This is only a preview of the October 1995 issue of Silicon Chip. You can view 27 of the 96 pages in the full issue, including the advertisments. For full access, purchase the issue for $10.00 or subscribe for access to the latest issues. Articles in this series:
Items relevant to "Build A Compact Geiger Counter":
Articles in this series:
Items relevant to "A Fast Charger For Nicad Batteries":
Articles in this series:
Articles in this series:
|
SERVICEMAN'S LOG
The view was fabulous, but ...
Yes, there’s usually a “but”, involving some
kind of a trade-off for what looks like a perfect
situation. In this case, a location with a fabulous
view exacted its own price in terms of appliance
reliability.
It really was a beautiful view. This
lady customer lives right on a beach
front and one would have thought that,
with paradise right on her doorstep,
she would hardly need a TV set. In fact,
she owned a very large double-ended
lowboy with an AWA-Mitsubishi
SC6341 AS630 chassis.
It was the size of the set that necessitated the house call. And I was
going to have to fix it in situ, because
I couldn’t move it unaided.
The problem was loss of vertical
scan, there being just a horizontal
line across the screen. I should have
realised from the state of the cabinet
veneer that the environment may have
been to blame.
When I removed the back, the cause
was obvious – salt air corrosion. All
the tinplate areas were rusty and
the aluminium was pitted. Also, the
horizontal output transformer didn’t
look long for this world, with a telltale
carbon track on the plastic.
But worse still was the state of a
lot of the small components, many of
which were green from copper oxide
Fig.1: the relevant section from the AWA-Mitsubishi SC6341 colour TV
set. The vertical oscillator section of IC201 is shown at top and this drives
the vertical output transistors (Q451 and Q452) at the bottom. The height
control, VR452, is to the left of Q452.
40 Silicon Chip
corrosion. Altogether, the long-term
reliability of the set looked very
poor and I informed the lady of this
prognosis. She asked me to see what
I could do.
This chassis is the stereo version of
the ML series and most of the deflection circuits are the same. The vertical
timebase is fairly simple in terms of
component numbers – a 48-pin IC
(IC201) carries the vertical oscillator
and drives the two output transistors
(Q451/Q452). The correct value of
11.4V was applied to pin 33 of the IC
but the collector of Q451 had 113V on
it, instead of around 65V, suggesting
the transistors were switched off and
not being driven.
Sometimes these circuits can be
difficult to service, as it is often a
chicken and egg situation, where
a fault in any sec
t ion, including
the feedback path, can stop it from
working. In this situation, it is hard
to know where to start, especially as
I didn’t have the CRO to turn to. But
as luck would have it, the problem
was fairly obvious from the state of
the height control (VR452) which was
badly corroded.
I tried to adjust it while watching
the screen. Impossible – the cabinet
was too large; I had to ask the lady
for some help. She was able to tell me
that the horizontal line had expanded
and was trying to fill the screen as I
adjusted the control; that is, until the
control disintegrated.
I replaced it and the picture was
restored. I then refitted the back and
was going through a final check when
I noticed that the stereo lights were
not on and the sound was in mono.
This was all I needed to remove the
back again.
This set uses the TDA3800G decoder and that was my initial suspect.
However, I had blamed this unit
unfairly on a previous occasion, so
I looked around for another possible
cause. The preset pots VR301, VR302
and VR303 caught my eye; they all
looked bad. But replacing them presented a problem because I didn’t have
any alignment equipment with me. I
took a punt and used an indelible felt
tip marker to mark the positions of
the wiper arms and then replaced all
three controls.
Fortunately, only VR302 and VR303
were the culprits and, by setting the
wipers at the same angle as the originals, full stereo sound was restored
and the LEDs were alight. I finally
emptied half a can of CRC 2-26 all over
the corroded areas and the horizontal
output transformer, then I wiped and
cleaned off the excess and dirt with
a cloth.
After replacing the back I had a word
with the lady on how best to protect
the set, at least for a while. I suggested
she move it away from the open window overlooking the sea and place it
as far as possible on the other side of
the room, or even in another room on
the other side of the house.
Also, I recommended that she cover
the set with a sheet, blanket, or even a
plastic tarp when she wasn’t watching
it, especially during any humid weather or when onshore winds prevailed.
She compromised by covering it with
a table cloth away from the window
and as far as I know it is still working,
six months later.
But, as I said earlier, there was a
price to pay for that fabulous view.
The red face
My next story involves a video
recorder that bounced. Anything that
bounces has the makings of a red face
situation and this was no exception.
But there is a twist to the story.
It started when a new lady customer brought a Philips VR6448/75
video recorder into the shop and
complained that it chewed the tape
on ejecting – sometimes. She added
that she used the machine a lot and
would appreciate it if I could fix it as
soon as possible.
It so happened I wasn’t particularly
busy that day, so I tackled it almost
immediately. The intermittent aspect
didn’t help. It took about 10 tries to
create the fault, whereupon it became
fairly obvious; the tape wasn’t being
fully wound back into the cassette
prior to unloading, leaving a length of
tape outside to be chewed up by the
ejecting action.
This turned out to be a partial failure
of the reel idler assembly. I removed
this, cleaned and tested it, replaced it,
and tested it again. I then checked the
idler shaft and found it to be sticking.
It didn’t respond to normal treatment and so I decided to fit a new idler
assembly and a set of belts and tyres.
This machine is made by Sharp and
so I rang the lady and quoted her on
the basis of Sharp replacement parts.
This worked out at $135.00 – $52.50
for the parts and $82.50 for labour. She
accepted quite happily and I told her it
would be ready that afternoon. I fitted
everything back in, cleaned the heads
and the machine generally, tested it,
and was quite confident that it was in
perfect condition.
The lady collected the machine later
October 1995 41
in the day, paid by cheque, and thank
ed me for being so prompt; another
satisfied customer, or so I thought.
A real blast
About three weeks later, I answered
the phone one morning and a bloke
identified himself as being from one
of the local TV stations. And without
waiting for any acknowledgement, he
let fly with “what sort of guarantee do
you give?”.
Then, again without waiting for an
answer, he went into a long diatribe
about how I had ripped him off and
that I didn’t know what I was doing.
What’s more, he demanded that I
should immediately call at his place
and fix his recorder properly. And
he added that the technicians at his
station could have fixed the recorder
properly at half the outrageous price
I had charged (I wondered why he
hadn’t used them).
I’m afraid the strength of his blast
caught me off guard and, initially,
I couldn’t get a word in edgeways
to even identify the recorder. I did
eventually and, of course, it was the
lady’s husband, But even then, it was
an effort to find out what the problem
was. All he would say was, “It’s doing
the same thing – it won’t eject” (which
wasn’t the same thing).
When he finally paused for breath
I told him that my warranty was 90
days for the parts I had used and for
my work; nothing else. I invited him
to bring the recorder back in and I
would look at it immediately. That
wasn’t good enough – I had to drive
out and fix it.
I baulked at that and repeated my
offer to check the machine but only in
my workshop. “Right”, he said, “I’m
going to go through you like a packet
of salts”. And he hung up.
The “packet of salts” took the form
of a call, shortly afterwards, from Consumer Affairs, acting on a complaint
from him that I wasn’t prepared to
fix his recorder. The C.A. man was
strictly neutral and listened politely
while I gave my side of the story and
explained that I would attend to the
matter as soon as the recorder was
brought back. He said he would relay
that to the complainant.
Another week went by, a somewhat
worrying period. No-one likes a repair
to bounce, for whatever reason. While
I was sure I had done a thorough job,
there is always the risk of something
being overlooked. But, try as I might,
I couldn’t think what.
Then he appeared, carrying the
recorder. He was a lot quieter now –
doubtless on the advice of the C.A.
man – and was even polite, in a very
reserved manner. I tried to be equally
polite. He offered to leave the recorder
with me and call back later. But I insisted that he wait while I examined
the machine in front of him, to which
he reluctantly agreed.
I plugged the recorder in and confirmed the nature of the fault; a cassette
was stuck inside and wouldn’t eject.
I could hear the motors trying to turn
but without result. It was clearly not
the original fault.
I removed the covers while he
watched and began to turn the eject
shaft gently by hand. And as the
cassette lifted clear of the deck floor I
experienced a wave of relief as I saw
the cause of the problem. And it was
simple enough for even the customer
to see and understand – a ballpoint
pen jammed underneath it.
Talk about a red face – his reserve
collapsed totally. To give him his due,
he did apologise and said he would
contact Consumer Affairs and put that
right. But he didn’t offer to pay for
having it fixed again. I had to realign
the ejector assembly with the loading
motor mode select switch, to restore
the correct sequence. And I tested it
to his satisfaction while he waited.
Technically, I could have charged
him again. But I wasn’t going to push
it – honour was satisfied.
J. L.’s video camera
And now, on a completely different
theme, I have a quite unusual story
from my southern colleague, J. L. of
42 Silicon Chip
Tasmania. Here’s how he tells it.
I’ve had a very interesting job over
the last few days. It was the sort of
job that usually goes only to specialist technicians, so I’ll tell it here as a
word of warning to others who might
get involved and as a gesture of thanks
to the highly skilled technicians who
helped me out of my trouble.
It concerned my own video camera,
a Panasonic model NV-MS4A. It’s a
full-size Super VHS camera, a big,
heavy thing that produces superb
pictures. Or at least, it did until my
son gave it a hefty thump while out
filming one day.
As far as he can recall the camera
was in its fitted case when the thump
occurred and there is no sign of damage on either the case or the camera.
But in fact, the camera had suffered
internally and would not work next
time he tried to shoot.
The deck would not load or unload a
tape but had stopped half way through
one or the other process. However,
it did eject the tape and a mangled
S-VHS cassette was the result.
Next day, I took it to the local Panasonic specialists for repair. I was over
optimistic because, as it turned out,
they had three weeks work on hand
and could not help me for at least
that long. And I needed it before that.
“Why not do it yourself?” they asked.
“You’ve done plenty of VCRs and this
is only a more compact version of the
same thing!”
Well, I had a manual for the camera
and they offered to make available
some vacant bench space and promised moral support, so I set to work.
First, I removed all the screws as
per the manual. There were about 17
of them altogether and I expected the
camera covers to more or less fall off.
Alas for my high hopes! I pulled and
tugged and pushed and prodded for
20 minutes but couldn’t get the thing
apart. I worked so hard that I feared
I might break the plastic panels but
nothing I could do would expose the
inside of the camera.
Then their senior camera technician
came over and said, “Here! What are
you doing? You’ll smash the thing,
handling it like that!” And with that,
he poked a small screwdriver in
through a couple of holes in the cover
and both sides simply fell off!
It seems that Panasonic designed
this camera to a “belts and braces”
standard. Not only are the covers
held on with lots of screws, they are
also held in place with plastic clips
moulded into the inside of each half
shell. Provision is made for pushing
the clips out of the way to release the
shells but no mention is made of this
in the manual.
You have to find out for yourself,
or be shown, where these clips are
before you can open the camera. One
could smash the thing to pieces trying to get it open but once the secret
is known, disassembly is quick and
almost painless.
Now that the mechanism was exposed, it was easy to see what had
happened. A pin on a lever, intended to ride in a groove on the master
cam, had jumped out and was sitting
jammed on the top surface of the cam.
It was easy enough to slip the pin back
into the groove but this left the mode
switch and mechanical timing way
out of place.
I struggled with gears and levers,
trying to get everything back into
position but I was getting nowhere.
The mechanical instructions in the
manual I was working from were written in excruciating Japanese English,
so I had to ask for help from one of
the other technicians. He is a better
interpreter than I (or else, he has been
through all this before) and he soon
had everything back into place and the
mechanism working properly.
I reassembled the camera, refitted
the covers and tested the unit to my
satisfaction. It was the first time I had
ever been inside a camcorder and I
came away thinking that it was not a
place in which I would like to spend
too much time. Apart from anything
else, my fingers are too thick and too
insensitive to handle the tiny parts.
K
ALEX
The UV People
ETCH TANKS
● Bubble Etch ● Circulating
LIGHT BOXES
● Portuvee 4 ● Portuvee 6
● Dual Level
TRIMMER
● Ideal
PCB DRILL
● Toyo HiSpeed
MATERIALS
● PC Board: Riston, Dynachem
● 3M Label/Panel Stock
● Dynamark: Metal, Plastic
✸ AUSTRALIA’S NO.1 STOCKIST ✸
K
ALEX
40 Wallis Ave, East Ivanhoe 3079.
Phone (03) 9497 3422, Fax (03) 9499 2381
TRANSFORMERS
• TOROIDAL
• CONVENTIONAL
• POWER • OUTPUT
• CURRENT • INVERTER
• PLUGPACKS
• CHOKES
It’s not fixed yet
Now, if you think that this is the
end of the story, you’re wrong. It’s
only just begun.
I used the camera that weekend and
shot some perfect footage. Then my
son took the camera on the Monday
and that evening complained that it
would not record in colour and had a
red line down the righthand side of the
picture. He felt it might be a physical
problem since the camera seemed to
work reasonably well when hand-held
but played up when mounted on the
tripod.
We soon found that we could make
the fault come and go by pressing
STOCK RANGE TOROIDALS
BEST PRICES
APPROVED TO AS 3108-1990
SPECIALS DESIGNED & MADE
15VA to 7.5kVA
Tortech Pty Ltd
24/31 Wentworth St, Greenacre 2190
Phone (02) 642 6003 Fax (02) 642 6127
October 1995 43
that suggested to him that this was a
delay line fault. As it turned out, he
wasn’t wrong.
I had quite a difficult job finding
the delay line. In fact, there are two
in the camera, one a 1H line and the
other a 2H. Neither looks anything like
a conventional TV delay line. The 1H
line is in an 8-pin IC package, similar
to but smaller than a 555 timer chip.
The 2H delay line looks like another
IC but is in a 16-pin package.
Once I had identified the delay lines,
I was able to examine them for signs
of dry joints. This was rather inconclusive since, under a strong glass, the
solder looked rather crystalline but no
more so than hundreds of other joints
on the board.
Still, I had been assured that at least
one of the 24 pins on these two chips
had to be loose, so I fitted the finest
point into my soldering iron and gave
each one a touch of heat. And that was
all it took. The fault disappeared and
has not returned.
I haven’t been able to learn if my
friend solved the problem using experience or theory. Chroma delay line
problems are so rare that I have never
had one in all my years of servicing
colour TV sets or video recorders.
They are not unknown, of course, but
are so unusual that few people build
up a fund of experience.
lightly on the side of the camera body,
in the vicinity of the main PCB. It was
as well that I’d learned the secret of
the plastic clips because I was going
to have the covers on and off many
times over the next few days.
With the main PCB exposed, I found
that the fault did indeed respond to
gentle pressure but only on one end of
the board. It was obviously a dry joint
but on a 100 x 150mm double sided
board, thickly coated with micro-miniature surface mount components, I
didn’t like my chances of finding it.
The fact that the fault seemed only
to affect the chroma circuits helped
to reduce the area of confusion but,
even so, it involved hundreds of tiny
components on both sides of the board.
I used a fine dental pick to gently
prod and poke all the components I
could identify as part of the chroma
circuitry. The PC patterns are given
in the manual but only the larger and
less crowded components are listed.
Dozens of chip resistors and capacitors
are simply not shown on the pattern,
44 Silicon Chip
which makes identifying the various
parts rather difficult.
Several times I poked at a component and the fault disappeared. Whenever it stayed “disappeared”, I hoped
that I might have cured the problem
by accident and so reassembled the
camera and gave it a test run.
This went on half a dozen times before I realised that, by myself, I would
never be able to solve the problem. In
the absence of more precise information about the exact nature of the fault
and therefore its physical location, I
could hunt forever and never track it
down. So it was back to my friends at
the service centre.
I played back some of the test tape
I had been running and their senior
technician said straight away “that’s a
delay line fault!” When I demonstrated
that it could be turned on and off by
pressing on the board, he opined that it
had to be a dry joint on one or another
of the delay line pins.
It seems that it was the red line
down the righthand side of the screen
Minor hassles
The job wasn’t quite over since I had
no end of trouble getting everything
back into place. I misaligned a 30-pin
plug and socket connector and had the
whole machine reassembled before I
found that the camera section wasn’t
working.
Then, when I fixed that, there was no
servo control because a 30-pin flexible
connector had slipped out of place.
Then the zoom lens wouldn’t work,
because I had somehow dislodged
its tiny 3-pin plug in the process of
replacing the side cover!
It’s been an interesting experience
but I have never been so pleased to
complete a job. I would never have
undertaken the task if the camera had
not been wanted urgently. I think my
friends at the service centre are entitled to every penny they make from
camera repairs.
Thanks, J. L., for a most interesting
and unusual story. It just goes to show
that you never know what you can do
SC
until you try.
|