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Vintage Radio
By RODNEY CHAMPNESS, VK3UG
The Harbros 12/54B transceiver
Designed specifically for rural fire brigade
networks in the early 1950s, the Harbros 12/54B
transceiver was a 12-valve unit with some
interesting design features. It superseded armysurplus transceivers that had been adapted for
the job and was much easier to operate.
FS6 and many other ex-service sets
did require changes, as their transmitting frequencies were controlled only
by a VFO. The Postmaster Generals
Department required the transmitters
to be crystal-controlled, which meant
they had to be modified and submitted
for approval.
By the end of World War 2, the
value of radio communications was
apparent and returned servicemen
from country areas quickly realised
that 2-way radio could help coordinate
fire-fighting activities. Not only would
it make such activities more effective
but it would ensure greater safety for
firefighters as well.
At that time, here were many thousands of high-frequency (HF) portable
transceivers available on the military
surplus market at very moderate
Although army-surplus transceivers
worked well in these roles, they did
have their disadvantages. Generally,
they were quite bulky and heavy, were
often difficult to service and could
often only be operated effectively by
someone with technical knowledge.
They also usually had limited power
outputs while at the same time drawing high currents when operated from
a vehicle battery.
That list of negatives didn’t prevent
the sets from being used for fire-brigade or fishing fleet communications
though. When you have nothing else
to use, you will work around any
problems you encounter – which
the various operators and networks
did with considerable success. More
suitable commercial transceivers were
rare and costly at that time.
As the supply of cheap armysurplus equipment gradually dried
up, manufacturers began releasing
commercial HF transceivers to
meet the increasing demand for
equipment. Naturally, this new
equipment was manufactured
to meet specific requirements,
rather than being adaptations
of military equipment.
For example, some manufacturers concentrated on producing marine equipment, while
others concentrated on land-based
applications. One such company,
Hardinge Brothers of Horsham, Victoria, specialised in HF transceivers
for the rural fire-brigade networks
prices. As a result, transceivers such
as the FS6 and the 122 (described in
May 2003 and October 2003 respectively) were quickly pressed into
service on rural fire-brigade services.
In addition, many of these sets were
used by the Flying Doctor Service and
by fishing fleets.
The 122 required no modifications
to make it suitable for use in these
services, as it had both a variable-frequency oscillator (VFO) and a crystalcontrolled transmitter. However, the
The view shows the author’s fully restored unit. The cabinet was repainted
a hammer-tone green colour, which closely matches the original finish.
100 Silicon Chip
Disadvantages
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An under-chassis view of the Harbros 12/54B transceiver. The receiver circuitry is to the left, while the transmitter
circuit is to the right.
– mainly the Country Fire Authority
networks in Victoria.
The Harbros 12/54B
Hardinge Brothers produced domestic radios before the war, although
apparently only in limited quantities.
The company subsequently tooled up
for the production of HF transceivers
in the early 1950s and the first unit
produced (as far as I am aware) was the
11/53M – an 11-valve, single channel,
HF transceiver with an output power
of 5W. The “11” in the model number
refers to the number of valves used,
“53” to the year of initial production
and the “M” to the fact that it was
primarily a mobile transceiver.
The later 12/54B model is a 12-valve
unit (not including power supply
rectifiers), first manufactured in 1954.
It was primarily intended as a base
transceiver and is rather more versatile
than the 11/53M, as it could transmit
on three crystal-locked channels. The
receiver could tune continuously from
2-6MHz and also boasted two crystallocked channels.
The controls on this set are somewhat simpler to understand and use
siliconchip.com.au
compared to the ex-service equipment,
as the more critical transmitter tuning
controls are preset within the case.
In fact, there are only five controls
in all: (1) receiver audio level; (2)
receiver tuning (2-6MHz); (3) transmitter frequency selector; (4) receiver
variable tune or crystal-locked tuning
selection; and (5) noise limiter on/off.
The power on/off switch has three
positions: (1) 12 VDC; (2) off; and (3)
240 VAC mains.
The 12/54B transceiver was expected to operate on AC power most of the
time, with 12V DC operation included
as a back-up in case the base station
location lost mains power.
Receiver circuit
The receiver circuit (see Fig.1) is
similar to that used in many high-performance domestic receivers of the era.
A 6BA6 (V1) acts as a tuned RF stage
and this is followed by a 6AE8 (V2)
as a frequency converter. Although a
conventional oscillator circuit is used
for the variable tuning, two frequencycontrolling quartz crystals in a Pierce
oscillator circuit are used for fixedfrequency reception.
Next comes a 455kHz IF amplifier
based on a 6BA6 (V3) and this is then
followed by a 6N8 (V4) as the second
detector, AGC diode and first audio
amplifier. The audio from the detector then goes to a noise limiter which
uses a 6AL5 (V6) dual diode. This
stage limits impulse interference, after which the audio is fed to the 6N8
pentode section.
A 6AQ5 (V5) functions as the second
audio amplifier which in turn drives
the loudspeaker.
Transmitter circuit
The transmitter section uses six
valves in all (V7-V12). A Pierce crystal
oscillator based on a 6AQ5 (V11) and
three switch-selectable crystals sets
the carrier frequency, although only
two crystals were usually fitted to the
unit. For example, in the unit I have,
the crystal frequencies are 2692kHz
and 4510kHz. The third position was
left vacant, as licences were usually
only issued for two frequencies.
The output of the crystal oscillator
is applied to the grid of the RF (radio
frequency) power amplifier, which is
based on a 6L6G (V10). V10’s output
October 2005 101
is then coupled via a tuned circuit to
the antenna. This stage is tuned to suit
the crystal frequency by switching different values of capacitance in parallel
with the output coil.
In operation, the “loading” of the
transmitter is adjusted to give optimum output. This is achieved by
varying the position of a coupling coil
which is wound onto a former and
placed over the main tuned circuit
winding – see photo.
The modulator is a 3-stage device
based on valves V7-V9. V7 (a 6AU6)
is wired as a grounded-grid audio
amplifier, with a carbon microphone
in the cathode circuit. Its output is fed
to another 6AU6 (V8) connected as a
triode and this in turn feeds a 6L6G
(V9) modulator output valve.
The resulting audio signal from V9
modulates the RF signal via a centretapped audio choke. As shown, this is
wired into the plate circuit of V9 and
into the plate and screen circuits of
the RF output stage (V10).
V12 (6U5/6G5) functioned as a
magic-eye tuning indicator (to indicate
modulation).
Fig.1: this is the complete circuit
for the Harbros 12/54B transceiver,
minus the power supply. The 6-valve
receiver section is along the top,
with the 6-valve transmitter below.
PTT switch
102 Silicon Chip
The changeover from receive to
send is accomplished by pressing
the PTT (press-to-talk) button on the
unit’s Zephyr carbon microphone.
This actuates a 3-pole relay and one
set of contacts transfers the HT (hightension) voltage from the receiver to
the transmitter. At the same time,
a second set of contacts swaps the
antenna from the receiver to the transmitter, while the third set removes a
short circuit from the HT at V7 in the
modulator and shorts the loudspeaker
voice-coil to earth.
The last operation is necessary to
prevent acoustic howl from occurring
at the changeover from transmit to
receive and vice-versa. It occurs because the transmitter and the receiver
remain in operation for a fraction of a
second after a changeover, as the filter
capacitors in the supply rails take a
finite time to discharge after the HT
is removed.
Mechanical clean-up
The transceiver featured here had
been in continuous service from 1961
until the early 1970s, when the Country Fire Authority changed to VHF radio communications. It then ended up
in a garage at a coastal location, where
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the salt-laden air rusted the cabinets.
When I used an angle-grinder to clean
the rust off the lid, I found that it had
penetrated some distance underneath
the paint.
Fortunately, the transceiver and
power supply cabinets were in much
better condition. After removing the
circuitry, they were rubbed down with
fine sandpaper to remove any loose
paint and rust. The cabinets were then
cleaned down with turpentine and
given a coat of Wattyl Killrust metal
primer undercoat.
That done, I went looking for a
spray paint that would roughly match
the original green. Eventually, I came
across a hammer-tone metal finish
in Jade Green. This closely matches
the original hammer-tone finish so I
bought a can, even though it is rather
expensive. It is labelled as Galmet
metal protection and is easy to use.
Next, the knobs were removed and
cleaned by scrubbing them with a nail
brush dipped in soapy water. They
were then polished with an automotive cut and polish compound and now
look much brighter.
Next stop was the volume control.
This was extremely stiff to rotate, so
I sprayed Inox cleaner onto the shaft
and rotated it back and forth until it
operated freely. The valves were then
cleaned with soapy water, with only
gentle rubbing on the glass envelopes
to ensure the labelling remained in
place.
As a precaution, the octal valves
were all held upside down while this
work was being done, so that no water
could seep into the valve bases. This
isn’t necessary with the miniature
valves, since the valve pins emerge
directly through the glass envelope.
After that, it was a matter of attending to a few sundry details. The front
panel was cleaned with a kerosenesoaked rag, after which the dents were
removed from the speaker grill. The
grill was then resprayed with flat-black
paint and came up looking like new.
A kerosene-soaked rag was also
used to clean the top of the transceiver
chassis. I also replaced the 240V power
lead (it was starting to perish), cleaned
the microphone and adjusted the PTT
switch.
Servicing the power supply
A combined 240VAC and 12V vibrator power supply is used in these units.
and this one wasn’t without its probsiliconchip.com.au
The major components are neatly laid out on the top of the chassis. Power
comes from an external mains/vibrator supply.
lems. A quick inspection revealed that
the 2nF buffer capacitor in the vibrator
section had been overheating and had
leaked wax onto the bottom cover of
the power supply.
I initially checked the capacitor with
my 1000V tester and found it had a
leakage resistance of about 30MW. I
then decided to heat the capacitor with
a hair drier and observe the change (if
any) in its leakage resistance. When I
did this, its resistance quickly dropped
to just 1.5MW, so it was replaced immediately.
Unfortunately, I didn’t have a suitable high-voltage (2000V) 2nF capacitor so I made one up using three 8.2nF
630V polyester capacitors in series
across the secondary of the transformer. The higher resulting value (about
2.7nF) gives a lower standing current
with no load, so the transformer is better tuned than it was with the original
2nF capacitor. The voltage rating of
the three capacitors in series (about
1890V) is slightly lower than the rating of the original capacitor but this is
unlikely to cause problems.
The circuit shows the vibrator to be
a V6612 Oak unit. However, a V6606
is fitted with a 20W resistor in series
with the reed drive to drop the voltage
to around 6V. The drive voltage was
9V, so I changed the resistor to 56W
and the voltage is now much nearer
to what it should be.
The vibrator itself is not mounted in
a resilient-mount socket, so the noise
is quite noticeable when the unit is
operating. It probably really doesn’t
matter, as this is a communications
transceiver and the receiver is likely
to be used in an area where interference and general background noise is
present anyway.
The supply was also checked for any
shorts or low-resistance readings from
the high-tension (HT) line to chassis.
There were no problems here, so the
two 6X5GT rectifiers that had previously been removed were reinstalled.
The supply was then switched on and
the voltage across the filter capacitors carefully monitored. Then, after
a few seconds, the supply was turned
back off again, this cycle then being
repeated several times to reform the
electrolytic capacitors.
It really pays to be rather gentle with
6X5GT rectifiers, as they are prone to
develop short circuits from cathode
to filament if they are abused to any
extent. When I had finished overhauling the transceiver, I took the same
precautions with it, as it is on a separate
chassis to the power supply.
Overhauling the receiver
As is my usual procedure, I commenced overhauling the receiver section by testing the paper capacitors.
And I have to say that the units fitted
to this set would have to be the worst
batch I have come across.
October 2005 103
Photo Gallery: Kingsley Kit Set KFT-1
First marketed in Australia in 1946, this Kingsley receiver used “ferrotuning” to tune in stations (as opposed to the more conventional variablecapacitance tuning). This new system used a grooved brass spindle to
actuate sliding iron-dust cores inside the tuning coils, thus varying their
inductance. The set came with a colourful dial and circuits for three, four
and 5-valve models were available. The unit shown here is a 5-valve KFT1 medium-wave model using 6J8G, 6U7G, 6G8G, 6V6G and 5Y3G valves.
Ferrotuning never gained widespread popularity and such sets are now a
rarity. (Restored by Maxwell Johnson; photo by Ross Johnson).
They consisted mostly of miniature
AEE units (brown coloured) and their
leakage resistances varied between
1-10MW (as measured on a high-voltage
tester set to the 500V range). A couple
of these capacitors were also buried
under shielded audio cables and unless
you went looking for them, they could
have been easily missed.
I had no option but to replace the lot,
the only exceptions being the cathode
bypasses on several of the valves. In
the end, some 26 capacitors in total
were replaced in the receiver and
transmitter circuits.
The resistors were mostly 20%
tolerance types and most had gone
high by about 20%, so I didn’t need to
replace any. I also checked the speaker
transformer to make sure there was
This close-up view
shows the power
amplifier tank coil,
together with the
coupling coil which
has too many turns.
The roughly-wound
3-turn coil over the
tuned winding gives
better performance.
104 Silicon Chip
continuity across the primary winding
and this proved to be intact.
Once these checks had been completed, it was time to apply power.
I began by reforming the electrolytic
capacitors as described previously,
then let the receiver run. There wasn’t
so much as a peep out of it – it was
dead quiet.
It was time for some troubleshooting
and I started by checking the voltages
around the 6AQ5 output stage (V5).
This showed that the cathode voltage
was zero, which meant that no current
was being drawn by the valve.
I also measured the heater voltage
and found that there was 12V across
the valve socket instead of 6V. This
indicated that the heater had probably
gone open circuit.
I removed the valve and found that
the heater was intact, so I replaced it
again. It still wasn’t drawing current,
so I removed it again, re-tensioned the
socket pins and gave the socket a spray
with Inox lubricant. This time there
was some action and the receiver came
to life, although it was very noisy.
I tried wriggling the valve around
in its socket and this produced loud
crackles. After moving the valve
around for a while (to clean the contacts), these crackles disappeared – or
at least, they did for this stage. There
were still problems elsewhere.
Next, I tried moving the 6BA6 RF
stage (V1) around in its socket and
the same crackling problem occurred.
Its socket was also then sprayed with
cleaner and the pins re-tensioned before replacing the valve. And again, the
crackling problem disappeared.
The set was now sounding much
better, so I attached a signal generator to the receiver’s antenna, tuned
to one of the crystal-locked channels
and adjusted the generator for an
audible signal. The sensitivity was
poor, so I checked around the 6AE8
converter stage (V2) and cleaned the
frequency selector switch which was
also noisy.
This made no difference to the sensitivity so the 6AE8 was removed and
its socket also given the “treatment”.
This did improve the performance
but when I subsequently touched
the 6BA6 IF valve (V3), the crackling
became quite bad and the sensitivity
varied widely.
This valve was also removed and
its socket cleaned and tensioned, after
which the sensitivity improved quite
siliconchip.com.au
The power supply is housed in a separate box, with a front panel switch
used to select between mains or battery (12V DC) operation.
noticeably. I then checked the remaining valves and found that their sockets
all had bad contacts.
These were all given a good clean
up and the receiver was now turning
in a reasonable performance. All those
years spent in a salt-laden atmosphere
had certainly caused some problems.
Receiver alignment
At this stage, I decided that a quick
realignment of the receiver’s front-end
was the way to go.
First, I set the tuning to the 2692kHz
crystal-locked position and rotated the
receiver’s tuning dial until an increase
in sensitivity was observed. That done,
the signal generator was adjusted until
the signal was audible. I then peaked
the RF and aerial coils slugs for best
performance, after which the receiver
was switched to 4510kHz and the
signal generator and receiver tuning
again adjusted for best performance.
The aerial and RF coil trimmers were
then adjusted.
Unfortunately, the variable frequency oscillator adjustments did
not line up with the settings for best
reception on crystal-controlled operation. As a result, I set the receiver up
for best performance on the 2692kHz
crystal-locked position with the
signal generator, then switched to
the tunable position and adjusted
the oscillator slug until the 2692kHz
signal was heard. I then did the same
on 4510kHz, this time adjusting the
oscillator trimmer.
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The set now tunes quite well and
signals well below a microvolt are
readily heard. It really is quite a “hot”
receiver!
I didn’t touch the IF alignment, as
it appears to be perfectly OK. Note
that care is needed in tuning the IF of
a crystal-locked receiver, as just peaking the IF alignment may mean that
the receiver is no longer tuning the
frequency it is intended to tune.
For example, to tune to 2692kHz,
the receiver’s crystal oscillator must
operate at 3147kHz. That’s assuming
an IF of 455kHz (ie, 3147 - 2692 = 455).
However, if the IF was aligned to say
465kHz, the actual frequency that the
receiver would now tune would be
2682kHz (ie, 3147 - 465 = 2682).
At this stage, there was just one
remaining problem with the receiver
– the hum level was quite noticeable.
It became inaudible when the volume
control was reduced to zero and I subsequently found that better shielding
around the detector and noise limiter
(6AL5) improved the situation.
When the set is on vibrator supply,
there is noticeable vibrator hash and
the use of the noise limiter is desirable. It’s not the best noise limiter in
the world but it does work.
Overhauling the transmitter
Like the receiver, the transmitter had
many leaky AEE capacitors that had to
be replaced. And like the receiver, the
resistors were all OK but just within
tolerance.
Having replaced the capacitors, it
was time to test the transmitter into a
dummy load/power meter. I pressed
the button on the microphone and
adjusted the tuning capacitor on each
of the transmit frequencies but could
only get 5W output on 2692kHz and
3W on 4510kHz with 15W input –
pathetic!
My suspicion was that the link
coupling coil to the antenna had too
many turns on it (12). To test this,
I temporarily converted the output
circuit to a Pi coupler and the output
increased to 7W on 2692kHz to 8W on
4510kHz. I then experimented with
the link coupling coil and found that
three turns (instead of 12) resulted in
an output of 6W.
This was still rather pathetic, as
with 15W input to the V10 plate
circuit, the output should have been
around 10W. The rated input to the
transmitter is 20W but I wasn’t pushing it that hard with my temporary link
coupling system.
The transmitter output stage doesn’t
gain any accolades from me. The ratio
of the inductance and capacitance in
the tank circuit (PA output tuned circuit) is not correct across most of the
band to which it tunes. Furthermore,
the link coupling method used for
extracting the RF energy from of the
tank circuit doesn’t work efficiently
in these transmitters. In my opinion,
a better-designed output circuit would
achieve an efficiency of 60-65% in the
SC
PA circuit.
October 2005 105
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