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Vintage Radio
By Rodney Champness, VK3UG
The upmarket 1950 HMV
R53A radiogram
For many well-off families, an expensive
radiogram was the focal point of the
family lounge room in the era from the
late 1920s up until the late 1960s. It not
only provided the entertainment but was
also an impressive piece of furniture.
R
ADIOGRAMS were first developed in the late 1920s and were
produced in various formats up until
the 1960s when TV took over as the
main source of family entertainment.
During that time, they evolved from
very basic units with a record player
on top of the cabinet to units that had
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automatic record changers alongside
the radio section.
Some of the very latest units also included a TV set and/or a tape recorder
and some even had a cocktail section
for good measure!
Of course, not all radiograms were
created equal and the quality of the
cabinets varied considerably. Some
were impressive units made of solid
high-quality timber, with timber veneers where necessary. These sets
were quite imposing and were heavy
but there were also many cabinets that
were built to a price and were much
lighter.
The radio chassis used also varied
considerably in quality. Most units
used a cheap and cheerful bog-standard 5-valve mantel receiver chassis
driving a large speaker mounted on
a baffle board. These sets often had a
rather restricted audio frequency range,
otherwise hum would have been quite
obvious due to minimal high-tension
supply ripple filtering and inadequate
(or non-existent) shielding of sensitive
audio leads.
By contrast, the more expensive
top-of-the-line radiograms used a
better-engineered chassis designed to
give high-quality sound and capable
of driving the speaker to high volume.
These sets also generally had better
RF sensitivity and stability than their
cheaper counterparts.
This was achieved by increasing
the filtering on the HT (high-tension)
line, adequate shielding of critical
leads and higher-quality audio output
transformers. The audio amplifier was
also beefed up, often by using a pushpull audio output stage.
Two Australian-made radiograms
that were excellent performers were
the STC A8551 from 1955 (featured
in the January 2010 issue of SILICON
CHIP) and the HMV R53A which came
onto the market in 1950. The R53A described here had quite a few problems
when it was obtained by its owner and
was passed on to the author so that the
chassis could be restored.
HMV R53A radiogram
Basically, the owner wanted to be
sure that the chassis could be repaired
before he undertook the cabinet restoration. As shown in the photos, the
R53A is quite a large unit, with the
radio chassis and the record changer
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Fig.1: the HMV R53A is a 6-valve superhet design
covering both the AM broadcast & shortwave
bands. Valve V1 is the converter and is followed by
IF amplifier/detector stage V2 and then a 3-stage
audio amplifier based on V3-V5. V6 (5Y3-GT) is the
rectifier. Note that the HT to the 807 audio output
valve is supplied via a separate filter choke (CK2).
mounted side-by-side in separate
compartments. These compartments
are accessed by opening separate doors
which hinge down.
It’s interesting to note that the same
chassis was also used in a variant
which had a top-opening lid to gain
access to the controls and the record
changer. This was probably a downmarket version as the cabinet is not
as large and is somewhat lighter than
the R53A’s.
As it came to me, the R53A radiogram featured here was 64 years old.
Its chassis was covered in dust and
when I removed it, I could find only
one resistor and one capacitor that had
been previously replaced, along with a
section of the dial cord. However, the
original record changer had obviously
proved to be less than reliable and had
been replaced by a more modern BSR
unit at some time in the past.
Circuit details
Fig.1 shows the circuit details of
the HMV R53A. It’s a 6-valve superhet design and covers the AM broadsiliconchip.com.au
cast band (nominally 540-1600kHz)
plus the shortwave band from 618MHz. The broadcast band tuning
range specified is what was allocated
in the 1940s and 1950s but in practice,
the R53A tunes a slightly wider range
of frequencies from 530-1660kHz.
As shown in Fig.1, the antenna coil’s
primary windings are in series with
each other, with the shortwave coil
acting as a low-value loading coil for
the antenna.
The broadcast coil primary winding
resonates below the broadcast band
due to the combination of L1 & C1.
This gives improved performance at
the low-frequency end of the band.
The 3pF capacitor (C2) between the
primary and secondary windings (L1
& L2) improves the performance at the
high-frequency end of the broadcast
band.
Unlike the broadcast-band coils,
the shortwave coils (L5 & L6) do not
use any elaborate coupling methods.
That’s because any antenna likely to
be employed would have sufficient
length to be resonant on some portion
of the shortwave band. L5 is in series
with L1 and although L1 will act as an
RF choke on shortwave, C1 (100pF)
acts as a low-impedance path to earth
for the ‘earthy’ side of L5. This was
a neat trick that was used by many
manufacturers; it worked well and
saved a switch section.
The antenna coils are switched
as appropriate in the grid circuit of
converter valve V1, depending on
the band selected. Alternatively, V1’s
grid is shorted to chassis when the set
is switched to ‘Gram’, to prevent RF
signals breaking through.
R4 and C9 ensure that no high
voltages are present in the oscillator’s
tuned circuits. This method was used
by many manufacturers but others
have the oscillator plate current flowing through the feedback winding.
Either method works well but you do
have to be aware that high voltages are
present in the tuned circuits of some
oscillator stages.
The converter stage is neutralised
using a small ‘gimmick’ capacitor
between the oscillator grid and the
July 2014 93
These two views show the chassis before and after restoration. Note the insulated
cap (red) on the top of the 807 output valve. This is the plate connection and
must not be touched due to the shock hazard.
signal input grid. This ‘gimmick’ capacitor was made using about 20mm
of insulated bell wire.
The 457.5kHz IF (intermediate
frequency) appears at V1’s plate and
is fed to the primary winding of IF
transformer IFT1. It also goes to a section of 4-position switch S1, which is
the band change and ‘Gram’ selector
switch.
In positions 1 & 2, the IF transformer
is coupled in the conventional manner.
94 Silicon Chip
However, when S1 is in position 3,
resistor R10 is switched across IFT1’s
primary while R6 is switched across
the secondary winding. Capacitor C13
is also connected between V1’s plate
and V2’s grid.
These switched parts lower the Q of
the tuned circuits and, along with the
heavy top-coupling due to C13, give
a wide frequency response with a dip
in the middle. IFT2 (which follows
V2) also has a wide response and this
means that signals out to about 10kHz
are amplified with little attenuation of
the higher audio frequencies.
V2, a 6N8, amplifies the IF signal
and, like the converter, this stage is
also neutralised. This is done by C17
in conjunction with C15. The signal at
the output of IFT2 is fed to the detector diode in V2. The resulting audio
signal is then fed to another section
of switch S1 which selects the audio
signal from either the radio or the
record changer and feeds it to a 4-pin
socket. The volume control is wired to
this socket and its output is then fed
back via this socket to the input of V3,
another 6N8.
It’s difficult to understand why the
volume control was attached via a
plug and cable to the chassis and not
mounted on the front of the chassis
like the other controls. In this case,
the volume control is mounted on a
side panel of the radiogram, possibly
so that it could be accessed with the
door to the radio section closed.
V3 amplifies the volume control
signal and in turn drives separate
bass and treble control networks. The
resulting signal then goes to V4, anoth
er 6N8, which further amplifies the
signal before feeding it via C44 to the
grid of an 807 output valve (V5).
V5 again amplifies the audio signal
and then feeds it via a substantial audio transformer to a 12-inch (~30cm)
loudspeaker. This circuit includes
voice-coil negative feedback which is
fed back to the cathode circuit of V4.
Note that the 807 is not bypassed at the
screen but via a 100Ω resistor (R36).
Some valves, including the 807, can
be unstable if they are not bypassed
in this manner.
The power supply is based on fullwave rectifier V6 (5Y3-GT) and is quite
conventional. The HT (high tension)
line has two filter chokes (CK1 & CK2),
with CK2 feeding just the 807 output
valve (V5) and CK1 feeding HT to the
remainder of the receiver. Note that
back bias is applied from the top of
resistor R9 to the AGC diode in V3
and to the grids of V1 & V2.
Conventional delayed AGC is used
with -2V of delay. As a result, both V1
& V2 are biased at -2V, as is the AGC
diode in V3. No additional bias is developed until the IF signal at the plate
of the AGC diode exceeds 2V peak.
Restoring the chassis
Removing the R53A’s chassis from
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The two tone controls, the tuning control and the bandswitch are mounted just below the dial, while the volume
control is mounted on a side-panel of the cabinet.
the cabinet is quite straightforward.
First, the plywood sheet covering the
back of the receiver is removed, then
the knobs are removed by pulling
them off their spindles. The volume
control is then removed by unplugging
its cable from the socket on the top of
the chassis, then undoing the three
screws which secure it to the side of
the chassis.
Next, the four screws underneath
the chassis shelf are removed and
various leads at the back of the chassis disconnected (ie, antenna/earth
leads, speaker lead, record changer
leads, etc). The ‘on’ light lead to the
bottom of the cabinet must also be
disconnected. This entire procedure
takes just few minutes.
Once it was out of the cabinet,
the chassis was carefully dusted using a paintbrush and cleaned with a
kerosene-soaked rag. This also worked
wonders on the black sealing material
used on the transformers. The cabinet
was then brushed down and a damp
sponge used to remove any ingrained
dust from the woodwork.
There was no corrosion to any extent
and the chassis looked quite presentable. This old HMV R53A has obviously been stored in a dry environment
to still be in such condition.
As is my usual practice, my next
step was to remove all the valves and
wash them in warm soapy water. The
miniature valves were simply dunked
in the water and the glass envelopes
rubbed clean. However, you have to be
careful not to remove the type markings, as these can easily be rubbed off.
These valves were then rinsed under
clean water and allowed to dry.
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The original record changer had obviously given trouble
because it had been swapped out for this more-modern
BSR unit. It sits on a shelf that slides out of the cabinet.
Valves like the 5Y3GT and the
807 have Bakelite bases and have to
be treated more carefully. For these
types, the valves were simply turned
upside-down and the envelopes carefully washed while taking not get any
water into the bases. They were then
rinsed with clean water and left to dry
upside-down.
all the movable controls were lubricated using either light machine oil or
Inox® lubricant. These controls then
all worked smoothly and were free of
mechanical noise. The original 2-core
power lead was also replaced with a
securely anchored 3-core lead so that
the chassis could be safely earthed.
Replacing faulty parts
It was now time for a smoke test
(well, actually I hoped that there
wouldn’t be any smoke).
First, the loudspeaker was removed
from its baffle inside the cabinet and
connected to the receiver, along with
an antenna and earth. The HT line was
then checked for any shorts to chassis,
after which the set was connected to
mains power and switched on with
the multimeter now monitoring the
HT voltage.
It was all something of an anti-climax because the HT voltage rose and
settled down as expected. Because the
5Y3-GT heats up more quickly than the
other valves in the set, the HT initially
rises up to around 400V before settling
down to about 290V out of the rectifier
when the other valves warm up. As
expected, the HT is somewhat lower
when measured at the filter capacitors
following the two filter chokes.
Once the valves had warmed up,
the set then burst into operation and
it sounded quite good except that hum
was evident in the audio. The cause
wasn’t hard to find – I had replaced
filter capacitor C31 with a 10µF unit
which was inadequate for this set.
I tried replacing this capacitor with
the only 16µF capacitor I had but the
hum was still quite evident. I then
The next job was to replace all the
electrolytic capacitors and any paper
capacitors that were excessively leaky.
The paper capacitors were tested for
leakage using a high-voltage insulation tester. This tester was then set to
its 1000V range and used to check the
insulation of the power transformer.
In this case, the resistance from the
mains winding to earth was found to
be in excess of 100MΩ, which is quite
satisfactory.
In order to maintain the original
appearance, the faulty electrolytic capacitors on the top of the chassis were
left in place but were disconnected
from the circuit. New capacitors were
then fitted in place under the chassis.
The most critical capacitor is the one
connected to the 5Y3GT as this rectifier doesn’t ‘like’ high surge currents
flowing through it. In this case, C31
was initially replaced with a 10µF
525V capacitor (see below).
The two components (one resistor and one capacitor) that had been
replaced earlier in the set’s life had
failed again and so new parts were
substituted for these. A couple of other
resistors were also found to be well out
of tolerance and were also replaced.
That done, the dial mechanism and
Getting it going
July 2014 95
tom coupling instead, the frequency
shift would have been in the opposite
direction. This means that the best
method of maintaining the same centre
frequency is to have both top and bottom coupling between the two tuned
circuits.
In the end, by carefully adjusting the
IF alignment, I was able to minimise
this effect and get close to a common
passband frequency centre for the local
and distance switch positions.
Record changer repairs
All the parts under the chassis of the HMV R53A are readily accessible. This
view shows the chassis prior to restoration – some parts were replaced to get the
set going, while the 2-core mains cable was later replaced with a 3-core cable so
that the chassis could be earthed.
installed a 22µF capacitor across C12
but it was still not enough so I decided
to try decoupling the plate and screen
leads to V3. This involved installing a
4.7µF capacitor between the junction
of R20 & R21 and chassis, plus a 10kΩ
resistor from R20/R21 to C12.
That finally reduced the hum to
quite a low level, such that it was just
audible with my ear near the speaker
cone and with the volume control
turned right down.
The set goes dead
The hum problem had no sooner
been solved when the set suddenly
went dead. There was no audio so
there was clearly something wrong
with the audio amplifier stage.
A few quick checks showed that
while there was plenty of voltage on
the plate and screen of the 807 output
valve, there was no voltage drop across
its cathode resistor. Substituting another 807 cured the problem, so that
problem was easily solved.
By the way, the 807 valve is a
moderately-large 5-pin valve that was
originally designed for use in mediumsized communications transmitters
during the 1940s. And here a word
of warning: if a set uses an 807 and
there is no protective top cap cover
on the connector, don’t be tempted to
put your finger on it while the set is
operating (ie, while power is applied).
This is the plate terminal, not the grid,
96 Silicon Chip
and you will get a nasty high-voltage
shock if you do.
Although the set was quite sensitive,
further checks revealed that very little AGC voltage was being developed
between the junction of R7 & R11 and
the chassis. I had expected around 10V
of AGC when the set was tuned to a
local broadcast station but I was only
getting about 2.5V.
I checked the voltages around valves
V1 & V2 and they appeared normal so
I tried substituting a new 6N8 for V2
and the performance improved quite
noticeably. The AGC voltage also shot
up to somewhere near the expected
level. The chassis was then left on
test for quite a few hours to make sure
there were no further problems lurking
in the background.
Checking the alignment
The next step was to check the
alignment. First, I tried tweaking the
antenna trimmers on both the broadcast and shortwave bands but couldn’t
improve the performance, so the original settings were retained. However,
when I checked the IF amplifier, I
found that the centre of the IF passband changed by about 4kHz when I
switched S1 between the distant and
local positions.
This shift in the passband centre is
caused by the top coupling between
the two tuned circuits in the first IF
transformer. If the set had used bot-
Observing the operation of a record
changer mechanism isn’t normally an
easy job. However, back in the October
2000 issue of SILICON CHIP, I described
a home-made servicing aid which allowed a changer to sit up on 300mmhigh dowels, so that the mechanism
could be observed during operation.
As shown in one of the photos, I also
used this device when I overhauled
the R53A’s changer. As mentioned, the
original changer had obviously given
trouble because it had been replaced
with a more-modern BSR unit.
The biggest problem with this
changer turned out to be the pick-up
cartridge – it simply had no output.
Unfortunately, a direct replacement is
now almost impossible to obtain and
after looking through many catalogs,
the only generic pick-up that was suitable was listed by WES Components
of Ashfield in Sydney.
It wasn’t a drop-in replacement,
however, and the tone-arm mounting
had to be carefully modified so that it
could be installed properly. It wasn’t a
difficult job but it did take more time
than expected.
Stylus pressure
One thing that’s important with the
pick-up is to correctly adjust the stylus
pressure. Up-market hifi turntables
may specify just 1.5g to 3g of stylus
pressure, whereas most record changers intended for the broad consumer
market have stylus pressures of 5-7g.
If more than this is required to get the
tone-arm to track the record properly,
then the sliding surfaces in the mechanism probably need lubricating.
The downward stylus pressure is
controlled by either a spring at the
vertical pivot point of the tone-arm
or, in some cases, the weight has to
be adjusted at the head. In this case,
the new pick-up was lighter than the
original, so I had to add some weight
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The record changer was serviced by
sitting it on top of this homemade jig.
Now that the radio and record changer have been repaired, the next job is the
cabinet restoration. One of the bottom doors is missing and will have to be made.
into the shell where the cartridge is
located. Some shells already have
weights installed but if not, metal
washers can sometimes be used to
increase the pressure on the stylus.
I didn’t have a stylus pressure gauge,
so I used our digital kitchen scales to
get the weight correct. These scales can
measure down to 1g, which is good
enough for this job.
Having set the stylus pressure, I then
cleaned any old congealed grease off
various surfaces and applied fresh,
light grease in its place. The motor
bearing and various pulley bearings
were then oiled. This was relatively
straightforward although I did have
to dismantle the motor to gain access
to its bearings. In fact, this should be
done every few years as these motors
can seize up if they are not lubricated
and this particular unit was very close
to that point.
The various other adjustments on
the changer were all spot on. The
stylus drop-in point was correct, the
speed change mechanism worked
well and the record dropping and cutout mechanisms all worked as they
should. BSR record changers were
relatively simple compared to some
other brands and it is rare for them to
have any major problems.
Summary
For its time (circa 1950), this is one
of the best radiograms I have ever
worked on. The receiver section is
quite sensitive, the dual-bandwidth
IF amplifier works well, the audio
output is more than adequate and the
audio bandwidth and clarity are excellent. And once the owner finishes the
cabinet restoration, the old HMV R53A
will look great too.
The chassis is also easy to work on
and is well laid out, with most components easily accessible. HMV used lots
of plastic-sheathed shielded audio and
RF cables which were only earthed at
one end to prevent induced hum from
the heater circuits.
One very worthwhile feature is
a ‘rollover cage’ over the top of the
chassis. This makes it easy to tip the
set over for servicing without risking
damage to fragile parts such as valves.
The circuitry also shows considerable attention to detail and includes
neutralised IF amplifier and converter
stages to ensure stability. It certainly
ticks most of the boxes for good design. The chassis was also obviously
designed to accommodate a number of
sets of the era as there is an extra cutout for an additional IF transformer
and the power transformer is mounted
on a plate at one end of the chassis.
In fact, I have a HMV model 268
receiver which started life as a vibrator-powered set but was converted
to 230VAC operation as described in
May 2000. Its chassis layout is almost
identical to the R53A’s, so HMV had
developed a layout that worked well
for many quite different models.
If you have the room and want to
enjoy the sound from one of the better early radiograms you couldn’t go
past the HMV R53A. And if it had
been fitted with a dual-cone speaker
it probably would have sounded even
SC
better than it already does.
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