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SERVICEMAN'S LOG
Around the world for sixpence
No, that heading is not a travel agency’s
advertisement; it is one from way back which, as
I recall, implies a whole sequence of frustrating
events which ultimately result in very little gain.
And that was exactly how I felt by the time I had
finished this particular job.
To be more precise, I can honestly
say that this job turned out to be one
of the most frustrating I have encountered for a very long time. I very nearly
decided not to relate it, however, because the fault eventually turned out
to be something quite simple. The only
reason I have told it is that it might
help someone else. Or that someone
else might be able to answer some of
the questions it poses.
The story concerns a Hitachi-Fujian
34cm colour TV set, model HFC1421B, chassis type F87PT. These sets
are made in China and were originally
marketed in Australia, several years
ago, through a Chinese Trade Commission, with offices in the Sydney
suburb of Botany. However, I can find
no reference to them in the current
directory.
The owner’s complaint was that the
picture was rolling but a quick check
revealed that this was not the case; the
Fig.1: this diagram shows the relevant portion of the circuit around IC501
in the Hitachi-Fujian HFC-1421B. The IC is at the top, with pin 40 near
it’s bottom lefthand corner. R710 is near the bottom of the diagram, in line
with pin 34 of the IC.
40 Silicon Chip
set had not lost vertical hold, it had lost
horizontal hold – something likely to
be rather more complicated. And as I
had no technical data for this set, my
first job was to try to acquire at least a
circuit. However, with the marketing
situation apparently changed, I was
unsure as to who to approach.
So I contacted my retailer colleague
who has sold a number of this brand
– but not this model – in the past.
It transpired that he had obtained
his stock from a wholesale outlet in
Canberra and he gladly supplied their
name and phone number.
They were very obliging but could
not help directly. Instead, they referred
me to a Sydney firm, Cumberland Electronic Services, 120 Old Canterbury
Rd, Lewisham 2049. Phone (02) 564
1700. If you are involved in servicing,
I suggest that you make a note of that.
I rang them and they were also
very obliging. They put me onto their
service department and the gentleman
in charge was most helpful. Yes, they
could supply either a copy of the
circuit diagram for $5.00 plus $2.00
postage, or a complete manual for
around $25.00.
I decided that, for what looked like
a fairly routine fault, I could probably
get by with a circuit, although the
price of the manual is quite reasonable
compared with some prices quoted
these days. So I posted off a cheque
and, in a few days, had a photocopy
of the circuit. And, as photocopies
go, it was not bad. By that I mean that
it was probably no worse than the
original, which was obviously much
reduced. At least most of the values
were readable, or at least decipherable.
But some of the closely packed lines
were hard to trace.
Anyway, it was a start. So why had
the set lost horizontal hold? The heart
of this part of the circuit is IC501, a
TA7698AP. This is a large, complicated 42-pin IC which handles the
video signal, sync separation, chroma
signals and matrixing, etc. It also has
pulse...”. In fact it looks like the top
half of a slightly impure sine wave.
But “from shaped”?
Anyway, terminology aside, I decided that it was good enough. So what
did that leave? If the horizontal oscillator was running free at a reasonable
rate and reference pulses were being
fed back from the horizontal output
transformer, I reasoned that it looked
like a sync pulse failure.
A composite video signal from the
front end of the set (pin 15 of IC201)
is applied to pin 39 of IC501 (INV
IN), goes through an inverting stage,
and emerges on pin 40 (INV OUT); ie,
the signal is inverted but otherwise
unchanged.
From here, the signal goes to pin
37 (SYNC SEP IN), which seems quite
logical, except that there is a network
of resistors, capacitors and a diode in
between – see Fig.2. And it is around
this network that I have encountered
faulty components in the past.
So, initially, I went over this network and checked every likely component, either by measurement or
substitution. And I could find nothing
wrong. But the mere presence of the
network itself kept nagging me. What
was its function anyway? Could there
still be a subtle fault in it somewhere
that I had missed? This was something
I was unsure about without knowing
what the network was supposed to
achieve.
Come in sucker
the facility to be wired to handle PAL,
NTSC or SECAM signals.
It is a very commonly used IC and
is found in a variety of brand names.
These include AWA, NEC and Orion.
And it so happens that I have an AWA
manual in which there is a section
purporting to describe some of the associated circuitry. Among other things,
it has an enlarged and detailed diagram
of the IC, with designations for the
various pins – something not available
on the Hitachi circuit. I have included
these designations in brackets in the
following discussion.
I concentrated on the circuitry
around the sync separator section,
partly because I have had problems
here before. In particular, I remembered encountering both vertical and
horizontal sync problems in this area.
But there were a couple of other
symptoms supporting this idea.
Most important was the fact that, by
carefully adjusting the horizontal
hold control (R709) and riding it,
it was possible to hold the picture
on the screen. This suggested that
the free-running frequency of the
horizontal oscillator was not grossly
out and that it should be capable of
locking if the sync pulses were being
processed correctly.
Further to this thought, I checked
the horizontal pulses from the horizontal output transformer, which
are used for comparison in the AFC
circuit. These come from pin 7 of
the transformer and are fed into pin
38 (H PULSE IN/GATE PULSE OUT)
of the IC. There was a substantial
pulse here, similar to one shown in
the AWA manual and described as
“a from shaped horizontal flyback
I suppose that, at this stage, I allowed myself to be sucked in to some
extent. I felt I should try to understand
the circuit, at least for future reference, rather than simply check each
component until I found a crook one.
A noble sentiment, perhaps, but not
necessarily a very practical one.
One reason I pursued this approach
was that, as I mentioned before, the
AWA manual purports to explain the
purpose of this network. If I could
digest that, I might have learned
something.
Alas for my hopes. The explanation turned out to be a mess of
badly-translated gobbledegook, with
spelling, grammatical, and composition mistakes that went far beyond the
ones we regularly encounter. Taken
together, they added up to incomprehensible garbage (I should have been
warned by that “from shaped” pulse
reference).
June 1994 41
heels. As far as I could tell, the external
network between pins 37 and 40 was
intact, the horizontal reference pulse
from the horizontal output transformer, was correct, and I had replaced the
IC. What had I overlooked?
Back to the circuit
According to the screed, “The
composite video signal from pin 40
is applied (to pin 37) through a sync
separator time constant circuit. The
slice levels of the horizontal sync
and vertical sync can be set independently”.
So now we know! Or we might if
we were sure what is meant by slice
level – I could hazard a guess – and,
more importantly, why it is apparently
so critical. And what is the purpose
of the “time constant”, which is also
mentioned?
I went over the screed several times,
cooked up several theories which had
to be discarded, and discussed it with
several colleagues. They all shrugged
their shoulders and one, to whom
I complained about the standard of
42 Silicon Chip
service manuals, muttered something
along the lines of “that’s life”.
Well, I know when I’m beaten. I had
wasted a lot of time and achieved nothing more than a sense of frustration.
I seemed to have exhausted all the
possibilities I could think of.
So what was left? The IC? Not very
likely and only as a last resort. But this
seemed like a last resort situation. And
I did have a spare on hand. Oh well,
at least it would prove the point, one
way or the other.
It is not such a big deal these days,
even with 42 pins involved. Twenty
minutes later I was ready switch on
again, fingers crossed. It was an anticlimax; the fault was still there, exactly
as before.
Well, that really set me back on my
I spent some time pouring over the
circuit again. As I’ve already stated,
some of the lines were very crowded,
making some long runs very difficult
to follow. And this was part of the
reason I had missed out on a vital
section.
I went back to pin 7 of the horizontal output transformer and once again,
but more carefully this time, traced
the circuit up to pin 38 (H PULSE IN
etc). And I suddenly realised what I
had missed. Branching off this rail
was resistor R701 (8.2kΩ). And this
led me to R706, a 2kΩ preset tab pot,
shunted by R707 (2.2kΩ) and connected to chassis via capacitor C709
(.01µF).
This tab pot is what some makers
call horizontal AFC, or horizontal
position, among other names. The
moving arm of R706 goes to pin 35
(AFC OUT) via C707 (.022µF) and its
obvious function is to allow the level
of the reference pulse to this pin to be
optimised during manufacture.
Of course, the fault just had to be
in this little branch of circuitry which
had been overlooked. And it was –
R701, the 8.2kΩ resistor, was virtually
open circuit. When it was replaced,
the picture locked up instantly and
set was ready to go back to the owner.
But why was it overlooked? There
is no point in trying to make excuses;
if you goof, you goof. The best one can
do is try to learn from it. But I think it
is fair to say that the crowded nature
of the circuit didn’t help, although
that is something we have to learn to
live with.
Another factor, and again this is no
excuse, was that the offending resistor
was not mounted anywhere near the
cluster of other components around
the IC, which I had tested as a matter
of routine without too much regard for
their place in the circuit. No, it was
mounted over near the horizontal output transformer, where it connected to
pin 7. Of course, it was all perfectly
logical from the physical layout point
of view.
So there it is; a happy ending for
the customer but a very unhappy
INVERTER
OUTPUT
40
R550
2.7k
R551
820
R552
620k
D591
C563
1
C564
.01
SYNC SEP
INPUT
37
R565
56k
C513
560pF
Fig.2: this network between pins 37 & 40 of IC501 in the
Hitachi-Fujian HFC-1421B has been redrawn from an
AWA manual & given the component markings from the
HFC-1421B circuit.
experience for yours truly. That one
won’t be putting any cream on the
custard – it won’t even pay for the
custard!
Bread & butter
Well, after all that, I think that something a little less traumatic is called
for; something more in line with the
routine day-to-day, bread-and-butter
jobs. (Why do I keep talking about
tucker?)
Anyway, this is a story about a
video recorder; a Hitachi model VTM818E. This is a current model and
the particular unit was virtually new,
being only about three months old.
That means, of course, that it was still
under warranty.
What follows is not about any long
and involved diagnosis; the fault was
plainly visible. The real point is the
unlikely coincidence of the forces
involved.
The lady who brought it in was
quite clear about the problem; it would
load a cassette, apparently correctly,
but would not play it. It would not
respond to the play button; at least not
properly. It would commence to play
the tape but would run for only about
10 seconds before stopping.
I didn’t doubt the lady’s description
but I must confess to being a little
surprised by it. It sounded like a mechanical fault of some kind but that
would be very unusual for a machine
with only three month’s use – and
particularly with this model, which
is a very reliable one.
After the lady had left and I had
finished another job, I set it up and
pushed in a tape. It loaded normally,
so I pressed the play button. And it
behaved exactly as described; it ran
for about 10 seconds, then shut down.
I pushed the eject button and the cassette unloaded normally.
OK, time to pull the cover off and
look at the works. The layout is fairly
conventional, with the tape deck on
the lefthand side and the PC board to
the right. I could see nothing obviously
wrong, so I pushed the tape in again
and watched it load.
This appeared to be normal. The machine employs the now fairly common
“half load” procedure; as soon as the
cassette settles on the deck, the tape
is loaded against the control head, an
arrangement designed to measure and
display the actual playing time of the
tape while it is being shuttled. Then,
when the play button is pressed, the
loading arms pick up the tape and
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June 1994 43
SERVICEMAN’S LOG – CTD
wrap it around the drum in the usual
way.
And that is exactly what happened.
The tape began to move, the take-up
and supply reels revolved, and nothing
appeared to be amiss. At least, not for
the first few seconds. Then, suddenly,
the take-up reel stopped and the tape
kept coming, forming a loop. I was
reaching for the on/off switch, when
the whole system shut down.
Well, that was normal too. The loss
of sensing pulses from the take-up reel
had indicated to the microprocessor
that there was something wrong and it
had done its job – including rewinding
the loop back onto the supply reel, to
avoid further damage. So all I had to
do was find out why the take-up reel
was malfunctioning.
And it was malfunctioning in a
rather peculiar way. Further observation, using a clear plastic dummy
cassette, allowed me to see the takeup reel directly and revealed that it
always made exactly one revolution
before it failed.
I unloaded the dummy cassette
and made a closer examination of the
take-up reel. Turning the reel with my
fingers confirmed that it was meeting
some obstruction after one turn. And
looking more closely it appeared that
there was something stuck to the side
of the reel. But in the confined space
of this particular unit, I was unable to
see what it was.
I decided that the simplest approach
would be to remove the cassette carrier. While this job is a bit fiddly, it is
no big deal provided the screws are
removed in the right order. I won’t
bore the reader with the procedure – it
varies from machine to machine anyway – but it does involve unclipping
the front panel of the machine and
moving it out of the way.
That done, the carrier can be slid
slightly towards the front of the machine, allowing a couple of locking
keys to be freed from their keyways.
The carrier can then be released and
laid to one side – the lead lengths are
quite adequate – thereby providing
ready access to the reel mechanisms.
The nest step was to remove the reel
itself. It is held in place with a small
circlip, the only precaution being to
ensure that the circlip doesn’t fly off
to the other side of the workshop. Well
it didn’t and I was then able to lift the
reel free.
Brake mechanism
And now all was clear. What
we were looking at was the brake
pad from the brake assembly of the
take-up reel. The brake mechanism
consists of a brake shoe which is
fitted with a felt pad. The brake shoe
moves horizontally and presses the
pad against the side of the reel, to prevent tape overrun when the transport
mechanism stops.
But there was no brake pad on this
brake shoe, where it should have been;
instead it was stuck to the side of the
reel. And that was what was hindering
the rotation of the take-up reel and
causing the machine to shut down.
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44 Silicon Chip
Now missing brake pads are fairly
common, though not in machines only
a few months old. More importantly,
they don’t cause this kind of problem.
Instead, they usually simply fall to the
bottom of the machine and, in most
cases, the user is not even aware of
what has happened; the bare brake
shoe usually continues to do the job,
even if a little less scientifically. It is
only when the machine is opened for
some other reason that this fault is
found.
The brake pads are attached to the
brake shoe with some kind of contact adhesive on the back of the pad.
Exactly why this failed, allowing the
pad to come free, is not clear. But
what is apparent is that, when it did
come adrift, it flipped over so that the
adhesive side was pressed against the
side of the reel, and it stuck there. And
it was right in the path of the brake
shoe, so that it fouled it after the first
revolution.
The cure was simple enough. Peel
off the pad, clean off any adhesive it
may have left behind, then refit it to
the brake shoe. But I added some extra
adhesive this time; a dab of Selleys
Kwik Grip® – reputedly strong enough
to mend a broken heart! Anyway, it
should do this job adequately.
As I said at the beginning, it was no
big deal to find and fix, but it surely
must have been one chance in a thousand that the pad behaved as it did and
finished up where it did.
So I can hardly expect that this story
will have anything more than novelty
value; I don’t imagine that anyone
else will ever encounter the same
fault. Still, stranger things have hapSC
pened.
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