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Vintage Radio
By Maurie Findlay, MIE Aust, VK2PW
Restoring The Hotpoint Bandmaster
J35DE console radio; Pt.2
Last month, we discussed the Hotpoint
Bandmaster J35DE in general terms. This
month, we describe how it was restored
to its original performance. The only
instrument required was an inexpensive
digital multimeter and the same general
ideas can be applied to most vintage sets.
M
ANY OF THE ARTICLES on
vintage radios in these columns
give some of the details of restoration
but rarely would a set which looks
potentially good on initial inspection
turn out to require so much work to
92 Silicon Chip
restore it to its original standard of operation. And while some people might
simply turn the set on and hope for the
best, that is not likely to be successful
in many cases.
The starting point with this set was
the power cord. It was originally fitted
with a twin-lead conductor power flex
which is not deemed safe these days,
especially when a 60-year old power
transformer is being used. It might be
OK for the present but that cannot be
guaranteed.
Accordingly, a 3-conductor flex
was fitted, with the chassis correctly
connected to mains earth for safety.
The power cord was securely anchored with an IP68 cable gland and
the green earth wire terminated to
the chassis with crimped lug, screw,
nut and lockwasher. This works well
although using a cable gland may not
be an approved method when it comes
to anchoring mains cords.
The next step was a resistance measurement of the primary of the power
transformer. Measured via the power
plug pins it was about 50Ω and from
the plug pins to the chassis it was a
large number of megohms. So that was
OK but the set has a double-pole rotary
power switch operated by one of the
front-panel knobs and it seemed very
tired. Turning the switch backwards
and forwards produced an occasional
flicker on the meter but not the original
50Ω reading. So it had to be replaced
but obtaining the same switch was
impossible.
A used switch potentiometer with
a double-pole switch rated at 240VAC
2A was found and fitted as a replacement but its shaft was too short. This
was extended using a short section
of shaft from another pot. They were
joined using a threaded bush from yet
another pot, the whole lot being glued
together with JB Weld epoxy adhesive.
Terminating wires to the switch was
yet another hurdle. The solder tags on
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the switch pot are of thin sheet metal
and not designed to take the strain
of stiff wires with mains insulation.
For this reason, the mains wires were
extended with flexible hook-up wire
which was in turn covered with thick
plastic tubing.
Fortunately, the original volume
control, which is separate from the
power switch, was quite usable.
Then we come to the valves. A natural tendency among these new to radio
restoration is to pull out the valves and
wipe away the dust and grime but this
can be a real trap since it is so easy
to clean off the label marking. Then
how do you identify them? Four of the
valves in this set are of similar size and
have no connection to a top cap, so it
would be easy to mix them up.
So before pulling any valves out of
the chassis, do a quick diagram showing the location of each valve and its
type. Then put a sticker on the base of
each valve and label it as well.
Turning the chassis upside down is
another hazard because it needs a rear
support to stop it from resting on one of
the IF transformers. A length of angle
bracket bolted to the back of the chassis
provided the necessary support.
Then we could have a detailed look
at the components underneath. One
manufacturer produced paper capacitors in a black plastic which melted
at soldering temperature. Servicemen
in the 1950s referred to them as the
“black death”. It was expected that
most of these would be leaky. Surprisingly though, most of the capacitors
were OK, both with regard to leakage
and capacitance, except for a couple
where the ends broke off when the
multimeter was connected!
Ultimately though, most of the paper
capacitors were replaced with modern
metallised polyester types (greencaps
etc) as the leads of the originals were
so fragile.
The resistors were carbon composition, most about 35mm long and 6mm
diameter, and were probably rated
at 1W dissipation. Measurements
showed that most of the resistors were
high in value, some by a factor of two
to one but the 325Ω V4 cathode resistor and the 50Ω resistor for the back
bias circuit measured both very close
to their marked values. They appeared
to be wirewound types.
Electrolytic capacitors
Electrolytic capacitors in old valve
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These faulty parts all had to be replaced in the old Hotpoint Bandmaster radio.
Most are capacitors but there are also quite a few resistors, a couple of dial
lamps and the 6J8G mixer valve.
This under-chassis view shows the radio after the above parts were replaced.
It’s normally fitted with a perforated steel cover.
radios usually have a high leakage or if
not, they have dried out and have low
capacitance. Still, replacements are
available from a number of suppliers.
In this particular case, the 4.7µF and
16µF capacitors were salvaged from
a junk box and reformed using the
electrolytic capacitor tester described
in the August and September 2010 issues of SILICON CHIP.
Resistance checks of the power
transformer high-tension secondary
and heater windings and the two
windings in each of the two IF transformers gave the expected readings,
being 400Ω for the HT, a low value
for the heater winding (since the valve
heaters are all in parallel) and about
10Ω for the IFs.
The broadcast-band (BC) aerial coil
primary checked out at about 30Ω
and the secondary (tuned winding) at
about 4Ω. The BC oscillator primary
and secondary both measured about
the same as the latter. Initially, the
shortwave coils were not checked.
Disintegrating wiring
A wire was removed from the 16µF
filter capacitor just to check for shorts
and its insulation disintegrated just as
the wire was moved. Quite a number
of other wires in the chassis looked as
though they would do the same.
So, the big decision had to be made.
Was it worth refurbishing the set to the
point where it would be reliable and
perform as it did originally? Having
August 2011 93
Some of the leads of the speaker transformer had broken off at the base. It was
repaired by digging away some of the pitch-like sealant, joining new leads to the
exposed wire ends and then resealing the unit.
proceeded this far, there could still be
other faults. For example, the tuning
slugs in the IF transformers might not
work, the rotary switch for BC/SW
selection could be intermittent and
so it goes on.
In all these cases the answer is as
follows: if you are prepared to spend
the money on components and hours
of fairly skilled work with a soldering iron, a multimeter and long-nose
pliers, and you regard the project as a
hobby, then it is worthwhile.
Components improved greatly in
the 1950s and many of the younger
radios that come up for refurbishment
would not have as many faults as this
Hotpoint. Hopefully, your set would
not require as much work.
A general tip: when working on
a radio that requires many hours of
concentration, don’t continue for more
than one or two hours without a rest. It
is very easy to make a mistake which
could be hard to find later.
In this set, many of the components
were soldered directly to the chassis
during manufacture. A large soldering
iron would be required to undo the
original connections. The way around
this is to cut the wire close to the component after which a new component
can be connected to the stub with a
normal soldering iron.
Modern components are almost
always smaller than vintage parts of
the same voltage rating (in the case of
capacitors) and power dissipation rating (in the case of resistors). So there is
a temptation to terminate the leads in
94 Silicon Chip
places different to the original. Don’t
do this. There are often cases where,
for example, a different earth termination point could lead to instability.
The original designer of the radio
would no doubt have spent a lot of
time determining the best component
connecting points.
The damaged wiring loom presented
real problems. There were cases where
a wire with damaged insulation was
bound up with other wires which
appeared OK. In those cases, it was
decided to leave the bad wire in place
and just cut off the ends. Binding the
new wire into the loom risked further
disturbing the crumbling insulation
so we tried to disturb it as little as
possible.
Keeping it original
Many restorers want to keep the
radio looking as original as possible.
In this case, we left the original electrolytic filter capacitors in place so that
the top the chassis looked the same.
However, it was just not practical to
make the inside of the chassis look
original since most of the components
have to be replaced in a relatively
small space.
No doubt the purists would be
aghast but taking the purist approach
would be far more time-consuming
and all for a result that no-one will see.
In particular, as shown on page 96 of
last month’s issue, the Hotpoint chassis has a screening panel underneath
which prevents you seeing inside unless it is removed.
With the passage of 60 years, there
are changes to the circuitry of the
Hotpoint which could be made to
improve performance. However, we
have resisted these temptations for the
moment and adhered to the original
circuit except for some modifications
to the output transformer connection
(the original circuit allowed the hightension to remain on the screen of the
6V6GT output valve when the speaker
cable was unplugged – see last month’s
article).
Incidentally, one reader emailed to
say that there wasn’t any design fault
since the circuit shown on page 94
clearly showed a plug with inbuilt
HT link. What he hadn’t realised was
that I had redrawn the circuit (also
mentioned in last month’s article) to
incorporate this modification. Perhaps
I should have emphasised that point.
Having replaced all the doubtful
parts there comes the critical time to
apply mains power. Measure from the
high-tension line to ground to make
sure that there is high resistance and
also from pin 3 to pin 4 of the 6V6GT,
to make sure that the primary of the
speaker transformer is intact. The
latter should measure a few hundred
ohms. Of, course the abovementioned
speaker plug should be in place.
Place the chassis on the bench so
that the valves can be viewed. Switch
the power on but have your hand on
the mains outlet switch in case anything shows distress. Check the valves.
With most types the cathode will glow
a dull red.
With the Hotpoint, there were no
fireworks and the cathodes were all
as expected. The heater element of the
6X6GT protruded out of the cylindrical cathode by about 8mm which isn’t
normal but the cathode was a normal
dull red, so the valve still did its job.
With luck, there will be a gentle
hiss from the set with the volume
control fully advanced. And with an
insulated wire connected to the aerial
terminal, you should be able to hear
some stations, even if weakly, as the
tuning knob is rotated.
But the chances are that you may not
be so lucky. In that case, a systematic
search through the circuitry will be
necessary. This is a good idea anyway
because it will pick up any more faulty
components, including valves.
Place the chassis so that you can
get at the underneath connections
and measure the high-tension (HT)
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This view shows the complicated dial stringing arrangement, necessary to ensure that the top and bottom horizontal
sections both travel in the same direction to carry the long vertical pointer. About 2.4 metres of dial cord is required to
complete the job.
voltage across the 16µF filter capacitor. It should be about 250V DC. Then
measure the voltage across the 325Ω
resistor from the 6V6GT cathode to
earth. It should be about 13V which
means that the cathode current of the
valve is 40mA. If it is much less, it is
probable that the valve is low in emission and due for replacement.
To check that the valve is amplifying, switch the meter to the ohms
scale, connect the red (normally
positive) lead to earth and touch the
black lead to the junction of the 47kΩ
and 0.47MΩ (470kΩ) resistors. There
should be a thump from the speaker.
If not, there is most likely a problem
in the speaker transformer, the speaker
or the connections.
All OK with the output stage? Measure the voltage at the plate (pin 6) of
the 6SQ7GT. It should measure about
90V and touching the probe on the
pin should result in a click from the
speaker. If the voltage is much higher
than 90V, the valve is probably low
in emission and should be replaced.
(Note: this is a case where the cathode current is only about 0.5mA and
a usable valve would be failed by an
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emission tester.) Again, use the ohms
setting of the meter from grid (pin 2)
to ground to confirm that the stage is
amplifying.
Also, the volume control can be
checked by using the meter on the
ohms scale. Start with the knob turned
fully clockwise and note that the
sound in the speaker is reduced as the
knob is turned anticlockwise.
The lefthand knob is marked
“PHONO – RADIO” and has positions
marked “TREB”, “MED” and “BASS”
for both the phono and radio functions – six positions altogether. The
frequency response of the Hotpoint
shown in Fig.1 is for the “TREB” position. The other two positions impose
very severe high-frequency audio attenuation.
The plate current of the 6SK7GT
can’t easily be checked because its
cathode is grounded. Measure the resistance of the IF transformer primary
with the set switched off. Then, after
making sure the screen voltage is about
80V, the plate voltage about 250V and
the grid -3V, measure the voltage drop
across the IF transformer winding.
This voltage divided by the resistance
and multiplied by 1000 will give the
plate current (in milliamps). With a
good valve, it should be about 5mA.
Now with the DMM on the ohms
range, briefly touch the probe to the
grid (pin 4) of the 6SK7GT. This should
result in a slight click in the speaker if
the valve is amplifying but not nearly
as loud as with the audio stages,
Testing the 6J8G is a special problem in the Hotpoint chassis. The
socket for the valve is hidden by the
broadcast-band oscillator coil and the
accompanying trimmer capacitor. It is
just not practical to make contact with
the two connections which are needed
to determine if the valve is OK, ie, the
cathode and the grid of the oscillator
section.
As a result, the trimmer was removed and a 1MΩ resistor soldered
to the oscillator grid connection on
the valve socket (pin 5). The other
end of the resistor was left to protrude
between the two trimmers so that the
meter connection could be made. The
voltage reading will be only slightly
reduced by the presence of the resistor (the capacitance of the meter leads
would affect the oscillator frequency if
August 2011 95
A 2.2Ω resistor was wired in series
with each dial lamp to improve its
reliability. This gives only a slight
reduction in brightness.
The shaft of the replacement switch
pot was extended using a short section
of shaft from another pot. The two
were joined using a threaded bush
from another pot, the lot held together
with JB Weld epoxy adhesive.
a direct connection were made).
In order to get at the 6J8G valve
socket cathode connection, the side of
the chassis which carries the support
for the dial glass and dial lamps had to
be removed. A length of hook-up wire
was soldered to pin 8 of the socket.
This pin is already bypassed to chassis so that the wire can be extended
without affecting the performance.
Altogether, this was a time-consuming
job.
The cathode resistor and the oscillator grid-return resistor were both
within 20% of their marked values and
because of the difficulty of replacing
them, they were left as is. The capacitors were difficult to undo and measure
but their effect is easy to determine.
96 Silicon Chip
If the 70pF capacitor is not about the
correct value, the oscillator will not
perform correctly across the band.
In addition, the gain of the valve will
be low if the bypass capacitor across
the 200Ω resistor is low in value. We
checked this by connecting a 0.1µF
capacitor from the extended wire to
earth.
Ohm’s law can be applied after
measuring the voltage across the cathode resistor. The calculation should
indicate about 6mA. It was much less
than this with our set and so a new
6J8G was fitted. This fixed the problem
of the set not receiving stations at the
high-frequency end of the band.
The operating conditions for the
6J8G in the Hotpoint circuit are really not optimum for performance.
The grid bias should be lower, giving
a higher cathode current and thus
increasing the gain and oscillator
amplitude.
We did, however, decide to retain
the original design where reasonable.
Shorting out the 220Ω cathode resistor on the broadcast band is an easy
way of proving the point. It improves
the sensitivity on the broadcast band
by about 6dB. However, to make the
grounded cathode legitimate, negative
bias has to be restored on shortwave.
The socket for the 6J8G in the
Hotpoint chassis is shock-mounted
from the chassis. We can only assume
that early production versions of the
valve tended to be microphonic and
that this was done to prevent acoustic feedback from the 12-inch (30cm)
speaker which was positioned close
to the chassis.
Stringing the dial cord
The dial cord had at some time been
re-strung with ordinary string and it
just wasn’t working as it should. Ordinary string doesn’t work as it is too
slippery to provide enough friction
around the pulley for the tuning knob.
And it has to be tensioned properly.
In the case of the Hotpoint, the dial
cord arrangement is quite complicated
since it supports the long pointer at
both the top and bottom of the dial.
Cord sections going in the same direction at top and bottom are provided by
the special stringing arrangement. In
fact, it requires about 2.4m of dial cord.
You have several choices if you cannot obtain dial cord. One approach is
to use the cord from slimline venetian
blinds and another is to use the thin
line used by bricklayers. A third possibility is to use dental floss. Fortunately,
the Hotpoint chassis has a diagram for
the dial stringing on the back of the
dial-plate.
Over-bright dial lamps
Dial lamps in typical vintage radios
present a reliability problem if operated at the full heater voltage of 6.3V.
They get very hot and they can even
lead to cabinet discolouration in those
with Bakelite cases.
In the case of the Hotpoint, I decided
to wire a 2.2Ω resistor in series with
each of the four lamps. This results
in a slight reduction in brilliance but
also reduces the amount of heat they
produce.
IF alignment
The next job was to align the tuned
circuits and correct the dial station
calibration positions. Bear in mind
that the dial was originally designed
when the stations were 10kHz apart in
frequency; now AM broadcast frequencies have 9kHz spacing. Having said
that, most of the major city stations are
still close to their original frequencies.
Alignment of the 455kHz intermediate transformers can be undertaken
using a local radio station and your
digital multimeter (DMM). With care,
the job can be done virtually as well
as with a signal generator.
The positive lead of the DMM can be
connected to chassis and the negative
lead to a point on the AGC (automatic
gain control) line which is bypassed. In
the case of the Hotpoint, this could be
across the .047µF capacitor at the bottom of the 1st IF transformer secondary. You may use the chosen point for
the whole of the alignment procedure
and it could be worthwhile arranging a
“hands free” connection to the meter.
You will probably stand the chassis on end so that you can access all
the adjustments. Tools such as small
screwdrivers should be on hand and
plastic alignment tools may be needed
if some of the adjustments involve
internal slugs.
An aerial wire, say five metres long,
should be connected and when you
tune accurately to a strong station
the meter should indicate a positive
value of a few volts. Carefully adjust
the tuning capacitor for maximum
reading. If there is a choice, use a station at the low-frequency end of the
broadcast band.
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Then, one by one, adjust the IF transformers for best meter reading. In most
cases, the increase in reading will be
small and accounted for by the aging
of components. If one adjustment does
not result in a peak meter reading then
the IF transformer is faulty may need
to be replaced. This doesn’t happen
with many sets.
Another possibility is that an adjustment screw or slug has jammed and
can’t be moved. A decision then has
to be made. If, eventually, the set is
sensitive enough to receive the stations
needed, it could well be a reasonable
decision to leave the component in
place rather than face a difficult replacement.
The next job is to make the dial
pointer agree with the station positions.
Tune to a known station at the
high-frequency end of the band and
then adjust the trimmer capacitor for
the oscillator coil (25pF) so that the
pointer indicates the station position
correctly. That done, tune to a station
at the low-frequency end of the band
and adjust the core of the oscillator
coil for the dial position.
When the set is tuned back to the
high-frequency station, the dial position may have shifted slightly. Correct
this again with the trimmer capacitor.
It may be necessary to go backwards
and forwards two or three times to
complete the oscillator line up.
Signal frequency circuits are lined
up for maximum sensitivity using the
same general idea: adjusting trimmer
capacitors towards the high-frequency
end and inductors towards the lowfrequency end. The tuning capacitor
rotates through 180°. Try to make the
adjustments near the 20° and 160°
points.
Note: the shape of the tuning capacitor plates is the same for both
the oscillator and signal-frequency
tuned circuits, so tracking can only
be perfect at three points on the dial:
near the ends and towards the centre.
The loss in sensitivity is not too serious, however. Some manufacturers in
the late 1950s overcame this problem
with tuning capacitors by having
differently-shaped plates for the oscillator section.
If your radio has an RF amplifier
stage, there will probably be two tuned
circuits to adjust but the principle is
the same: inductors towards the lowfrequency end and trimmer capacitors
siliconchip.com.au
Fig.1: the audio response curve for the Hotpoint J35DE radio. It’s 10dB down at
5kHz but most people were happy with a “mellow” tone in the 1950s.
Measured Performance
Audio Output................................................................................................. Max. 3W; undistorted 1W.
Frequency Response................................................................-3dB <at> 100Hz & 3kHz, -10dB <at> 5kHz.
Receiver Sensitivity.............................................. 12μV <at> 600kHz; 8μV <at> 1500kHz; 20μV <at> 10MHz
(Signal level at receiver aerial terminal: AM signal 30% modulated <at> 1 kHz for 50mW output)
towards the high-frequency end.
Our Hotpoint presented another
design problem: there is no means of
adjusting the inductance of the aerial
tuned circuits on either the broadcast
or shortwave band. All we can do is
adjust the trimmer capacitors.
Shortwave alignment without a signal generator does present a problem.
The Hotpoint could never be considered as a set for the serious shortwave
listener but something should be done
so that strong stations can be heard.
Simply turn the dial to the middle
of the range and with the aerial connected, adjust the trimmer capacitor
for maximum noise. This may be sufficient for some.
For those who wish to go further,
use can be made of the American station WWV which transmits accurate
frequency and time signals from both
Hawaii and Colorado. The 10MHz
signals can usually be heard at good
strength in Australia in the early evening and are identified by a one-second
pulse on the audio.
Simply adjust the shortwave oscillator trimmer so that WWV appears
at the calibration point on the dial
and then adjust the aerial trimmer for
maximum volume
Once the dial calibration is correct
at 10MHz, it will be easy to find the
25-metre (11.6-12.1MHz) and 31-metre
(9.4-9.99MHz) bands. A long outside
aerial will be desirable with sets like
the Hotpoint because of limited sensitivity.
Shortwave propagation conditions
around the world at the present time
and probably for the next few years,
tend to favour stations between about
4MHz and 12MHz so that it would be
reasonable to adjust the aerial trimmer
somewhere in the middle of that range.
How accurate is the alignment using
the above methods?
We checked the Hotpoint with a
laboratory signal generator, output
test set and oscilloscope. The centre
frequency of the intermediate stage
was a few kHz away from the normal
455kHz but this really doesn’t matter.
We were unable to improve on any
other adjustments.
The performance of the receiver
is listed in the accompanying panel.
The poor audio response is due to the
narrow selectivity of the 455kHz IF
stage attenuating the sidebands and is
typical of AM receivers manufactured
in the 1940s and 1950s, when people
were happy with a “mellow” tone. The
sensitivity, although not outstanding,
is adequate for receiving local stations
given about 5m of aerial wire extended
SC
away from shielding objects.
August 2011 97
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