I was surprised at the condition
of the head drum. The working face
was reasonably clean, although
there was some oxide build-up on
the guides and auxiliary heads;
rather more, in fact, than I expected in a new machine. But the
real surprise was the amount of
muck on the top of head drum.
This took the form of a sticky
coating and a pattern of spots; the
latter, I assumed, being excreta
from the now departed tarantula.
Anyway, I cleaned everything up,
including the oxide build-up, then
put the machine through its paces
again.
And that was it; everything worked perfectly. I can only guess as to
the exact manner in which the corpse was gumming up the works and
I can't even be sure that it was exactly the same on my bench as it
was in the customer's home (it may
well have moved around in transit).
It might have been fouling the brake
mechanism and the machine sensed
this fault and refused to accept the
cassette for this reason.
Another query concerns just how
the monster got into the machine.
Like most such devices, it is well
enclosed but there are ventilation
slots in several places, some of
them a little wider than typical.
And knowing just how small a
space these creatures can negotiate, it wouldn't surprise me if this
was the explanation.
Alternatively, it is just possible
that it gained entry via a cassette,
there being two large pockets on
the underside which could easily
accommodate it.
Technically, that was the end of
the story. However, I had to inform
the lady that the warranty did not
cover the entry of tarantula spiders
into the machine, so I would have to
charge her. Fortunately, she accepted this philosophically.
So what will we find next?
-~
APRIL 1989
75
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