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SERVICEMAN'S LOG
Some jobs aren’t worth the trouble
Some jobs really aren’t worth the trouble,
particularly if the equipment is old or if the
fault is intermittent. The trouble is, my
persistent nature often stops me from giving
up on jobs that have become uneconomic.
I thought that fixing Mr Hilda’s JVC
HR-D750EA VCR would be relatively
simple. His story was that he went
away on holidays and switched it off
when he left but when he came back,
it wouldn’t switch on straight away.
Instead, he could only get it to work
intermittently. Finally, it wouldn’t
start at all, giving only a “squeak”
and then nothing.
I quizzed him further and established that he was trying to get it to
start by switching it off and on using
the power point switch on the wall.
He wasn’t using the remote control or
the power switch on the front of the
VCR for this job.
To me, this all suggested that one
or more electrolytic capacitors had
gone leaky in this now 10-year-old
VCR, especially the start-up capacitor (which ever one it was) in the
switchmode power supply.
In this machine, the main section
of the power supply con
sists of a
separate module in a metal cage, in
the far righthand corner of the chassis.
The rest of the power supply is on
the main circuit board and consists
mostly of IC regulators. My initial
attention was drawn to a regulator
in the cage, which was fairly easy
to remove due to good access to the
printed side of the board.
The first thing I did was scrape
off the liberal quantities of corrosive
brown goo that had been applied to
both sides of the board. The component side proved to be a bit of a
nightmare as the parts were packed
tightly between various metal screens
and heatsinks.
That done, I examined the service
manual which is marked “switing
regurator”. Anyway, there were two
electrolytic capacitors on the primary
side of the switchmode transformer
(T1) that looked like the suspects I
was seeking. These were C14 1µF 50V
and C13 180µF 16V.
I could see that all the electrolytics had been replaced some years
previously but these two were now
well and truly dried out due to their
proximity to the heatsinks. I fitted
two new EXR 105°C capacitors, substituting a 220µF unit for the 180µF
capaci
tor and also increasing the
working voltage of both values. The
new capacitors were smaller than the
originals so this was straightforward.
By the way, the EXR range of
electrolytic capacitors is specially
designed for high-frequency switchmode power supplies. They have
very low impedance and low leakage,
typically around 4µA, which should
give extra long life.
The equivalent (effective) series
resistance, or ESR, of an electrolytic
capacitor defines its performance
and life; the lower it is, the better the
capacitor. An Australian engineer,
Sets Covered This Month
Fig.1: part of the switchmode power supply circuitry in the JVC HR-D750EA
VCR. There were several problems that prevented the supply from starting.
• JVC HR-D750EA VCR
• National TC1407 portable TV set
• National NV-H70A VCR
• Mitsubishi CT2584AS stereo TV set
March 2000 65
Serviceman’s Log – continued
Bob Parker, has designed an ESR
meter kit (available from Dick Smith
Electronics, Cat.K-7204) to measure
this. Having just bought and built one
of these, I was itching to give it a go.
The two capacitors I had taken out
both measured high impedance, the
180µF unit reading 44Ω and the 1µF
unit not reading at all. I had fitted an
additional buzzer circuit, designed
66 Silicon Chip
by Mark Stevenson, that gives an
audible sound if the capacitor is OK
(ie, below 1Ω) and a slight noise if it
is less than 10Ω.
While I was at it, I measured all
the remaining electrolytics in-circuit
with the ESR meter and the buzzer
indicated that they were OK, with
two or three giving the lesser noise,
(ie, possibly borderline). I then
resoldered any suspicious joints
before putting it all back together
and switching it on, confident that it
would work.
To my surprise, nothing happened.
However, I was still convinced it
was really an electrolytic capacitor
that was at fault, so I replaced the
three units that had given a doubtful
reading on the ESR meter. That didn’t
fix it either.
Finally, I took the advice of a colleague who always maintained that it
was quicker and more reliable to just
change the lot at one go. I did this,
replacing all 11 of them, and bombed
out again!
Next, I checked the high value
resistors R2, R3, R4, R7, R8 but still
no joy. I then checked the secondary
output rails for shorts and was finally
rewarded by finding that D25, a 39V
zener, was short circuit. But this still
did not fix the fault. To make matters
worse, I then introduced a red herring
by unplugging the power supply
from the VCR (in case the load was
too much).
This time the power supply finally
fired up and I had voltages on all the
rails. However, when I plugged it back
into the VCR, it died again and so I
checked for shorts on the main VCR
rails. Again, nothing was found – this
sorry tale was just too frustrating but
worse was to come. I reconnected the
two plugs while the power supply
was on – fairly risky, I know, but I
was desperate – and the whole video
burst into life!
I checked all the functions and
apart from lines across the screen in
playback mode, everything worked
fine, including the power on/off on
the set. But when I switched it off at
the power point and then back on, it
was dead again!
By now I was feeling considerably
older – I think my own electrolytics
were past their use-by date! The
only thing left I hadn’t tried was IC1
(STR1006), which I really doubted
could be the problem – but naturally
it was. It only has three transistors,
one zener and three resistors but it
was the culprit. My theory is that
the two original electrolytics failed,
causing the output voltages to rise.
And this in turn destroyed D25 and,
presumably, the zener diode in IC1.
But I still wasn’t out of the woods
– I still had the lines on playback,
although they slowly weakened, the
longer the set was on. From experience these are also usually caused
by faulty electrolytic capacitors, this
time on the 5V and 12V rails feed
ing the head amplifier. As a result, I
checked C802 to C807 with the ESR
meter and they all checked OK. The
ESR meter makes it so much quicker, as they can be checked in-circuit
and the meter was proving to be very
accurate.
It was then that I remembered a
previous repair I had done on a JVC
HR-D400EA with the same fault. After
a long saga, the fault had been traced
to the underside of a small soldered
metal shield on the main video board.
This shield conceals a patch of brown
goo which holds a 1kΩ resistor between pins 1 and 32 of IC102 (pin
3 being +5V Vcc and pin 1 9V Vss
(PB12V) for the MS6967RS 1H delay).
As before, removing the goo and
corrosion also removed the final problem. However, my persistence with
this job had been a little uneconomic
and I really should have drawn the
line sooner. I was, however, very impressed with the ESR meter and can
recommend it to you – good one, Bob!
National TV set
My next story involves a complete
change of scene. The local motel
brought in a National portable TV
set, complaining of horizontal white
lines across the picture but only on
Channel 7.
I wasn’t all that keen about repairing such an old (1984) chassis – a
TC1407 (M12H) – but was intrigued
by the symptoms. Initially, I suspected the CATV (cable antenna television
system) antenna used in the motel but
when I connected my own antenna to
the set, the same fault occurred. When
I tuned to Channel 7 there were bright
white horizontal retrace lines about
two thirds the way down the screen
from the top.
Because it was only on Channel 7, I
reasoned that this was because this is
the only channel transmitting Teletext
during the vertical flyback interval.
The motel owner, while appreciating that the set was over 15 years
old, was prepared to pay up to $100
to get it fixed. Apart from its current
problem, the set produced a good
picture and had been very reliable.
Well, how difficult could it be to
find a vertical blanking fault? Surely
this would be an easy $100, I foolish-
ly told myself. In fact, I still had an
original service manual for this set,
although the circuit diagram is a bit
of a mess and difficult to follow.
I discounted the AGC and IF stages
and concentrated my efforts on the
blanking circuit between IC401 (the
vertical output IC, AN5521), IC601
(the chroma decoder IC, AN5625) and
IC301 (the video output IC, AN5615).
By using an oscilloscope, I thought
that it wouldn’t take long too find
out where the blanking pulses disappeared. My assumption was that
it was probably a leaky electrolytic
capacitor somewhere that was causing the problem.
I started at pin 6 of the vertical
output IC (IC401) and measured
waveform 20, which is a 28V peakto-peak vertical pulse (the DC value
being 0.3V). This turned out to be spot
on. This pulse then goes through C416
and R424 where it joins the horizon
tal blanking pulse from pin 2 of the
horizontal output transform
er via
R553, C650, R678, R642 and D601.
The horizontal waveform (waveform 37) started out at 30V peakto-peak on pin 2 and is reduced to
about 9V on the anode of D601 but no
information on the waveform at this
point is supplied in the service manual. However, the 5ms vertical pulse,
embedded between the horizontal
pulses, was clearly visible.
Because I was expecting something
dramatic, I was rather perplexed to
find that this waveform reached pin
18 of IC601 and pin 11 of IC301 quite
correctly. This waveform (24) shows
the horizontal pulse as 6.2V p-p,
which was spot on at a DC voltage of
1.2V. The vertical pulse was still there
too, so where was the obvious fault?
In my notes of previous repairs, I
had recorded that a TC1408 (M12C)
had displayed the same symptoms
due to a faulty AN5615 (IC301). I
now felt sure this must also be the
culprit here so I changed IC301, then
IC601 and then IC401 – all without
result. Clutching at straws, I then replaced C414, C416, C420 and C650.
This made no difference either, so I
measured the resistors and diodes in
circuit and all read OK.
By now I was really frustrated –
by rights, I should have fixed this
supposedly simple fault and moved
onto another job. Unfortunately, I still
didn’t have a clue but I was determined that it wasn’t going to beat me.
My next theory was that perhaps
it was the width of the vertical pulse
that was the significant factor. An
hour later I abandoned this idea in
a bad temper, even though I could
vary the number of retrace lines by
carefully adjusting the vertical hold.
March 2000 67
Serviceman’s Log – continued
Fig.2: this circuit section for the National NV-G30 proved to an effective
substitute for a National NV-H70A. In particular, it allowed me to identify
transistors Q6005 and Q6006, both of which had been “cooked”.
I even changed IC501, the jungle IC
(AN5435) but the retrace lines were
still visible on Channel 7.
In the past, I have had similar
symptoms due to poor smoothing of
the 198V rail to the RGB outputs so
I replaced C556 (10µF 250V). When
that didn’t work, I checked the screen
volts but I was getting nowhere fast.
I had obviously overlooked something but I couldn’t think what it
was. All I could do now was go back
over what I had done and recheck
my work.
A previous fault I had encountered
with another set with no colour had
turned out to be a leaky diode (D602)
which had distorted the horizontal
pulses to the burst gate. I remembered that, at the time, I couldn’t
measure this in-circuit to determine
its leakage.
Therefore, I felt it would be a good
idea to measure D402, D601 and D602
out of circuit with the ohmmeter on
the 100kΩ range. And it was when I
measured D601 that I found the answer – there was significant reverse
leakage. Replacing it with a 1N4148
fixed the fault and the vertical pulse
on its cathode was double what it was
previously.
I richly deserved the $100 I charged
68 Silicon Chip
for this job but when will I ever learn?
National NV-H70A VCR
Mr Peterson’s ageing National NVH70A VCR came into the workshop
with the complaint that a tape was
stuck inside. He neglected to mention
that the set was otherwise dead but
on removing the covers the cause was
fairly obvious. F1102, a 2A fuse, was
open circuit on the UNREG 18V rail
that also supplies several other rails:
12V, 7.2V, 6V and 5V. Replacing the
fuse restored all functions and I could
do whatever I wanted with the tape.
Next, the phone rang and I had to
deal with an enquiry that took some
time. Suddenly, towards the end of
the conversation, I began to smell
burning.
I wound up the call as fast as I
could and started sniffing around for
the source. And when there is a lot
of electrical gear spread out and all
switched on, it can be hard to trace
the source of a smell. Fortunately it
didn’t take long to trace this one; it
was coming from Mr Peterson’s VCR!
Although it had been doing all its
tricks minutes earlier, the tape was
now firmly stuck inside and wouldn’t
budge. Sniffing carefully, I traced the
smell to two transistors on the right
hand side of the motherboard. These
had become so hot that they had un
soldered themselves and fallen out of
the PC board so that they were now
resting on the bottom of the cabinet
(the PC board is horizontal, with the
wiring pattern on the top and the
components underneath).
Pretty neat trick, I thought – at least
I wouldn’t have to unsolder them. But
that was the easy part. After scooping
them up, I was faced with the problem
of identifying them; they had been
carbonised and I didn’t have a circuit
diagram.
My approach was to find a similar
National Panasonic cir
c uit – one
with the same microprocessor chip
set used on the main CBA (Circuit
Board Assembly VEP03309). That
way, I would have a good chance of
identifying the transistors used.
The best substitute circuit I could
find was for the NV-G30 model. The
clue was IC6001, an MN15342VEB,
which is used in both units. And the
transistors in this part of the NV-G30
circuit, Q6005 and Q6006, turned out
to be 2SB790s, which are general-purpose PNP transistors.
Before replacing these, I checked
the circuit board for burn marks.
The two transistors are controlled
by the microprocessor, with Q6006
switching a regulated +12V rail via
the Record Safety Switch and Q6005
driven by pin 43 D-REC (Delayed
Record). Similarly, Q6008 is driven
by pin 42 DA-REC (Delayed Audio
Record).
Apart from the two transistors
there was no other apparent damage
so why did they get so hot and fail?
This wasn’t easy to deduce but with
the common denominator being the
regulated 12.3V supply, the source of
the problem had to be in the power
supply itself.
Access to the power supply is not
easy, with a lot of short leads and metalwork in the way. Once it was out, I
decided to adopt a blanket approach
and replace all 10 electrolytics with
EXR 105° types. It was a fiddly job but
most of the capacitors looked pretty
sorry anyway, especially C1101,
C1107 and C1104. Finally, I left it on
soak test and I’m pleased to report
that there were no more pyrotechnics.
Mr Peterson is once again a happy
man though I did advise him to get
a new one if it played up again. He
would be surprised how cheap they
are now compared with what he paid
some 13 years ago.
Mitsubishi stereo TV
Mr Crane requested a service call for
his 1992 59cm Mitsubishi CT2584AS
(ASV59S/AS2 stereo chassis), which
he said had an intermittent crackle in
the sound.
Initially, I was emphatic that an
intermittent fault would have to be
fixed in the workshop but he was
equally emphatic that it really wasn’t
intermittent and that because he was
76 years old, he couldn’t possibly get
it down the stairs of his duplex and
into his car to deliver it to me. I saw
his point and relented.
When I arrived the next afternoon, I
switched it on and sure enough, there
was a faint crackle on all channels. He
assured me that it was normally a lot
louder. I knew I was going to regret
it later but I decided to take a quick
look anyway, in the hope that I could
fix it on the spot.
I pulled the set away from the wall,
removed the back and started tapping
around, looking for a dry joint or a
bad connection. After a few minutes,
I emerged from behind the set having
achieved nothing except that when I
looked at the picture it was line tearing. “Oh yes”, said Mr Crane, “it does
that too sometimes”. I secretly sighed
with relief – I hated to think I might
have been held responsible for this
“new” problem. “Well”, I said authoritatively, “that settles that, I will have
to take it back to the workshop”. I lent
him a portable set and with immense
difficulty finally got his set into the
car and back to the workshop.
The set must have enjoyed the ride
because when I switched it on, all the
faults had cleared and the picture was
excellent. Such is life, I thought and
left it to soak test. The crackling in the
sound refused to come back but the
line tearing did occasionally.
I took the chassis out and reworked
the soldering for any potential dry
joints – there were none that were
significant. I also noticed that the
heatshrink tubing on some of the
electrolytics had peeled back. Initially, I replaced three capacitors in the
power supply secondary – C917 and
C453 on the 28V rail to the vertical
output IC (IC451) and C920 on the
15V input to the two 12V regulators
(IC902 & IC103). I also replaced C552
(1µF 160V) which connects to the line
driver Q551/T552.
The two significant capacitors were
C917 and C920 as they smelt “fishy”
when I unsoldered them. They had
spilt their electrolyte and this had
attacked the copper tracks on the
board. Anyway, this finally fixed the
line tearing but I didn’t know what to
do about the sound.
I left it on soak test for another
two weeks before Mr Crane finally
demanded I return it. Reluctantly, I
agreed but didn’t have much faith in
the long-term reliability of the set and
told him so.
The set bounces
As I expected, Mr Crane was back
on the phone just two months later to
let me know that didn’t last long. And
despite my previous explanations,
he seemed to think that it was all my
fault (which I also expected).
I called the next afternoon and
listened attentively to the elusive
crackle. This time I established that
it wasn’t due to interference from an
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external source. Instead, it sounded
as though it was due to arcing somewhere inside the set. With the speakers switched off I couldn’t hear it at
all but I thought it might have been
arcing internally inside the flyback
transformer or even the deflection
yoke and that the interference was
finding its way into the audio chain.
I disconnected the yoke momentarily and it wasn’t that. I also unplugged
the CRT socket in case it was arcing
inside the tube guns but it wasn’t from
that either. Finally, I decided that it
was the flyback transformer that was
the cause of the problem and told
Mr Crane that it would be expensive
to replace. It was time now for him
to put up or shut up. He decided to
invest in a new transformer.
It took the set back to the workshop
to wait for a new flyback transformer.
And although I had sounded confident, it was really only an intelligent
guess. I knew that if this didn’t fix it,
I would have to keep at it until I had
cracked it.
Finally the new part arrived. I unsoldered the old one using a solder
sucker but I ran into problems when
I tried to remove the EHT final anode/
ultor cap to the tube. The type of
rubber that Mitsubishi uses is quite
hard and resilient compared to others
and getting a screwdriver underneath
it was difficult. Then I had to push in
the side clips that hold it on to the
tube before one side came away and
I finally got it off.
The reason I had problems removing it was that it was extremely
rusty underneath, with heaps of fine
brown-red rust powder everywhere.
This mystified me, as there was absolutely no sign of rust or water damage
anywhere else but it got me thinking
– was this the cause of the invisible
arcing and crackling in the sound?
I cleaned up the rust with a wire
brush and CRC 2-26 and fitted the new
flyback transformer – I didn’t have the
time or patience to refit the old one
and because of the intermittent nature
of the fault, I felt that the result would
have been inconclusive.
As additional insurance, I replaced
all the electrolytics feeding the audio
output stages and reworked the sound
module. Once again I soak tested the
set before returning it to an anxious
Mr Crane. It is now over three months
since it went back so I feel confident
that it has really been fixed.
SC
March 2000 69
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