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SERVICEMAN'S LOG
It sounds like Donald Duck
Poor old Donald! He takes the blame for a
multitude of problems, not the least of which is
the way people use him to describe a multitude
of distortion effects. So much so that I
sometimes wonder what they would do without
him. Perhaps he should charge for this service.
Truth to tell, not many forms of
distortion really do sound like Donald
Duck. And that's not surprising I
suppose, because I imagine that the
true Donald Duck sound is a lot more
complex than most common forms of
distortion.
Anyway, to get down to business,
the problem involved another National NV-G7 video recorder, at which
I recoiled slightly after recounting last
month's notes. However, one has to
take the good with the bad.
The customer - one of my regulars simply dumped it on the counter and
came out with the above heading; "It
sounds like Donald Duck".
"Any problem with the picture?"
"No - picture's perfect. But the
sound's just like Donald Duck".
And that was about it, as far as the
customer was concerned. He was
obviously convinced that all I had to
do was wave my magic screwdriver
and all would be well. I find such
faith quite touching.
When most people use the Donald
Duck analogy they mean a recording
that is running fast, even though this
is not strictly accurate - at least from
Donald's point of view.
But I couldn't reconcile such an
effect with the fact that the picture
was supposedly perfect. If the tape
was running that fast the picture
would also be running fast - assuming that it remained locked.
So I set the machine up and pushed
in a test tape. And the result was
quite surprising. Yes, the sound was
funny and it did seem to be some
kind of speed abnormality, although I
couldn't define it initially. And, yes,
the picture was perfect; normal speed,
no noise bars, rock steady.
So what was happening to the
sound? I listened to it long and carefully a number of times before I came
to any conclusion. Finally, it seemed
to me that the sound would run at
normal speed for one period, then
hesitate briefly as though the tape had
stopped or slowed significantly, then
resume normal speed, then hesitate,
and so on.
I also judged that the normal period was longer than the hesitant one,
while the whole process was happening quite rapidly, producing a high
speed chopping effect. The end result
was certainly strange, though I doubt
whether Donald would have been flattered by the comparison.
But Donald's sensitivities aside, I
had a problem to solve; what was the
most likely cause of such an effect which I had certainly never encountered before - and how was I going to
track it down?
Transport problem
This is the stator from the capstan motor in the National NV-G7 video recorder.
It consi!!ts of 6 flat windings on a PC board, together with three small surfacemounted solid state devices at the centre of three of these windings.
48
SILICON CHIP
Well, it had to be a transport problem of some kind: the capstan drive,
the drum drive or, more specifically,
the servo systems associated with
them. But which or what? And why
was it not affecting the picture?
I sat down and had a good long
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think about it, going back to basic
principles for some inspiration. In the
normal way, the drum speed is locked
to the tape, because it is locked to the
reference pulses on the tape. So, if
the tape speed varies for some reason
the drum will try to follow it, more or
less successfully, depending on how
drastic the variation.
·
But the sound system has no such
refinement. A variation of tape speed
will affect the sound directly. So it
was conceivable that we had a capstan speed variation which was upsetting the sound, but was within the
capture range of the drum servo system. In short, a capstan motor fault.
It was all pure theory, of course,
but I felt it was strong enough to justify checking the capstan motor and
replacing it if that was the only way
to prove the point. And at that point I
had no knowledge of just what kind
of motor was involved. Nor was there
much about it in the manual.
But when I delved into the innards
of the machine I found a capstan
motor like no other I had ever seen
before. Not that I'm knocking it; on
the contrary, it is a robust, well designed component, much larger than
the usual run , easy to get at and take
apart and, in this case anyway, economical to repair.
The two main parts are the rotor
and stator. The rotor is simply a metal
disc, about 75mm in diameter, which
runs in close proximity to the stator.
Being such a simple device, I felt it
was unlikely to be at fault and turned
my attention to the stator.
The accompanying photograph
gives a good idea of the stator construction. As can be seen, it consists
of six flat windings mounted on a PC
board. A circle enclosing the windings would have a diameter of about
75mm, matching the rotor diameter.
The stator board itself is about 90mm
across. In the centre of three of the
coils is a solid state device, the purpose of which is not clear. The external connections to these devices and
to the coils run via a flexible copper
pattern which mates with an edge
connector.
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DECEMBER1990
49
SERVICEMAN'S LOG - CTD
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As encountered in the machine, the
stator is the other way up to that
shown in the photo. It is held by three
screws, the holes for which can be
seen, and across the back of the board
is a bar, held by two screws, which
carries one bearing for the rotor shaft.
So undoing five screws takes the
whole thing apart.
But before I took it apart, I gave it a
physical check-out. In particular, I
checked for free movement of the rotor, adjustment of the bearings, etc.
As far as I could tell there was nothing wrong here, which really left only
the stator assembly.
That led me to another pleasant
surprise; a replacement stator was
available for around $30 which is
quite a modest figure considering that
some capstan motors are well over
the $100 mark. On that basis I decided on a replacement rotor. Even if
I was wrong (and I felt pretty sure I
was right), it wasn't a great deal to
risk.
50
SILICON CHIP
But I was right; the new rotor fixed
it and Donald was sent packing. And
the final cost was quite reasonable,
partly because of the modest replacement cost, plus the relative ease of
fitting.
So I finally had another satisfied
customer.
Two Donald's
While on the subject of Donald and
his mutilation of the English language,
I had another video recorder recently
against which the same accusation
was levelled. In some respects, the
cases were similar, in others quite
different. It was one of those sameonly-differnt situations.
For a start, it was a completely different brand of recorder; a Sharp VC381X. It was also intermittent and,
probably as a by-product of this, had
something of a history to it.
The customer was a stranger, having recently moved into my area from
the Orange district. And that was
where the fault first appeared and
was tackled by a local serviceman.
Judging from what I found later, he
had tackled the problem logically, had
obviously gone to a lot of trouble, and
had done everything in a thoroughly
professional manner.
And, according to the customer, he
seemed to have fixed it. It ran for a
couple of months before they moved
and apparently survived the move,
for a few weeks at least! But then suddenly the old fault was back.
And the nature of the fault? "It goes
Donald Duck. Y'know, everything
speeds up. But only sometimes; usually after it's been on for about 20
minutes".
The speed-up included the picture
which, he explained, was still visible
but running fast, with lines across it.
"Y'know, like in fast forward, only
with Donald Duck sound" .
All of which was a pretty good fault
description; better than I get from
most customers. That, and the history I related above, at least gave me a
head start. In fact, I had already mentally .registered that it sounded very
much like a capstan fault; possibly in
the capstan servo system.
At first switch-on, the machine
behaved normally and I let it run with
a test tape. Then, just as the owner
had predicted, after about 20 minutes
it suddenly ran amok, with speeded
up picture and sound. I switched it
off and let it rest for half an hour or
so, then tried again. But it was still
faulty.
I removed the top cover, then lifted
the top board, which is hinged at the
back, thus gaining access to the mechanical area. The machine performed
in the same faulty manner while I
looked over this section but there was
nothing obvious.
I turned the machine off, turned it
on its side, removed the bottom cover,
and swung out the bottom board,
which also hinges at the back. This
carries the capstan and drum servo
circuits, although it was the capstan
system that I suspected.
As I explained in the first story,
incorrect capstan speed can normally
be accommodated by the head drum,
which is locked to the reference
pulses on the tape. The picture speed
will be incorrect and it may display
cross-over lines, but it should remain
locked. The sound speed will likewise be incorrect.
completely aimless exercise. I turned
it off in disgust.
Later, I switched the machine on
again, only to find that all the faults
had vanished; it was working perfectly. So what had I done during my
aimless probing. I didn't wake up
immediately, but at that stage the
machine was on its side, with the top
and bottom boards folded out at right
angles. In order to turn the machine
over and get a better look from the
top, I closed the bottom board. Whereupon it shut down. I swung the board
out again and it was working.
I immediately suspected a hairline
crack in one of the tracks, and went
through the routine of twisting, prodding, and generally abusing the board
in an effort to get a lead on it. All of
which proved completely fruitless.
Suddenly, I woke up to the fact that
it was the position of the board that
was critical. Swing it in from the open
position and all would be well until
it was within about 50mm of fully
closed, whereupon the machine
would suddenly shut down. Open
this gap ever so slightly and it would
work; close it again and it would stop.
But then, when the board was fully
Closer inspection of the bottom
board around the relevant servo IC,
IC706, revealed that the previous serviceman had had the same idea. The
IC had obviously been removed and
no doubt replaced, along with several
other components in this section.
And, as I said earlier, it had all been
very neatly done.
At this point, I turned the machine
on again. And lo and behold, it was
back to normal. But not for long. Its
next trick was to really run amok,
displaying not only the high speed
fault, but a swag of other faults as
well.
A revolting development
Pressing the PLAY button could
send it into the fast forward wind
function. Or rewind the tape. Then
the dew light came up and the machine shut down completely. As another cartoon character is wont to
exclaim, "What a revolting development"!
Yes, revolting it was because, right
then, I didn't have a clue where to
look next. I went through the motions
of going over all the components,
prodding and poking, but it was a
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closed, it would work again.
I left the board fully closed and
went over it again; prodding, twisting, bashing (yes , and calling it
names), but all to no avail. I couldn't
fault it.
But I did latch on to something.
Running from the back of the bottom
board, and soldered to the copper
tracks, are two ribbon cables, about
100mm long. These run up into the
mechanism area and terminate in
suitable plugs in this section. One
ribbon is designated AB and the other
AN.
I left the bottom board closed and
lay the machine flat, under which
conditions it was working normally.
And, with the top board swung out, I
had ready access to the ribbons and
plugs. I wiggled the plugs, without
any effect, then started poking at the
ribbons.
This was where I struck oil, though
not immediately. After several tries, I
happened to move the AN (12-conductor) cable a certain way and the
dew light came on and the machine
shut down. The necessary movement
was quite critical but, with care, also
quite predictable. So, after putting it
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-.,•
DECEMBER 1990
51
SERVICEMAN'S LOG - CTD
through the go/no-go cycle several
times, I knew I was close.
After the first failure I imagined
that the plug and socket assembly
would be the most likely culprit but,
after several of the above cycles, I
changed my mind. The fault was definitely close to the bottom board end
of the cable, where it was soldered
directly to the copper tracks. So it
was either a break in one of the conductors, or a dry joint at the board.
Now I reckon, after all these years,
I can pick a suspect joint with the
best of them; which is not the same as
claiming to be infallible. Nevertheless, if there was a dry joint there I
felt sure a close examination would
reveal it.
So I turned the machine over,
reached for the jeweller's loupe, and
went over each of the 12 connections
from every angle and with every lighting angle. And I would have passed
every one of them as a perfect joint;
there was absolutely nothing I could
see to arouse any suspicion.
On the other hand, a broken lead
was a long shot. There is no flexing of
the cable, apart from servicing activities, so why should it fail. In any
case, the easiest thing to try was the
soldering. I reached for the iron, unsoldered each joint, examined it, and
carefully remade it.
And this exercise did nothing to
change my mind; I found no evidence
of any fault. I was convinced that I
would have to replace the cable. But I
was wrong; when I put the recorder
back into operation it came good
immediately, and nothing I could do
with the bottom board would create
the fault.
I was only partly convinced, of
course; I've been caught like that before. I closed both boards, refitted the
covers, set the machine up on the end
of the bench, and put it through a
number of cycles for the rest of the
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SILICON CHIP
TETIA TV TIP
Hitachi CTP-229
(NP8CA Chassis)
Symptom: excessive brightness
and not enough control to bring it
down. A "sort of" picture could be
obtained by reducing the screen
voltage but this revealed heavy
shading on the left hand side of
the screen.
Cure: C719, a 4. 7µF 250V electro, open circuit. This capacitor is
a bypass on the 180V rail feeding
the video output transistors. This
fault is rather like a screen-voltage
problem but the clue is that with
this one there are no retrace lines
visible.
TETIA TV Tip is supplied by the
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7015.
day. It never missed a beat.
Dew sensor
At the end of the day I disconnected it completely from the mains
and let it cool over night. But when I
switched it on next morning we were
in trouble again. No, it didn't Donald
Duck but the dew sensor came up.
My first reaction was to rip everything apart and start again. Fortunately, second thoughts prevailed. I
simply left it on with the dew sensor
flashing. After about an hour, the
sensor shut down and the machine
came good and stayed that way for
the rest of the day.
I shut it down again that night, and
the dew sensor came on again next
morning, clearing itself after an hour.
And the same thing happened the
next day. By which time I was more
than a little suspicious of the dew
sensor itself. So much so that I ripped
it out and fitted a new one.
And that really fixed everything.
Many days of testing, under all conditions, failed to reveal any problems.
So Donald had been sent packing
again, and everyone was happy. But I
make it a practice in all cases involving intermittent faults to warn the
customer that it might recur, and to
come back immediately if it does.
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