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SERVICEMAN'S LOG
Odyssey Stratos amplifier voltage conversion
Staff member Nicholas Vinen loves big amplifiers.
Well, big anything actually – big speakers, big
engines, big cars, big monitors, big . . . you name
it! Many years ago, he bought a big amplifier in
the USA but then had to convert it to operate
from 230VAC for use in Australia.
The Odyssey Stratos is an impressively large stereo amplifier, with a
power output of 150W RMS per channel. I bought this beast around the year
2000 while living in the USA. It was
during those heady “Dot Com Boom”
days when venture capitalists were
just about giving away free money
to anybody with a business plan that
included the word “Internet” in it.
The company I worked for was bought
by another company which was then
bought by another company which
wasn’t quite sure what to do with my
division. In the end, I was sent home
and I brought the Stratos with me.
These amplifiers are still being sold
today – see www.odysseyaudio.com/
products-stratos-stereo.html I didn’t
know much about amplifiers when I
bought it (how things change) but the
reviews were good, the “specs” were
impressive and it came with a 20-year
warranty. I also liked the idea of the
whole aluminium chassis being the
heatsink, so cooling wouldn’t be a
problem no matter how hard I drove it.
Anyway, having brought the Stratos
home, I had to figure out how to power
it. It’s a 115VAC model and for years
I used a 2kW step-down transformer.
But this arrangement had a few drawbacks. First, the step-down transformer
was quite large, as was the amplifier,
and the whole shebang took up a lot
of space. Second, it was inefficient
The Odyssey Stratos stereo amplifier is quite a large beast and is capable of
pumping out 150W RMS per channel. Converting it from 115VAC to 230VAC
operation proved to be a bit of a challenge.
54 Silicon Chip
Items Covered This Month
•
•
•
•
Converting an Odyssey Stratos
amplifier from 110VAC to
230VAC.
Faulty home lighting system
Dave’s faulty air-compressor
Digitor T-1333 sound system
and consumed a lot of power at idle,
meaning I had to turn it on and off at
the wall, which I found inconvenient.
And third, if I wanted to transport the
amplifier, I had to cart the transformer
around too.
Before bringing it home I spoke to the
bloke I bought it from (at the factory)
and he told me that they sold 220VAC
versions of the same amplifier for the
European market and there were only
a few slight differences. So I knew it
would be possible to change it to run
from 230VAC but, at the time, I didn’t
press him for details.
Having put up with the step-down
transformer for so long, I recently
thought that I’d open it up and see
how hard it would be to convert it to
230VAC operation. As expected, the
mains transformer (a 400VA toroid)
has two primary windings and these
are connected in parallel for 115VAC
operation. This meant that I could
change the transformer configuration
so that the primaries were connected
in series for 230VAC operation. And
thanks to the IEC mains input socket,
I could easily replace the mains cord
after doing this.
Before starting, I checked that the
socket and mains switch were both
rated for 250VAC and this was indeed
the case. The mains switch contained
a neon lamp with an in-built resistor
but I figured since it was 250VAC rated,
this wouldn’t need any modification.
But how should I reconfigure the transformer? I didn’t want to reconnect it
with the wrong phasing and burn it out.
The problem was that I didn’t know
siliconchip.com.au
which colour wire was which and with
the windings connected in parallel,
there was no obvious way to measure
it and find out. After some thought, I
realised that if I disconnected one of
the primary wires going to Neutral
(at the IEC socket) and one going to
Active (at the switch), then as long as
they weren’t from the same winding,
connecting these two together would
give the desired result.
The primary wires emerge from the
transformer in this order: brown, black,
red, orange and green/yellow. Green/
yellow is presumably for an earthed
screen and I guessed that brown/black
and red/orange were the two winding
pairs, with brown and orange being
connected to Neutral and red and
black to Active. Tentatively, I clipped
off the black and orange wires as it
was difficult to de-solder them (there
were multiple wires looped through
and then soldered to each terminal).
As well as the outer insulation jacket, the wires were enamelled so I placed
a plastic tray under them and scraped
away the enamel insulation from the
ends. I then checked the continuity
of the windings. The resistance of the
brown/black and red/orange pairs was
about 1.5Ω, confirming my suspicion
that these were the two primaries.
The odd thing was that I was still
getting a continuity reading between
the two primary pairs which should
have now been disconnected. The
resistance was much higher though,
at around 200Ω. However, I was pretty
confident that I had the right wires so
I soldered the orange and black wires
together and insulated the joint with
yellow heatshrink tubing.
I was still puzzled as to why I was
getting such a low reading between
what should have been disconnected
pairs though and decided to investigate
further. And then it hit me. The front
of the amplifier has a glass panel with
the Odyssey logo sandblasted into it.
This logo is lit by a pair of incandescent
lamps. Duh, the black and white pair
of wires I noticed earlier running from
the mains sockets must be to supply
these lamps with 115VAC!
Had I plugged it into 230VAC, the
lamps would have immediately blown
and I’d have had buckley’s chance of
finding exact replacements locally.
Anyway, I dodged that bullet and since
there were two lamps, I reasoned that I
could connect them in series and they
would happily run off 230VAC, at least
siliconchip.com.au
until one eventually blew, when they
would both go out.
This wasn’t difficult to arrange. All
I had to do was clip the white wire
going into the first lamp and the black
wire running between the two, strip
the ends back and connect the incoming white wire to the black wire from
the second lamp. The two would then
be in series. I did this, then insulated
the solder joint and the two wire ends
which now connected to nothing.
Finally, I changed the mains fuse
from 6.3A to 3.15A 250VAC, stood
back and powered it up. You beauty, it
worked! It did blow the fuse the second
time I turned it on though, obviously
due to the transformer inrush current.
Replacing the fuse with a 3A slow-blow
fuse fixed that problem.
At last, I could say goodbye to that
clunky step-down transformer.
Home lighting system
Sometimes, a puzzling fault can
have a very simple explanation as
G. B. of Ararat, Victoria discovered
when he was recently called out to
service a large diesel-powered generator. Here’s what happened . . .
Many years ago (more than I care
to remember, in fact), I learnt the art
of servicing Cooper engines from my
father. Very popular from the 1930s
though to the 1950s, these engines
could be found on practically every
farm in Victoria that hadn’t yet been
connected to the SEC, as the elec-
tricity grid was then known.
Basically, they were single-cylinder
petrol engines that were used to drive
shearing machines and 32V home
lighting plants. And it was not uncommon for some farms to have several
such machines.
One day back then, we got a call from
the father of a lad I went to school with.
“Rodney says you’re pretty smart. Will
you come and see if you can fix our
lighting plant? It won’t run properly
and every electrician we can find hasn’t
been able to fix it.” I should have woken
up then: electricians don’t fix engines
and I don’t fix electrical problems.
I know better now but then I said
“OK” and collected the tools to give
the engine the usual required valve
grind. A faulty valve seat was about
the only thing that could make one of
those things hard to start.
The trouble was I either hadn’t listened or hadn’t been told the full story.
I arrived at the farm and was pointed to
the engine shed with the comment “It
starts OK but won’t keep going.” Well,
this was going to be easy, I thought. If
an engine has fuel, air, compression,
ignition and exhaust, it must run.
The first shock came as I walked into
the engine shed. Instead of a Cooper
engine happily turning a generator to
charge a bank of 32V batteries, I was
faced with a huge Lister diesel rigged
as a “Startamatic” plant.
The principle of the Startamatic
was that if somebody turned on a
April 2016 55
Serviceman’s Log – continued
One thing leads to another with DIY
It’s marvellous how one thing can lead to another.
All I wanted to do was paint a room but I ended up
stripping down an air-compressor.
By Dave Thompson
One of the tasks I undertook during
my recent workshop clean-out was
to improve accessibility to my aircompressor. Until then, the compressor had been sitting beneath my drill
press-bench. Whenever I needed it, I
had to drag the thing into the middle
of the workshop floor and clear away
all the dust and swarf from it before
rolling out its retractable hose.
For the amount of times I used the
compressor, it was a tolerable workaround. However, as I was moving
stuff around during the clean-up, I
finally decided to find a better position for it.
Recently, I took delivery of a heavyduty transformer-winding machine
and it came with its own solid worktable that fitted perfectly into a corner
of my workshop. There was an area
under the table, beside the treadleoperated clutch, that begged to have
something stored in it and I soon discovered that my air-compressor fitted
into that space as if it was specifically
designed for it. I then mounted the
retractable air-hose reel onto one of
the 10 x 75mm legs of the table and
from there I can now roll the hose
out anywhere into the workshop or
into an adjacent garage.
That’s the way things remained until I needed the compressor recently.
Nina and I had decided to redo one of
our bedrooms because the previous
owner of our house had done a slapup job of throwing up some wall
paper without properly preparing
the wall. As a result, several patches
of unsightly and unhealthy-looking
mildew had begun peeking through
the wall covering.
Stripping away the old paper fell
to Nina. The theory was that once
she’d removed it all, we’d throw
an anti-mildew undercoat onto the
now-bare wall, followed by a couple
of top-coats to finish it. But, as we
56 Silicon Chip
all know, DIY doesn’t always follow
one’s nicely laid-out plans.
First, we discovered that instead
of standard plasterboard (or drywall),
whoever built the house in 1959 had
decided to go for fibrous plaster. It’s
an absolute <at>!%$# to work with!
The molecule-thin top-coat of plaster
on fibrous plasterboard breaks away
with just the slightest provocation to
reveal the true make-up of the board,
which appears to be plaster mixed
with horse-hair bristles.
This meant that wherever the
wallpaper had been stuck on with a
bit more glue than usual, the plaster
had pulled away and there were now
decent-sized patches of rough, hairy
bristles showing through.
Being a serviceman, I did what
anyone else in my position would
do and retrieved the biggest randomorbital sander I could find in my
workshop. However, all the sander
did was remove more of the plaster
holding the bristles together. As a result, the patch I was working on grew
slowly larger until I had to chuck in
the towel and admit that that particular strategy wasn’t helping.
I then decided that what I needed
to do was trim the hairs off the wall
altogether and since there weren’t
that many patches, I could simply
use a sharp blade to “shave” the
walls. After that, a bit of filler added
here and there would be all I’d have
to do to prep the walls for painting.
Except, of course, it didn’t work
out like that (but you probably knew
that already). It turns out that the fibres used in fibrous plaster are made
of the same stuff used to sew Superman’s cape and underpants together.
Nothing short of a freshly-stropped
straight razor would cut them and
then only by direct perpendicular
pressure from blade to bristle. This
also left more marks on the wall.
At the rate I could trim hairs back,
it would take until Christmas 2019
before I’d done half the room so I
called in my builder friend Dave for
some advice. He told me that the best
solution was to put what he called
a “skim coat” of plaster on the wall.
Once we had that, we could then
prime, paint and be done with it
Anyway, as usual I digress. One
of the other reasons I stopped my
initial sanding was that the dust
being generated choked everything.
While the sander itself has a dustextraction nozzle, which I married up
to a backpack-style vacuum cleaner,
even this set-up couldn’t cope with
the sheer amount and texture of the
plaster dust. It was as fine as talcum
powder and it spread out every
where. What’s more, the vacuum
cleaner’s bag choked after just a few
minutes, rendering it useless.
So what’s all this got to do with
my air-compressor? Well, another
problem I encountered was that the
sander got so hot I couldn’t hold onto
it and that was only after 10 minute’s
sanding. So it was out to the workshop to clean those tools and filters
with my trusty air-compressor, only
to have it run out of puff after a just
few seconds of cleaning.
Thinking that I must have a loose
power lead, I checked the connection
but that seemed to be in order. I then
tried switching the compressor off
and on again, only for it to start and
then immediately stop. Just what I
needed – a faulty air-compressor.
siliconchip.com.au
Mildly annoyed because my plans
for that afternoon hadn’t included
stripping down the air-compressor, I
pulled it out from its new hidey-hole
and lifted it onto the bench. This machine is one of Dad’s old compressors
and isn’t one of those cheap units that
are available these days. On the contrary, it’s a high-quality Italian-made
unit with impressive specifications
for such a small unit.
Usually, with a compressor, it’s
the seals and gaskets that wear out
and you simply replace them to get
things huffing and puffing again. As
a result, I stripped it down with the
aim of doing just that. The head of the
pump was held on by four long bolts
and they were soon out and the head
lifted clear. This revealed what looked
like stainless-steel spring valves, all
embedded into the head itself.
Inside the pump body was a piston and con-rod assembly. However,
instead of a gudgeon pin joining the
two parts together, the piston and
con-rod were a single forged item,
with a hard-rubber and plastic ring
arrangement built into the crown of
the piston. An electric motor ran the
crankshaft directly, driving the piston up and down in the aluminium
(yes, aluminium!) sleeved bore.
Due to the very short stroke, the
crown of the piston simply pivoted
from side to side as it moved up and
down inside the bore, relying on the
seal to make and keep contact with
the bore all through the stroke. It was
a nice, simple system but one that’s
prone to wearing out pretty quickly
I’d imagine.
I was going to need a new piston
and bore, plus a new head assembly,
and that sounded expensive to me.
There was a service sticker on the
compressor so I dialled the number
only to discover that it was now
disconnected. I then hit the Internet
and discovered that the company in
question had shut its doors in 1997,
after more than 50 years operation.
I then found the manufacturer’s website and
sent off an email asking if they had an NZ
agent. A week later, I
received a response
which recommended
I contact a Hamilton
company, which I did
but they dealt mainly
in $10,000 plus air
systems and weren’t
overly interested in one
small compressor.
After a bit more searching, I found
another company who had the
compressor manufacturer’s logo on
their website, so I emailed them and
received a prompt response asking
me what model I had. I’d included all
that detail in the first email, so they
obviously hadn’t read it carefully.
I repeated what I’d previously told
them and after some email to-and-fro,
they finally sent me some explodedview diagrams of the pump unit.
I went through them and supplied the relevant part numbers plus
photos and details of my worn-out
parts as well. That was weeks ago
and despite sending off two emails
in the interim, I’ve heard nothing.
In the meantime, I still needed an
air-compressor and so I ended up
shelling out for a budget one which
did the job nicely. If I ever hear back
from the parts company, I expect that
the replacement parts for my Italian job will cost far more than this
new compressor but I’m hoping I’ll
be pleasantly surprised. I’ll let you
know what happens.
Last week, a chap brought in two
rather large, powered PA speakers, complaining they had blown
woofers. They’d been using the
speakers at a function and according to the owner, they hadn’t been
playing them “that loudly” when
suddenly the sound level dropped
dramatically and became “tinny”
and “screechy”.
After connecting a signal injector
to each amplifier’s input, I quickly
confirmed that the two big 15-inch
woofers had indeed stopped working. A bit of research then revealed
that these speakers are supposed to
be able to cope with 150W RMS and
I soon found suitable replacements
on an online auction site.
The owner subsequently purchas
ed the required units and brought
them around for me to fit. They
were about twice the weight of the
old ones and the voice coils half as
big again. Given the difference, I’d
estimate the original speakers to be
100W maximum, though the stickers
on the plastic-moulded speaker cases
claimed they delivered up to 800W!
In my opinion, they might get
to 800W peak music power output
(PMPO) but certainly not 800W RMS.
Swapping the speakers over was
a doddle; I simply removed the 10
large screws holding each woofer in
place, pulled the old speakers out
and slipped the new ones in. Pushon terminals had been utilised for
the speaker connections but as the
terminals seemed rather flimsy, I cut
them off and soldered the output wiring directly to the speaker terminals.
Once both were done, I paired
the speakers with my phone using
Bluetooth and gave the neighbours a
short demonstration of my favourite
music.
light (or something else) in the house,
the engine came to life and supplied
240VAC power. It then automatically
shut down again when the last appliance was turned off.
I was informed that every electrician
they could get had looked at the thing
and none of them could fix it. The
problem was that the engine would
start OK, the voltage would start to rise
and then the engine would go into its
shut-down routine.
Ah-ha, I thought. No wonder the
electricians couldn’t fix it; what would
they know about air, fuel, compression
etc? This was going to be easy. And
so I began my checks. The air-cleaner
was OK, the fuel tank was full (and
it was diesel, as it should have been)
and compression could be felt when
turning the engine over by hand. Of
course, ignition in a diesel has to be
taken on faith unless there is an obvious mechanical failure.
siliconchip.com.au
PA speakers
April 2016 57
Serviceman’s Log – continued
This photo shows the
burnt-out windings in
the toroidal transformer, caused by a hotspot
created by the insulation under the thermal
sensor.
There was only one thing left; the
engine muffler must be blocked. My
theory was that as the exhaust pressure built up, there was nowhere for
the exhaust to go and the engine was
choking itself.
At this stage, I needed to go back to
my car to see if I had enough tools to
strip down the exhaust system. As I
walked back down the yard, I noticed
that the junior members of the household were having great fun kicking
a football over the open power lines
going to the house. And then I saw
it; they had managed to twist the two
wires around each other.
This meant that as the voltage came
up, the control circuit sensed an excess load and rather than burn out the
alternator, it shut down the engine. I
grabbed a long stick (quite safe with
the engine not running), sorted out
the twist, then went back to the engine shed and flicked the light switch.
The engine sprang into life, the lights
came up and the owner came tearing
out of the house. “What, you’ve fixed
it already? You’re as smart as Rodney
said you were!”
After that praise, it was indeed hard
to tell him that it would be better if his
offspring kicked the football around
the other side of the house.
Digitor T-1333 sound system
Protection devices can be added to
transformers and electronic circuits
with the best of intentions but they
themselves can also be the cause of
puzzling faults. A. L. S. of Turramurra,
NSW recently encountered one such
puzzling situation . . .
My daughter recently complained
that her Digitor T-1333 Sound System
would not turn on. She used it when
watching movies in her bedroom; it
58 Silicon Chip
was small enough to fit around her
dressing table and she also liked the
sound.
I had previously repaired this unit
about four years ago and this had
involved replacing a blown toroidal
power transformer. As a quick check,
I removed the 1A fuse and it was
completely black. This indicated a
catastrophic short circuit, as per the
previous fault.
So it was the same symptom but how
could it be the transformer again? I told
her that it may be the same problem
and suggested that the repair may not
be worth it. “No no!”, she said, “it is
just the right size for my room and
the tiny speakers fit in all the right
places”. Then with a tilt of the head
and a smile she pleaded: “Please, can
you fix it for me?”
How could Dad say no?
The unit itself has a switch for
“aux/5.1 surround” and a ganged volume control for five amplifiers which
are basically five LM1875 power amplifier chips for front left & right, centre
and rear left & right. Another LM1875
feeds a subwoofer and all of this is
mounted inside the subwoofer speaker
box which fits neatly into a bookshelf.
There are five external speakers included with the unit, each of which
is only marginally bigger than a can
of baked beans and has a single 75mm
driver unit (ie, no tweeter).
Power for the unit is derived via a
120VA toroidal transformer, which I
had previously upgraded to a 150VA
unit. This has a 12VAC secondary
which is fed to rectifier diodes and two
4700µF electrolytic capacitors for the
power amplifier.
At the time, I felt that the larger transformer would offer more protection. It
was also labelled “heat protected” and
120VA units were no longer readily
available.
Because of the new transformer’s
higher rating, I was very confident
back then that the unit would be more
reliable than before. I certainly never
expected it to return with what appeared to be the same fault!
I dismantled the amplifier unit
and checked out the primary resistance of the transformer. And just as I
suspected, it was open circuit! I then
proceeded to replace it, which was a
fairly easy job as I had done it all before.
As soon as power was applied, the
unit sprang to life and all the channels
and the subwoofer worked perfectly! I
was, however, rather worried because I
had already upgraded the transformer
and it should have been virtually
bullet-proof. So why had two transformers now burnt out and would the
latest replacement be reliable? After
all, it was identical to the previous
transformer and there was no room
for a beefier unit, rated at say 300VA.
What’s more the unit only drew a
maximum of 70W, which is well within
the transformer’s rating.
But what if something peculiar was
going on inside the unit and it got some
“killer” stress from another part of the
circuit – would this destroy the transformer again? My thoughts were that a
thorough investigation was necessary
to see if there was a hidden fault and
that a long soak period would not be
enough to prove it one way or the other.
After fitting the new 150VA toroidal
transformer, I decided to check out the
rest of the circuitry for possible problems. The first stop was to check each of
the five LM1875 ICs and all the voltages
were fine. There are two 3.15A fuses
between the transformer secondaries
and the rectifier diodes. These were
OK, indicating that there was little or
no stress from the amplifier chips.
LM1875s have very good protection
against heat and short circuits and
any faulty loudspeakers couldn’t hurt
the unit unduly. So, what could the
underlying problem be? In the past,
I have replaced many toroidal power
transformers from 25VA up to 300VA
and all of them had blown primary
windings, probably due to the higher
voltage and the small diameter wire
on that side. This is nearly always
due to manufacturing problems such
as pinholes in the insulation, or damaged or faulty wire.
In fact, one year, I replaced over 100
siliconchip.com.au
power transformers in just one model
of TV (all under guarantee) due to
faulty manufacture! If a customer rang
up and said that they had smoke and
a nasty smell, I could invariably get
the repair done in minutes once I had
arrived at the scene!
However, in the case of this Digitor, I
was not entirely convinced it was due
to faulty manufacture of the transformers. After all, there were two different
manufacturers involved, so surely I
wasn’t that unlucky?
The next step in my investigation
was to check each of the six LM875s
for total harmonic distortion and noise
(THD+N). If there were any damaged
chips, or voltage supply problems, or
a lack of cooling, the distortion and
noise levels would be very high. This
only took a few minutes on my Audio
Precision ATS-1 test set and they all
came through with flying colours.
Next, I decided to have closer look
at the burnt-out transformer. This had
the words “130deg Thermal Cutoff”
printed clearly on the side. What if it
siliconchip.com.au
had failed simply because the thermal
device had cut out and either hadn’t
reset or wasn’t a resetting type?
There was only one way to find out:
unwind the transformer and examine
the thermal cut-out.
After removing all the exterior insulation and the heavy secondary windings, I began to question my own sanity
for doing all this. However, I managed
to justify it because the secondary wire
is over 1.5mm diameter and I find it
very handy to keep for those repairs
which need heavy-duty wiring.
When the primary winding was
exposed I could clearly see the burntout wires. Amazingly, they were only
about 20mm away from the thermal
device, an “AUPO A4-3AN3 130°C
250VAC” made by Xiamin Electronics Ltd. This device is about the size
of a small transistor and it goes open
circuit at about 128-132°C and stays
that way until the temperature drops
back to about 100°C.
As usual, the thermal cut-out had
been soldered in series with the pri-
mary windings. However, the manufacturer had also sandwiched it between
some rather thick cardboard to insulate
it from the secondary windings but, in
doing this, had inadvertently insulated
it thermally as well! So what happened
is that a hot spot developed under the
cardboard and this had eventually
caused the primary windings to short
circuit and burn out!
So it would seem that the transformer manufacturer had actually created
the problem. By trying to protect the
transformer using a thermal cut-out
device, they created a “hot spot” due
to the arrangement used, which caused
the windings and insulation to fail.
Now that I felt sure that I knew what
the problem was, I introduced some extra ventilation around the transformer
to try to keep it cool. We’ll have to wait
a few years to see if works though.
In the meantime, I’ve examined the
two dozen or so toroidal transformers
in my stock and I’m happy to report
that none of them have “heat proSC
tected” printed on the side.
April 2016 59
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