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SERVICEMAN'S LOG
All the IDakings of a Chinese puzzle
Servicing often involves more than electronic
expertise, experience and a set of service
manuals. Knowing what to expect in particular
sets often means knowing something of the
manufacturer's history and even, as in this
case, where the set was made.
This was brought home quite forcibly by a recent experience with two
TV sets, supposedly identical but
actually as different as chalk from
cheese. Both were 36cm GC-149 colour sets, made under the General
label.
Now the General label has had a
somewhat chequered history. Originally a modest-size Japanese company
in its own right, its sets were very
popular and they appeared on the
Australian market with the introduction of colour TV.
More recently - about five years ago
- the company was taken over by
Fujitsu and many models are now
sold under the Fujitsu General label.
On the other hand, and rather
strangely, some still carry the simple
General label.
(The company is represented in
Australia by General Corporation
Australia Pty Ltd , 10-16 South St,
Rydalmere, NSW 2116).
Routine but interesting
The first set did not present any
complex problems and was fairly
routine in fact. But it was interesting
in other ways. It was a faily new set,
only some six months old and still
under warranty, and was owned by
one of my long-standing customers.
More importantly, in this context, he
is one of those loyal customers who
would never consider taking a set to
anyone else.
The complaint was straightforward
enough: sound and raster, but no picture. I pulled the back off the cabinet
and this gave good access to several
72
SILICON CHIP
useful check points. These included
the R,G,B stages and I checked the
voltages on the relevant transistor
collectors. These all came up very
close to the 123V shown on the circuit.
I checked these same points with
the CRO and wasn't particularly surprised to find no signal. Nor was there
any signal on the bases of these stages.
Again, no great surprise.
From here I jumped back to the
luminance circuit and, specifically,
to the video drive stage, Q201
(2SA733AP), which is fed from pin
48 o( the jungle IC, IC201
(UPC1420CA) - see Fig.1. An output
is taken from the emitter of this stage
but there was no luminance signal at
TETIA TV TIP
Rank C-1851
Symptom: weak sync. Flagwav•
ing at top of picture on reception
of TV channels, total breakup of
picture when viewing video recordings.
Cure: C556 (10µF 16V electro)
dried out. This capacitor passes
pulses from the AFC pulse amp
(TR505) to the flywheel discriminator ahead of the line oscillator.
TET/A TV Tip is supplied by the
Tasmanian branch of The Electronic Technicians' Institute of
Australia. Contact Jim Lawler. 16
Adina St. Geifston Bay, Tasmania
7015.
this point. Nor was there any at the
base, which couples to pin 48.
Back tracking from here took me to
transistor Q3, the first video amplifier. There was luminance signal at
the base of this stage, and also at the
emitter, from whence the signal goes
to pin 42 of the IC.
So yVe had signal into the IC but no
signal out. Before jumping to conclusions, I checked the voltages on the
IC pins. These voltages did not tally
exactly with those on the circuit they seldom do - but there were no
gross abnormalities, and I felt my
original suspicion was justified; the
IC was crook.
I didn't have a replacement and it
is a type I don't normally stock. The
failure rate is low and it would be
stock lying idle. Nor was I keen on
buying a replacement since, under
warranty, I would not be reimbursed
financially but only with a replacement device - which I might not use
for years. So the plan was to remove
the suspect unit and return it to the
local company for direct replacement.
A real mess
It was only then that I removed the
main board and turned it over to attack the IC connections. And what a
sight met my gaze. If I hadn't known .
the set's history and the honesty of
the owner, I would have assumed that
some striped apron merchant had
been at it with his traditional tools of
trade.
Not to put too fine a point on it, it
was a right proper mess. And since I
did know its history, it was obvious
that this was the way it had come
from the factory. Now it is not unusual to find, in any new set, that
there has been some additional work
done in the factory. As sets come off
the production line and are given a
preliminary test, there will inevitably
be a small proportion that don't work. ·
These will be diverted to a production service bay, the faulty compo-
3 /l4BLII
C15
NA TERM! NAL
o.o,
·o
Cl
51
1------1
CHROMA PROCESSOR VIDEO AMP
SYNC AMP.VERT OSC.HOR.OSC
IC201
UPC1420CA
R.l06
s.&<
C31 \
\!S(]P
C3\2
\!S(]P
C3\3
1110P
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.
Fig.I: relevant portion of the General GC-149 circuit. The jungle chip is at the bottom, the video driver stage (Q201)
at left above it, and the 1st video amplifier transistor (Q3) at top centre. The problem turned out to be simple
enough, although the PC board on which the parts were mounted was a real mess.
nent or connection tracked down and
replaced or repaired, and the set returned to the testing line. And one
can usually spot such work; a hand
soldered connection will leave a ring
of rosin flux - something which
doesn't happen with the flow soldering process.
Nor is there any objection to this
procedure. After all, it would be stupid to discard a whole board, simply
because one minor component was
faulty.
But there was nothing minor about
what had happened to this board. For
starters, cuts and scratches had been
made in the board between most of
the pins of the IC in question, and
pretty roughly at that. The green varnish which normally covers the board
had been scraped and cut, and some
of the cuts were quite deep. But it
wasn't only around the IC. There were
quite a number of cuts at odd random
spots on the rest of the board.
The meaning of life
What did it all mean? Was I wrong
in my diagnosis of a faulty IC? Was
there some more subtle fault, possibly intermittent, which had eluded
the factory tests and was now in my
court?
JANUARY
1991
73
arrived and was fitted. And that was
it, the set worked first time and turned
in a first class performance. Beauty
really is only skin deep!
So the set was duly returned to the
customer, who was delighted with the
performance. But he was quite
shocked to learn that it had been made
in China, rather than Japan, where he
imagined it had been made. Truth to
tell, I doubt if he would have bought
it had he known.
On the other hand, there was no
point in worrying him unnecessarily
- the set could go for years and never
miss a beat. So I kept my findings and
impressions to myself, simply answering his inevitable question with the
truth; it was a faulty IC.
SERVICEMAN'S LOG - CTD
Perish the thought! In any case, the
IC would have to come out and be
replaced. If my worst fears were realised, someone else, like the local
General Corporation, could take on
the job.
But the whole situation alerted me
to something I had overlooked up
until this point. The set had not been
made in Japan - they would never
allow a set like this to reach the market. Nor had it been made in Korea,
where the quality control, while not
quite as good as that in Japan, would
never pass anything like this.
No, the fine print on the spec. plate
indicated that this set had been made
in The People's Republic of China.
This was the first time I had encountered anything from this region and,
superficially at least, it appeared to
be exactly the same as the versions
made in Japan - even down to the
components used.
A grotty effort
There was only one exception; the
printed circuit board. Forced to look
at it closely I realised that it was a
pretty grotty effort, with very rough
edges and dags on the copper tracks.
While the other major components
had obviously been imported, I tip
that the board had been made in
China.
And this, I suspect, was the reason
for all the cuts and scratches; the
rough copper pattern had resulted in
bridges between tracks, preventing the
set from working in the first place.
There may have been only one or
two such bridges, but the technician
had adopted a blanket approach, cutting and scratching between all suspect tracks until the set came good.
This, in turn, suggested a fairly low
level of service expertise, low labour
cost, and a situation where time was
of little consequence. And in support
of that last point I would judge that
several hours had been spent working on that board; a lot longer than
would be tolerated in most factories.
Nor was this service confined to
cuts between tracks; closer investigation revealed that several copper
tracks had been cut and subsequently
bridged. Obviously another blind
approach to solving the problem. And
in a couple of cases, the tracks haq.
been cut and left cut; apparently part
of some modification process which
must have been legitimate, because
the set had ·worked (and eventually
worked again).
Anyway, there was little I could do
about that; time did not permit a detailed analysis of situation. I simply
pulled the IC out and sent it back to
the company for replacement. Then I
went over the board and did my best
to clean it up. There wasn't a great
deal I could do but it did look a little
better when I'd finished. Granted, it
wouldn't make the set perform any
better, but it did give me some satisfaction.
In due course, the replacement IC
Dropped General
And that brings me to the second
version of this set. In fact, it came
into the workshop while I was still
working on the first one. The owner
is another regular customer and he
was somewhat agitated. He was leaving on an extended caravan holiday
the following day and was loading
the set into the van when he dropped
it. Now it didn't go! Could I have a
look at it and perhaps do an emergency repair?
Surprisingly, there wasn't a mark
on the cabinet even though, by all
accounts, it had taken a pretty hard
knock. But one glance inside told the
whole story and points up what I
consider is a serious weakness in
many sets on the market today.
The main board sits in the bottom
of the cabinet, supported by its right
and left hand edges, which slide into
0
••• ~-r TM~ TV
,
1'HE 'PEOPLES 'RePUSt.-1C OF ClilN~ ••
74
SILICON CHIP
slots moulded in the cabinet. And
that's all the support there is. When it
receives a jolt, even a relatively mild
one, the weight of the horizontal output transformer is just too much, and
the board cracks.
That was exactly what had happened in this case, which didn't really surprise me. In fact, I already had
an AWA Mitsubishi in the workshop
which had suffered the same fate.
Again, there was no damage to the
cabinet and, as far as I could determine, the drop had been quite moderate. Nevertheless, the board had
cracked under the horizontal transformer, severing about 10 tracks in
the process. But that's another story.
The damage to the General was
more severe. It had cracked roughly
diagonally across the rear right hand
corner, under the transformer. Fortunately, it had not cracked right across,
so there was still some mechanical
support. I went over it with a glass
and, at a rough count, there were 37
broken tracks. And those were only
the ones I could be sure of. I shook
my head; even assuming that I could
find time to do the job in the few
hours available, there was no way that
I could guarantee it, with the set being
jolted around in a van.
To have any chance of a permanent
cure I would need to run it on the
bench for a substantial period, give it
a good shaking from time to time and,
ideally, subject it to a range of temperatures. And even then, we'd both
have to accept that it might bounce
after several months. But a quick fix
for use in a van? No way.
When I made these points to the
owner, he accepted the situation
philosophically. "I'll go out and buy
another portable. You hang on to that
one and see what you can do with it
while I'm away. See ya in a few
months".
Easier than I thought
And so the set was pushed into a
corner until such time as things were
slack; an ideal way to tackle a job like
this. In fact, the repairs to the board
took less time than I had anticipated
and went without any problems. But
I couldn't help noticing the difference between this board and the previous one. Both sets were made in
China but this one was as neat and
well made as any I have seen.
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So I pass. More to the point, the set
functioned at first switch-on, which
was more than I had hoped for.
Unfortunately, after my initial elation, I realised that all was not perfect. It was exhibiting more than normal purity error in the top left corner
(bluish) and about halfway down the
right hand side (magenta).
Apparently, the fall had moved or
distorted the shadow mask slightly,
and there is little that one can do
about that, at least directly. The real
solution would be a new tube but the
cost would be hard to justify.
The best I could do was give it a
purity adjustment and hope that I
might score some improvement. So I
slackened off the yoke retaining screw,
and juggled the assembly for the best
result. I didn't score a great deal but
any improvement was worthwhile.
Then I re-converged it and this
came up very well. So the final result
was usable even if something less than
perfect. To tell the truth, I imagine
most viewers would probably be unaware of the fault unless their attention was drawn to it.
And there this job rests, still in the
workshop, waiting for the owner to
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return from holidays. I hope he won't
be too disappointed. But the moral is
obvious; TV sets don't like being
dropped.
The ghostly antenna
And now, for a change of scene,
here's a funny one from my southern
correspondent, J. L. of Tasmania. And
when I say "funny" , it was more
"funny peculiar" than "funny ha ha".
Here's how he tells it.
This is a tale about a ghostly car
radio installation. It comes from a
colleague who runs a small business
specialising in mobile communications. To appreciate the story, it is
76
SILICON CHIP
first necessary to understand how an
automatic radio antenna works.
These systems usually have two
leads (plus an earth) attached to the
antenna actuating motor. One is a
permanent connection to the 12V
supply while the other is a control
line and is usually connected to a
switched 12V output from the radio.
This operates a DPDT relay to control
the direction of current flow through
the motor. When the control line is
low (ie, at 0V), the relay connects the
antenna motor in the "down" configuration and the antenna retracts
until, in the fully retracted position, a
limit switch is activated.
Conversely, when the control line
is energised, the relay switches the
motor to the "up" configuration and
the antenna extends until, at full
height, another limit switch is activated (see SILICON CHIP, March 1990,
page 30, for additional details),
In the ideal case, the control line is
connected to the switched 12V output on the radio. This is energised
when the radio is switched on, thus
causing the motor to run forward and
raise the antenna. If the radio has no
such outlet, an alternative approach
is to connect the control line to the
accessory position on the ignition
switch. In this case, the antenna will
be raised whenever the ignition
switch is in the running or accessory
position, and will be retracted when
the ignition is turned off.
Now to the story. It seems that a
new radio had just been fitted to a
vehicle, along with an automatic antenna, when the customer arrived to
take delivery. The last connections to
the antenna control circuit were still
to be made and the installer was working against time.
And, since this radio did not have
an automatic antenna power outlet,
the control line had to be connected
to the accessories terminal of the ignition switch.
The installer turned on the ignition
and searched for an active 12V line.
He found one and connected the control line to it. The antenna worked
perfectly, and so did the radio - for
about three days.
Then the owner found that whenever he turned sharply left the antenna retracted, then went up again
as he straightened up. The same thing
happened when he accelerated - the
antenna would retract and then shoot
up again as he eased off the pedal. It
reached the point where, in stop-start
traffic, the antenna was continually
winding itself up and down, which
made reception virtually impossible.
This pattern continued for a couple
of days then cleared up, only to show
up again later in the week. The owner
wasn't too happy about it and brought
the car back to have the antenna system checked.
Just fill 'er up
This time it was examined by a
technician, rather than the installer,
·and he found a most bizarre reason
for the problem. The 12V control line
had not been connected to the accesories side of the ignition switch,
as intended, but to the petrol gauge
line. At the time the installation was
done this line measured 12V, but this
value was fated to vary as the fuel
level dropped.
With a full tank the system worked
normally but, as the level dropped,
the fuel sloshing about put lower and varying - voltages on the antenna
control line, which eventually
dropped below the hold-in level of
the relay. Hence the mysterious effect. In fact, if the tank had been taken
down to nearly empty the antenna
would not have worked at all.
The symptoms cleared each time
the tank was filled but, in between,
the owner thought his car was
haunted!
Which just goes to show that it
doesn't pay to rush any job that even
remotely involves electrical connections.
Serviceman's boo-boos
Thank you J. L. That's a new one on
me. Very early in my career I earned
HAUN"i'E.D( NO StR;
'(OUR CAR IS ~ST
E.X_C-1 i""E:-D
:I
my bread and dripping fitting car
radios to the then popular vehicles like the Austin A40 and the first
Holden. And we had our fair share of
boo-boos.
I once witnessed an incorrect connection behind the dash destroy a
whole wiring loom on a brand new
car. What the boss said to the hapless
perpetrator doesn't bear repeating.
At a personal level, the worst experience was more painful than anything. Groping behind the dash for a
connection I managed to bridge an
active terminal to chassis via the metal
strap on my wristwatch. Almost before the pain registered it had melted
two links out of the strap, and left
their imprint burned into my wrist.
The scar has now faded but was visible for several years.
But patching into the petrol gauge no, we never did anything like that;
that takes the prize.
Correspondence
And finally, I feel bound to reply to
a reader, R.W.H. of TasmanJa, who
has written to the editor, questioning
some points raised in my October
notes. His letter was reproduced on
the Mailbag page of the November
issue, together with a brief editorial
comment. I refer readers to this for
the full text.
As far as the transformer is concerned, there is little that I can add to
the editorial comment; my sentiments
entirely. However, the transformer in
question is sitting on my desk as I
w:&ite and, if R.W.H. would like to
conduct his own research, he can have
it for the price of postage and packing!
And the supposed excessive
charges? Nowhere in my notes did I
state that the customer was charged
for the replaced driver transistor,
Q501. Experimental replacement of
minor components like this are a normal part of everyday sevicing. If it
cures the fault, well and good; if it
doesn't, one writes it off as a few
cents - or even dollars, sometimes well spent. And it is a lot cheaper
than wasting hours using alternative
approaches.
In fact, all the customer was
charged for was the transformer and
the output transistor, Q551. And, yes,
the customer was told to " ... bring the
set in right away"; and he agreed to
do that. I rest my case.
SC
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77
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