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SERVICEMAN'S LOG
Doing the rounds with remote control
This month’s notes have turned out to be a
continuation of last month’s. It wasn’t planned
that way; it just happened. As readers will
recall, they were about remote control units &
this month’s notes describe two more faults.
One of last month’s stories was
about some funny goings on with the
infrared LEDs in a particular model
remote control unit (NEC RD-309E).
They would work when the unit was
upside down but not when it was right
way up.
And it wasn’t just a one-off; I had
two with identical symptoms, which
was enough to suggest that it involved
an inher
ent weakness in the LEDs
themselves. Replacing them was all
that was required to cure the fault but
the exact failure mechanism remained
a mystery.
Which was where we left things last
month. But hardly had the presses
begun to roll, than there was another
episode. It was the same model unit
and it came in with a familiar complaint: “it doesn’t work.”
And with very good reason, as I
found when I opened the case. It was
another case of a broken crystal lead,
only this time the break was so close
to the case that there was no chance
of salvaging it. Fortunately, a scrabble
through the junk box produced another such unit from which I was able to
retrieve a perfectly good crystal.
So it all looked like plain sailing.
I fitted the substi
tute crystal, put
everything back together, and gave it a
try. No joy. For a moment I wondered
whether I had tricked myself and fitted
another dud crystal.
But then I remembered the upside
down behaviour. Surely not another
one? But it was; I turned it over and
it worked, and when I turned it back
again it was dead. I could hardly
believe it. I fitted another LED and
that was it; its behaviour was back to
normal.
So there it is – mystery fault number
three. And that means there must be
some inherent fault in those LEDs. I
had hoped to make some attempt to
find out what it is but, as I mentioned
last month, the LEDs involved are
coated with an infrared filter which
excludes visible light and makes them
appear black.
My idea was to try to break one
open, with a minimum of force, in an
effort to preserve the electrodes and,
hopefully, reveal the fault. No such
luck. These things are not hollow, as
I had thought, but solid plastic.
But one final thought. With two
Fig.1: Der Fernbedienungstester RCT 5502 (ie, the remote control tester).
It carries a microphone (marked “US”), an infrared sensor (marked “IR”),
two LEDs (shown on the top of the case), & a 3.5mm socket on one side.
46 Silicon Chip
faults in this last unit, which came
first; which one prompted the customer to call me? We shall never know.
The main event
So much for that little preliminary
bout. The main event this month
concerns a Philips colour TV set, a
63cm model using the KL9A chassis.
This chassis first appeared about 1012 years ago and was used in a whole
range of sets. In many sets, it was
used in its basic form, without any
frills, but in this case it came with the
works: remote control, stereo sound
and Teletext.
The customer’s complaint came
in the form of a phone call along the
now familiar lines, “the remote control
doesn’t work.” So I said, “bring it in
and we’ll test it”.
At this stage, it may help the reader
to follow the story if I describe the test
unit I use for situations like this. It is
a commercial unit of German manufacture and carries the Konig brand
name (type number RCT 5502). As a
matter of interest, the German term for
remote control transmitter appears to
be “Fernbedienung”, so the name of
this device becomes “Fernbedienungs
tester” (I wonder if they play scrabble
in Germany!).
I understand that there is also at
least one locally made unit available.
This is carried by J. V. Tuners, 216
Canterbury Rd, Revesby, NSW 2212.
Phone (02) 774 1154.
The unit I have is basically a remote
control receiver, similar to that used
in TV sets but, for reasons which
will become apparent, is a good deal
simpler.
It is designed for use with both
infrared transmitters and the older
ultrasonic transmitters, being fitted
with both an IR photocell and a small
microphone. It is housed in a small
plastic case about 35mm wide, 25mm
thick and 120mm long. There is an on/
off switch on one side of the case, two
LEDs (one red & one green) on the top,
and a 3.5mm socket on the other side.
The red LED indicates that the power is on, while the green LED indicates
when pulses are being received from
the remote control. The 3.5mm socket
may be used to bring the pulses out
for checking on a frequency counter
or CRO. Power is supplied by a 9V
alkaline battery, while the internal
circuit consists of just four transistors
and a few minor components.
It’s all quite simple really but it
works very well. However, it is not
infallible.
Anyway, the customer brought in
his control unit and I put it through
its paces on the tester. This initially
involves setting up the remote control transmitter and the tester so that
they are about 150mm apart on a flat
surface. The tester is then switched
on and each of the transmitter buttons
pressed in turn. It is important to test
every button because only one or two
may be faulty. Many customers don’t
bother with such subtle points; to them
it is all summed up in the phrase, “it
doesn’t work.”
There were no such problems in this
case. Each button produced a response
from the green LED and I pronounced
the unit OK. Unfortunately, this wasn’t
the good news one might imagine
because it meant that the fault was in
the TV set. This would now have to
be brought in for service.
Fortunately, the customer had a
second set and he duly organised
delivery of the Philips set to the workshop. So, at the first opportunity, I put
it up on the bench for a preliminary
check. And this produced a surprise;
there were no channels programmed
into it.
This was rather strange, particularly
as the customer had not mentioned
it, but I considered that it might be a
byproduct of whatever fault there was
in the remote control section.
Anyway, I programmed the local
channels into it, just to get it working,
and this caused no problems. Nor did
there appear to be any problems with
the set’s overall behaviour; it was
first class. But, as the customer had
indicated, it would not respond to the
remote control.
No circuit
At this point, I fished out my circuit
of the KL9A but very quickly realised
that it was for the basic chassis only;
there was no remote control circuitry
in it. And that was about it for then;
there was little point in wasting time
working blind and so I rang Philips
and placed a manual on order. But I left the set running
on the bench for the rest of
the day, until I shut down
and pulled the main switch
for the night.
Next morning, when I
pushed in the main switch,
everything came up as normal except for the Philips set.
All it produced was snow and
noise. It didn’t take long to
confirm that all the channels
I had programmed into its
memory the day before had
been lost.
Fortunately, the reason
wasn’t hard to find. This set
uses a nicad battery backup
for the memory, designated
as part No. 1675. And since
it was the original, it was not
surprising that it had failed
after about 12 years.
I rang the customer and
explained that I would have
to wait on a manual before I
could fix the remote control
problem. At the same time, I
took the opportunity to point
out the additional problem with the
channel memory system.
He was quite understanding about
any delay caused by the manual. And
when I mentioned the memory loss
his reaction was immediate. “Oh yes,
I forgot to mention that – it’s all right
as long as I leave the power point on
but it loses it if I turn it off”.
Well, that figured; the channels had
been lost when he unplugged the set
to bring it in. But at least I could go
ahead with this problem. In greater
detail, the battery is a 2.4V 110mAh
type, about 7mm in diameter and
30mm long. It was readily available
from one of my regular parts suppliers
and, after fitting it, we had no more
memory problems. With luck, it might
last another 12 years.
I now had to solve the problem
with the remote control. Eventually, the manual arrived and, after
some confusion due to the fact that
it contains two different versions
of the circuit, I was finally able to
tackle the job.
The relevant part of the circuit is
reproduced here – see Fig.2. It shows
the IR receiver (part 1725) and a couple
of voltages and waveforms. I decided
to start by checking the voltages.
The two points involved were 3C1
March 1995 47
Fig.2: the IR receiver circuitry in the Philips KL9A. The incoming pulses from the transmitter are processed by the
IR receiver at extreme left & then fed to the base of a BC548 transistor via a 1µF capacitor. The resulting signal on
the emitter of this transistor in then fed via a 10kΩ resistor to pin 13 of the data processor IC at right.
and 2C1 on the IR receiver. And, in a
moment of carelessness, I neglected to
observe the polarity signs at these two
points, assuming instead that the 5V
marking indicated two separate rails,
each at 5V with respect to chassis.
The habit of measuring all voltages to
chassis is strongly ingrained but it is
not always the right thing to do.
I woke up to this very quickly but,
by a strange twist of fate, both points
measured very close to 5V with respect
to chassis. In practice, of course, the
5V is supposed to be read between
2C1 and 3C1, with 2C1 being at 5V
with respect to chassis and 3C1 being
at 10V with respect to chassis.
Or that was how it was supposed to
be. But 3C1 was not at 10V; instead,
it was almost exactly at 5V, so there
was virtually no voltage between the
two points. By now, having realised
my mistake and analysed the circuit
correctly, I realised that there was
something amiss around 3C1.
The easiest thing to do was to pull
the 3-pin plug to the IR receiver,
whereupon the 3C1 supply line from
the main part of the circuit jumped to
10V. Pushing the plug back in again
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pulled it back down to around 5V,
which suggested a fault in the IR receiver module.
The IR receiver
I pulled the entire IR receiver out
for a closer look. It is housed in a
small but substantial aluminium box
and consists of a PC board carrying a
16-pin IC, an IR photodiode, a couple
of coils, and a few other components.
I quickly concluded that there was
little point in thinking about repairs.
There was no circuit available and, as
far as I could determine, the IC wasn’t
This photo shows the IR receiver board after it has been slid out of its metal
case. The IR photodiode is on the board at right, while the 3-pin socket is at left.
Note the IR lens on the end of the case.
available as a separate item.
Trying to troubleshoot a problem in
these circumstances can be very risky.
One can waste hours, only to finish
up being unable to repair it anyway.
The only logical answer was a new
receiver.
And that posed a whole new set of
questions. Was a replacement readily
available? What would it cost? And,
most importantly, would the customer
want to incur such cost?
While I was fairly confident that a
replacement would be available, the
cost was another matter. Receivers
for other brands retail from $25 to $50
and I had a gut feeling that the higher
figure would be the place to start from.
I rang the customer and explained
the situation. Naturally, he wanted
some idea as to what it was all going
to cost. I went over the cost of the work
already done, added my estimate of
the receiver price plus labour, and we
came up with a guesstimate of between
$150 and $200. Did he consider it
worthwhile to go this far? Yes, he did
– I should go ahead.
And so I contacted Philips. Yes,
the receiver was avail
able and my
gut feeling was not far out; the retail
price I should charge my customer was
$75. Since this kept the overall cost
within my guesstimate, I went ahead
and ordered it.
It duly arrived and, at the first opportunity, I set about fitting it. This
took no more than a few minutes work
but when I gave it a trial run, it simply
would not respond to the remote unit.
So much for my optimistic “she’ll be
right now mate” attitude! She wasn’t
right at all.
All kinds of horrible possibilities
raced through my mind. Had I fouled
up the receiver installation, which
seemed so straightforward? Was it a
modified receiver design, unsuitable
for a set of this age? Was it a much
more subtle fault, somewhere in the
bowels of the set itself? Was the fault
really in the transmitter, in spite of my
previous tests? And had I invested unnecessarily in a replacement receiver,
which would sit in my stock for years
to come?
When the panic subsided, I decided
that the first two thoughts were the
least likely, so I concentrated on the
possibility of a fault in the set. The
first step was to check the rail voltages
at 2C1 and 3C1. These now measured
5V and 10V respectively, exactly as
marked on the circuit.
Next I turned to the CRO. The circuit
shows a waveform coming out of the
receiver at terminal 1C1. The circuit
depicts square wave pulses with an
amplitude of 5V but, unfortunately,
there is no indication as to the frequency of these pulses, nor is there any
other data on the coding used.
Anyway, this was the first check
point. And on the basis of the limited
information in the manual, everything
appeared to be OK at this point. From
there, the signal goes via a 1µF electro
lytic capacitor to the base of a BC548
transistor. The resulting signal on
the emitter of this transistor is then
fed via a 10kΩ resistor to pin 13 of
the data processor IC, where another
waveform is shown. This is similar
to the first but with a slightly lower
(4V) amplitude.
I traced the signal along this path
and finished up with the correct
waveform at pin 13, as shown on the
circuit. So pulses were coming out of
the remote transmitter, being picked
March 1995 49
up by the receiver, processed, and
passed to the data processor IC.
So why wouldn’t it work? The most
logical suggestion seemed to be a fault
in the data processor IC, which wasn’t
a very happy thought. From previous
experience, I tipped that it would
be quite expensive and that, in turn,
meant that the cost situation would be
getting out of hand.
But there were other factors to be
considered. How could I be absolutely sure it was that IC? Granted,
the evidence was strong but if I was
wrong, I would be down the drain for
an expensive IC.
What else could it be? One slim
possibility was the trans
mitter, in
spite of the tests I’d already made.
Remember that I said earlier that the
transmitter tester was not infallible.
Its weakness is that it can only confirm that pulses are being transmitted;
it has no way of confirming that they
have the correct coding sequence for
a particular set.
No gambling
So although the risk appeared to
be slight, I wasn’t prepared to gamble
the cost of an IC until I was absolutely
sure that the transmitter was clean.
Ideally, this could be confirmed by
acquiring another transmitter, perhaps
borrowed from a colleague if I was
lucky enough.
But first I decided to have a look
inside the transmitter for any clues
or obvious faults. A general once over
didn’t show up anything obvious,
such as dry joints or obviously faulty
components, and the voltages seemed
to be at least sensible, which was the
best I could do.
Next, I connected the CRO across
the crystal oscillator circuit and
confirmed that this was working
correctly. Its frequency was around
4MHz, which is similar to many other
systems. So it looked as though I had
drawn a blank.
And then the system suddenly came
good. Acting on an impulse, I pressed
one of the control buttons, whereupon
the receiver immediately responded.
I went through the whole range of
control functions and they all worked
perfectly.
The trouble was, I hadn’t a clue as
to why this had happened. I could
only assume that there was faulty
connection in the transmitter somewhere (perhaps the battery contacts),
which had come good as a result of
my prodding and probing. But, try as
I might, I couldn’t recreate the fault.
So I simply went over the board with
a hot iron and resoldered all the joints,
with particular attention to those
around the crystal oscillator circuit. I
didn’t find anything suspicious in the
process and the unit still functioned
in all modes afterwards.
By now, I imagine, some readers are
querying whether I goofed over the
receiver; was it really faulty, or had it
been a transmitter fault all the time?
Well, the same thought occurred
to me and I couldn’t rest until I had
plugged the old receiver back in. No
question; it pulled the 10V rail down
as before and simply wouldn’t work,
so that was the end of that theory.
Finally, after putting the system
through a week’s hard yakka, I returned the set to the customer with a
warning to contact me immediately if
the fault recurred. That all happened
nearly 12 months ago and the system
hasn’t missed a beat since. And what
did it cost? It all added up to $149, so
my initial estimate of $150-200 wasn’t
SC
too far out.
March 1995 51
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