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Vintage Radio
By RODNEY CHAMPNESS, VK3UG
This Little Nipper was a dog
HMV’s “Little Nipper” was usually a reliable
and pleasant companion. However, I recently
had to restore one that was a real “dog’s
breakfast”.
H
MV used the name “Little Nipper”
for a popular line of mantel receivers made from the 1940s through to the
1960s - just as Astor used the name
“Mickey” for some of its receivers.
The line-up included many different
models in various formats, including
the 62-52 unit featured here.
Basically, the “Little Nipper” receivers came with either four or five
valves and were usually broadcast
band receivers only. However, some
dual-wave sets also carried the “Little
Nipper” name.
These sets were all “middle-of-theroad” in terms of quality, with good
performance and an attractive appearance. The various designs were well
thought out and they were generally
easy to work on.
Naturally, the circuit designs and
the appearance evolved as time went
by. The cabinets changed too, progressing from bakelite to plastic in the
later years.
Restoring A 62-52
A rather sad looking Model 62-52
Little Nipper was recently brought to
me for servicing. The owner didn’t
want me to do a complete restoration.
Instead, he would restore the cabinet
This view shows the Little Nipper receiver as it landed on my workbench. It
was dirty and fitted with the wrong knobs – and that was just the outside.
80 Silicon Chip
The original knobs fitted to the “Little
Nipper” had a tendency to break in
the centre.
and find suitable knobs himself (the
original knobs were either broken or
missing).
Unfortunately, the correct knobs
for these sets are rather hard to come
by and I had none spare. In use, they
often break in the centre but they can
be repaired using Araldite or a similar
epoxy adhesive. If any of the plastic
that normally surrounds the shaft is
left, a greased short length of shaft
from an old control can be sat in the
shaft groove. The trick is to make sure
it is vertical (as it would have been
originally) and before sitting the shaft
in place, score the plastic on the underside of the knob to give the Araldite
something to adhere to.
Most of the underside of the control
can then be filled with Araldite and
allowed to set. The shaft can then be
removed after the Araldite has set, as
the grease prevents it from adhering to
the shaft. The repaired knob will work
as good as new and will be stronger
than before.
To give even greater strength, a small
key ring can be slightly spread and
slid over the end of the knob’s shaft.
However, this will not be possible with
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the knobs from some sets, as the hole
through the receiver’s escutcheon may
only be slightly bigger than the knob’s
shaft extension. If necessary, the split
control shafts can be spread slightly
so that the knobs are a firm fit and
remain in place.
The process of repairing the knob
can be seen in the accompanying
photos.
Fortunately, this particular set
hadn’t had a rough life, with the knobs
being the only obvious casualties over
its lifetime. The cabinet was given a
quick clean-up to make it a little more
presentable and to make the set more
pleasant to work on but it certainly
wasn’t a full restoration.
Getting it working
According to the owner, the set
wasn’t working because the power
transformer had “burnt out”. I had one
spare, so if that was all that was wrong
with it, getting it working again would
not be difficult.
Fig.1 shows the circuit details of the
set. Note, however, that this is actually
the circuit for a 61-51 but it’s virtually
identical to the 62-52.
Because there was no smell of burnt
insulation, I wondered if the transformer really had failed.” As a result,
my first step was to test the transformer for any insulation breakdown
using a 1000V insulation tester. This
showed that there was a least 200MΩ
of resistance between each of the three
windings and transformer frame.
The only other thing likely was
shorted turns in one of the windings.
To check this, the rectifier was first
removed and the set connected to
power and switched on. The voltage
between each end of the high-voltage
winding and earth was then measured.
They were within a volt or two of each
other at around 350VAC, which is to
be expected with no load.
This meant that the high-voltage
secondary winding was probably OK.
In addition, the dial lamps were alight
and the voltage across the filament line
was around 6.8V, which was quite reasonable as both secondary windings
were lightly loaded.
What if the primary had shorted
turns? In that case, the secondary
voltages would probably have been
higher than they were. In addition,
the smell of burning insulation would
have been evident and the transformer
would probably have been making a
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The layout on the top of the chassis is uncluttered, so access to individual parts
is easy. It’s just as well, because this set had more faults than you could imagine.
This is the under-chassis view before restoration. The 2-core mains flex was
later replaced with a 3-core cord, so that the chassis could be earthed.
“fizzing” noise. There may even be
wisps of smoke but none of these
symptoms was evident.
As a result, I left the set run like
this for several minutes and the transformer showed absolutely no sign of
heating. It just went about its job with
no fuss, so all was apparently well.
It was at this point that one of the
dial lamps suddenly decided to go
out. It was easily fixed – the lamp
had come loose in its socket and
tightening it immediately fixed this
intermittent fault.
Finding an HT short
It was now time to look further into
the set and try to discover why the
owner thought that the transformer
had burnt out. My first step here was
to switch the set off and check the
resistance of the HT line to earth – it
measured just 80Ω which, for all practical purposes, is nearly a dead short!
I then checked electrolytic capacitor
C21 on the output of the rectifier but
it was OK, so I set about isolating everything at that point (with the rectifier
still removed).
It didn’t take long to discover the
problem – when I lifted the speaker
transformer clear of the chassis, the
short disappeared. A quick check
with a multimeter showed that it had
a low-resistance short from its primary
winding to the frame. So this was the
“burnt out” transformer.
Obviously, a replacement transformer was needed, so I rummaged through
my collection of speaker transformers.
September 2004 81
The Araldite is “poured” into the
underside of the control knob, while
the keyring prevents the centre boss
from breaking again.
The control knobs can usually be repaired using Araldite (or a similar epoxy
adhesive), a small key ring and a scrounged (greased) control shaft. The control
shaft is removed after the Araldite has set.
Unfortunately, I couldn’t find one with
a 7000Ω to 3.5Ω impedance ratio that
was small enough to fit into the available space.
In the end, I used a transformer
with a 5000Ω to 3.5Ω impedance ratio and installed a small resistance in
series with the secondary. This gave
an ideal match to the audio output
stage, although the total audio output
to the speaker would be reduced by a
few percent.
By the way, please note that for safety reasons, all sets should be switched
off and the power lead removed from
the power point before doing any
work on the circuitry; eg, soldering or
desoldering leads, etc.
Disintegrating valve socket
During the course of my investiga-
tions, the four leads from of the speaker
transformer had to be disconnected (by
desoldering them). Three came off as
expected but the fourth which went to
the plate of the 6M5 valve just came
out of the socket. In fact, the whole
wafer socket just disintegrated, which
is something I haven’t seen before.
This meant that before I could wire
in the new transformer, I had to replace
the valve socket. To avoid errors later
on, I drew a diagram of the wiring
before removing the wrecked socket
by drilling out its retaining rivets and
replacing it with a moulded insulation type.
The only problem was that when I
went to fit the new socket, I found that
the mounting holes were in different
positions relative to the valve pins
as compared to the previous socket.
These are just some
of the parts that were
replaced in the set. It’s
a good idea to replace
paper capacitors as a
matter of course.
82 Silicon Chip
This problem was solved by cleaning
the chassis and then soldering the
mounting lugs in the new position, so
that the socket pins were in the same
place as before.
The leads from the valve were then
resoldered to the socket except that I
made one small modification. Originally, pin 6 of the 6M5 was connected
to chassis. This pin is shown as an
“Internal Connection” in the valve
data books, which means that it may
be used as a support for various elements within the valve. As a result,
it should be left free even though
nothing was connected to it with this
particular 6M5.
A replacement valve might have
something connected to it, however
– such as the plate!
Testing resistors & capacitors
With all this completed, it was now
time to test the audio coupling and
AGC capacitors. The audio coupler
(C18) from the plate of the 6AV6 to
the grid of the 6M5 had no measurable
leakage but someone had previously
replaced it with one a tenth of the
correct value. This was replaced, as
were audio coupler C16 and the two
AGC capacitors (C3 and C9), which
were all leaky.
Note that in this circuit, C9 must
be replaced with the same value, as
it is part of a bridge neutralisation
circuit in the intermediate frequency
(IF) amplifier.
Moving on to the resistors, R7, R8,
R9 and R13 had all gone high and
were way out of tolerance. They were
also replaced, so what was originally
supposed to be a simple servicing job
was becoming quite involved. And
I still hadn’t even turned it on with
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the rectifier in place to see how it
was going!
Switching on
Fig.1: the “Little Nipper” is a fairly conventional 5-valve superhet.
It was time for the smoke test but
before switching on, I removed the
6M5 and inserted the 6X4 rectifier
into its socket. That done, I checked
for a short-circuit between the HT
line and earth. This was necessary
because it was possible for the 6X4 to
have a filament to cathode short after
being subjected to output transformer
short circuit. There was no short with
the valve cold, so I gingerly turned
the set on and checked the voltages
in the set.
The DC voltages all came up as they
should and the 6X4 was apparently
none the worse for the savage overload
it had experienced.
By the way, early 6M5 valves experienced silver migration between
pins 1 and 2 of the valve after some
use, which causes a positive voltage
to appear on the grid. To overcome
this, I lightly scored the glass with a
sharp scriber between these two pins
to break up any silver film between
them (in fact, I always do this whether
there is a problem or not). That done, I
plugged the 6M5 valve into its socket
but there were immediate problems.
The set came on with a howl and was
whistling, even with the volume control turned down.
The whistling 6M5
So what was wrong? The output
stage (6M5) has negative feedback applied from the secondary of the speaker transformer via C22. Of course, it is
necessary to wire the transformer so
that the feedback is negative but I’d
managed to get positive feedback! This
was easily fixed - all I had to do was
swap the two leads on the secondary
of the transformer.
That done, the audio amplifier stage
was stable, although it appeared to
have some hum. And it still had annoying crackles and some hiss (but
no stations) when the volume control
was turned up.
I tried moving the valves in their
sockets and this made the crackling
worse so it appeared that the socket
contacts were causing problems. It was
time to turn the set off and clean and
tighten the valve socket pins.
The pins were cleaned with “Inox”
lubricant, after which a sharp “modified” screwdriver was pushed in
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alongside each socket pin and the
two sides levered closer together. The
valves were then re-inserted and the
set turned on again.
That stopped the valves from making extra noises when they were
moved but it wasn’t the complete cure
- the set was still full of “crackles”.
I then tried tapping around various
parts of the set with the plastic handle
of a small screwdriver and this caused
the crackling to vary in intensity, espeSeptember 2004 83
Photo Gallery: 1933 Essenay M447
Produced by the Essenay Manufacturing Company Pty Ltd in 1933,
this compact wooden receiver was fitted with five valves and tuned
the medium-wave broadcast band. A feature of the cabinet was the
ornate speaker opening and the “peep-hole” dial. The valve line-up
was as follows: 57 autodyne mixer, 58 IF amplifier, 57 anode bend
detector, 2A5 audio output, and 80 rectifier. Photo: Historical Radio
Society of Australia, Inc.
cially when I tapped around the first
IF transformer.
Fun in the IF amplifier
To diagnose this problem, I first fed
a high-level tone-modulated 455kHz
signal into the antenna terminal. This
gave some output from the speaker,
which varied with the tapping. Using
a digital multimeter, I then measured
the voltage across C9 and initially it
was negative. However, after running
the set for a few minutes, it gradually
increased to 0V and then started to
climb in a positive direction.
During this time, the output variations seemed to remain consistent and
the output from the detector was still
negative. Thinking that there must be
some leakage resistance between the
two windings in the IF transformer
which occurred as the set warmed up,
I disconnected the secondary winding
and checked for leakage using a highvoltage tester. However, even with
84 Silicon Chip
the high-voltage tester applying 500V
between the two windings, no measurable resistance was observed.
With the transformer rewired into
circuit, my next step was to check the
valve itself. A new 6BA6 was fitted
and that fixed the positive grid voltage problem, so the original 6BA6 was
faulty (gassy maybe?). The IF amplifier
was now amplifying as it should but
the crackling was still quite evident.
A new 6BE6 frequency changer enabled the set to now tune stations. However, it didn’t fix the crackling and the
set would even occasionally “jump”
off station. I initially thought that this
might be due to poor contacts between
the moving surfaces of the tuning gang,
thus causing the frequency to jump.
Unfortunately, lubricating these made
no difference so I checked to see if the
gang plates were shorting.
At first glance, they didn’t appear
to be, so I put a strong light in line
with the tuning gang vanes and looked
through the gangs from the other side.
This showed that two plates were
probably shorting so I carefully bent
one away from its neighbour which
gave some improvement.
Closer inspection then revealed that
some of the other plates were close
(perhaps too close) to their neighbours
as well. To check this, I disconnected
the tuning gang from all other parts
of the circuit (including the trimmer
capacitors) and connected a highvoltage tester set to the 1000V volt
range across each gang section in turn
and rotated the tuning shaft. As I rotated the shaft, there were occasional
“flickers” in the reading, indicating
where the shorts were.
A little more judicious bending of
the plates finally cured the crackles
problem once and for all.
However, that wasn’t the end of the
story as the frequency jump problem
was still occurring. I’d checked all the
soldered joints and the moving points
on the tuning gang and all appeared to
be in good order, so the problem wasn’t
here. I even swapped the 6BE6 but it
made no difference, so I took a close
look at the oscillator circuit.
Sleuthing the oscillator
It was about this time that the crackles also reappeared. Obviously, there
was a problem with the oscillator
circuit but which component could
be causing it?
L3, C4 and TC2/VC2 are all frequency determining components, so
this was they obvious place to start.
TC2 and VC2 had been previously
attended to, so I assumed they were
OK. C4, however, consisted of two
mica capacitors in parallel, one a
much larger than the other. Perhaps
the low value one was intermittently
going open circuit, thus causing the
oscillator to change frequency?
I removed the capacitor and checked
it using both a capacitance meter and
the high-voltage tester but it checked
OK. In addition, a substitute capacitor made no difference, so padder
capacitor C4 was OK. So much for
that theory!
Coil L3 was my next suspect – perhaps it had an intermittent 1-turn short
circuit in the winding?
A multimeter test was inconclusive
but pulling the coil out, I decided to
check R2 and C5. These components
are not part of the tuned circuit but
they do have an effect on the oscillator
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frequency to a small degree.
R2 was in tolerance and even with
the multimeter and showed no variation in resistance over time. Similarly,
C5 tested OK for capacitance (50pF)
and no leakage resistance was detected
using a digital multimeter.
However, C5 was a different story
when tested on the 500V range of the
high voltage tester. This showed a
leakage resistance of about one megohm , with the meter needle regularly
flickering slightly. Eureka! - the rotten
little beast tested OK on all bar the high
voltage tester, so you can understand
why I consider this an essential item
of test equipment.
I have had very few faulty mica capacitors in receivers but when they do
become faulty, some weird symptoms
can appear. A noisy oscillator, as in
this case, can give some very misleading symptoms.
Alignment
Having cured the circuit faults, the
next step was to align the IF amplifier,
antenna and oscillator circuits. This
was done using a signal generator and
this showed that the IF amplifier was
well out of alignment. It responded
well to adjustment but in the course
of endeavouring to lock one of the
cores with core-locking compound,
it shattered at the end of the adjustment slot. As a result, the alignment
was completed with one core slightly
out of tune.
Despite all my “playing around”
with the oscillator circuit, it was almost perfectly aligned, with the stations appearing on the correct spots.
Well at least something went right with
the overhaul!
Improving the hum
From the very beginning, this set
had exhibited a background hum, even
with the volume control turned right
down. My first suspects were filter
capacitors C17 and C21 in the power
supply. They were both down slightly
at 14µF but not enough to warrant
replacement. However, I found that I
could reduce the background hum by
paralleling these two capacitors with
similar values.
The real cure lay in modifying the
plate circuit of the 6AV6. This was
made similar to other many older
receivers by adding a 33kΩ resistor
in series with the bottom end of R8
and installing a 1µF 350V electrolytic
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capacitor from the junction of these
two resistors to earth.
This simple modification cleared
the hum up nicely. It appears that
the ripple filtering circuitry in many
later receivers was the minimum that
manufacturers thought that they could
get away with.
A microphonic valve
The “Little Nipper” receiver was
now running quite well. It was sensitive, stable, the audio sounded good
and there was virtually no hum.
As a final check, I decided to test the
valves by gently tapping them with the
plastic handle of a small screwdriver.
All went well until I tapped the 6AV6,
which then squealed and crackled.
This is not an uncommon fault in
valves. In this case, one of the grid
welds had probably come loose, causing the valve to become very microphonic. What’s more, as the grid wire
scratched against the failed weld, it
became “crackly” as well. A new valve
soon fixed the problem.
Power lead
Before starting work on this set, I
had attached an earthed lead to the
chassis as a safety measure (eg, in case
the power transformer developed a
short to chassis). With the restoration
work now completed, the final job was
to fit a 3-core power lead, since there’s
no longer a risk of it getting marked on
a dirty work bench.
A 3-metre 3-core extension lead can
be used as the new lead. These extension leads can be obtained for around
$3-4. You simply cut off the socket and
wire the lead into the set.
Note that the power leads in most
radios from the valve era were knotted
where they left the chassis, to prevent
the cord from being pulled out. Today
the lead should be clamped into position, for legal and safety reasons.
An even cheaper proposition than
using a modified extension lead, is to
scrounge a lead from a defunct electrical appliance (provided it is in good
condition). Of course, if you keep a
clean workbench, the cord can be
replaced at the start of the restoration.
Summary
The “Little Nipper” 62-52 is a typical 5-valve mantel set from the 1950s
and 1960s. It is easy to work on, is a
good performer and generally gives
little trouble.
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However, there is the occasional set
from any make that proves to be a real
“dog” and it requires all the restorers knowledge and patience to get it
working properly. A set like this one
will be a severe test for a newcomer
to electronic restoration.
The important thing is not to go
“bush-ranging” through a set, replacing parts willy-nilly, as the results are
usually disappointing. Don’t give up
and if possible enlist the aid of someone more experienced than yourself if
you get a “dog” like this one. That way,
SC
you can share the headache!
September 2004 85
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