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SERVICEMAN'S LOG
No magic hammers with smart TVs
You don’t always win in the servicing game.
I recently took on a large-screen (140cm)
LCD TV set but despite my best efforts, I
ended up coming off second best.
I’m not usually into repairing TV
sets, preferring instead to let professional TV servicemen handle those
specialised jobs. However, when a
client recently asked me if I “did TVs”,
I answered “yes, I do”, surprising myself even as the words came out.
Not wanting to obviously back-pedal,
I then asked him what was wrong with
it. My thinking was that he might describe a symptom that would give me
the chance to bail out gracefully by
claiming that, unfortunately, I couldn’t
repair “that” type of problem.
His response was that it worked fine
at switch-on but that the screen then
went dark a minute or so later. To me,
that sounded like it should be quite
straightforward to repair, my thoughts
being that it was probably just a dud
connection or something along those
lines. He then told me that the TV was
only about a week old, so why hadn’t
he simply taken it back for a warranty
claim? It turned out that he’d lost the
receipt and apparently the retailer was
being extremely pedantic about not
taking the set back without it.
While I can understand this stance
on one hand, surely they could have
dug around and found the relevant
sales details, especially as the set had
only been purchased from them the
week before. However, they wouldn’t
budge and so the customer was at a bit
of a loss as to what to do.
Dave Thompson*
Items Covered This Month
•
•
•
•
My first smart TV repair
CPR on an Engel fridge
Sobering up a groggy pH meter
Penny’s air-conditioner
Feeling his pain, I said I’d look at
it for him but that I couldn’t promise
anything. It was a neat little exit strategy to fall back on if necessary. If the
job proved too difficult, I could simply
point out that I’m really a computer
technician rather than a bona-fide TV
repair guy.
With the customer’s expectations
dealt with, it was just a matter of him
hauling the TV in from his vehicle. For
some reason, I was expecting a relatively small set but he turned the corner
cradling a monster 55-inch (140cm)
flat-screen TV. It took just one look to
convince me that the tiny cabin I currently use as a temporary workshop
was not going to be the best place to
troubleshoot this device!
Despite its size, it was as light as
a feather and in fact a child could’ve
lifted this TV! Nevertheless, I took
one end and helped him carry it down
the driveway to my garage workshop,
which is a lot larger and better set up
for electronic repairs than the cabin.
Signs of life
When we got there, I plugged the set
in, switched it on and instantly saw a
bright blue splash screen. After a few
seconds, the TV circuitry switched in
but the screen was all hash due to the
lack of an antenna. However, rather
than connect an antenna, I plugged in
a flash drive I had hanging about the
workshop and used the remote to select
the USB input, whereupon the media
menu came into view. I then chose a
random AVI file from the flash drive
and away it went.
To be completely honest, it wasn’t
the best picture I’d seen on a TV but
42 Silicon Chip
siliconchip.com.au
My first smart TV
This was the first big smart TV I’d disassembled and to
be honest, I expected a little more inside than I discovered. Pretty much 80% was fresh air, there being just two
moderately-sized circuit boards and one smaller board
screwed to pillar mounts on the rear of the screen panel.
The power supply was up near the middle left side of the
panel, while down at the centre bottom sat the smaller
T-Con (timing and control) board. On the mid-right side
sat the main audio/video/tuner board.
Of these, the biggest was the power supply board and
it measured just 120 x 180mm. As a result, all the boards
looked rather lost in the vast, empty expanse behind the
screen area.
Being a “more common” type of serviceman, I reached
for my hammer to begin troubleshooting the TV! Yes, my
hammer and while you may well picture a large engineers’
ball-pein hammer wreaking its havoc among the chips
and transistors, you’d be wrong. This particular hammer
is a small, hard plastic type and is an ideal tool for gently
tapping on boards and even individual components to induce any loose connections or bad solder joints to reveal
themselves.
I plugged the set in and leant it against my workbench,
portrait style, with the screen facing a set of plastic drawers
sitting under the bench. The faces of these drawers acted
as a mirror, one of the vital aids real TV service people
have in their workshops but which I don’t happen to have.
Admittedly, it wasn’t exactly a perfect TV repair set-up
but it would suffice; I could easily make out the reflected
screen images on the drawers.
As soon as it was plugged in, the TV again displayed
the blue splash screen, then the file menu for the USB input. As before, I chose a random movie to play and sure
enough, after a minute or so, the screen went black. I then
switched it off using the remote (ie, to standby rather than
“‘right off”), then immediately restarted it and found that
the screen stayed black.
I turned it off again and decided to wait for a few minutes before switching it on again, amusing myself in the
meantime by taping a row of microswitch controls safely
out of the way of the power supply board. These usually
mounted into the back panel but once that had been resiliconchip.com.au
LG24713
this set was a “cheapie” and given its relatively low sale
price (about half the cost of a similar “big-name” branded
set), it was perfectly acceptable. We watched the video for
about two minutes and then the screen suddenly flickered
and quickly faded to black, although the sound was unaffected and continued along happily in the background.
“That’s what it does to me too!”, the customer exclaimed.
I promised again that I would do my best and the customer left to allow me to carry on with more pressing
work. I subsequently returned to the TV a few days later
and this time, before plugging it in, I whipped the back off.
This initially involved removing the relatively heavy
base and stand assembly (the two weighing as much as the
rest of the set put together) before removing half a dozen
large panel screws situated around the perimeter of the
case. It was then just a matter of cracking the clips holding it together in between the screw points, after which
the back panel lifted away easily to reveal, well . . . not
very much at all.
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moved, had been dangling just above the power supply
board via a flexible connecting strap.
I also checked every flying lead connection (there weren’t
actually that many) between the boards and various satellite components like speakers, external sockets and controls. All seemed to be well-connected, using the same
industry-standard connecting plugs and sockets that I’d
seen in plenty of other devices. I paid particular attention
to all the power supply connections, including a line of
2-pin connectors that fed the LED backlights. Everything
seemed in good order; I could see nothing that would account for the screen “dying”.
A red herring
When I started the TV again after the pause, the blue
splash screen came up again and then the menu as before.
This time though, I didn’t select an input and instead began tapping away on the power supply board, hoping to
induce the fade-out sooner so that I could isolate the cause
of the problem. This approach seemed to pay off, because
when I tapped on one of the small transformers near the
centre of the board, the screen went dark.
So was I onto something or was this merely a coincidence?
I waited the prerequisite few minutes before repeating
the exercise and this time, no amount of tapping would induce the problem. I tried it again with a movie playing, tapping in all directions and then once again after switching
July 2016 43
Serr v ice
Se
ceman’s
man’s Log – continued
off and waiting. I even tried physically
manipulating the transformer casing
(it felt very solid to me) but I couldn’t
replicate the fault, which meant that
it was probably a coincidence.
No magic hammer
When the screen did eventually fade
out, I powered it up again after a suitable interval and this time hit the other
boards with my plastic hammer. However, nothing stood out and the screen
again faded away in its own good time.
As I proceeded through the testing process, I took note of how long it took the
screen to fade out, in case there was
a repeatable time-span. There wasn’t;
it was seemingly random. Sometimes
it went for just 20 seconds and sometimes for as long as three minutes.
Once, after tapping the main board, it
ran for almost five minutes and here
was naive me thinking my magic hammer had done the business.
In the end, the bottom line was that I
couldn’t find any mechanical fault that
caused the screen to
die. This meant that
magic hammers are for
the movies and I’d have
to look further afield
and utilise my troubleshooting skills to discover the cause of the
problem.
Before proceeding further though, I
stripped all the connectors from the power supply board and
removed it from its
mounts on the back of
the panel. I then took it
to my other workshop
and proceeded to examine it under my microscope, looking for fractured or incompletely soldered joints, etc. However, it looked to be very well made
and a quick Google search for the part
numbers revealed that this same power supply graces many smart TVs, including models made by Blaupunkt
and Seiki.
A replacement power supply on
eBay was only about $US30 but I
wasn’t convinced that that was where
the problem lay. In fact, more Googling revealed information posted on
TV repair forums that indicated that
the most likely cause of this issue was
the T-Con board. This is the smallest
board in the set and it connected directly to the screen via two large, flexible cables.
I removed this board and gave it
the microscope treatment but once
again, nothing obvious was apparent. A web search turned up several
used-but-guaranteed replacements for
Servicing Stories Wanted
Do you have any good servicing stories that you would like to share in The Serviceman column in SILICON CHIP? If so, why not send those stories in to us? In doesn’t
matter what the story is about as long as it’s in some way related to the electronics
or electrical industries, to computers or even to car electronics.
We pay for all contributions published but please note that your material must
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Please be sure to include your full name and address details.
44 Silicon Chip
only $40, so I hit the buy button and
got one on the way. This component
is also used in Blaupunkt TVs and as
that brand has a good reputation for
quality, I wouldn’t consider it secondtier hardware.
The new board arrived in just five
days (not bad from the USA) and I installed it in minutes. This time, when
I fired up the TV, it ran for 20 minutes
but that was hardly cause for celebration. At the end of that time, the screen
flickered to black. It would then recover seemingly at random but would only
run without glitching for a couple of
minutes at the very most.
A faulty board?
That was a real blow because it
meant that I was dealing with something else, unless I’d had the misfortune of getting a faulty secondhand
T-Con board. However, at this stage
it wasn’t worth sending it all the way
back to try another one, even though
the vendor kindly offered to swap it
for me. He was surprised at the outcome and had been reasonably confident that it would have fixed the issue.
I went back to the power supply
board and started taking voltage measurements at various points when the
screen went dark, comparing these
with the voltages obtained when the
screen was working. I found that the
backlight voltage remained relatively
stable, although it did drop slightly
when the backlighting went dark.
By now, any talent I have for repairing TVs had long since been exhausted
and so, clutching at straws, I ordered
another power supply. During this
process, I’d kept the customer up-todate with what I was doing and he’d
agreed to cover the costs of any parts I
needed to get it going. Because the TV
was a cheap model, he figured that he
had a little leeway as far as spending
money on it went and thus he could
afford to take a gamble and buy these
less expensive parts for it.
Once again, the power supply arrived quickly and I soon had it fitted
into the set. And once again it worked
fine at first but the screen soon went
black and that was that!
Love lost
I was seriously starting to fall out of
love with this thing by now. Not only
was it taking up room in my workshop but it was also soaking up a lot
of my time and it wasn’t the simple fix
siliconchip.com.au
I thought it would be. The input board
was the only part left that I could easily
replace and although I tracked down
a replacement, it was new and a lot
more expensive than the other parts.
What’s more, from what I’d read in the
online forums, it was unlikely that this
board was the problem and this was
borne out by even more research I did
on the issue.
Apparently, this board couldn’t
“do” anything that would cause the
backlights to go dark. It could fill the
screen with artefacts and other related faults but not make it go black, according to the “experts” on the forums
and the various parts guys I talked to
when buying the other replacement
boards. I also had a gut instinct that
I’d be wasting my time and my customer’s money by swapping that board
out with a new one.
And then I discovered some interesting information on one of the forums.
I stumbled on this while searching
for scraps of information about the
various boards used in this TV and
learned that while many 55-inch sets
utilised the exact same power supply,
some of the cheaper sets shipped with
bad LED arrays. When they went dark,
repair technicians assumed that the
power supply was the problem but it
was actually a screen issue; or, more
accurately, a problem with the LED
backlights.
This made sense; if the various circuit boards were first rate, one place
left for the manufacturers of these second-tier products to cut costs would be
the screen. From my research, I knew
that the boards were good enough for
brand-name sets, which made it even
more likely that the problem lay in
the one part I couldn’t easily replace
– the screen!
I was now going to have to break this
news to the owner who was not going
to be a happy camper.
The fact is, we’d have to buy a whole
new screen assembly to get this TV going and while there may be one available somewhere out there, I haven’t
looked for one as my time and the
customer’s expenses so far have edged
this repair into the “not economically
feasible” bracket. The best I could do
was recommend that he place a wanted
ad on some of the local sales sites on
the web, in the hope that someone has
a dead version of the same model TV
but which has a good screen.
Provided the dead set was cheap
enough, we could swap the good bits
out of his set into that one. In addition,
he could then advertise any leftover
good boards for sale while he was at it.
You win some and you lose some;
that’s the servicing business!
CPR on an Engel fridge
Compact fridges capable of running
off mains or battery power can really
come in handy. B. C. of Dungog, NSW
recently resurrected one such unit that
had been rescued from the recyclers . . .
Deciding that it might make a good
project, a friend recently bought an Engel 240VAC/12V DC (Model MT45FG4) refrigerator at the recyclers. The
leaves and mud were washed away
and we carefully dismantled the unit.
Eventually, an enclosed metal box was
removed and after the four connecting
leads were unplugged, it was eased out
from under the external condenser.
This box, which contained all the
electronics, had been beside the compressor (which is basically a solenoid
pump). With a grin, he handed it to
me and said “what’s inside is your department”.
At the bottom end of the box was an
input connector for the 240VAC, along
with a 12V DC input which is protected
by a blade type 10A DC fuse. Removing a number of screws and pop rivets
subsequently revealed two rectangular
PCBs and some flood residue inside.
Everything was then thoroughly
washed in warm water, after which
the two PCBs and the input connector block were immersed in methylated spirits for a few hours. All these
were then allowed to dry in the sun for
a number of days.
Switchmode supply
Closer examination of the two PCBs
then revealed that one was a 240VAC
SMPS (switchmode power supply),
while the other was the compressor driver unit. My main concern at
this stage was to try to ensure that the
switchmode transformer (T1) was completely free of moisture. I also removed
the silicone insulator (which encased
Q101) to ensure it was dry inside. The
compressor driver PCB had all opentype toroidal coils fitted and it had
fully dried out.
At this stage, we decided to test-run
the refrigeration unit from 12V DC,
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July 2016 45
Serr v ice
Se
ceman’s
man’s Log – continued
Sobering up a groggy pH meter
A little wine is supposedly good
for the heart but not when it gets into
the heart of a pH meter. P. E. of Heathcote, Victoria was able to cure the
groggy instrument of its hangover . . .
I was recently given a “simple”
job to repair a Hanna Instruments HI
8314 pH meter, which was used to
measure the pH of wine. I was told
that it originally cost several hundred dollars and that it had stopped
working. Well, that narrows it down!
The instrument looks like a fancy
multimeter and is used in a similar
way. My first thoughts were that copper and wine don’t mix and while it
may have been an expensive instrument, it wasn’t very well sealed from
liquids. The buttons on the front
were similar to a modern dishwasher
and while they were well sealed, the
calibration adjustment screws at the
bottom would allow liquids (including wine) to enter inside the case.
It was a simple matter to open it
with power coming from a DC output
socket in the back of his Landrover. The
correct protected 12V DC Engel power
lead had been borrowed from another
member of the family but before plugging it in and running the test, a timber
cover was placed on top of the fridge
where the lid normally sits.
The various leads from the compressor, thermostat, temperature sensor,
24V DC cooling fan and 12V DC input
connector were then all plugged into
the correct compressor driver PCB terminals. A digital multimeter set on a
low AC range was then connected to
the compressor terminals, after which
the Engel power lead was plugged into
the Landrover’s DC output socket. The
multimeter immediately displayed
close to 12VAC and a steady hum came
from the compressor.
After it had been running for a few
minutes, I could feel the temperature
getting colder on the inside condenser.
And then, with the thermostat knob on
position 2, the unit cut out after about
10 minutes. It subsequently cut back
in again about 10 minutes later, so all
was good so far.
Now for the 240VAC SMPS. Back
46 Silicon Chip
up; just undo four screws and pry
the two halves of the case apart. It
wasn’t clipped together like a typical TV remote though. Instead, I had
to pry it because it was stuck with
dry, gooey wine.
Sure enough, the main PCB had
been awash with wine and this wine
was now dry and had done its deed
on the copper tracks and on the two
100kΩ multi-turn trimpots used to
calibrate the instrument. Two copper tracks had gone completely but
I was able to see where they’d been
due to the green solder mask.
Removing the trimpots was like
pulling teeth as the PCB is doublesided with plated-through holes and
the pots were also stuck fast with
wine goo. I ended up destroying another track on the board getting them
out but it was easy to replace this and
the two missing tracks with fine insulated copper wire.
I then soaked the PCB in methylon the workbench, I replaced the
33µF/35V electrolytic capacitor near
the M51995 IC (IC101), as its measured
ESR was borderline. I then removed
the T3.15AMP ceramic fuse (F101) and
soldered a test lamp (240VAC/60W)
in its place.
That done, a dummy load (2 x 470Ω
5W wirewound resistors in parallel)
was connected to the DC output terminals. The original 240VAC input
connector and lead were then plugged
into the other end of the PCB and an
IEC power lead plugged into the outlet of a 240VAC-to-240VAC isolation
transformer.
Switching it on
The time had now come to switch
it on! When I did so, the test lamp
lit briefly on the input surge and the
multimeter displayed +39V DC at the
output. I tried adjusting the 1kΩ trimpot at the output end of the supply but
this only allowed the output voltage
to be varied by about ±1V.
At this stage, I decided to turn the
power off and draw a mud-map of the
output circuit. There were two PC123
optocouplers, one set up as an over-
ated spirits for about 10 minutes and
then very gently scrubbed it with a
small paintbrush. Eventually, the goo
all came free and, fortunately, there
didn’t seem to be any more damage
to the copper tracks. I also gave the
second, smaller PCB that held the
lead sockets a quick clean in metho
(although it already looked clean)
and tested the connections from the
leads to this board. One of these connections was open circuit but was
easy to fix by carefully bending the
contacts using a small screwdriver and spraying on some WD40 for
good measure.
Fitting new 100kΩ trimpots was
child’s play compared to removing
the old ones. The battery lead was
also replaced, after which the plastic case was given a good clean with
soapy water and everything allowed
to air-dry in the sun.
After reassembling it, I was greeted
with an LCD screen with numbers on
it so it was all looking good. I had
no idea how to use it but the owner
subsequently reported that it works.
I advised him to keep wine well
away from it!
voltage protector via a 47V zener diode (ZD103) and the other controlled
by an LM431 precision voltage reference and an 18V zener diode (ZD102).
There was also a voltage divider set up
on the input pin of the LM431.
I “googled” for an LM431 data sheet
and browsed through the pages to find
this important formula: Voltage Out =
2.5(1 + R1/R2). Using a calculator, the
resistor values were plugged into this
formula and I found that these gave
an output voltage of close to +38V. So
I had to assume that the previously
measured +39V DC was close to the
correct output voltage!
That established, fuse F101 was then
refitted and the 240VAC SMPS with its
240V/240V mains isolation transformer connected to the Engel fridge. This
meant that the +39V DC was now going to go through the compressor driver
PCB! The 240VAC power was turned
on and the multimeter, which was still
connected across the compressor terminals, displayed about 13VAC.
Somehow on the way through the
compressor driver board circuitry, this
had all occurred correctly without any
of that magic blue smoke escaping!
siliconchip.com.au
The fridge was then allowed to run
for about an hour and it performed
perfectly. After that, the two PCBs and
the input connector block were shoehorned back into their box with all the
associated covers, screws and pop rivets. It was then just a matter of refitting
the box and soak-testing the unit for a
number of hours.
My friend tells me that the resuscitated Engel fridge will be used as a
drink fridge in his shed and for shopping trips.
As a postscript, there appears to be
some conjecture about what is really
inside the $8 Engel 3AG glass fuse, located inside the cigarette plug end of
the 12V DC Engel power lead. I took
the opportunity to find out and found
a 168°C 10A thermal fuse in series with
a 10A Pico fuse.
These Engel fridges can also run
from +24V DC but it is not recommended to run these units on 240VAC from
the cheaper square-wave type inverters or from the unregulated 12V DC
outlets on generators.
Finally, always check for the correct
polarity if you are making up DC extension leads or doing other lead modifications. There are many tales of woe
on this subject on the grey nomad online forums!
Penny’s air-conditioner
A split-system air-conditioner that’s
only seven years old shouldn’t have
to be replaced if it breaks down. D. P.
of Faulconbridge, NSW recently did a
friend a favour and got one such unit
going again . . .
Recently, my wife and I were discussing the evils of the throwaway
society with a friend. In particular, we
were lamenting the fact that consumers
are often forced to replace faulty appliances because of the difficulty and high
cost of even getting a fault diagnosed,
let alone repaired.
Who knows what otherwise potential gems with minor faults are now
languishing in the nation’s landfills,
or worse still, have been shipped off
to third-world countries where they
are dismantled for scrap in dangerous
sweatshops? Gone are the days when
your dead toaster could be taken to
your local friendly electrical shop,
where the element would be replaced,
on the spot, for a few dollars.
It was during this conversation
that Penny mentioned the case of her
air-conditioner. It was a split-system
siliconchip.com.au
and had simply stopped working one
day. Their children were in the room
when it failed and reported that they
had heard a loud “pop” from the indoor unit.
A short time later, our friends asked
an electrician who happened to be at
their house doing other work if he
would look at the air conditioner. He
took one look at it and his reply was
short and to the point: “Nope . . . too
old!”.
They subsequently found that it
was impossible to get anyone to even
come and look at the air-conditioner!
In each case, the advice was either that
the job was too small or that the unit
was too old to even consider repairing
and should be replaced (it was about
seven years old – plainly a dinosaur!).
So our friends were left with the
prospect of replacing the whole system at considerable cost, despite the
possibility that it may have had only
a minor fault. As well, this was one of
two identical NEC units that had been
installed in the house at the same time
and both had done about the same
amount of service. The other unit was
still functioning normally, so the catastrophic failure of a major component
in the faulty unit seemed unlikely. Understandably, they hesitated to make a
decision and so the dead air-conditioner languished where it was for quite
some time.
When I heard this, I volunteered to
have a look at their air-conditioner,
to see whether or not it was fixable. I
didn’t promise anything but from what
the children had reported, it sounded
suspiciously like something electronic
which meant that the repair could be
straightforward.
I knew that these indoor units contain an electronics module that controls the fans and the compressor and
that this module usually includes a
microprocessor, various sensors, some
relays and other electronic-type bits
and pieces.
There is also typically a switchmode
power supply with its highly-stressed
electrolytics, as well as various other
capacitors and relays carrying serious
current in there. In short, there are
plenty of things that might go “pop”!
When I arrived at the scene, the first
thing I noted was that the air-conditioner wouldn’t even try to start. In fact,
there was no sign of life at all. I checked
the circuit breaker on the power board
and it was on, so I turned it off before
The component side of the bottom
PCB in the NEC air-conditioner looked
pristine but the underside was a different story! The black rectangular
component at top right is the compressor relay, while the grey cylindrical
part next to it is the T2 fuse.
starting work on the unit.
Dismantling the indoor unit to get
at the electronics module was easy
enough. The outer cover was secured
with three screws along the lower edge
and after undoing these, the cover
then had to be detached from snap-on
mouldings along the top edge. I managed to do it without breaking anything
but it would be great if more manufacturers would include markings, such
as arrows, to show us where the snapon mouldings are.
Having removed the cover, I then
turned the circuit breaker back on so
that I could check that power was getting to the air-conditioner. This proved
to be the case so whatever was wrong
was definitely in the unit itself. I then
turned the circuit breaker back off so
that I could take a closer look at what
was going on.
Several layers
The electronics module was in a plastic box which contained several layers,
the top layer carrying only mains terminals. The next layer consisted of a
PCB which carried a microcontroller
and numerous surface-mount components, while the bottom layer consisted of a second PCB, this time carrying
through-hole components.
This second PCB looked like a
switchmode power supply and carried
several electrolytic capacitors, several
AC-rated capacitors and various relays
– in short, all the usual suspects!
I was expecting, or more precisely,
hoping, to see something obvious like
July 2016 47
Serr v ice
Se
ceman’s
man’s Log – continued
This view shows the underside of the
switchmode supply after it had been
cleaned up. The burnt-out circuit
board track with the relay pin in the
middle is circled in red.
an exploded electrolytic capacitor but
as I delved deeper into the innards, my
hopes were rapidly fading. Everything
looked pristine but when I removed
the bottom PCB and turned it over, it
was a completely different story. The
top of the board was completely clean
but about a third of the underside was
covered with thick black soot.
It was impossible to determine the
source of the soot at this stage and all
the parts on the top of the board looked
perfect. Perhaps something had once
been underneath the board which was
there no more?
Missing solder pad
It all became clearer once I had
cleaned up the underside of the board,
however. There was a relay marked
“RY – COMP” (compressor relay) on
the board. And where one pin of this
relay had once been soldered to a PCB
pad, there was now just a hole. The pad
was missing!
The pin was still there though, apparently undamaged, but was now surrounded by empty space. There was
no sign of solder, this apparently having been completely vaporised along
with several millimetres of copper surrounding the pin.
This track had once connected the
relay to the compressor, so it carried
the full compressor load. As a result, I
bridged the gap with copper wire and
plenty of solder, making sure that the
solder had wetted everything properly so that I had a good, low-resistance
connection between the relay and the
compressor.
The question was, what had caused
the failure of the original soldered
48 Silicon Chip
joint? Was it a power surge, due possibly to a lightning strike (quite common in this area)? Or had the relay pin
never been properly soldered (a “dry”
joint) so that over time, a cycle of progressive heating and oxidisation had
eventually produced a high resistance
joint which generated enough heat to
melt the solder completely? Or had the
heating originated in the relay itself,
due to increasing contact resistance?
The other question was, whatever
the process, had the relay itself survived? There was no sign of its plastic
body overheating but I reasoned that its
contact resistance could be high without any damage being visible on the
outside. I was not able to find any data
on this particular relay but looking at
the specifications for similar devices,
it seemed that the typical contact resistance for this type of relay was less
than 100mΩ (milliohms).
I didn’t have anything that could
measure such a low resistance value
but my DMM has a 200mV range, so
I figured that if I passed some current
through the contacts, I should be able
to measure the voltage across them and
accurately calculate the resistance. After some thought, I decided to use a
12V DC supply with a car tail-lamp in
series to limit the current through the
contacts and to also use this same 12V
supply to activate the relay.
This set-up gave a contact current of
1.85A, while the voltage drop across
the contacts measured 9mV. Using
Ohm’s Law, this then gave a calculated
resistance reading of just 4.9mΩ, so it
looked like the relay was OK.
However, the open circuit to the
compressor did not explain the general
lack of signs of life. Had the control circuitry survived the trauma? It was not
going to be possible to test the entire
control circuitry with it removed from
the air-conditioner but I could test the
power supplies. If these had survived,
then there was a reasonable chance that
the logic circuits were OK.
There was a switchmode supply
with a +12V output, which supplied
the various relays. This also fed a +5V
linear regulator which supplied the
logic circuits. In order to check these
rails, I would need to apply 230V mains
to the switchmode board itself.
Fortunately, I have an isolated (float-
ing) mains supply in my workshop,
which dates from the “hot chassis”
(AC/DC transformerless) radio days
and still comes in handy from time to
time. It consists of two 240-110VAC
transformers connected back-to-back,
with a lamp socket in series with the
output. I can also take the output from
the first transformer only to get 110VAC
if required and various incandescent
lamps can be plugged into the lamp
socket to limit the current to the required level. A shorting plug can be
plugged into the lamp socket if full
current is required.
Open circuit fuse
The switchmode regulator is fed
from the mains via a slow-blow 2A
fuse marked “T2 250V”. This fuse is
a small, grey, cylindrical, vertically
mounted component and looks like an
inductor at first sight. Apparently these
have very specific delay characteristics
and are soldered in, so presumably are
not expected to blow very often.
I checked the fuse and it was open
circuit, so apparently it had received
a fair surge and it remained to be seen
whether it had effectively protected the
switchmode supply. I didn’t have one
of these specialised fuses on hand but
I figured that by bridging it out temporarily and by using a 15W lamp to
limit the current, I would be able to
determine whether or not the power
supply was working.
I connected it all up, connected the
control board to the supply and applied power. The lamp didn’t glow,
no smoke came out, the switchmode
regulator produced a nice clean +12V
rail and the linear regulator produced
a steady +5V. It was all looking good,
so I decided to order a new fuse and
proceed to the next step – a smoke test
in the air-conditioner!
Thankfully, the final smoke test went
well and our friends have a cool house
again. But the question remains as to
what caused the original failure. I am
inclined to think that it was simply
due to a bad solder joint on the relay
pin, because internal heating in the relay would have damaged the contacts,
while a power surge would probably
have tripped the circuit breaker on the
power board.
But what caused the fuse to blow?
The likely answer is that it was due to
a current spike that was produced by
arcing as the soldered connection was
SC
burning out.
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