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SERVICEMAN'S LOG
Two crook MacBook Pro laptops
A failing battery pack is a fact of life for
laptops once they’re more than a few years
old. Most aging batteries simply fail to hold
a charge but some can fail catastrophically
and damage the laptop’s case in the process.
A few weeks ago, a long-standing
customer called to ask if I would have
a look at a couple of malfunctioning
Apple Mac laptops belonging to his
daughters. While he knows I focus
mainly on Windows-based computers, he was enquiring on the off-chance
that I might at least give them a quick
once-over and perhaps even get them
working again.
As this chap is a loyal customer of
mine, I couldn’t really say no and one
of his daughters duly brought the two
computers in to the workshop. Both
were Apple MacBook Pro laptops and
one of them looked as if it had been
run over. I immediately assumed (even
though I know assuming makes an
“ass” out of “u” and “me”), that it had
been dropped and I opened the conversation with that observation.
The young lady, who was the worried owner of the bent MacBook, was
adamant it hadn’t suffered any such
event. This puzzled me, so I asked for
more information. She told me that
she was working with it the day before and it had just stopped working
by turning itself off. She had managed
to get it going again but when it booted, an error dialog popped up stating
58 Silicon Chip
that the date and time were incorrect.
It then died again but not before she’d
observed that it hadn’t automatically
logged onto their WiFi network, which
it usually did on start-up.
After that, she couldn’t get it going
again and thinking that the battery
might be flat, she put it on charge and
went out to do some chores. When she
returned just a couple of hours later,
the laptop’s case was twisted and distorted and the touchpad assembly was
protruding from its enclosure, as if it
had been punched out from the inside.
The other machine belonged to her
sister and it too had ceased working
properly, though this one had the infamous Mac grey screen of death, indicating an issue with either the operating system or the hard drive.
The two machines were identical devices around four or five years old and
apart from the obvious damage to one
machine, both appeared to have been
very well looked after. By now, I was
keen to find out what had happened
to them, especially the damaged one.
That one had really piqued my interest.
One of my initial thoughts was some
kind of paranormal event. OK, I’m just
kidding but it did fit – a laptop goes
from happily working to physically
ruined within a matter of hours, without anyone so much as touching it.
And there’s even a teenager or two in
the house to act as a “focus” so what
else could it be?
Of course, in the real world there’s
a rational explanation for everything
and I’ll wager that many readers have
already guessed what had happened
here. I’d heard of it many times in
the past but had never previously encountered an actual “live” case in the
Dave Thompson*
Items Covered This Month
•
Battery problems in a MacBook
Pro laptop
•
•
•
Vintage AWA B&W TV set
Denon twin-drawer CD player
Fan cooling for a Sony LCD TV
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
workshop. And that’s surprising, given the number of years I’ve been doing this stuff.
As with all Macs, the internal circuitry is accessed by first removing
the plate aluminium back (or base).
True to form, there were a dozen tiny
(but different-sized) screws holding
the base on and one has to take note
of their positions and be careful not to
swap them around during re-assembly.
Unfortunately, because the base on
this laptop was twisted and seriously
puffed up, removing the screws was an
act in itself. I had assumed that as soon
as the tension on the screws caused by
the warped case overcame the strength
of the remaining threads holding the
screws in, everything would let go and
the threads would be stripped or otherwise damaged. So, to counter-act this
force (and prevent further damage), I
maintained a lot of downwards pressure on the screws with the driver until I felt them clear the threads. Only
then was the case allowed to slowly
pop open.
However, after the first couple of
screws had been removed this way,
instead of the pressure decreasing, the
warped back was putting even more
tension on the remaining screws. As a
result, I now used elephant tape (I’m
assured no elephants were harmed in
the making of this tape) to bind the case
together and take the tension while I
removed the remaining screws, adding
a strip of tape as each screw came out.
With the back off, it was patently
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obvious what had happened; the battery, which takes up almost the entire
bottom third of the area inside of the
case, had become seriously distended.
In fact, the plastic case that usually
held the individual cells together had
completely ripped open, with a couple
of the cells inside the opened package
looking like small pillows.
These two cells are usually about
4mm thick; now they measured 40mm!
They were at the centre of the 6-cell
package and it appeared that they were
the only ones that had failed in this
manner and had caused all the internal pressure.
The chassis of this laptop is made
from cast aluminium, while the case
components are sheet aluminium and
plastics. When these are sandwiched
and screwed together, the result is a
very strong unit but when the cells began expanding, they had nowhere else
to go but outwards.
Basically, they took the path of least
resistance, which explains the distorted chassis and pillowed bottom. Furthermore, because the touchpad assembly sat immediately above the battery, when the cells beneath swelled,
the touchpad simply popped straight
up and out through the hole it usually sits in.
Battery mounting
The plastic frame of the battery locates into the chassis with embedded
tabs along one side, while three screws
on the other side secure it in place. A
sticker warns users not to remove the
battery, something a bit tough to comply with in this case!
Since the battery’s plastic enclosure
had no chance of containing the innards when they “went off”, it simply
snapped apart at the weakest points.
The mounting lugs had broken off from
the case and were all still held fast to
the chassis, left behind when the rest
of the plastic case went west. To make
matters just that bit more complicated,
the screws were those annoying antitamper types that many manufacturers
love so much.
If you want to work on Apple products, then you’d better have a good set
of specialised screwdrivers. That’s because Apple uses lots of different antitamper “security” screw types. In this
instance, the screws holding the back
on (and those used in other locations
inside the device) are tiny and appear
to be a type of Frearson-head screw,
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similar to a very narrow Phillips style
head. A small Phillips driver can usually remove them without making too
much of a mess of the screw.
By contrast, the anti-tamper screws
used to hold the battery in are a variation of the Tri-wing type, called a Y1.
I’ve seen cases where people have
mangled Tri-wing screws by using
non-Tri-Wing bits to get them out, so
it’s obviously better to use the correct
bit, especially if they are in as tightly
as these ones were. It amazes me that
they deemed it necessary to hold the
battery in with this type of fastener but
that’s Apple for you.
As an aside, sets of security drivers
are inexpensive from the likes of Ali
Express and are a valuable addition
to any serviceman’s toolbox. It really
is staggering to think of the number of
anti-tamper screws one comes across
during servicing. I’ve seen them used
in all sort of products, including Bluray players, kettles, mobile phones
and garden blowers; in short, anywhere the manufacturer doesn’t want
Joe Lunchbox messing around with
their products.
Of course, determined DIYers won’t
let anti-tamper screws stop them from
getting in and I’ve even seen cases
where bloody-minded individuals
have opted to physically break the
case open rather than kowtow to these
manufacturer-imposed restrictions. Either that, or they’ve completely mangled the screws while attempting to
extract them.
In the past, I’ll admit to having “seen
the red mist” where such screws are
concerned, because not having the correct bit to remove them really kills the
natural flow of working on a job. The
silly part is that I can always jump in
the van and go and get a suitable bit.
They are usually readily available,
which defeats the purpose of using
anti-tamper screws in the first place.
OK, back to the chase. Once the
battery was out of the machine and
stored safely outside, I began checking out the collateral damage. Fortunately, the thin aluminium back cov-
These photos show the battery as it
appeared inside the case (top) and
after it had been removed from the
case. It had swelled enough to distort
the chassis and the back.
er was easily coaxed back into shape
with some careful manual tweaking
and though the metal had stretched a
little, it would sit flat enough once all
the screws were back in.
More worrying was the cast aluminium chassis. I assume that it’s cast and
then machined to add threaded holes
and other anchor points. Of course, it
could also have been C&C machined
from a single billet of aluminium (I
wouldn’t put it past Apple) but I think
that casting is more likely. There’s no
doubt the manufacturers make a beautiful job of making components for
these machines and of course, this is
one of the alluring features of Apple
products.
The downside is that it makes them
expensive to repair if any spare parts
are required. To straighten out the
warped chassis, someone would have
to have the gear to remove the lateral
twists and then the skills and tools
to panel-beat things back into shape.
However, no matter how good someone
was at this, any repair would still be
Servicing Stories Wanted
Do you have any good servicing stories that you would like to share in The Serviceman column? If so, why not send those stories in to us?
We pay for all contributions published but please note that your material must
be original. Send your contribution by email to: editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
December 2016 59
Serr v ice
Se
ceman’s
man’s Log – continued
obvious (and it would be expensive),
making replacement of the chassis the
only feasible repair option.
Touchpad repair
Repairing the touchpad was fiddly
but successful. The assembly is selfcontained and is mounted into the
chassis using an aluminium locating
tab on one side and two wafer-thin
spring-steel strips on the opposite
side, to provide a “button” feel for the
device. A microswitch is mounted at
the bottom centre of the touchpad and
spring tension keeps the pad raised until someone presses on it to activate the
button (Macs use a single-click system
so there are no complicated twin-button assemblies to worry about).
The expanding battery had forced
the touchpad assembly out of its chassis aperture, easily overcoming the
resistance of the two thin steel hinges (or strips) which had partly folded
back on themselves as the pad was
ejected. These steel strips were each
removed by undoing two extremely
small screws and the spring steel then
gently pushed back into shape.
Fortunately, no hard bends had
been made in them. If there had been,
they would have simply broken when
straightened.
Once the spring strips had been
reformed, they were refitted and the
touchpad screwed back into place
again. Some minor fettling then saw
it operating properly again.
Buying spare parts from the local
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Apple agents is expensive and there
is no need to do so. All the Mac parts
one could ever want are available from
our eastern friends via the Internet. As
an example, a battery (an original Apple part) from a Chinese vendor cost
me US$80 including shipping, roughly one-third the cost for the same part
here. The chassis was a bit more expensive but still remarkably cheap compared to one from the local supplier.
Fortunately, nothing else was amiss
and once these items had later been
replaced, the owner was back “Instagramming” and “Facebooking” to her
heart’s consent. It really was just a
matter of fitting the parts and making
sure that all the different screws went
back in the right place. Fortunately, a
screw map is available from Apple to
help with this.
Fixing the second machine
The second MacBook Pro machine
was a bit more interesting but I’m not
going to relate the boring resolution
of the grey screen issue. The relevant
thing here is that I initially decided to
swap in the hard drive from the first
machine (ie, the one with the battery
problem). That way, I could quickly
get this second machine going again. I
could then replace the hard drive and
the parts in the first machine when
they arrived from overseas.
Anyway, I swapped the drive in and
fired up this second machine with the
back still off, to make sure it worked.
It booted OK but the battery indicator
showed only 10% remaining. Fortunately, the owners had supplied one
of their chargers, so I plugged it in and
went about my work.
My intentions were that once it had
charged and was operating properly,
the client could come and grab that
one. Unfortunately, it didn’t quite
work out that way. I was sitting at my
desk doing some important YouTube
research when I suddenly heard an
almighty CRACK! It sounded as if a
machine had fallen from the bench
and smashed the LCD panel but an
anxious glance towards the direction
of the noise soon revealed that it was
still in place.
Mind you, that’s difficult to tell at the
moment as my workshop looks like a
bomb has gone off in it. That’s because
I’m in the process of renovating my
garage/workshops while I’m trying to
run the business. Normally, I’m very
neat and tidy.
On closer inspection, the charging
MacBook was sitting at a funny angle
and when I turned it over, I could see
why. Its battery had just blown out its
last set of cells and the cracking noise
had been the battery’s plastic frame
giving way, similar to the first machine. After a quick underwear check,
I whipped the charging lead off and
removed the battery, before placing it
outside with the other one.
I immediately suspected the charger but a call to the client quickly revealed that this wasn’t the charger
used with the first MacBook. What’s
more, a check with my multimeter indicated that the output voltage from the
charger was spot on. So it looked like
the charger was in the clear.
I began to smell a rat with the batteries. Fortunately, this laptop hadn’t
been damaged as badly as the first because with the back off, the “exploding” battery had somewhere to go. The
touchpad still suffered but the chassis
wasn’t as warped as the first one.
I repaired the touchpad and got
everything ready for when the spares
finally arrived. It was all rather frustrating though, because it meant that neither machine could be repaired until
the spare parts arrived.
A week later, while I still had those
two MacBooks in the workshop, I got
a call from a new client. She told me
that she had just fired up her MacBook
and it had given her a time and date
warning and wouldn’t connect to the
WiFi. My alarm bells immediately rang
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Vintage AWA B&W TV set
Vintage B&W TV sets and AM
valve radios can be quite collectible
these days. K. W. of Riverstone, NSW
recently got two such sets going
again . . .
I recently had to help a friend
whose brother had died and who
had kept all sorts of junk, including lots of TVs. In one room, there
was an old 1970s Rank Arena colour
TV that had a VHF turret tuner (no
UHF). Normally, these are reasonably collectible but in this case the
woodgrain vinyl had faded to white
after some 40 years of exposure to an
un-curtained window.
However, I wasn’t really interested in the old Rank Arena. Instead, I
was interested in what was sitting on
top of it – an AWA P1 portable B&W
TV dating from around 1965. These
are now very collectible and many
still give a first-class picture despite
their age, often with the original
AWV valves.
The P1 was an all-valve portable
and was basically a full-size TV chassis crammed into a portable cabinet.
Thanks to the full-power 6.3V heaters they used, their picture tubes
lasted the distance, unlike the ones
used in the all-transistor portables
that came later.
Jim said I could have it as it was no
good since the analog broadcasts had
stopped and anyway, it had “no horizontal hold”. Across four decades, I
and I advised her not to charge it but to
give it to me (or someone else) so that
the battery could be checked.
When she brought it around, a quick
check of the back panel confirmed
that it too had a swollen battery. It
was enough of a coincidence for me to
send a warning to my email database,
recommending that owners of three to
5-year-old MacBook Pro laptops have
the batteries checked out. It might just
save them a lot of grief.
Denon twin-drawer CD player
DVD/CD players are dirt cheap these
days so why bother fixing them? R. W.
of Lismore, NSW didn’t want to part
with his Denon twin-drawer CD player
so when it began playing up, he rose
to the challenge and fixed it. Here’s
what happened . . .
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remembered that the most common
fault in the P1 was a leaky 0.0068µF
paper capacitor in the vertical oscillator circuit. I also knew that people
invariably confused loss of vertical
hold with lack of “horizontal hold”.
Back home, I put it on my workbench and applied power. I could
see that the valves were lighting up
but there were no other signs of life,
which usually meant that the HT fuse
had blown. This is a common occurrence if such sets haven’t been run
for a few years and usually occurs
because the power supply electrolytics need re-forming. The usual cure
is to connect an ammeter across the
fuseholder and then carefully bring
up the mains voltage from zero with
a Variac, while monitoring the current until it stabilises.
Sure enough, after half an hour
or so, everything began to work and
I was rewarded with a crisp snowy
screen and a healthy hiss from the
speaker. I hooked up my old TV pattern generator and yep, the vertical
hold was way off and there was the
dodgy 0.0068µF “Hi Qual” capacitor
exactly where I remembered it (“Hi
Quals” were basically a paper capacitor with a plastic case!).
I replaced this capacitor and the
old AWA P1 then worked perfectly.
I was even able to download a PDF
of the complete 1965 model service
manual but I didn’t really need it. I
I have had a Denon DN2000F MkIII
twin CD player for many years. This is
a rugged 2RU rack-mounting unit with
a separate 2RU controller connected
via a proprietary lead.
I first obtained this unit in the 1990s
after being retrenched from the airline
industry and deciding to try my hand
at being a DJ. That wasn’t a success but
I kept the player as its cueing facility
and variable pitch was something I had
grown used to. It gave reliable performance until recently, some 25 years
after purchase.
The problem was that disc drawer
one would load a CD but would not
cue it. However, assisting the drawer to
close or turning the power off and then
back on again (doesn’t that “fix” everything these days?) with a disc inside
allowed it to cue and play normally.
fully expected it to start to play up
after a couple of hours but remarkably, apart from dirty tuner contacts
and a noisy volume control pot, the
capacitor was the only real fault!
I then wired up the luminance output from a digital set-top box (STB)
to the grid of the video amplifier
valve and got a really good picture.
The sound was just as easy; I simply
wired the left and right audio channels from the STB in parallel to the
volume pot.
The next time I went down to Jim’s
place I said, “Good news! I got your
old black and white TV running”.
He was unimpressed because, as he
said, “you’ll still need a set-top box”.
While I was there, Jim brought out
his 1940s-era Mullard 5-valve radio.
It was faulty and he wanted me to
have a look at it.
Back home, I quickly discovered
that it required two new 22µF 450V
electrolytic capacitors and a few
other minor parts to restore it to full
working order.
Interestingly, a note had been attached to the back, detailing how the
set had been repaired by a service
centre back in 1986 – which would
have been a bit of an ask even then.
Oddly, they had changed quite a few
capacitors but not the one you must
always change: the grid coupler from
the plate of the audio preamp to the
grid of the output valve. It was still
there when I got the set and leaking
like the proverbial sieve!
When listening to the drawer operate, it was obvious that the transport
motor was running for a short time after the drawer either closed or opened,
so I suspected that the limit switches
either weren’t being actuated or had
developed a fault. Fixing it wasn’t urgent and so I put up with this minor
fault for quite some time, preferring to
use drawer two instead.
Eventually though, drawer two also
started playing up. In this case though,
the transport motor was stopping when
the drawer reached the open or close
limits while being assisted. This was
the impetus I needed to take it apart
and see what the problem was.
After dismantling the unit, which
appeared to be well-made, I inspected
the PCBs for bulging electrolytics and
discoloured components and found
December 2016 61
Serr v ice
Se
ceman’s
man’s Log – continued
Left: the fault condition was triggered in the LCD panel of
the Sony set about 40 minutes after switch-on. Fitting a
couple of fans to the rear cover helped cure the problem.
Cooling fans were commonly used
in the plasma sets of yesteryear but
in this instance, retrofitting fans to
a 132cm Sony LCD TV saved it from
the scrapheap. G. S. of Castle Hill,
NSW was the retrofitter . . .
The Sony KDL52Z5500 LCD TV
was a top-of-the-range model costing over $3000 back in 2009. However, after just five few years of use,
the 132cm LCD panel in my set suddenly began giving trouble.
Initially, the problem showed up
as a narrow vertical flickering band
on the lefthand side of the screen at
power up. This would then disappear after a few minutes as the set
warmed up and so the fault was initially considered trivial.
It didn’t stay that way though and
over the next few weeks, the switchon fault progressively became more
serious. It eventually got to the point
where the entire lefthand side of the
screen would take on a reddish hue
with very dark shading, picture tearing and vertical ghosting. It would
then invariably come good and display a perfect picture after 30 or
40 minutes (when the panel had
warmed up) until one day it didn’t,
despite leaving it running for several hours.
This sort of problem is often due
to faulty “tab” connections between
external flat ribbon cables and the
transparent electrodes just inside
the edge of the LCD panel. With repeated thermal cycling, the bonding
contacts inside the LCD can become
intermittent and a panel failure of
this sort generally means that the
set is a write-off.
However, there’s one neat trick
you can pull to try to save it: remove
the metal frame that runs around
the outside of the LCD panel (and
secures it in position), run draught
excluder around the inside of the
frame and reassemble it. The idea
here is that the draught excluder applies extra pressure to the tabs when
the metal frame is fastened back into
place and will hopefully “cure” the
problem.
This fix initially worked a treat
for my Sony set, as detailed in Serviceman’s Log in the November 2014
issue. However, after a few months,
the problem reappeared but with
one important difference: the timing
of its appearance had been “transposed”. Now, instead of the fault
occurring when the set was cold,
it was appearing about 40 minutes
after switch-on, after the panel had
thoroughly warmed up.
What was frustrating was that the
picture was perfect for those first
40 minutes or so. After that, the
dark shading, ghosting and reddish
hue would suddenly appear and it
none. I then removed drawer one and
located a small PCB which held the
two limit switches and interfaced them
to a flat lead with a polarised header.
There were no other electronic parts
on this board other than the switches.
One was a very small unit similar to
a microswitch and this was the closelimit switch. By contrast, the openlimit switch consisted of a flimsy pair
of contacts in a rubberised cover that
was actuated by a slider on the drawer
unit (which also contained the end-oftravel buffer springs).
Both switches measured greater than
500Ω when closed, so I applied some
contact cleaner, reassembled the unit
and tested it. That fixed it but the fault
was back less than a week later.
I tried looking everywhere on the internet for a replacement board or, failing that, replacement switches but to
no avail. I then emailed Denon but was
told that this player was no longer supported. A supplier in the UK had complete drawer and laser assemblies but
at £300 (about $550), that was too much
to spend, especially as I needed two.
Then I had a brainwave. If I could
replace the existing switches with
suitable microswitches, I just might
be able to resurrect the unit. After a
brief search, I found some at Jaycar
(Cat. SM1038) and bought four at just
$4.95 each to try.
After removing the old switch PCB,
I actuated the existing switches and
checked the resistance. The open-limit
switch was now open-circuit but the
close-limit switch was OK, although
the drawer motor still ran when the
drawer was closed. I gave this no further thought and decided to replace
both. And that’s where the fun began.
The new switches were several
times larger than the old ones and it
was difficult to determine where to
mount them. After much trial and er-
Fan-Cooling For A Sony LCD TV
62 Silicon Chip
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was so bad that the picture was unwatchable.
Clearly, the fault was heat-sensitive; the LCD panel had to get nice
and warm in order to trigger it. So
what could be done about it? The
obvious answer was to somehow
keep the panel from reaching the
critical “trigger” temperature and
using computer fans to extract the
set’s warm interior air seemed to be
the way to go.
After some hunting around on the
internet, I came across a CoolerMaster 120mm case fan from a local retailer that seemed ideal for the job. It
ran at 1200 RPM, had a quoted noise
level of just 19.3dBA (so it would
be nice and quiet) and came in a
dual pack for just $19.00. Mounted
together side-by-side, the two fans
would be just large enough to cover
a large ventilation panel towards the
top righthand side of the rear cover.
When I got the fans home, the first
thing to do was to figure out whether to mount them inside the rear
cover or on the outside. After some
thought, I decided to mount them
on the outside and power them from
an external 12V DC plugpack. That
way, they wouldn’t block the airflow
to the horizontal ventilation slots at
the very top of the rear cover.
With that decided, I undid the
umpteen-dozen screws that secured
the rear cover, laid it flat on the floor
and used one of the fans as a template to drill two diagonally-opposite mounting holes. This fan was
then secured in position using Nylon
M4 x 15mm screws, nuts and wash-
ers, after which the second fan was
mounted in position, butted hard
up against the first. Nylon mounting screws were used at all four
mounting positions because I didn’t
want metal screws protruding into
the chassis, with the risk that they
might contact a high voltage or short
something out.
Once the fans were in place, I replaced the rear cover, then sorted
through my spare parts and found a
2.5mm DC socket. This was mounted on a small Perspex bracket which
in turn was attached to an outside
corner mounting hole of one of the
fans. The DC socket itself was wired
to two paralleled 3-pin polarised
pin headers and the two fans then
plugged directly into these headers.
Several cable ties were then used to
tidy up the wiring and secure it all
in place.
Now for a power supply. A quick
ferret around in my workshop soon
turned up a 12V DC plugpack supply
rated at 600mA – more than enough
to power the two 160mA fans. I
plugged it in, switched on and the
two fans whirred into action. And
just as their noise specification indicated, they were nice and quiet – so
quiet in fact that you weren’t aware
they were running from a normal
viewing position.
So did the idea work? It sure did –
well almost! The set now runs for 3-4
hours before giving trouble, as opposed to the measly 30-40 minutes
before the fans were fitted. Running
the fans at a higher speed (eg, by increasing the supply voltage by 1-2V)
or adding extra fans would probably
solve the problem completely.
ror, I settled on the two positions and
after soldering fly-leads to both, temporarily secured them in place using
a dab of contact adhesive. I then operated the drawer manually and the positions seemed correct.
It was then that things went pearshaped quickly. To gain access, I had
removed the cover to the drawer which
held the top-clamp for the disc when
the laser is in position. This cover also
holds the drawer mechanism in place
and while I was testing the switches,
the drawer fell out and took one of the
sliders with it.
I tried to get the mechanism back
together but just couldn’t find the
right position. I wished then that I
had a time-machine to take me back
to just before it fell apart. However,
perseverance eventually paid off and
somehow it all eventually clicked back
into place.
Operating the drawer now revealed
that the drawer rack was not correctly aligned with the drive pinion and
wouldn’t run to its full travel. The drive
mechanism winds the drawer in and
on reaching the inner limit, a mechanical disconnect operates and the drawer
motor then drives the laser assembly
into position before finally operating
Inside or outside
siliconchip.com.au
Substituting microswitches for the
original limit switches and relocating
the switch PCB helped get a Denon
twin-drawer CD player working again.
the close-limit switch. After more fiddling, I finally got it right but don’t
ask me how.
The next day, I verified the switch
operation and applied a 2-part epoxy
adhesive to permanently secure the
microswitches. The fly leads were then
soldered to the switch PCB which was
trimmed and encapsulated in clear
heatshrink tubing and relocated to the
side of the mechanism. It all looked
good, so I reassembled the player and
put it through its paces.
It failed and as can be imagined, I
was rather crestfallen. Neither of the
switches was being activated. The
open-limit one was out by about 1mm
but the close-limit switch wasn’t activating at all. The drawer would close
but the laser assembly wasn’t lifting
into position.
So I had another fault that I had
failed to notice and that was that the
motor didn’t seem to have enough
torque to operate the laser lifting mechanism due to a slipping belt. So why
hadn’t I noticed the belt? It couldn’t
possibly be OK after 25 years and indeed it wasn’t.
I went back to the internet to see
if I could find spares and eventually
came across a supplier in Portugal from
whom I bought two generic 25mm diameter 1.2mm belts for under $10, including postage.
These were installed and after a
slight adjustment to the open-limit
switch actuator, the player was reassembled and tested. That was it – both
drawers now worked faultlessly, although drawer two may also need to
have its limit switches replaced sometime in the future.
And so, for an outlay of less than
$30, the old Denon DN2000F CD player
was given a new lease of life and may
well last another 25 years. Will CDs still
be around in 2041 and if they are, will
SC
I still be around to use them?
December 2016 63
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