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SERVICEMAN'S LOG
Working within the customer’s budget
With smaller sets, the cost of any repairs must
be kept under control. My main story this month
is a good demonstation of that & is also an
excellent example of how a minor component
can cause inconvenience.
The story concerns a Hanimex
colour TV set, model CTV-10. It is
a semi-portable type, with a 25cm
screen, and is designed to operate
from either 240V AC or 12V DC (eg,
from a car battery). And it is around
this dual operation feature that the
story revolves.
The owner had bought it when he
retired, primarily for use in his caravan on a round-Australia trip which
lasted some 12 months. And, as can
be imagined, the 12V system came
in for a fair amount of use during
that time.
But shortly after returning home,
he realised that the 12V system could
no longer be used, although the set
continued to perform perfectly well
on 240V. Well, that wasn’t much of a
bind; they were not planning any long
34 Silicon Chip
caravan trips in the future and, as long
it functioned on the mains, it would
suit their needs quite well.
So that was how things went for the
next 12 months or so. In fact, it would
probably have continued along these
lines indefinitely, if the set had not
also failed on the mains. And that’s
where I came in.
The owner was a new customer and
he set out the above history before
asking the vital question, “Can you
fix it?” I couldn’t be sure, of course.
As I explained to him, it was a set I
hadn’t seen before and I had no circuit
or service manual. Hopefully, I could
get data from Hanimex if necessary
but, initially, I would simply look for
what was obvious.
Filthy lucre
That was OK but then came the
vital question of filthy lucre; how
much was he prepared to spend
on it? It was an important question
because I didn’t know what I would
find or what data or spare parts were
available.
After some discussion, we settled
on a figure of $100. If it looked like
exceeding that figure, I would consult
him first.
And so he left it with me. On closer
examination, I learned that the set
was made in China. Later, when I
delved into the innards, I wasn’t all
that impressed with the construction
in general. I’d seen worse but I’d seen
better too.
At a more basic level, I had to try
to work out the power supply system
and decide where to start looking. The
only thing I felt reasonably sure about
TC-48P10 Has Live Chassis
In the Serviceman story in the
October 1993 issue, I mentioned
that the Panasonic TC-48P10,
and by implication the TC-1480A,
had an M15D “dead” chassis. This
is wrong – both sets have the
M15L “live” chassis. The mistake
has come about partly because I
test and repair all sets using an
isolation transformer.
was that there were two separate faults,
since the two failures had occurred at
different times.
As it turned out, the set was basically a 12V device, with the addition of a 12V mains-driven power
supply. The mains cord was fitted
permanently, while the 12V cord
connected to the set via a plug and
socket arrangement.
There was no switching involved.
The 12V positive battery lead went
straight to the 12V rail derived from
the mains power supply. The voltage
regulator IC isolated the 12V from the
rest of the supply circuitry – quite an
elegant system.
It was the plug and socket arrangement connecting the 12V lead to the
set that provided the first clue. It is
a commonly used fitting, typically
referred to as a DC power plug or DC
jack – with matching socket. The plug,
which fits on the cable, is a female fitting, and the socket, normally chassis
mounted, is the male version.
When I tried to push the plug into
the socket it wouldn’t fit properly.
Closer examination revealed that the
end of the plug had been damaged. The
insulation between the inner and outer
conductors was deformed, as was the
end of the inner conductor.
Thus alerted, I pulled the back off
the set for a closer examination of the
socket. And this was the real culprit;
it had obviously been seriously over-
heated and was grossly deformed. I
subsequently measured the current
involved and it varied from 2.25A to
2.5A over the range 12-13.8V. That’s
pretty solid for a miniature connector
like this, particularly as the set would
typically run for quite long periods.
As a quick test, I patched a couple
of leads into the circuit and connected
them to the 12V bench power supply.
And the set sprang to life immediately, with good sound and a first-class
picture. I gave it a quick check across
all the channels and satisfied myself
that there was nothing wrong with its
operation. This clearly suggested that
its failure to operate on 240V must
involve the power supply.
In the meantime, what was to be
done about the damaged connectors?
The easy way out would be to simply
replace them with new units of the
same design. However, knowing that
they appeared to be inadequate, at least
on a long-term basis, should I try to fit
something better?
I mulled over this latter idea at some
length and was eventually forced to
the conclusion that, desirable though
it might be in theory, it was not physically practical. It would have meant
hacking into the chassis in an awkward
spot, could not have been done neatly,
and would have only added to the cost.
I even discussed the problem with
the owner and he agreed that it was
unlikely that the 12V system would
get much use from now on.
So I took the easy way out. But
why wasn’t the set designed to take
an adequate plug and socket – even if
it cost a fraction more?
The supply fault
Putting such questions aside, I now
had to find the fault in the mains supply. It was a simple circuit, consisting
of a power transformer delivering
around 16V, a bridge rectifier, a 3-terminal voltage regulator and a filter
capacitor.
It didn’t take long to pinpoint the
culprit – the transformer primary was
open circuit. It was a simple job to
remove the transformer and, when I
did, it revealed a small sticker saying,
“Internal Thermal Fuse”. So my guess
is that it was this that had failed but
for what reason we will never know.
In any case, the transformer was a
write-off.
So where to from here? There were
two points to be clari
fied: (1) the
availability of a replacement and (2)
the cost. This latter point was most
important. Transformers are not cheap
and I could see that, with labour costs,
the $100 limit might be exceeded.
So it was back to the customer. I
had to be honest and point out that,
depending on the best transformer
deal I could swing, the job might cost
up to $150. Was he prepared
to go that far? He wasn’t too
keen at first but I pointed out
that we knew the set itself
was OK, performed well,
and that to replace it, would
probably set him back $300
to $350. So, after some hesitation, he agreed.
So began the search for
the best transformer deal.
My first choice was a Sam
sung unit I had on hand. It
was electrically suitable,
was fitted with a magnetic
shield similar to the origi
nal, and looked as though
it would fit physically. And,
most importantly, it only
cost me $36, including tax.
At that price, I could do the
job well under the limit.
But alas for my clever
thought; it was just marginally too large and there was
no way I could fit it. So the
next step was a call to the
Hanimex spare parts department. It
was a good news/bad news situation.
Yes, they could supply a transformer
ex-stock but the price was $73 plus
tax, or about $95. Pack and post would
add another $6, giving a total of about
$100. I said “Ouch” under my breath
and thanked them for their help.
That simply was not a proposition.
Even without any mark-up on the
transformer, labour costs – including
the work done on the 12V system –
would put the total above the agreed
figure. And I couldn’t justify pushing
the limit any higher. I had to find a
better way.
Substitute transformer
A colleague dropped in for a chat
around this time and I filled him in
on the problem, displaying the faulty
transformer. His reaction was immediate: “Have a look at an old Akai
video recorder, a VS-3 or VS-4. They
had a transformer with a number of
windings on it and it might just fit.”
Being thus reminded, I realised that
he could be right and that I might just
have one. So it was out to the junk
room where we scrabbled through the
discards and, sure enough, there was
a junked VS-3. So it was back to the
bench and out came the transformer.
And it looked quite promising, being of a shape and size which would
clearly fit. All that remained was to
November 1993 35
SERVICEMAN'S LOG – CTD
sort out the secondary windings and,
hopefully, find one that would suit.
The primary winding was easily identified, so the quickest way was to fit a
power cord and plug it into the mains.
Unfortunately this proved to be another setback. At switch-on there was
a protesting splat and a puff of smoke;
storage had apparently not been kind
to this device and it was write off.
But the exercise had not been completely wasted. My col
league had
started a useful train of thought and
I remembered another Akai video
recorder in the junk room, this time a
VS-112 which is a much later model.
And again, the transformer looked very
promising. It was smaller that the VS-3
unit and should fit easily.
In fact, when I pulled it out and
tried it in position, I realised that I
36 Silicon Chip
could bolt it directly into place; a real
win. So another mains test was set up.
And it didn’t go splat this time. More
importantly, it had three secondary
windings, one at 30V and two at 16V,
the latter being the more useful value.
Initially, I sat the transformer on
the bench and patched one of the
16V windings into the circuit for a
trial run. And it worked but with one
reservation; the DC voltage out was
barely holding its value. I plugged it
into the Variac and reduced the input
voltage slightly. Sure enough the picture started to bend and pull. In short,
there was not quite enough voltage at
the regulator input to cope with line
voltage variations.
The 16V AC should have been
enough but I sensed that the winding
was a rather light one and that the load
of the set was pulling it down. The
logical reaction was to connect
both 16V windings in parallel –
suitably phased of course –and
that solved that problem. And
an hour’s bench test confirmed
that the transformer was running
quite cool.
But we weren’t out of the
woods yet. The transformer had
no magnetic shield and, while
it worked fine when sitting on
the bench, I was worried that
it could cause trouble when
mounted in the set.
So the next step was to
mount it in the set, wire it
neatly in the final form, and
hope. Well, we won. There
wasn’t the slightest hint
of interference from the
transformer, even when
check
e d on blank red,
green and blue rasters. I gave the set
a soak test on a daily basis for about
a week before finally delivering it to
the customer.
So what did it all cost? I charged
him $125. Yes, I know, the transformer
didn’t cost me anything – well not in
hard cash – but it did cost me a lot in
time, taking into account the problem
with the first unit. So I reckoned it was
a fair price. The customer thought so
too; he was delighted.
A day in the life ...
And now, for a change of scene –
and a change of pace – here are some
short stories from my colleague J. L.,
across Bass Strait. He has sent me a
number of such items and I am including as many as space will permit this
time around. More next time. Over to
you, J. L.
The stories selected for this column
are usually about unusual faults, or
about common faults that require
some kind of mental gymnastics to
resolve.
The simple faults, like replacing
a shorted chopper transistor and the
resulting blown fuse, never seem to
make these pages. Yet they constitute
99% of all jobs passing through the
average serviceman’s workshop.
There are times when I have a long
run of routine tasks that provide no
inspiration for Serviceman stories and
I’m left bereft of any material to write
about. So, at the suggestion of the Editor, I have decided to put together a
list of common but interesting faults.
One that I have just finished was an
AWA video recorder, an AV47. It came
in with the complaint that it “would
not play through the TV set”. This
was a rather ambiguous statement,
since it could mean that it would not
feed playback signals to the TV set, or
it could mean that it would not pass
off-air signals as well.
The only thing to do in a case like
this is to set the machine up and operate it in the way an average owner
might drive it. This is not as easy as
it seems, since a technician usually
knows what the “TV/VCR” switch
and other controls mean and would
be expected to put them in the correct
position.
To operate a VCR in “average citizen” mode means that the serviceman
has to try to forget everything he has
ever learned about these devices.
Then, with any luck, he will hit on
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This close-up view shows the heat-damaged DC plug & socket from the Hanimex
CTV-10 12V supply system.
the same problem as the customer
did and be able to diagnose the fault
straight away.
In this case, I was lucky. I connected the machine to the bench monitor
and tuned one to the other. The off-air
picture was decidedly snowy and the
off-tape picture was also extremely
poor. It was snowy, had no colour and
often rolled.
I recorded a few minutes of program
material and then played it back on
another machine. The results seemed
to be reasonable but I did detect some
snowy scenes. It was not what I would
have called a prime quality picture.
Booster/modulator unit
A glance at the circuit diagram in
the service manual showed that both
the antenna booster and the output
modulator were contained in a single
unit. I had a horrible suspicion that
this was the source of the trouble.
By attaching a test tuner I was able
to determine that the output of the
booster was far from up to scratch. In
fact, there was far less signal coming
out of the booster than there was going
into it.
Similarly, I was able to feed a good
video signal into the modulator part
of the unit and found the output to be
far less than one would have expected.
There is no circuit diagram published
for the booster/modulator unit but I
would hazard a guess that some part
of the supply rail to the chips inside
the unit had failed.
Unfortunately, there is no way to
repair these devices so I had to place
an order for a new one from Mitsubishi AWA. It wasn’t cheap but the new
unit cured all the problems and so the
customer is satisfied with the result, if
not really happy about the cost.
The next job was a Sharp VC-8300X
VCR, one of the first of Sharp’s front
loading models. The problem here was
that the machine would load and begin
to play but then shut down before it
showed any sign of a picture.
I took the cover off the machine and
tried again to play a tape. The cause of
the trouble was immediately apparent.
The drum was not rotating.
The drum motor in this machine is
not one of those modern direct drive
types. It consists of a very conventional
brush type motor, driving the drum by
means of a wide flat belt.
It didn’t take long to discover that
the motor was being provided with a
healthy drive voltage yet showed no
signs of life. I disconnected the leads
from the motor and tested it for con
tinuity. There was none.
The VC-8300X is a very old machine
and probably not worth all that much.
I checked with the owner to see if he
was prepared to pay something like
$80 for a new motor. He wasn’t, so
we decided that the machine would
probably have to be junked.
But before taking that step, I enquired among some of my colleagues
who have a stock of junk sets in
their store rooms. One of them did
have an 8300 and it had a seemingly
good motor on the deck. We struck
a quick deal and I took the motor off
the wreck.
I had the motor fitted and the machine up and running just 15 minutes
after my return to the workshop. The
owner was quite happy to have a secondhand motor fitted to his machine.
The alternative would have been very
much more expensive.
(I later found that one of the brush
springs in the original motor had been
bent slightly, thus holding the brush
away from the commutator. I might
have been able to repair it but as I had
already fitted the replacement there
was no point).
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The next job involved another
mechanical problem, this time in a
Sharp cassette deck. I plugged in a
set of headphones, dropped my test
cassette into the deck and pressed play.
The sound in the phones was hardly
recognisable. It was suffering from the
most hideous warble I have ever heard.
When I looked inside the cassette
well, my eye was immediately caught
by a large dollop of black gloop on the
capstan shaft. In fact, it turned out to
be a part of the pinch roller. What had
happened was that the roller rubber
had perished and become very soft
and sticky. Part of it had torn off and
stuck to the capstan.
The job was relatively easy to fix. I
first had to work out how to remove
the pinch roller arm before I could
remove the roller spindle. After that,
I had to find out if I could get a proper
replacement. In the event, I found an
alternative in a junked deck so once
again the customer scored a quick fix
at a reasonable price.
Thank you J. L. I like the idea of
dealing with the more mundane, dayto-day, bread-and-butter jobs; it helps
strike a balance. More next time. SC
November 1993 37
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