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SERVICEMAN'S LOG
The ISP help desk from hell
Arranging an internet service for our new
house while keeping an existing service for
our current house should have been a simple
procedure. Not so for our local ISP provider
who have just put me through help-desk hell.
It’s been a rough month; once again,
I’ve been thrust into the public hospital system, though this time my Dad
is the patient.
I’ve mentioned Dad before in the
context of the Serviceman’s Log as
the most influential of my mentors,
teaching me engineering from a very
early age and planting the seeds that
grew into a fascination of all things
mechanical and electronic. To see Dad
in his present state is terrible but as I
write this, his prognosis is cautiously
optimistic, which is miraculous considering he suffered what is typically
a non-survivable event.
As if things weren’t difficult enough,
my wife and I are currently renovating
a recently-purchased house and workshop across town. When completed,
it will become our new home and my
new workplace.
If you’ve ever renovated anything
larger than a hall closet, you’ll know
that it’s an enormous job. And along
with all the tasks there are a hundred
other little things to be done, such as
arranging phones, insurance, an internet service, power and gas and so on.
However, things didn’t go too smoothly when I called our internet service
provider (ISP) to arrange for the internet to be connected at the new house.
At the moment, we have a relatively brisk 50Mb/s cable connection
that allows us to browse the web and
download stuff with no pesky waiting. It was natural then for us to want
a similar broadband set-up at our new
place. The company that originally set
up that cable network had sold out to
another company a few years ago but
our custom had simply been transferred across to the new company and
everything had carried on as normal.
The cable Internet ring around
Christchurch was installed around 10
years ago and yet strangely, many areas
of the city aren’t covered. I clearly remember the salespeople door-knocking
everyone in Christchurch at the time
and as I understood it, if two households on any given street signed up
for the proposed new cable service,
the telco would run the cable down
that street. This meant that some small
streets offered it while some larger
thoroughfares didn’t.
No cable
Unfortunately, our new address
doesn’t have the cable laid, so cable
Internet simply isn’t available. As luck
would have it though, this new ISP offers
Ultra-Fast Broadband (UFB) and with
plans including 100Mb/s and 200Mb/s
Servicing Stories Wanted
Do you have any good servicing stories that you would like to share in The Serviceman column in SILICON CHIP? If so, why not send those stories in to us? In doesn’t
matter what the story is about as long as it’s in some way related to the electronics
or electrical industries, to computers or even to car electronics.
We pay for all contributions published but please note that your material must
be original. Send your contribution by email to: editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
siliconchip.com.au
Dave Thompson*
Items Covered This Month
• Dave’s help-desk hell
• Rolling machine repairs
• Faulty Australian Monitor
AMC+120 audio amplifier
fibre-optic connections, this seemed
like a more than decent alternative.
However, when I called to ask about
it, the help-desk lady apologised for
the fact it would take at least eight
weeks for UFB to be connected to our
new address. As we’d be in the house
long before that, they could offer us a
“standard” ADSL connection in the
meantime. It would only give us a paltry 10Mb/s on a good day with a tail
wind but it was better than nothing.
After some thought, I agreed to this
arrangement and rang off with the understanding that the technician who
was to connect the ADSL would call
me the following day to arrange a site
visit. The next few days then passed
quickly, with most of my time taken up
with tearing out a very dated kitchen,
laundry and bathroom so that renovations could begin.
As arranged, the phone contractor eventually called and said that he
would be around to wire up the place
the following day. He duly turned up,
connected everything in place and a
quick test with the new modem they
had previously couriered out to us
proved that we were online. Now we
just had a few more weeks to wait for
the UFB connection to be installed!
My mood darkens
I was happy with the new ADSL
connection but my mood quickly
darkened when I got home that afternoon to our “old” house (which we
are keeping) to find that the internet
was down. With a sense of foreboding,
my first thought was that they’d cut
us off instead of keeping the current
connection alive as arranged. My suspicion was that they’d done a service
August 2016 57
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ceman’s
man’s Log – continued
“relocation”, which of course meant
cutting us off “here” when connecting us “there”.
I hate calling help lines at the best
of times; it’s often difficult to get any
thing done, even after you actually get
through to someone. Therefore, it was
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58 Silicon Chip
with dread that I telephoned the ISP’s
help desk and after the obligatory waiting period and ghastly piped music,
the operator confirmed my worst fears.
That was when I could actually hear
what she was saying; she was so quiet
on the line that I had to keep asking
her to speak up!
Finding out that they had indeed
made a mistake was something I
didn’t need to hear at that time of the
day; we were under enough stress as
it was. That said, I could accept that
they had made a mistake but I now
wanted them to rectify it and to do
so as quickly as possible. I’d already
spent some 15 minutes on hold before
they’d answered and my mood was
rapidly deteriorating.
My suggestion at that point was to
get whoever disconnected us to reconnect it, as my wife needed the internet
to work from home the next day. After
again asking her to speak up so that I
could hear what she was saying, she
then put me on hold while she went
and asked someone what was going
on. After another 10 minutes, she was
back and said that she was transferring me to the contractor who had, in
her words, “climbed up the pole and
disconnected us”.
At least, I think that’s what she said.
I admit that my hearing is not the best
after years of playing in bands and
spending my teen years racing model
aircraft with very noisy motors but
I was sure that it was her low voice
(and not my hearing) that was causing
our communication difficulties. Quite
simply, that bit about climbing up the
pole didn’t sound right to me but what
would I know? Perhaps that’s how they
did it with cable connections?
All I knew was that I could ping my
modem and gateway, so it seemed we
were still physically connected to the
system at any rate. I just couldn’t send
or receive any data through it,
After another holding period, where
the recorded message chimed in over
the music every 30 seconds to tell me
that my call was important, an operator answered. When I explained the
whole story to him, he said he had no
idea why the ISP would bounce me to
them because they could do nothing
without an order from the ISP. What’s
more, he informed me that they controlled the cable connections and nobody climbs up poles to connect or
disconnect subscribers.
As can be imagined, I was rather
miffed by now but managed to stay
nice and calm while I was transferred
back to the ISP. Eventually, after another wait, the same quiet woman answered the call and after a brief recap
of what the contractors had said, put
me on hold yet again to go and talk to
her manager. I was certainly rediscovering why I so dislike calling so-called
help desks but since I still had a good
hour before the close of business for
the day, I was cautiously optimistic of
being reconnected that evening.
When the operator came back, I
again had to ask her to please speak
louder so that I could hear her. She
then began by saying that the only
way we could get reconnected was to
apply for a new connection. When I
asked how long that would take, she
replied “a couple of weeks”!
I couldn’t believe it. This was so obviously not a resolution to this problem that I almost laughed out loud. I
asked her if she would be happy with
that if she was in my shoes but I didn’t
hear what her answer was.
By now, I’d had enough and asked
to be put through to her manager. She
responded that it was her manager
who had told her to offer a new connection and despite my insistence that
I wanted to speak to someone else,
she seemed very reluctant to put me
through. And she again told me that
a contractor had come to our address,
climbed the pole and disconnected
us, and it wasn’t simply a matter of
siliconchip.com.au
him coming back and hooking it up
because they’d moved our service to
our new place.
She then offered to put through another relocation order and have the
service moved back but as this would
also take a few weeks, that wasn’t going to fly. I interrupted her, my manners fast disappearing and demanded
I talk to her manager. She put me on
hold for another five minutes before
returning and telling me he had gone
home for the day.
No call-back
Eventually, after further argument
and more gnashing of teeth, she told
me that she would have to talk another
manager. She also told me that she
would call me back within the hour.
Three hours later, I finally accepted
that she wasn’t going to be calling back.
So much for their help desk. It was
now obvious that we’d be without an
internet service for the night, which is
of course a first-world problem and no
real biggie for us. However, it meant
that I’d have to call first thing in the
morning and argue the case again if
Nina was to have connectivity the next
day so that she could work from home.
Round two the next morning initially couldn’t have been more different. Unlike the previous evening, I got
straight through to a young technical
operator who scoffed when I reported
what his colleague had told me the
previous day. And he was horrified to
learn that she didn’t call back.
He checked the records and discovered that she hadn’t notated any of
the conversation we’d had, so he was
in the dark about what the problem
was. When I told him, he said that all
they needed to do was to reactivate
the connection in their system and
we’d be away.
As he was talking, I could hear him
typing and after about 30 seconds he
asked me to reboot my cable modem
and see if we had connectivity; I did
and the world was once again at our
fingertips. But why couldn’t that silly
woman I’d spoken to the previous day
do that or at least put me through to
someone who could? It was all quite
baffling and left me more than a little
annoyed. I was very satisfied with this
guy’s help though and when he asked
me if there was anything else he could
help me with, I asked him about the
UFB connection at the new place.
He again looked through the records
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and discovered that no order had
been placed for it to be installed!
As I said earlier, I had previously ordered the UFB installation
weeks ago when the ISP representative made arrangements
for the stop-gap ADSL service. It
now had to be reordered which
meant that we would be bumped
back to the end of the queue.
These companies exasperate
me! They make millions and
their CEOs enjoy a privileged
lifestyle, yet they continually
fall short with customer service.
Anyway, he said he’d have to
transfer me to someone who
could help with that and after a
short hold period, who should
come onto the line but the same
woman from the day before! And
I still couldn’t hear her!
After asking her to yet again please
speak louder, I outlined what we want
ed for the new place, which was to
get in the queue for UFB. She went
through the same questions I had answered weeks previously but for the
sake of not making waves, I patiently
answered them all again.
It all went OK until she asked
whether we’d be having a monitored
alarm and then things started getting
weird. I answered “yes” and then
she said they couldn’t give us UFB
because they couldn’t guarantee the
alarm monitoring would work. I told
her that the alarm used the phone line,
which was a completely separate system from the fibre that was yet to be
installed, so it wouldn’t matter. She
told me that the engineers would remove the copper line system altogether
before installing fibre, so that would
affect the alarm.
Thoroughly taken aback by this, I
told her that another telco provided
those copper wires and that we were
happy with their service. I also told her
that I seriously doubted that their contractors would remove another telco’s
wires but she was adamant that they
would remove the copper lines altogether. By this time my blood pressure
was dangerously high, so my wife, who
had been listening over my shoulder,
took over the conversation.
Nina couldn’t make much sense of
what she was saying either but it appeared that the operator was trying to
tell us that in order to have UFB connected, we had to ditch our current
telephone provider and use their sys-
tem instead. And that sounded completely wrong to me. Their website
contradicted everything this woman
was saying, so we went through the
whole “let me speak to someone else
malarkey” before Nina simply hung
up when it became obvious that she
wasn’t going to put us through.
We ended up going to one of their
stores in the local mall and after 10
minutes’ conversation, we were in
the queue for UFB, with our existing
copper lines intact. This has to be my
worst help-line experience ever and I
won’t be calling them again any time
soon.
Rolling machine repairs
A couple of rolling machines recently provided a real challenge for G. S.
of Montrose, Tasmania but he was able
to eventually get them rolling again.
Here’s what happened . . .
I was recently called out to check
a “D” profile gutter-rolling machine.
The operator complained that he was
getting a shock at times when feeding
the steel into the machine, so the job
was urgent.
The feed arrangement was fairly
simple. First, the flat metal strip was
pushed into the machine by hand until
it engaged the first set of rollers. The
operator then used an “inch” button
located on the side of the machine,
behind a low steel handrail, to mechanically drag the strip in a little
further, after which the machine was
ready to run.
Sometimes, however, he needed to
lean over the handrail and give the
August 2016 59
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man’s Log – continued
Faulty AMC+120 audio amplifier
Nobody likes a trip to the dentist but
music can help calm those waiting-room
nerves. G. C., of The Gap, Qld was recently
called on to fix the audio amplifier in one
such practice and unlike the patients, it put
up quite a struggle . . .
My eldest son owns a busy dental practice in a Queensland coastal town and to
soothe the nerves of his trembling patients,
he plays relaxing music via an Australian
Monitor AMC+120 amplifier. He tells me
that the amplifier is now many years old and
was repaired by the manufacturer’s agent
just over two years ago. When it failed again
recently, the agent had a look at it and advised my son to replace it, given “its age”.
So, on his next trip to Brisbane, the amplifier was duly delivered to me to see if it was
indeed uneconomic to repair. The first thing
I noticed about it was its not insignificant
weight, due mainly to a very large power
transformer and a large toroidal-core output transformer for the 100V speaker feed.
When I subsequently removed the top
cover, I noticed that it had three PCB assemblies: (1) a preamp board catering for
four inputs, (2) a mixer and tone/volume
control board and (3) a main amplifier and
power supply board. These boards were
daisy-chained together by ribbon cable,
each terminating in a plug/socket assembly.
Switching the unit on, I found that it was
as dead as a doornail with not even the
power indicator LED lit. It was soon apparent that the 8A DC fuse was open circuit but
the 2A AC fuse was intact. What was surprising though was that the DC fuseholder
had partially melted. I also discovered that
solder from the ends of the ceramic M205
fuse had been deposited into this fuseholder,
so clearly there was a major fault.
I checked every semiconductor on the
main amplifier board but couldn’t find any
short circuits. The fuseholder had a minuscule amount of metal touching the fuse-caps
so I surmised that the contact resistance
led to heating and subsequently complete
failure. I replaced the fuseholder with one
which had a large contact area, so hopefully this type of failure will be eliminated
in the future.
On the main board there were four 2-way
screw terminal blocks. One of these was
used to terminate leads from the power
transformer and had melted due to a very
loose connection. By contrast, its companion terminal block was fine.
After this part had been replaced, I turned
my attention to the electrolytic capacitors
on the main board. There were only six
and two had an unacceptably high ESR so
I replaced all of them.
In order to test the amplifier, I connected
the output to one of my Wharfedale speaker
boxes. Unfortunately, it had appreciable
mains hum and when the volume control
strip a bit of a nudge to get it moving
and this is when he was receiving the
shocks.
The steel rail was bolted directly
to the floor and had no connection
to the machine. I checked the voltage
between the rail and the machine and
there was no reading to speak of but
that all changed when the inch button was pressed. As the speed control
ramped up, so did the potential difference between the machine and the
handrail, the reading quickly heading
for 100V or more.
So what was going on? The control cabinet was a free-standing metal
console type enclosure with a number
of disused buttons and switches. It
looked as though it had been salvaged
from some other machine and the installer didn’t bother to clean it up.
I opened the control cabinet to be
greeted by an ancient VSD (variable
speed drive) and a rat’s nest of wire, all
liberally covered in hydraulic oil and
caked-on dirt. The earthing arrangement consisted of a stud on the case
with the clamp nut almost completely
unwound. It was probably only being
kept in place by the dirt lodged in the
last couple of threads!
I cleaned it all up and clamped
down the earth properly but it made no
difference to our problem; the voltage
between the machine and the handrail
still climbed with the VSD speed.
Next, I checked the earthing between the control cabinet and the
machine and found there wasn’t any.
I fitted a temporary earth and the
voltage disappeared. That meant that
there had to be a problem with either
the VSD, the motor or the connecting
cable (or perhaps all three).
60 Silicon Chip
was advanced to near maximum, the unit
squealed but not with delight. I disconnected the cable between the mixer board and
the main amplifier and it was as quiet as a
mouse. However, when I re-connected these
two boards but disconnected the preamp
board, the hum and instability remained.
This indicated that the problem was due
to a fault on the mixer board. This board
had 23 electrolytic capacitors and I checked
each for capacitance and ESR. All were
within tolerance. I then discovered some
poor-looking solder joints, so I re-soldered
the entire board. During this process, one
of the copper pads around the lead of an
electrolytic capacitor literally fell off and
had to be repaired.
Feeling hopeful that the hum problem had
now been cured, I re-installed the board and
switched the amplifier on. However, there
was no improvement.
I don’t know why but I only seem to use
my oscilloscope as a last resort. I stoked it
up and found that the power supplies were
clean and that there was little noise on the
op amp inputs and outputs. In the end, all
my prodding and probing revealed nothing
and so my inherent reluctance to use an
oscilloscope felt validated.
By now though, there was a bell ringing
but I only heard a faint tinkle until I finally
realised that it might be an earthing problem.
There were two earth leads in the ribbon
cable between the main amplifier and the
mixer boards and I checked the continuity
of these with my ESR meter. They were intact, as were the earth leads from the mixer
to the preamp board.
I placed a clamp meter on the feed
earth to the machine and ran the motor
at full speed. The current increased to
over 2A, so there was current leakage
somewhere. The VSD was not complaining about earth faults but it was
an old unit and might not have had
the internal diagnostics to indicate
that sort of problem.
No cable screening
The motor was a very nice 18kW
ASEA unit in very good order. However, the motor cable wasn’t screened and
was simply lying on the floor soaked
in oil and subject to all sorts of abuse.
In the end, we decided to stop chasing the fault and to rebuild the control
gear. He had purchased a number of
old machines over the years and we
had salvaged quite a bit of equipment
that was still in good order. This meant
siliconchip.com.au
The preamp board itself was earthed to
the chassis via a cable that was terminated in
an eyelet at the chassis end and clamped by
a metal-thread screw. When I checked this
earth, I discovered that it was open-circuit,
mainly because the black powder-coated
finish on both sides of the chassis had not
been removed. Even though serrated washers had been used on both sides, they had
obviously oxidised over time.
I fired up my trusty Dremel and ground
the coating off both sides of the chassis,
then reattached the earth wire. The earth
resistance then measured just a couple
of hundredths of an ohm. I also checked
the mains earth which had been installed
the same way as the signal earth. It read
just 0.2Ω but I removed it and ground off
the coating to ensure its reliability, before
reattaching it.
This time, when the amplifier was switch
ed on, the hum and instability were completely absent. However, when I connected
a CD player to the amplifier, I was dismayed
to find that the sound was extremely distorted at lower frequencies. I tried to borrow
a neighbour’s audio function generator to
help troubleshoot this problem only to find
that it had died quite some time ago.
As an afterthought, I connected the amplifier to my other speaker box and was
greeted with perfect sound at long last. It
turned out that the woofer in the first box
that I used was poling badly and will need
extensive surgery. These Wharfedale speakers (E50 Series) are only 35 years old, so
it just goes to show that they don’t make
things the way they used to!
that I was able fit a reasonably new Italian Santerno VSD, Swiss-made control
buttons, Japanese circuit breakers, a
Korean-made length-measuring counter and a German-made encoder into
a the console, along with a new fullyscreened cable to the motor.
That got it all running nicely again
and there were no further shocks.
Following my success with that
job, I was then called out a couple of
weeks later to look at a fascia rolling
machine. This is a similar set-up to the
gutter roller but uses different roller
profiles and was made by a different
manufacturer. The machine was still
working but was it making a racket
that sounded rather like a collapsed
bearing in the motor, clutch or gearbox.
Unlike the gutter roller, there was
no speed control. Instead, the motor
ran continuously and was connected
siliconchip.com.au
to a very large worm-drive gearbox
via an air-driven clutch/brake system.
It wasn’t super accurate but it didn’t
need to be.
In order to troubleshoot the problem, we needed to pull the motor and
gearbox assembly out. Unfortunately,
it’s all buried down inside the frame
of the machine, which is essentially a
large steel box with all the roller stations bolted on top and coupled up by
large (100mm) bike chains. That meant
that in order to get to the motor, these
roller stations had to be removed.
Welded roller stations
Unfortunately, whoever built the
machine had way too much faith in the
longevity of the power train and had
decided to weld the roller stations in
place. As a result, it took a fair bit of
grinding to remove the stations, after
which a crane was used to remove the
motor/gearbox assembly.
We soon found that the fault lay in
the clutch unit. Its bearings were seriously damaged but it was too old to get
an off-the-shelf replacement, which
meant that a new one would have to
be made. The owner then decided that
it wasn’t worth repairing and instead
asked me to make up a new control
panel with a proper speed control, just
as I did for the gutter rolling machine.
After digging through his store of
parts, I came up with a SEW VSD,
another Chinese-made cabinet and a
few assorted switches. The only parts
I needed to purchase were a new encoder and a counter.
It all went together quite well and
I even managed to find a book for the
VSD, so I was able to get that programmed without too much trouble.
It all seemed to work OK, so the roller
stations were welded back into place.
We didn’t have time to come up with
a different mounting arrangement,
because by now there was a backlog
of work and we needed to get the machine back into operation.
Some time later, the machine’s operator reported that the counter was
freezing every now and then (and
without warning), which meant that
it wasn’t shutting the roll off at the set
length. This was a real problem when
specified 12m lengths kept on going
and hit the factory wall. As a result,
the operator was now hanging over
the emergency stop button just in case.
Interference
It was all a bit of a mystery but I
suspected interference from the VSD,
as this unit didn’t seem to have any
EMC components built in. My guess
was that noise was probably finding its
way onto the encoder cable which was
quite long, so I clipped a ferrite choke
around it. That seemed to improve
things but it wasn’t a complete cure.
In the end, I took the “more is better”
approach and clipped ferrite chokes
around the power supply and control
wiring leading to the counter, plus an
extra one on the encoder cable. That
did the trick and the machine now
performs without any problems. SC
August 2016 61
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