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SERVICEMAN'S LOG
Putting the wind up an anemometer
When the wind blows but the anemometer
doesn’t go, it should be a breeze to fix.
Actually, Dad’s entire weather station was
playing up but first, I had to figure out why
the batteries in his transistor radio were
quickly going flat.
I got a call from Dad the other day,
asking if I could help him out with a
couple of jobs that he can no longer
do. It’s tough seeing time taking its
inevitable toll and watching my oncecapable father growing old just doesn’t
seem fair somehow.
Once upon a time, he could repair
anything and I’ll never forget the story
one of his friends from his younger
days told me. Apparently, they’d taken
their motorbikes on an up-country run
and the friend’s bike had spluttered to
a stop out in the middle of nowhere.
No problem for Dad; he took out his
tool kit and stripped down the bike’s
engine by the roadside and while his
mate couldn’t recall exactly what had
been wrong with it, it ran well enough
after it had been re-assembled to get
them home.
There were other times too, like
when we got stranded out in the middle of the ocean in a boat because the
“V” drive failed. On that occasion, Dad
jury-rigged something up so we could
limp back to port. It seemed that no
matter what pickle we got into, Dad
could fix it. I loved that feeling of security and it was only natural I’d become a serviceman; it’s in my blood.
Over the past few years, Dad has
been breaking down his workshop and
it’s now strangely empty. The various
machines and tools have gone to either
my brother or to myself but I doubt
they’ll ever be used as they were in
Dad’s workshop.
He still has the basics though; a soldering station and other smaller tools
and it was these I used recently to repair his old Panasonic workshop radio.
This particular transistorised receiver
has been in his workshop longer than
I can remember and with its leather
case and strap, it’s the epitome of the
late 1960s to early 1970s style of portable radio.
I well remember working in his
workshop after school, listening to the
latest music (and the rubbish the DJs
always seemed to come out with) on
this radio, so it really was part of the
furniture. I doubt that anything made
today would last anything near as long
as this one but now it had a problem.
Flat batteries
A couple of months ago, Dad finally
got around to putting some batteries
in it after it had been sitting silent on
a shelf for some years. It initially appeared to work OK but when he tried
it the following day, the batteries had
gone flat overnight, even though it had
siliconchip.com.au
Dave Thompson*
Items Covered This Month
•
•
•
•
Fixing a weather station
Electric plunge furnace repair
Kenwood TS-450S transceiver
Beyonwiz DP-P2 HD PVR
been switched off. Thinking he might
have chosen some half-flat batteries
from the pile in his battery drawer,
he replaced them with some known
good cells and the same thing happened; they were dead flat the following morning.
Obviously, something was draining
the batteries but what? Could the workshop elves be coming out and partying
all night? It was up to me to find out!
Years ago, in an effort to avoid going
broke due to constantly buying batteries to feed this radio, Dad had installed
a power socket so he could run the
radio from a small plugpack supply
instead. This simply involved breaking the positive line from the battery
holder to the circuit board and wiring
the socket so that when the plugpack
supply was plugged in, the battery
was disconnected. Conversely, when
the plug was removed, it would run
on batteries once again.
Basically, the socket had to be wired
this way because the batteries weren’t
rechargeable types and wouldn’t take
kindly to being connected across an
external power supply!
To be honest, I was half-expecting to
open it up and find everything covered
in leaked battery gunk. It’s so easy to
leave batteries sitting in a device and
forget all about it, only to come back
years later and find it in a sorry (and
usually non-working) state. I’ve done
it myself, leaving many very cool and
probably now highly-collectible toys
and other 60s-era gadgets ruined.
The goo that leaks out of old, dead
batteries can be highly corrosive and
it tends to attack everything it touches.
Over the years, I’ve often had to tell
customers who have left batteries in
June 2016 57
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man’s Log – continued
devices that those items were now
fit only for the rubbish bin. It’s a real
shame, because it’s a totally avoidable
waste of good electronic gear.
Anyway, when I got to the radio, I
discovered that Dad and my sister had
already had a go at it. Impatient, like
many good servicemen, Dad had “sis”
take the covers off and, acting as his
eyes, have a look to see if they could
determine what was going on. My sister
isn’t really into electronics, so it isn’t
surprising that she and Dad couldn’t
find anything wrong.
When it was shown to me, I was
pleasantly surprised to find there
were no leaked batteries; just a wire
adrift from the old power socket. Dad
mentioned it’d come off when they
were poking around in there but that
I should be able to see where it came
from and take that into account when
trying to find out what was going on.
I removed the already-loosened case
and had a good look around inside it.
I could see the power socket that Dad
had put in all those years ago and it
was now looking very old and corrod-
ed. It also looked to be a bit
mangled, as if something
other than a plug had been
forced into it at some stage.
On closer inspection, the
spring-loaded contact that
broke the battery circuit
when the power plug was
inserted appeared to have
been twisted around and
appeared to be shorting out
across the other contacts.
My guess was that it was
this that was draining the
batteries.
Dad wasn’t interested in
keeping the power socket
there so I just fired up his
soldering iron, de-soldered
all the wires that were left
on the socket and reinstated the original connections directly from the
battery holder to the PCB. However,
before I connected the positive lead, I
put my multimeter in series with the
wiring and after setting it to measure
current, turned the radio on. It drew
around 15mA at medium volume,
which seemed reasonable to me and
certainly wouldn’t drain the three Csized batteries overnight.
Finally, I reconnected everything,
replaced the back, switched the set on
and marvelled at how much better this
radio sounded than anything else I’d
heard in a long time. They really don’t
make them like they used to!
Weather station
With the radio now working, my
next job involved taking a look Dad’s
weather station. My parents have had
this station for years; it consists of a
bunch of stuff sitting at the top of a
3-metre pole rising from a deck at the
front of the house and an LCD screen
in a frame hanging on a wall in the
lounge room. The two sections con-
Servicing Stories Wanted
Do you have any good servicing stories that you would like to share in The Serviceman column in SILICON CHIP? If so, why not send those stories in to us? In doesn’t
matter what the story is about as long as it’s in some way related to the electronics
or electrical industries, to computers or even to car electronics.
We pay for all contributions published but please note that your material must
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Please be sure to include your full name and address details.
58 Silicon Chip
nect wirelessly, the sensors on the top
of the pole sending the data to the base
unit which displays all the relevant information, including indoor/outdoor
temperature, humidity, air pressure,
wind speed and direction and rainfall.
As well as showing all this weather
information, the touch-screen base
unit also shows the date and time. At
least, it should display all that stuff
but there were a few issues with Dad’s
unit. For a start, the wind speed indicator showed nothing, which wasn’t
surprising as the anemometer had lost
most of one of the three little cups it
uses to catch the wind and measure
its speed. This meant that the device
didn’t turn much at all, leaving a flatline display on the base unit.
Several other functions were also
displaying either a “0” or flat-lining,
indicating that the batteries in the remote sensors were probably dead (or
dying).
Dad had reminded me to bring over
some tools to drop the pole and so
armed with a Phillips screwdriver I
first removed the screws holding the
supporting brackets. After carefully
removing the last one, I then gently
lowered the pole down before laying
it on the deck in order to get to the
sensor units.
Before I could do anything though, I
had to remove the mass of cobwebs and
dead insects that seemed to fill every
nook and cranny of the array. I had to
be a careful though, as the plastic was
almost powdery in places due to UV
and weather exposure.
There was nothing for it but to remove the anemometer entirely so that I
could take it home and fit another cup
to it. To do this, I had to undo three
small machine screws and carefully
release the wire from the clips holding it in place along the plastic shaft.
A few of these clips literally shattered
as I put pressure on them, such was
the state of the framework.
With that part clear, I needed to
remove some of the plastic covers in
order to unplug the anemometer unit.
The device utilises RJ11 plugs and
sockets (the same as US-style phone
connectors) and these are removed by
pushing a small plastic tab in on one
side in order to release the plug from
the socket.
Once again, spider webs and the
remains of their insect meals were
everywhere underneath the covers,
which probably wouldn’t be helping
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the accuracy of some of the sensors!
Indeed, some webs were so thick I literally had to push them off with the
screwdriver and then pull them away
with my fingers.
Finally, I uncovered the battery compartment and removed the two old AAsize cells. One had started leaking a
little, so they had obviously done their
dash, with Dad complaining tonguein-cheek that batteries don’t last like
they used to, as these had only been
in service six or seven years! I gave
the terminals a quick rub over to make
sure there was nothing on them, then
installed two new cells and replaced
the battery cover.
Leaving the anemometer to one side,
I then hoisted the pole with one hand
and attached the supporting brackets with the other. We then made our
way inside and tried the base unit but,
rather disappointingly, it still showed
nothing. Suspecting that the problem
may lie in the base unit itself, I took it
down and replaced the batteries with
fresh ones, even though Dad had told
me that he’d recently changed them
because he thought that might be why
it hadn’t been displaying the data from
the sensors.
When I put the last new cell in and
replaced the cover, most of the readings were now being displayed. The
wind speed wasn’t showing up because I had removed the anemometer
but the outside temperature wasn’t
showing up either, so there was still
a fault on the pole.
Once again, I went through the process of dropping the pole and removing all the covers. I was thinking that
perhaps the anemometer had to be
plugged in for the outside temperature to be shown; that maybe they
were on the same circuit, or something
like that.
I plugged the wind speed sensor
back in and checked the base unit,
which I’d cleverly taken with me to
save my ageing serviceman’s legs
from making repeated trips into and
out of the house. Of course, plugging
the anemometer back in had no effect
on the temperature reading (but you
probably already knew that) so I had
to look elsewhere.
I stripped the other sensors off again
and cleaned all the phone-style sockets, then made sure that the various
plugs had perfectly clean contacts
before putting everything back together again. This time, after “rebooting” the base unit again (by removing
and replacing the cells), all the figures
showed up and appeared to be accurate, if the old mercury thermometer
mounted outside the house was any-
thing to go by. And so the pole went
back up again and the base unit was
placed back in its niche on the wall.
That just left the wind speed sensor
which I then took home with me. It’s
really just a brush-motor fitted with
three small hollow cups mounted at
120° intervals to catch the wind. Depending on the wind speed, the motor’s armature generates a small voltage
at the output of the field and this is
fed to the wireless sender via a single
RJ11 connector.
As mentioned, a large section of one
of the cups was missing. I’m not sure
how it got knocked off but going by the
state of the remaining plastic, heavy
rain drops could have done the job!
I thought that half a ping-pong ball
might make a good replacement so
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June 2016 59
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Electric Plunge Furnace Repair
A simple but puzzling fault can completely cripple a large piece of industrial equipment. D. T. of Prospect, SA recently got a
large metal furnace going again with replacement parts costing less than $5.00 . . .
A friend’s brother recently rang me, enquiring if I had any experience with repairing electric smelting furnaces. Apparently,
they were in big trouble as no-one had been
able to repair their plunge furnace and they
desperately needed to get it going again.
This was definitely not in my normal line
of work but I’m always up for this kind of
challenge. And so I offered to have a look
at it and see if I could help.
It was just like a massive machine monster from a horror movie! It consisted of
a large crucible some two metres across
which could be tipped to pour molten metal
into moulds. I was fascinated to see recipe
books which listed the exact mix of different
scrap metals required (in carefully weighed
portions) in order to produce just the type
of metal needed for each project. Included
in their metal stockpile were copper pipes,
scrap stainless steel and even steel parts
from an old bike!
Three 150mm x 3m-long rods made of
what looked like carbon were suspended
at the ends of chains above the pot. These
were in turn connected to three motors
hanging from the roof. The control panel
consisted of three very large current meters with full-scale readings of over 250A,
press buttons to raise and lower the rods
and a power on/off switch with an auto
position.
It was all quite daunting, even while sitting there turned off and not moving.
When the power was turned on, it turned
into a loud fire-breathing monster. The rods
were lowered into the mix and as soon as
a rod touched the mix it started arcing
through the load to the crucible, causing
fireworks and lots of noise. The problem
quickly became apparent. As soon as an
arc was struck, two of the three rods would
correctly retreat and then return again to
maintain the arc and thus continue heating the metal.
By contrast, the third carbon rod just
continued to push on into the load. At the
same time, its associated current meter
was pinning its needle at full scale until
the whole system tripped out.
I began my troubleshooting procedure
by analysing how it was all meant to work.
The plunge motors on the carbon rods were
3-phase 1hp (750W) types driven by three
3-phase contactors, one to activate the
drawer and compared it with one of the
remaining cups for size. Amazingly, it
was exactly the same!
The problem now was cutting the
ball in half. I don’t know if you’ve ever
tried it, but cutting a ping-pong ball in
half is really, really difficult!
I initially tried using my old Dremel
Moto-Tool scroll saw but gave up after nearly taking one of my fingers off.
I did manage to cut about half-way
through the ball but in the interests
of keeping my fingers intact, did the
rest with a new blade in my scalpel.
Even then it was as rough as guts
but at least the ping-pong ball was
now in two bits. I cleaned up one half
down to the seam and then did the
same with the other half, which was
actually a little smaller than the first
one. I then smeared epoxy resin glue
over the inside of the smaller half and
glued it to the larger half, making sure
it lined up neatly.
Once hardened, this made the ball
very sturdy, and I made good use of
that to rub the edge down on a piece of
400-grit wet-and-dry sandpaper. After
sanding, it looked perfectly flat and I
then used the same resin to glue the
cup onto the remains of the previous
cup. It was impossible to tape it into
place while the glue set so I just sat
and held it for five minutes until the
glue hardened enough for me to sit it
on the bench to fully cure.
The finished job looked great and
the overall balance of the complete
assembly is good enough for this purpose. All I have to do now is put it
back up the pole and that’s job done!
60 Silicon Chip
Kenwood TS-450S transceiver
K. G., of One Tree Hill, SA recently had a Kenwood HF amateur-band
transceiver fall into his lap. The only
catch was that he had to get it working
before he could use it. Here’s how he
went about it . . .
I was recently given an amateur ra-
motor and the others to swap two of the
phases over to reverse the motor direction
and therefore the direction of the carbon
rod attached to it.
Each rod and motor was supplied from
the 3-phase supply via a large transformer
which I estimated to be rated at around
350kVA. In addition, each carbon rod had
a current sensor coil fitted to its supply
to monitor the current through that rod.
This obviously supplied a feedback circuit
to activate the reversing function of each
motor to maintain the arc from that particular carbon rod.
I found that I could raise or lower the
rods manually which indicated that the motors and any associated mechanical gear
were OK. That meant that the fault had to
be in the electronic control circuitry.
This control circuitry was spread across
three identical, sparsely-populated PCBs.
These PCBs were so old that they were
made from the now obsolete phenolic
material. Unfortunately, spare PCBs were
no longer available (and hadn’t been for
years), while obtaining a circuit diagram
was also out of the question.
In order to prove that the faulty rod’s
corresponding control PCB was the problem, I decided to swap it with one of the
other PCBs. They were reasonably easy to
unplug and remove, so I carefully labelled
all the wires and swapped them over. The
problem then moved to the other rod, so
the fault was definitely on the control board.
dio transceiver with the message that if
I could get it working and make use of
it, it was mine. It did not transmit and
the receiver was a little “deaf”, resulting in very little audio output.
The model concerned is a Kenwood
TS-450S which covers the HF amateur
bands from 1.8-30MHz and is rated at
100W PEP on transmit. In good working order, this model is still quite a capable transceiver, even though it is now
15-20 years old. As a result, I thought
it was worth spending some time on it
to see if I could fix its faults.
An age of 15-20 years may seem to
be quite old for electronic equipment,
given that so much gear is discarded
after just a few years. Some of it is now
binned in less than five years even if
it still working, the reason being that
it has been superseded by the latest
whiz-bang gizmo. However, amateur
radio equipment generally has a much
greater life-span than the average piece
of consumer electronics.
siliconchip.com.au
I took both the faulty unit and a good
board back to my workshop and had a
closer look at the circuit. It proved to be a
very basic feedback arrangement with an
output much like that used to control the
servo in a radio-controlled toy. I’ve fixed
hundreds of these but the scale was different for this job.
One advantage of being in the electronics game since the days of valve black and
white TV is that you accumulate a lot of
parts. The faulty board required a couple
of very early transistors on the outputs to
be replaced, since they had become leaky.
As it turned out, I had the exact devices in
stock, as they were used in some of the
first solid-state portable TV sets.
The two new transistors were duly fitted
and I then replaced a couple of electrolytic
capacitors which had high ESR readings. I
then returned to the monster and refitted
the two boards.
I had everything crossed when the Auto
button was pushed but it all worked perfectly, with the three amp meters settling
down to about half-scale and remaining surprisingly stable. What’s more, the mix was
reduced to liquid metal surprisingly quickly.
This was definitely a diversion from my
normal work but was very rewarding and
interesting. I found out later that if the repair hadn’t worked, a replacement furnace
would have had to have been purchased
and shipped from South Africa at massive expense.
With the radio set up on my testbench, I applied a 10µV signal in the
7MHz amateur band to the antenna
terminals and tuned it in. Despite this
strong input signal, the signal strength
meter showed only quite a low reading
and the audio level from the speaker
was anything but strong. That said,
the signal was there and was on the
expected frequency. So the various
local oscillators in the set were on the
correct frequencies.
Next, I connected the radio to a 50ohm dummy load with an RF power
meter in the line. Pressing the pushto-talk lever on the microphone and
whistling into the mike should have
produced an output power of 50W or
more but in this case, no output at all
was shown on my power meter or on
the radio’s internal meter.
Removing the top cover revealed a
large empty space where the optional
automatic antenna tuner would go.
There were several shielded boxes
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with other parts of the transceiver
in them, including (most likely) the
transmitter’s 100W power amplifier. I
concluded that the low-level parts in
the transmitter chain were underneath.
Although it was possible that the
fault lay in the power amplifier, I figured that the best place to start was
early in the transmit signal path. Fortunately, there was a comprehensive
user manual with the radio and this
included the circuit diagrams. These
showed that there were separate RF
and IF units in the set and these were
easily identified once the bottom cover
had been removed.
I expected that the audio signal from
the microphone would go to the IF unit
first, where it is converted to 455kHz.
However, when I attempted to transmit, I couldn’t detect any 455kHz signal at the output of the IF unit which
was clearly labelled on the circuit as
“TXIF” on pin 4 of connector W1.
However, there was obviously audio
coming from the microphone and there
was also audio on the output pin of the
microphone amplifier IC (IC15, pin 7).
From there, the signal path went to a
mic gain control on the front panel and
then through a further amplifier to balanced modulator stage IC8. Attempts
to transmit resulted in a 455kHz signal
at IC8’s output, so everything was OK
up to there.
Following the modulator is a set
of three ceramic filters with different
bandwidths, each selected according to
the mode of transmission. For example,
the 2.4kHz filter would normally be
selected for SSB mode. The selection
is done by diode switches and one of
the switched DC voltages which controls the diodes is called “TXB” which
I measured at a shade under 8V at the
input to the IF unit on pin 4 of CN1.
I then looked for the TXB voltage on
diodes D11 & D12 but the swing from
receive to transmit was nowhere near
what I had expected. Next, I looked
for the TXB voltage on pin 4 of CN5
but it was way below the 8V measured
previously on CN1, even though the
two connector pins are supposed to
be directly connected together. Now
we were getting somewhere.
Measuring the resistance between
the two connector pins resulted in a
reading in the kilohms region. It was
time to remove the IF PCB completely
for a close examination and that simply
involved undoing five or six screws
and unplugging all the connectors.
Once it was out, I put my multimeter
probes on the two connector pins for
another check and got the same high
reading as before. As an aside, I had
recently bought a pair of multimeter
probes with needle-sharp gold-plated
points. They’re just the shot for probing small pads and tracks on PCBs and
for poking through tarnished leads and
solder to get a good connection.
I followed the track from one connector pin to the other and soon found
the discontinuity at a small via. I then
noticed some black “gunk” on the
board which I realised had come from
a nearby large electrolytic capacitor.
On checking the circuit again, I discovered that this capacitor coupled signal
from the audio power amplifier to the
loudspeaker.
I checked this capacitor using my
trusty ESR meter and found that the
ESR was about 80Ω when it should
have been just a small fraction of an
ohm. No wonder the audio output level
was low on receive.
I replaced the faulty capacitor with
a new one and cleaned off as much
of the gunk as I could with isopropyl
alcohol (IPA). It was then necessary
to link the two connector pins with a
thin wire to restore continuity. With the
PCB back in place in the chassis and
all connectors replaced, I then tried the
transmitter again and was delighted to
find that it now worked. After making
a few adjustments, I found that I could
measure 120W peak at the output.
June 2016 61
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Beyonwiz HD PVR Repair
Regular contributor B. P. of Dundathu,
Qld likes to rescue and repair non-working PVRs that are advertised on eBay. He
bought this one for a song and repaired it
using parts on hand . . .
I recently noticed a Beyonwiz DP-P2
HD PVR listed on eBay as not working or
for parts. The auction had a few days to
run, with several bids already, so I kept
an eye on it. As the auction neared the
end, I placed a bid, which I considered a
fair price for a non-working unit. I’ve repaired a few Beyonwiz PVRs in the past,
so I thought I would take a chance on this
one as it was a top model in the Beyonwiz
range at the time.
I won the auction and the unit arrived
in the mail a few days later. To initially test
it, I plugged it into the power and fired it
up and sure enough, it stopped with “Error 0000” indicated on the display. I then
unplugged it and took the lid off. I hadn’t
heard the 500GB HDD running when I’d
first turned it on, so I unplugged the drive
cables, reconnected them and fired the
unit up again.
It still came up showing “Error 0000” but
I could now hear the HDD running. However, it was very quiet, which explained why
I couldn’t hear it with the lid on.
Things weren’t quite so rosy on
receive though. Certainly, the audio
output had improved and the sensitivity was better but it still wasn’t up to
scratch. The receiver’s internal noise
could be heard and in addition, there
was a faint but noticeable crackling in
the audio with no input to the radio.
Unplugging the RXIF input to the
IF unit at connector W1 gave a drop in
the noise but the crackling remained.
An IF gain trimpot is positioned halfway along the IF amplifier chain and
turning this right down reduced the
noise and crackling to zero. That meant
that the problem lay somewhere between the input to the IF board and
the trimpot.
To track this fault down, I first connected a 100nF capacitor across the
output of the first IF amplifier just
prior to the ceramic filters. The idea
here was that this would act as a short
circuit for the IF signal. The crackling
remained, so that meant that the fault
62 Silicon Chip
I then noticed some muck on one of the
larger electrolytic capacitors on the power
supply board. A closer look indicated that
the capacitor had “erupted” and I then
noticed that an identical one nearby was
slightly bulging at the top.
I whipped out my soldering iron and
allowed it to heat up while I removed the
power supply board. The two faulty capacitors were both 3300µF 10V types and
these were quickly replaced and the power
supply board refitted.
I fired the unit up again and the “Error
0000” message had now cleared. In its
place was a TV channel indicator on the
front panel, so I connected the unit via an
AV cable to a small TV set but I couldn’t
get a picture, despite pressing the TV-OUT
button on the remote to change the video
output several times.
I didn’t have a spare monitor or portable
TV with an HDMI input, so I took the unit
into my lounge room and hooked it up to
our main TV set. I then got a picture and
after connecting the antenna, I was able to
tune in all the local channels. A quick flick
through all the channels indicated that everything was working well, at least as far as
TV reception was concerned.
Next, I checked the recordings on the
was likely to be in the vicinity of the
ceramic filters. Just to be sure, I then
placed the 100nF capacitor across the
output of the ceramic filters and the
crackling disappeared.
I then remembered a similar problem that I had encountered in the past,
when leaking electrolyte from a faulty
capacitor had caused just the sort of
crackling I was hearing. What’s more,
the ceramic filters in the set I was working on were adjacent to the leaking capacitor I had replaced earlier and it was
quite possible that some of the goo had
spread out under one or more of them.
That meant that all three filters had
to come out so that the board could be
properly inspected. Removing them
from the closely packed board was a
bit of a challenge to say the least. Two
of them were small black rectangular
blocks with five pins, while the third
was a much larger device with a pair
of pins at each end and a ground pin
for the metal case.
HDD and found that the oldest recording
took place 24/8/11, while the most recent
one was on 10/11/12. This indicated that
the unit had been used for over a year but
had not been used to make any recordings
for the past three years. So was the unit
able to record properly?
It was time to find out. I set it up to record
a program for that evening and all worked
correctly. So the power supply had apparently failed in its first year of use.
In view of that, it’s likely that the unit
had been used in a poorly ventilated area
(possibly enclosed in a cabinet), which
caused the power supply to run hot and
the capacitors to fail. All the other capacitors were still good but the two that had
failed looked like a cheaper brand than the
others, so they were probably doomed to
fail anyway.
I used two recycled Nichicon capacitors
to replace the two faulty ones, so the unit
should now have a new lease on life. It will
eventually be used in our family room but I
will need to find a monitor or TV that has an
HDMI input, because it may not work on AV
on our current TV, although I can test that
later. In fact, it could well be the AV input
on our small TV that isn’t working and I’ll
check that when I get time.
And so another piece of useful (and still
reasonably modern) piece of equipment
was saved from the scrap heap. The best
part was that it cost nothing to repair it,
since I used recycled parts.
Eventually, I was able to remove
the three filters without damage to the
board and wasn’t surprised to see that
some of the black goo had spread under
the filter closest to the electro. Some
more cleaning with IPA ensued, followed by a blow-off with compressed
air. The filters were then reinstalled
and the board put back into the chassis.
Powering up the radio now resulted
in just the expected noise from the
speaker without any of the crackling.
So I’d nailed it!
A quick check with a signal generator set to 50µV showed that the receiver’s gain was now back to what was
expected. While I was at it, I adjusted
the signal strength meter to read S9.
This is the standard setting for a 50µV
signal at the antenna terminals for HF
amateur radio receivers.
The old Kenwood TS-450S transceiver now works well and is a useful
addition for contacts on the HF amaSC
teur bands.
siliconchip.com.au
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