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SERVICEMAN'S LOG
Murphy has two bob each way
Coincidence, chance, luck, law of probability,
Murphy's law - call it what you will, it plays a
large part in servicing. Sometimes it helps;
sometimes it hinders. And when it hinders it has
the potential to make an innocent serviceman
look like a rogue.
No, it didn't happen this time; but
that was mainly because the customer
has been dealing with me for nearly
20 years and he does trust me. Had it
been a new customer, of the suspicious type, it could well have been a
different story.
In more detail, the customer is the
proprietor of a local motel and the
story concerns two colour TV sets
from his units. They were identical
sets - 48cm HMV Model B4803s - but
with quite different faults.
When he rang me, he explained
20
SILICON CHIP
that the more serious fault was a complete picture failure, although there
was still normal sound. The other set
was still working but had a pronounced red cast. He suggested I take
the more serious one first, since the
second one was still usable to some
extent.
When customers say "no picture"
it prompts a series of logical questions. Is there any light on the screen?
If so, is it a steady raster or is it just a
snowstorm? Provided the customer
can give clear answers to these questions, one can usually get a pretty
good idea of what it looks like
and where, in broad terms, the
fault is likely to be.
In this case, the customer was
able to give a clear answer; it was
a steady raster, suggesting that
the sync pulses were being processed but that the video was being lost somewhere down the
track. But that was about as far as
I could go at that stage and so I
left it to him to bring the set in.
I was familiar with the set in
general terms and didn't anticipate any real problems. This
model is about 12 years old and
although carrying the HMV label, with the doggie on the front,
it is actually a Japanese chassis,
from JVC. And since I was very
familiar with most JVC chassis
and had a good stock of manuals,
I reckoned it would be straightforward.
When it turned up, I found it
much as the customer had described; normal sound and a nor-
mal raster. The only difference was
that I detected a faint image and a few
faint blobs of colour, particularly when
I subsequently fed in a test card. But
there was another effect which the
customer hadn't mentioned; the raster
on the screen was very bright and the
brightness control had virtually no
control over it.
On the other hand, I noted that
adjusting the colour control did have
an effect on the brightness - not a very
great effect mind you, but it was there.
It also had a slight effect on the saturation of such colour blobs as were
visible.
A strange chassis
I pulled the back off and took a
closer look at the works. And that was
the first setback. I thought I knew
most of the JVC chassis but this was a
strange one. More to the point, a thorough search through both my HMV
and JVC manuals confirmed that I
didn't have the correct manual, or
even a circuit, for it.
Tracking down a circuit diagram
was obviously going to take some time
and so I rang the customer to explain
that there was going to be some delay.
And that was the first bit of good
news; he had kept the instruction
books for each of the sets he had
bought and these included a circuit.
He had a stack of them and I was
welcome to one for keeps. As he put
it, they were double Dutch to him and
so that problem was solved.
He duly delivered one of the books
and the relevant portion of the circuit
is reproduced here (see Fig.1). On the
left is the video sync separator, IC201,
and to the right of it the video output
transistor, X201, fed from pin 16 of
IC201.
Next on the right is the matrix/
colour IC, IC302. This delivers the RY, B-Y and G-Y signals from pins 6, 2
and 4 respectively to the CRT board,
SU-3033A, at extreme right. Also, pin
16 of this IC takes the colour control
voltage from the colour control pot
(R13) which is on the control board,
SU-4205A, at top right.
(As an aside, note that the 7.2V on
pins 2, 4 and 6 mysteriously becomes
7.4V on the bases of the blue, red and
green output transistors, XlOl, 102
and 103. But contradictions like this
are nothing unusual in modern circuits.)
I checked the voltage on pin 16 of
IC302 and this appeared to be responding normally to any adjustment of the
colour control. From there, I moved
to the three output transistors on the
CRT board and checked the collector
voltages. These were significantly
lower - by about 20V - than the figures suggested on the circuit and
enough to make them suspect.
Similarly, the base voltages seemed
to be marginally high, as one might
expect, although it was difficult to be
sure since it doesn't take much change
here to upset the collector values. In
any case, this all added up to a theory
that all three guns were being turned
hard on, effectively masking any video
that might be present.
And that was the next check; the
luminance path. This starts at pin 16
of IC201 and goes to the base of the
video output transistor, X201. The output appears at the emitter of this stage
and is fed to pin 1 on the CRT board
and thence to the emitter circuits of
the RGB output stages.
A voltage check around X201 produced figures very close to those on
the circuit; nothing really suspicious
there. The CRO also confirmed that
there was normal video into and out
of this transistor and from there into
the emitters of the three output transistors-all of which further supported
the idea that it was a hard turn-on
problem.
So what about the brightness control, R30, on the control board? Basically, this is between the +12V rail
and chassis, with the moving arm coming out on pin 1 and connecting to pin
14 of IC201. However, the voltage
range that this provides is nothing
like 12V. Limiting resistors R31, R32,
R33 and R34 restrict the range considerably.
But by how much? I had no way of
knowing but a measurement on pin
14 indicated from 9.5V to a little over
10V; only about half a volt. This
seemed to be rather small but, on the
other hand, seemed to tally with the
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[f ___ f]Oa- ~:'i 0
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L-..J--------1-+------H----+--'
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Fig.1: relevant section of the faulty HMV B4803. IC201 is the video sync
separator and drives video output transistor X201 which in turn drives
the emitter circuits of the RGB driver transistors (X101, X102 & X103).
OCT0BER1991
21
SERVICEMAN'S LOG - CTD
1-\0W M\JC~ WOOL.'0
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the almost unbelievable; two faulty
ICs in the one set and both contributing to the same major symptom. See
what I mean by Murphy having two
bob each way!
Of course, the prognosis still had to
be confirmed. So another IC was ordered, delivered and fitted. And that
really fixed everything. The set was
given a routine grey scale adjustment,
a soak test for a day or so and returned
to the customer.
And that was the end of that story.
It had taken a lot longer and cost more
than either I or the customer had anticipated. But he accepted it all philosophically, collected the set and delivered the second one; the one with
the red cast.
Too much red
9.6V shown on pin 14 ofIC201. So we
put that one on hold for the moment.
My thoughts went back to IC302
and the fact that adjusting the colour
control not only affected what colour
there was to be seen, but also the
brightness which, in my book, was all
wrong.
A toss-up
So what it all boiled down to was a
toss-up between these two ICs. Was it
IC201, as suggested by the seemingly
small voltage change on pin 14, but
about which I was not sure? Or was it
IC302, as suggested by the interaction
between the colour control and the
brightness function and which I felt
sure was incorrect?
Not having either IC in stock, I had
to make a choice and hope I ordered
the right one. If Murphy had his way,
of course, which ever one I ordered
would be wrong, but I had to make a
decision. After some thought I
plumped for IC302 but, as it turned
out, Murphy was having two bob each
way.
So the IC was ordered, was duly
delivered and fitted. I then switched
on and waited for the tube to warm
22
SILICON CHIP
up. As it did, I was relieved to see a
picture come up on the screen; it
seemed I had made the right choice.
But the joy was short lived. We had
a picture all right and we had proper
colour saturation control, but the picture was still too bright. It was not as
bright as before but was still brighter
than normal and, more importantly,
there was insignificant control from
the brightness pot, R30.
So it was back to IC201 and the
brightness control voltage. It appeared
that my original doubts about the voltage range might be justified. In an
effort to determine what this range
should be, I disconnected this line
from the main board, at pin 1 on the
control board (this is actually a wirewrap connection).
It was a different story now. With
the line effectively disconnected from
IC201, the voltage ranged from 9.5V
to 11.5V; figures which made a lot
more sense. But there was still about
9.5V on pin 14 and the picture was
still too bright. I tried bridging pin 14
to chassis with some low value resistors, hoping to brute force the situation, but this had little effect.
All of which forced me to accept
Once again, his description of the
fault was quite accurate; it was very
red. Initially, I tried juggling the cutoff and drive presets, R102, R104,
R106, R108 & Rl 10. However, it
quickly became obvious that, while
this produced some improvement, the
error was far beyond such adjustments, even assuming that such an
approach could be justified. And
clearly, it wasn't.
A voltage check around the red output stage confirmed what I now suspected; the stage was turned hard on.
The voltages marked on the circuit
suggested that this stage was normally
turned on the least, but its collector
voltage was now well below the other
two.
So, after a few more routine checks,
I was forced once again to the conclusion that it was IC302. It was all getting rather monotonous but I ordered
another one, which duly arrived and
was fitted.
And that fixed it. Or, rather, it did
after a grey scale routine, my fiddling
with the drives and cut-offs having
put everything out of whack. So that
finished that job and, after the customer had taken delivery, I mentally
wrote both sets off.
Murphy strikes
But there was more to come. Some
six weeks went by and then the customer was on the phone again. The
first set was in trouble again and, judging by the customer's description, behaving just as it had the first time. I
didn't trust myself to say more than,
"Bring it in again".
TETIA TV TIP
Philips KT3A-2 chassis.
Symptom: Bright red, blue or
green screen, with similarly coloured retrace lines. The effect is
exactly like a heater-cathode short
in the picture tube but the heatercathode voltages remain near normal. The other cathode voltages
can be greatly modified.
Cure: Transistors 0241 (red),
0257 (green) or 0273 (blue) short
circuited. The transistor is a PNP
type BC558. On this occasion the
fault was heat sensitive and was
totally absent while the cabinet
back was removed.
is
TETIA TV Tip
supplied by the
Tasmanian branch of the Electronic Technician's Institute ofAustralia. Contact Jim Lawler, 16
Adina St, Geilston Bay, 7015.
Privately, I had a horrible fear that
one of the ICs had shot its bolt again
and that wasn't going to look very
good, even to a trusting customer. And
a quick check on the bench did little
to reassure me; it was turned on just
as hard as before, if not harder.
The only bright spot was that I was
now much more familiar with the circuit and layout. I went straight to the
collectors of the three driver transistors, which all turned out to be well
down; more so than before. This difference encouraged me a little; perhaps it wasn't an IC after all but something more fundamental.
I went straight to pin 16 (video out)
of IC201 and checked the voltage. It
was close enough to normal. I moved
on to the base of the video output
transistor, X201. This was still normal, being virtually the same point,
but the emitter and collector voltages
told a different story.
The emitter should have been at
6.5V but was actually closer to the
+12V on the supply rail. And the collector, normally at 0.3V, was also way
up, only slightly below the emitter
voltage.
Well, that was the answer, at least
in broad terms. But why? My first
impulse was to suspect the video output transistor and I went through the
voltage check again, while I speculated. And as I prodded one of the
legs , the set suddenly came good.
And that was it. I had moved the
collector resistor, R214, and further
investigation revealed a subtle, but
quite definite, dry joint between one
of its pigtails and the copper pattern.
A hot iron and some solder had it
fixed in a jiffy.
Well , that was a relief. But imagine
the fuss a suspicious customer could
have made. I can just hear the complaint. "Had the set for nearly a fortnight, charged me "x" dollars , then
six weeks later it broke down again.
Y'can't trust these blokes; leave themselves another job every time".
Of course, nothing like that happened with this customer. In fact, we
both had a bit of a laugh about it when
I explained what had happened. And
I didn't even charge him; it was on the
house. But it can be a trap.
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To change the subject, I have had
several examples recently of a new
twist to an old fault; a twist which
fooled me the first time and cost me a
couple of wasted hours.
The sets in question were the old
faithfuls, the Philips K9 and K11. I
have had three of these in for repair
recently, in as many weeks. And, yes,
there is still a lot of them around,
alive and kicking.
The twist was that, while it was a
fault with which I was very familiar,
the symptoms were quite different.
Add to that a sneaky red herring and
one of them had me running around
in circles.
The K9 and Kl 1 use very similar
circuits, the main difference being that
the K11 uses a varicap pushbutton
type tuner. However, the sections of
interest in this story, the power supplies, are so similar as to be virtually
interchangeable.
The set that caused me all the problems was a Kl 1. It belonged to a long
standing customer and I had serviced
it on a number of occasions over the
years. This time, it was suffering from
a madly hiccuping power supply. It's
not an unusual fault in these sets and,
over the years, I have developed various approaches to it.
Basically, one needs to determine
whether the fault is in the power supply itself or whether it is a fault in the
set which the power supply doesn't
like. Often, one can get a clue by monitoring the main HT rail, which nor-
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(02) 774 1154
OCT0BER1991
23
SERVICEMAN'S LOG - CTD
But replacing it, essential though it
undoubtedly was, did nothing for the
hiccups.
By now there was only one component left; the chopper transistor,
TSl 70. Initially, I simply disconnected
the leads to it and made an in -situ
test. This indicated that the transistor
was perfect but, having been caught
that way before, I decided to pull it
out and replace it anyway.
And what a mess I found. The insulating washer between the transistor
and the heatsink had carbonised to
the point where it fell to pieces when
I tried to remove it. And that was it; I
fitted a new washer and the set was
up and running.
Damaged T0-3 insulating washers are a common problem in the power supplies
of old Philips K9 & Kll sets. A third washer completely disintegrated when it
was removed.
Why didn't I twig?
mally sits at around 155V, and noting I had a chance to look at it again. By
the value it reaches before it collapses.
this time, however, the Variac was
I do this by connecting the set to a tied up with another job, which I
Variac and winding the supply voltdidn't want to disturb.
age up until the set hiccups. In this
I thus decided to apply full mains
case, the system collapsed at around voltage and see what happened;
65V which is similar to the effect cre- maybe the faulty component would
ated by a faulty tripler. I tended to
show itself under pressure. Imagine
doubt this possibility in this case, bemy surprise when the set produced a
normal picture, without so much as
cause a new tripler had been fitted
only a few months previously. Still,
any sign of a hiccup.
stranger things have happened, so I
An intermittent fault? There was
disconnected the tripler. But it had no nothing for it but to pull the Variac
effect.
out of its current role and go through
The next trick is to substitute a the previous test again. And, sure
known good power supply. This is
enough, at around 130V it hiccuped.
somewhat easier with these sets than
But when I notched the Variac up a
with many others, for a couple ofrea- few more volts it stopped and I pressed
on until I had the normal 155V HT.
sons. One is that it is physically relatively simple and the other is that I And there it ran for the next half hour
have several such units on hand, sal- and never missed a beat.
I fished out a second spare board,
vaged from other sets which have long
fitted it and went through the whole
gone to their last resting place.
procedure again, with exactly the same
It took only a few minutes to fit a
spare, then I wound the supply ·volt- result. By now I realised I'd been had.
I couldn't explain the spurious hicage up again, while monitoring the
HT rail. This time, all went well as it cup, but spurious it certainly was; the
went past the previous 65V limit and whole incident was a red herring.
I was hoping for a clear run. But at
It was all very frustrating but at
around 130V the system began hic- . least I was now sure that the fault was
on the set's own power board. So I
cuping again.
This different voltage level was a proceeded to go over the board, combit of a puzzle but I now felt sure that ponent by component. A frequent
the power supply was not at fault . cause of this fault is the 225µF smoothHowever, after spending some coning capacitor, Cl 78a, following the
siderable time checking out all the bridge rectifier. This sometimes has a
other likely possibilities in the set, I dry joint to the board pattern and
drew a complete blank.
sometimes it simply dries out.
Pressure of other work intervened
In this case, the capacitor was
.at this stage and, in any case, I needed quickly cleared. Next, I discovered
time to think. So it was that the set sat that a 680kQ resistor, R171, was open
on the bench for a couple days before
circuit and I thought I'd struck oil.
Now I know that someone is going
to say that I should have twigged to
this fault in the first place, since it is
a regular problem in this set - and
others. What's more , I have described
this breakdown, in the K9 and Kl 1, in
these notes in the past.
Which is fair enough. Except that,
in all previous cases, this fault has
taken out the chopper transistor and
the 2A fuse between it and the bridge
rectifier. They are classic symptoms;
never has it simply caused hiccuping.
In fact, the first of the three sets exhibited those classic symptoms and I had
it up and running in short order.
And that's what threw me. That
and the aforementioned red herring.
Of course, I swore I'd know better
next time. And I did too but the next
time came sooner than I had expected;
less than a week later, there was a K9
on the bench, hiccuping away merrily. I despatched it in short order.
More to the point, I am wondering
about that insulating washer. While
we tend to refer to these as mica washers, they are not always mica and this
one certainly wasn't. It was (blue) plastic. Now I've no doubt that, commercially, the plastic version has much to
recommend it; it's probably cheaper,
more robust and easier to store, to
name just a few of the advantages that
I can think of.
But is it as good as mica? Is it, in the
long term, chemically unstable with a
couple of hundred volts across it?
Some plastic capacitor dielectrics
have exhibited characteristics along
these general lines, limiting their use
in certain applications.
Well, it's just a thought.
SC
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SILICON CHIP
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