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Vintage Radio
By Leith Tebbit
A rare 1929 AWA C54 Radiola
set rescued from oblivion
Some vintage radios are in such a dilapidated
state when discovered that you wonder why
anyone would even attempt to restore them.
Such was the case with this rare AWA C54 –
its cabinet was badly water-damaged and the
chassis was dirty, dusty and rusting.
R
ADIOS FROM THE 1920s, such
as the AWA C54, are now hard to
find, with occasional exciting exceptions making collecting worthwhile.
This particular discovery was made
back in May 2012 during a trip from
Queensland to Nowra in NSW. We
82 Silicon Chip
were passing through a little village
called Wingen on the New England
Highway (near Scone) and decided
to visit an excellent secondhand and
antique business.
When I visit such places, I always
ask “do you have any old radios that
aren’t in good condition or are not
operating, in particular vintage valve
radios?” In this case, the proprietor
declared “yes, out in the back shed”.
It’s hard to describe the condition
of the decrepit old AWA C54 console
we found there. It was extremely dusty
and dirty and on first sight, it was a
“no-go zone”. The console originally
came from the Tamworth district before spending the last six years in its
present location.
On closer inspection, it was obvious
it wouldn’t be just a clean, dust and repair project, as there was considerable
damage to the cabinet itself. The chassis components were all there though,
which was encouraging, although the
corroded metalwork, and especially
the tuning capacitors, would be a
challenge. The asking price was $200
which I thought was very reasonable
considering that I’ve seen several TRF
chassis alone (ie, without a cabinet) sell
for well over that figure.
Despite the dilapidated condition
of the cabinet, it was well within my
capabilities, as I’m a woodworking
enthusiast. Restoring it to its former
glory would be a monumental task but
once finished, it would make a very
nice addition to my collection.
On the plus side, the front speaker
grille, dial-scale and controls were
all in reasonable condition due to the
fact that the console’s bat-wing doors
had been closed during storage. But
that’s where the good news ended.
Pieces were missing from the turned
cabinet legs due to the animal-based
glue crystallising, while the lower battery compartment had been severely
damaged following leakage from the
lead-acid “A” filament supply battery.
In addition, some parts were missing
from the battery compartment.
The accompanying photos of the
radio chassis and upper battery storage
compartment show the condition they
were in – and that’s after the removal of
a hornets’ nest that occupied much of
the inside of the cabinet. Surprisingly,
there was no sign of spiders or other
siliconchip.com.au
Fig.1: the circuit details of the AWA C54. It’s a 6-valve TRF receiver
and consists of three non-neutralised RF amplifier stages followed by
a grid-leak detector stage and two audio amplifier stages.
pests that are normally found inside a
cabinet of this age. Perhaps the hornets
had kept them at bay!
Circuit details
Fig.1 shows the circuit details of the
C54. It’s a 6-valve TRF receiver and is
similar to the 1928 C50 model, except
that “losser” (or stopper) resistors are
used whereas in the C50, the RF stages
were neutralised using capacitors. A
likely reason for this is that AWA was
unwilling to pay the necessary licence
fee to Hazeltine to use their neutralisation patent.
In addition, the C54 receiver was a
very different mechanical design to
the C50. It bore a striking resemblance
to the Atwater Kent model 33, with
its L-shaped metal chassis, binocular
coils and losser resistors in the RF
grid circuits, among other things. The
Atwater Kent 33 came out in 1927 and
must have inspired AWA’s designers
during 1928.
In summary, stages 1-3 are non-neutralised RF amplifier stages with series
resistors between the tuned circuit
and the grid of each valve to ensure
stability. This, combined with a fairly
small number of turns on the primary
of each coupling transformer, resulted
in adequate gain without instability.
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The 84-year-old AWA C54 was obtained by the author in very poor condition,
with a badly water-damaged cabinet and a dirty, rusting chassis. Restoring it to
full working condition was a monumental task.
The “binocular” coils limited their
external field and allowed them to be
used without any screening between
the RF stages. This differed from the
C50 which was also known as the
“screened six” because each RF stage
was mounted in its own screened
compartment.
Stage 4 is a grid-leak detector with
no regeneration, while stage 5 is the
first audio stage. This is then followed
by the audio output stage (stage 6).
October 2013 83
These four photos illustrate the damage to the loudspeaker
(top, left), the chassis and the cabinet of the old C54 radio.
Many of the cabinet sections had to be remade.
It’s interesting to note that the chassis is connected to the -1.5V tap of the
bias (C) battery, resulting in the negative side of the filament (A) battery
being 1.5V above the chassis. This was
done so that the three RF stages could
be biased with the bottom ends of their
coils and tuning capacitors grounded
directly to the chassis.
The rheostat in the filament supply
to the RF stages serves as the volume
control, a popular method in the
1920s. This simple scheme generally
worked well with valves with thori-
ated filaments such as the 01A and
99 but was not very satisfactory with
oxide-coated valves as used in this set.
Basically, it worked OK but it shortened the life of the valves by poisoning
the emitting material. Oxide-coated
cathodes did not like operating in
saturated mode, particularly with the
relatively high plate voltage used in
this set.
The pick-up connection to the primary of the first audio transformer was
fairly standard and the small amount
of current running through the pick-up
coil (which had 45V on it) didn’t seem
to affect the operation.
Restoration
The author’s home-made copy wood lathe came in handy when it came to making
new sections for the turned legs that are fitted to the cabinet.
84 Silicon Chip
I started the restoration by lightly
dusting the chassis and cabinet using a soft brush and a low-pressure
compressed-air nozzle. A brush gives
much better control and has less
chance of damaging components than
heavy-handed cleaning using a cloth.
That done, I removed the set’s TRF
(tuned radio frequency) chassis and
a quick inspection revealed severely
corroded metalwork, plus oxidised
brass and copper components. By
now, it was obvious that a considerable
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These two views show the fully-restored chassis of the AWA C54 Radiola. The metalwork, including the four tuning
capacitors, had to be dismantled and bead-blasted to get everything looking like new again.
amount of work would be required to
restore the chassis. The good news
was that all the components appeared
to be in their original condition and
in position.
As previously indicated, the cabinet
was in poor condition and there was
no choice but to completely disassemble it in order to restore the severely
water-damaged veneer panels and to
replace missing parts. But that was
easier said than done, as pulling it
apart without inflicting further damage
took considerable effort and patience.
Each section had to be slowly wriggled apart until there was a sufficient
gap to use a fine metal saw to cut the
original nails and wooden dowels.
Basically, it was better to sacrifice the
dowels rather than damage other parts
during the cabinet disassembly. Fortunately, some sections came apart easily
due to the original glue breaking down.
As well as using a small hacksaw
blade, I also used a very fine metalcutting oscillating blade fitted to an
electric multi-tool to cut the dowels
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and nails, while a rubber mallet also
came in handy to gently “persuade”
the sections to separate. Naturally, any
missing or damaged pieces would have
to be re-manufactured.
Surprisingly, the solid timber parts
were in reasonable condition, with no
severe chips or bruising, leaving only
minor dents to be filled. However,
the weathered and aged ply veneered
panels were nowhere near as simple
to repair.
Water damage to the front of the
bat-wing doors and the radio compartment lid meant that major restoration
work was required on these parts.
The lid had missing veneer and had
separated from the ply panel in quite
a few places as well. Fortunately, the
two side panels of the cabinet were
in reasonable condition and only required routine sanding and filling of
small imperfections.
Once the cabinet had been completely dismantled and these repairs
completed, there was no turning back.
The legs had been damaged, so new
sections were manufactured, using a
copy wood lathe I made several years
ago. This lathe not only made it much
easier to make the parts but also enabled them to be virtually exact.
The upper sections of the turned
legs were fabricated from four separate pieces, each glued to a central leg
component. This made it possible to
turn such a large section without using
a single piece of solid timber, thereby
conserving material.
Melunak timber was used to remanufacture the missing or damaged
components. It’s the first time I’d used
it and it’s very much like teak, with a
very similar grain (it’s hard to detect
the difference, in fact). It machines
cleanly without any tearing of the
grain, after which it’s possible to give
the timber a light sanding and apply
sanding sealer directly. Most of the
new parts were given two or three
coats of sanding sealer and I sanded
back with 320 grain dry paper between
coats.
The lid of the cabinet had to be comOctober 2013 85
The underside of the C54’s chassis is relatively uncluttered, with point-to-point wiring between the valve sockets, coils
and other parts. Note the copper bands used to couple the dial-drive pulleys.
pletely re-manufactured. First, a tim
ber frame was fabricated using a router,
then reassembled using the more
modern biscuit-jointing method. This
then became the base onto which the
veneer panels were glued, with the
frame edge around the panel enabling
better machining, rather than trying to
machine across the ply panel’s grain
when finishing off the edge.
Using biscuit-jointing, rather than
the nails and staples used in the original assembly, makes it easier to align
the parts while re-gluing. Also, you can
test-assemble the various parts prior
to the final gluing process, to ensure
no imperfections have been missed
during restoration.
That done, the lower battery compartment was also completely remanufactured, since there appeared to
be no other alternative. The restored
cabinet parts were then finished with
Nitrocellulose HY-Tech 70% Matt
Sheen Pre-Catalysed Lacquer. This
involved applying three coats with
sanding between coats using 400 grit
dry paper.
In 1929, AWA assembled the cabinet
prior to applying the finishing coats.
In my case, the finishing coats were
completed prior to the final assembly. As a bonus, biscuit joints don’t
have nail-holes or staples that need
filling. However, it was necessary to
thoroughly remove any excess glue
immediately after clamping the components tightly together, to ensure a
near-perfect joint.
Restoring the chassis
Because of its poor state, I began
the chassis restoration by first taking
a series of photos before removing all
the parts. I then glass-bead blasted all
the metalwork, including the tuning
capacitors and the speaker components. Surprisingly, the speaker had
no obvious damage whatsoever to
the cone! There was not one hole to
be seen, which is quite incredible
considering the age of radio, although
the back protection cloth was almost
non-existent.
The balanced magnetic speaker
arm was also disassembled in order
to glass-bead blast the iron surfaces
and coils. It’s worth noting that the
text stamped into the coil former was
still intact after this process, indicating
just how “gentle” glass-bead blasting
can be at low pressures. Basically, it
removes the rust and dirt while leaving delicate text and markings. It’s a
slow process but well worth doing in
cases like this.
Following this bead-blasting process, a fine film of Penetrol oil was
applied to the metal chassis, tuning
condensers and the surfaces of all
Bakelite components.
Open-circuit inductor
This close-up view shows how the copper bands used to couple the dial-drive
pulleys are joined together and tensioned.
86 Silicon Chip
Having cleaned the chassis, I began
making a few continuity checks on the
major parts and discovered that the
inductor in the LC network on the side
of the speaker housing was open circuit. As a result, I carefully melted the
black pitch from the container using a
hot-air gun to reveal the components.
This revealed that the internal solder
connections to the terminals were
open circuit, so it turned out to be an
easy repair.
Fortunately, the audio-coupling and
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output transformers were all intact
and in good working order. They only
needed repainting to restore their appearance.
Other repairs included replacing
the valves in the first TRF and audio
output stages. The 800Ω series grid
resistor in the second TRF stage also
required attention, since it had gone
open circuit. This resistor is wound on
a Bakelite former, so it was possible to
unwind part of the resistance wire and
re-solder the faulty joint.
No capacitors had to be replaced,
as they all tested and performed perfectly. The set is battery-operated, so
there were no electrolytic capacitors
to cause problems. Even so, the fact
that the other capacitors were all OK
is amazing considering that the set was
manufactured in 1929!
Despite the pure simplicity of the
chassis, this was one of the most
involved chassis restoration projects
I’ve ever attempted. That’s basically
because all the parts had to be removed prior to cleaning the chassis.
Every wire and connection had to be
de-soldered and each connection then
cleaned and/or glass-bead blasted.
Each wire was then cleaned and
re-soldered back in place using the
photos taken earlier as a reference.
Fortunately, no rubber-covered wires
were used, except for the DC battery
harness, so the original wiring was
largely retained.
Aligning the tuning capacitors
The four variable tuning capacitors
were aligned by first setting the dial
indicator to “0” and all the gangs to
their fully open position with their
set-screws tightened. I then tuned
through their range to find a weak local
station, before individually loosening
the set-screw for each tuning gang in
turn and rotating its shaft back and
forth to peak the received signal.
This alignment procedure was carried out by working backwards from
the output end of the receiver towards
the front-end stages.
Once completed, this process was
repeated, again by first tuning into a
weak station. There appears to be no
difference between tuning from the
antenna RF stages to the final stages or
in the opposite direction as described
above. However, starting from the final
stage and working towards the front is
usually the way most radios are tuned.
TRF receivers with coil-coupling adj
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A major part of the restoration involved rebuilding the cabinet. This view shows
the various pieces, many of them completely re-made, before the final assembly.
ustments are generally much more
complicated to tune but in this AWA
C54 set, the coils cannot be adjusted.
Copper bands are used as belts to
couple the drive pulleys. Each pulley
has a hole in its centre for a location
pin, thereby eliminating any slippage
once the belt is tightened by small
cylindrical clamps.
When I first reassembled the tuning
capacitors, I didn’t realise that the unit
in the first TRF stage used a different
stator to compensate for the antenna
circuit. As a result, it wound up in the
wrong place which meant that I was
initially unable to get the TRF stages
to track properly across the entire RF
band.
When I eventually corrected this error, the receiver performed extremely
well right across the band using just
a short antenna. In fact, the old TRF
set picks up 12 stations without any
drift or fading – an outstanding result
considering we are dominated by
a very high-power ABC transmitter
only 2km from our location in Dalby,
Queensland.
Once the chassis restoration had
been completed, the receiver was fitted
into the top compartment of the cabinet. The finished cabinet really looks
the part and the veneer on the inside
of the lift-up lid is joined in the middle
for a mirror pattern-match, producing
a diamond shape pattern on both the
top and bottom. The hinges, handles
and latches were also all fully restored.
The battery compartment now has
an illustration only of the dry battery
pack that was originally used. Batteries
are no longer used to power this set.
Instead, power is now supplied from
a custom-built mains power supply.
The result
The accompanying photos show the
finished result. This is the first TRF
receiver I’ve restored and I can only
imagine the pride its original owner
must have had for the set – the more
so given its performance and ease of
operation due to the coupled tuning
capacitors which were all controlled
by a single knob. The quality of the
audio from the efficient moving-iron
speaker is also very good and it’s all
built into a very elegant cabinet.
I never expected this restoration
project would end up in Melbourne at
the 30th Anniversary of the Historical
Radio Society of Australia (HRSA) in
September 2012. When three members
of the HRSA encouraged me to enter
it for the Ray Kelly award, I only had
two weeks left to complete the project,
build a multi-voltage power supply
and travel to Melbourne. The set won
the Ray Kelly “best in show” award, so
the effort was well worthwhile.
Acknowledgement: photographs and text
edited by Kevin Poulter; circuit description
SC
by Mike Osborne.
October 2013 87
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