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SERVICEMAN'S LOG
Sorting my quake-damaged workshop
I absolutely love test equipment and have
recently been given some very nice test gear by
a friend who’s just retired. Fortunately, I now
have somewhere to stash this gear, having just
got my quake-damaged workshop properly
sorted out and functioning again.
O
NE THING that makes being a serviceman so much fun is that we
get to have a cool workshop to hang
out in. There are as many different
workshops as there are servicemen
and I always find it fascinating to take
a look at the workshops of other people I meet in the industry.
I especially like to check out what
tools and gadgets they have, to find out
whether similar tools could be used in
my workshop to make my job easier
(or would just be cool to have).
54 Silicon Chip
A good friend of mine, who was involved in 2-way radios, has just retired
and he and his wife are now looking
to down-size the family home into
something more manageable for a retired couple. And that means he must
clear out his workshop.
His man-cave is a particularly interesting place for me to visit. His hobbies have involved all things to do
with radio and his collection of radiocontrolled aircraft, especially rotarywing models (helicopters to the uninitiated), is quite impressive.
To say that this guy’s single-garagesized workshop is packed to the rafters
would be an understatement. Choppers and fixed-wing models in various
states of repair hang both above and
below the rafters, requiring those of
us taller than about 5-feet 5-inches
(1.65m) to walk slightly stooped
to avoid taking out an eye out
on an errant skid or a piece
damaged landing gear.
The floor is covered
with pretty much the
same blend of models, half-built kit-sets
and associated gear.
All that’s left uncovered is a well-beaten
path from the door to
the light-switch and to
the equally-cluttered
workbench. The single
light bulb (an energysaver that takes 10 minutes to warm up) casts
a yellow glow over the
scene and this and the
associated shadows
Dave Thompson*
Items Covered This Month
•
•
•
•
•
Dave finally gets his workshop
functioning again
Faulty Sunbeam Retro KE5200E kettle
Deckel FP4 CNC milling
machine
Maison vacuum cleaner
Faulty Zen-on Justina guitar
tuner
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
add to the atmosphere.
It’s no exaggeration to say that I love
it there and I’ll be very sad when he
down-sizes to some tiny shed that I
guarantee won’t have anything like
the feel of this haven.
However, there is a silver lining;
Keith has had to get rid of his old
scopes, frequency counters and other
flashing-light-infested test gear and,
in the spirit of friendship, he kindly
offered to give some of these instruments to me. The deal is that I can be
their guardian for as long as I want
them and for as long as he can come
over and use them if he ever needs to.
Since he hasn’t used some of them for
a few years now, it’s unlikely he’ll ever
take me up on that but that’s OK; I’m
happy for him to come and use my facilities any time he likes.
So far, I have been given a digital
oscilloscope (an older, 60MHz dualchannel monochrome model) and a
top-quality 20MHz CRT scope, both
of which are in excellent working order. They really do look great on my
shelf along with my existing scope
and various multimeters, soldering
stations and power supplies.
I admit it; I love test equipment and
if I won the lottery I’d have the best
spectrum analysers, audio generators,
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frequency counters and all manner of
other suitably-adorned boxes stacked
from bench-top to ceiling. The beauty
of having this equipment is learning
how to use it to better do my job and
enjoy my hobby, the two curiously
crossing over more often these days.
I’ve already put the scopes to good use
and I’m now looking forward to taking
possession of a very nice AF/RF frequency generator/counter that’s next
on the list to go from Keith’s workshop.
Quake-damaged workshop
Some years ago, my own workshop,
which is about double-garage sized,
was rendered a complete disaster area
by the swarms of quakes we had here
in Christchurch five years ago. Prior
to those cursed quakes, I had a lot of
stuff neatly set up in cupboards, on
shelves and in drawers and other storage units all around the walls of my
workshop. This “stuff” included small
bucket-sized bins of resistors, capacitors, diodes, transistors, ICs and other
components one tends to accumulate
over 40 years of hobby and professional electronics work.
These parts were all neatly arranged
and stored in their own compartments
and trays until 12.51PM on the 22nd
February, 2011, wherein the shelves,
drawers and cupboards were literally
torn from the walls and everything in
and on them ended up dumped onto
the workbenches and floor below. The
benches run around the entire workshop at a height of 900mm, with gaps
only for the entry door and a couple of
larger machines along the back wall.
During the subsequent aftershocks,
of which there were many, everything else that lived in racks, drawers, shelves and boxes under, on or
around the benches also ended up on
the floor, along with my lathe, drillpress, sander, band-saw, scroll-saw
and electronic test gear.
I almost cried when I first opened the
door but soon forgot about that because
my lathe had fallen across the doorway,
preventing it from opening properly.
The lathe had also taken out a tall metal
cabinet of drawers that lived next to it.
Fortunately, all the drawers (A4-sized
and full of lathe tools, components,
half-finished projects and other electronic bric-a-brac) had fired out into the
middle of the room, so they avoided
getting crushed. However, their contents added to the pile that now covered most of the workshop floor.
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I initially surveyed the damage
through the gap in the door and after checking nothing was on fire and
that the workshop power was disconnected (fortunately, the mains were off
and would stay off for another 20-odd
hours), I locked the door and vowed
to sort it all out later.
It took about a year to get the workshop into some semblance of order,
which basically meant I could walk
around most of it. It was still a right
mess though and remained like that for
another few years as our focus was on
other things. Besides, with on-going
after-shocks, there was an air of “why
bother?” about it all. It was a terrifying
time and I didn’t want my epitaph to
read: buried in his workshop!
As a result, my workshop space
became a little-utilised repository for
anything that didn’t fit in the house,
or was too valuable to leave in the
often-open garage that fronted the
workshop itself. My workbenches,
which had been clear and organised,
were now covered entirely in stuff and
if I wanted to do anything, I had to
literally push things aside until I had
room for the new job.
Over the years, I chipped away at
clearing it up by doing things like
sorting out the resistors from the capacitors and then separating other
components – no easy task when literally thousands had been mixed together into a scrambled and hard-topull-apart pile that would likely have
filled a bathtub. Part of me wanted to
just toss the lot and start again but the
miser in me prevented me from tossing
perfectly good components.
It took quite some time to sort it all
out and I while I was at it I also separated the electrolytics and tantalums
from the non-polarised capacitors and
sorted miscellaneous items like terminals from screws, nuts and bolts. One
of the most frustrating jobs involved
separating about 200 assorted springs
from all the other bits; they gripped
and grabbed onto everything and I very
nearly just chucked the lot but decided
against it after considering how long it
took me to accumulate them (and how
handy they can be).
Once I had all that small stuff squared
away, I began looking at shelving and
other storage options that wouldn’t be
susceptible to falling down in quakes.
A lot of bits and pieces originally lived
on shelves around the walls but I now
had to find homes for them in drawers
and other solid storage options.
We haven’t had any sizable aftershocks for the last 12 months (touch
wood) but I’m reasonably confident the
storage I now have will take anything
up to and including a quake that would
drop the garage. And if that happened,
I’d have bigger problems than sorting
out some resistors!
At least we don’t have to worry
about bushfires, which would be absolutely terrible. Give me a quake any
day over fires (well, a smaller jolt at
least).
To chuck or not to chuck
Over the recent Christmas break, I
March 2016 55
Serviceman’s Log – continued
D. A. of Shepparton, Victoria recently encountered a string of faults
in an old Deckel FP4 CNC milling
machine. Here’s how he got it going again . . .
Earlier this year, I was asked by a
relative if I’d have a look at one of
his CNC milling machines. The machine in question was a Deckel FP4
unit from the mid-late 1980s and it
had developed a fault in the CNC
console. I’m no expert when it comes
to engineering but I’ve spent many
years repairing electronic/electrical
and mechanical equipment, both
as a career and as a hobby, and so I
thought “why not?”.
CNC stands for “computer numerical control” and a CNC mill/lathe has
a computer console which allows the
user to push buttons and enter commands to drive the machine’s servos
and motors. These in turn control the
movement of various tools and/or the
job itself in the machine to achieve
the desired cutting and turning, etc.
The story starts when the machine
began displaying an FP00 error code
which, according to the manual, indicates an emergency shut-down,
tripped overloads and/or pressed
emergency stop buttons. The first
step then is to check the overloads
and emergency stops and in fact the
owner had already done this but had
found nothing amiss.
My first thought was that a power
supply fuse had probably blown or
the supply itself was faulty. When
I took a look inside, I found that a
fuse had indeed blown. I replaced
it and the console came back to life
but there was no vertical sync, thus
causing the picture to roll continuously. However, I was told that the
vertical rolling fault had been there
for some time and that the picture
stopped rolling after the machine
had warmed up. And indeed that
turned out to be the case.
What was encouraging was that
there was no longer an FP00 error on
the display. However, the unit still
refused to work.
Thankfully, the owner has the
operator’s manual and the service
manual for the machine. Unfortunately, the service manual is printed in German (since the machine is
German-made) so I spent quite some
time going over the circuits diagrams
and checking for continuity in the
emergency stop circuit. Eventually,
I found that a track on the circuit
board had been burnt off.
Fixing this cured the fault with
the emergency stop circuit and the
machine worked again. However, I
was puzzled as to what had caused
the fault, as it appeared that the circuit board track damage would have
been caused by an inadvertent short.
The next day, the FP00 error was
back so I again checked the emergency stop circuit and found that it was
functioning as intended. The FP00
fault code can also mean that one of
a few overload circuit breakers had
tripped, so I now turned my attention to those. These were all intact
so I consulted the circuit diagrams
and after some time found that these
overload circuit breakers are 3-phase
with an auxiliary contact. This auxiliary contact is used to relay the fact
that one of the circuit breakers has
tripped, thereby halting the machine
and bringing up the FP00 code.
I soon found that one of the wires
going to one of the auxiliary contact’s
terminals had been clamped mostly
on the insulation rather than on the
copper wire and a quick check with
a multimeter confirmed no continuity. I re-terminated it and the problem was solved. This was probably
a manufacturing defect, the wire just
touching the terminal for all those
years before it finally went open
circuit.
In the end, it was a very simple
fault but it wasn’t easy to find. Of
course, that left the vertical rolling
fault but because it quickly disappeared as the machine warmed up,
we decided to leave it for the time
being.
That situation didn’t last long because as winter came on, the vertical
rolling fault got progressively worse.
Eventually, it was taking around
five hours for the display to stop
rolling after the machine had been
switched on.
Having worked on many CRT
TV sets, I was fairly sure that this
wouldn’t just involve adjusting the
internal vertical hold control. Instead, the nature of the fault suggested component drift and I suspected
faulty electrolytic capacitors due to
the age of the unit.
Armed with the circuit and an ESR
meter, I checked all the electrolytic
capacitors on the deflection/HV circuit board. Most of them measured
open-circuit which wasn’t surprising
after 30 years or so of service.
I replaced the lot, then reassembled the console and switched the
unit on. The picture was now locked
solid and that finally cured the annoying rolling problem.
That wasn’t to be the end of the sto-
finally got onto the home straight with
the workshop. I spent around three
hours each day that I was off work
sorting out what I wanted to keep and
what I wanted to chuck.
I’ve mentioned before that while I’m
not a pack-rat, I do tend to gather items
that could come in useful for my servicing work. However, I had to modify my philosophy with this clean up.
My criteria before starting the clean-up
was: will I conceivably ever use this
item; yes or no? If “no”, the item went
into a rubbish box.
I also asked “do I really need this
item”? Again, if the answer was no,
the article went straight into the bin.
It was actually quite liberating to get
rid of the junk and tidy the workshop;
I’d had some of that stuff for so long
and the workshop had been such a
mess that it hung over me like a black
cloud and I dreaded going in there. In
fact, there’s a book currently sweeping
the USA about the very subject of getting rid of unwanted clutter and how
life-affirming it can be.
In this book, the author poses the
question: does this item “spark joy”
in my life? If it doesn’t, out it goes.
While I liked my criteria a little better
and thought it a little more practical,
it was interesting that I had much the
same experience while cleaning out
my workshop that this person wrote
about. At the same time, I quietly
Deckel FP4 CNC milling machine
56 Silicon Chip
siliconchip.com.au
ry though. A couple of days passed
and, much to my frustration, the
Deckel FP4 again had a problem.
This time, it was tripping one of its
overload circuit breakers as soon as
there was any attempt to start the
hydraulic pump motor. Apparently,
this machine uses hydraulics to actuate some of the bed axis movements
but I’m no expert on how the whole
machine works.
In this case, an FP02 error code
was appearing on the console. The
manual was quite helpful here because it stated that an FP02 error
code meant hydraulic pump overload and this indicated the relevant
overload breaker to check. It was
tripping the overload at switch-on
alright and my first thought was that
the pump/motor may have seized or
something along those lines.
The only other option would be
a power issue. Sure enough, when I
checked the mains voltage on each
phase at the overload circuit breaker
with respect to ground, two phases
were at 230VAC while the centre
measured just 63VAC. Three-phase
motors don’t appreciate a missing
phase and will draw lots of current
and generally refuse to start.
I then did the same measurements
at the 3-phase power point for this
machine only to find the same readings. So we had a power issue, rather that a fault in the machine itself.
When I inspected the main switchboard, I discovered that the machine
was on a circuit with individual
phase fuses rather than a 3-phase
“ganged” circuit breaker. In the end,
it was a simple case of removing the
blown centre fuse and replacing it.
Once all three phases had been restored, the old Deckel CNC machine
operated normally once more and
should live on for many more years.
cursed the fact that I hadn’t thought
about writing a book about it. It could
have made millions of dollars, which
of course would enable me to buy
even more stuff to fill my workshop
with! Perhaps it all worked out OK
after all . . .
After dumping/recycling 350-odd
kilograms of rubbish from the workshop, I had a lot of spare space left over.
It now feels great to be able to walk to
any part of the bench and have room
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to work on it without having to move
stuff around. The best thing about it is
that it’s a proper workshop again and
I’m not embarrassed to show people
around without making lame excuses as to why it was such a bomb-site.
While I could legitimately claim it was
caused by something beyond my control, it certainly wasn’t beyond my control to tidy it properly long before now.
Of course, it didn’t take long for
someone to ask me if I had something
that I’d just chucked away! It had been
in my workshop for years but hadn’t
met my criteria for keeping it. The fact
is, this will happen every so often and
I’ll just have to live with it.
The kettle carks it
Another thing I’d gotten rid of was
a kettle we’d replaced a few years ago
with a nice new “digital” model. There
was nothing wrong with the old one; it
just didn’t colour-match our new toaster so, of course, it had to go. And so,
after all those years in the workshop,
out it went to the recycling station,
no doubt to eventually turn up in one
of those eco-shops for a few dollars.
I mention this now because just the
other day Nina pushed the power button on our kettle to boil some water.
As she did so, it gave a nasty electrical
“pop!” and its LED display went dead.
And so, being a serviceman, the first
thing I did was grab it and withdraw
to my now-tidy workshop to find out
what was wrong with it.
“It’s probably just a fuse or something just as simple,” I said to Nina as
I made off with it. Yeah, right – famous
last words, as many servicemen will
no doubt confirm.
After negotiating the usual annoying
security-type screws and removing the
base of the kettle, the electronic gubbins were revealed. No simple switch,
thermostat and element for this kettle;
instead, inside was a PCB assembly
that wouldn’t look out of place in a
GPS unit or a portable radio.
The top side of the PCB carried a
number of parts and a 28-pin IC, most
likely a microcontroller of some description. This side appeared to be OK,
so I then had to remove quite a bit of
plastic mounting hardware and unplug various peripherals such as thermostats, wiring looms for the display
and the element wiring in order to gain
access to the underside of the PCB.
As soon as I flipped it over, the cause
of the “pop” was all too obvious; four
very blackened surface-mounted diodes and at least one transistor (or
similar SOT-23 type component) were
clearly damaged. A quick search with
Google confirmed my assumption that
there would be nothing like a circuit
diagram floating around for this appliance and with all active components
sanded or with their part numbers
otherwise obfuscated (thanks manufacturer), this was likely going to be
another guesswork fix.
And so, for the time being, I’m
stumped. If anyone out there in SILICON CHIP “reader-land” has a circuit
diagram for a Sunbeam Retro KE5200E
kettle and is willing to share it, please
contact me.
The rest of the board appears to be
in pristine condition, probably because
the whole thing is covered in some sort
of soft, clear “goop” to waterproof it.
This goop had melted away from the
dead components, making it easy to
access them, but I suppose any “fix”
will require a similar covering once
done. I’ll use epoxy resin. I think –
should I succeed in getting it going
again, that is . . .
All the failed components surround
a relay whose contacts switch mainslevel voltage to the element, so I’m
wondering if the relay has shorted or
something similar. The output track
of this relay has been damaged so it’ll
have to be replaced too.
The diodes shouldn’t be a problem;
the silk-screen at least is very clear
as to polarities etc and they look like
1N4001s or similar for rectifying AC
to DC for the rest of the circuit. The
SOT-23 “transistor” may be a regulator and if I can’t get a diagram, I’ll try
to “reverse engineer” this part of the
circuit and draw a diagram.
That way, I might be able to figure
out what this part does, so that I can
March 2016 57
Serviceman’s Log – continued
Identifying some of the charred parts
on the kettle’s PCB will be extremely
difficult without a circuit.
try to replicate it. Finding another relay should be simple enough too; the
manufacturer has kindly left the part
numbers intact so if I can’t locate the
exact one, any similar 24V DC, 16A
relay that fits the board layout will do
the job. I’ll let you know how it goes.
In the meantime, we went looking
for another one of those kettles but they
aren’t sold any more and the new ones
either seem cheap and nasty by comparison or don’t match the rest of our
kitchen appliances. We’ve settled on
“cheap” for time being in the hope that
I can get the faulty unit going again.
But whatever happens, at least I’ve
once again got a pristine workshop
in which to work. It really is a much
more pleasant place to be than before
the big clean-up.
Maison vacuum cleaner
Regular contributor B. P. of Dundathu, Qld has no particular love for
vacuum cleaners. But why chuck out
old faithful when you can fix it yourself and save money into the bargain?
Here’s his story . . .
Our middle (teenage) son had been
doing some vacuuming (yes, really!)
58 Silicon Chip
when the machine suddenly started
making a loud rumbling noise. Not
wanting to risk further damage, he
turned it off straightaway and I decided to check out what the problem
could be.
My first test was to turn the vacuum
cleaner on and then off again quickly,
so that I could briefly hear it running.
We’ve had this vacuum cleaner for
quite a long time and I had already repaired it several times previously. I’d
also fitted new brushes to it around 18
months ago.
This time, however, I wasn’t sure if
it was repairable, because it sounded
like the bearings were shot. The brushes were also arcing badly, which could
indicate that the armature had shorted
turns. Despite this, I decided to delve
deeper and find out just exactly what
the problem was.
I started by dismantling it and I initially checked the brushes. My suspicion was that they may have been poor
quality and had worn down already, as
the cleaner had had a lot of use since I
fitted them. However, they were fine,
with plenty of “meat” left on each one.
I then noticed that the rear bearing next to the commutator had blue
marks on it, indicating that it had been
running very hot. This wasn’t looking good!
After some further dismantling, I
had the armature free and I could then
assess the situation more thoroughly.
This revealed that the rear bearing had
virtually disintegrated – the plastic retainer that keeps the ball bearings correctly spaced was no longer present,
the metal shield on one side had fallen off and the rubber seal on the other
side had also fallen off.
At that point, the bearing literally
fell apart and the ball bearings dropped
onto the ground. I also noticed that the
metal shield had been distorted, which
indicated that the bearing had been
running out of true. Because the armature would have been moving around
so much, this could explain why there
had been arcing on the brushes.
I then checked the front bearing and
found that it was only slightly worn.
Even so, I decided that I would replace
both bearings and this is where I ran
into difficulty. My automotive bearing
puller was just too big to remove the
front bearing and it would not grip the
inner race of the rear bearing.
As a result, I decided to reassemble the rear bearing, so that it would
have a larger area for the bearing puller to grip. I retrieved the ball bearings,
greased them and placed them in the
outer race, then put the inner race back
in. After turning the bearing, the individual ball bearings distributed evenly
around the unit and I was able to use
the bearing puller to remove it.
That done, I turned my attention to
the front bearing. After some thought,
I decided that because it wasn’t badly
worn and because I couldn’t easily remove it, I would simply service it and
leave it in place. First, I removed the
outer metal shield to access the inside
of the bearing. It had some dirt in it
and the balls were devoid of grease, so
I cleaned it using a pressure-pack can
of multi-purpose spray and then blew
out the remaining liquid with an aircompressor. I then searched for some
suitable grease.
Because I do my own vehicle and
equipment servicing, I have a variety
of greases on hand. In the end, I chose
some automotive “no melt” disc brake
wheel-bearing grease, as this would be
ideal for the purpose. After greasing the
bearing, I refitted the metal shield and
then noticed that there was some wear
on the commutator. This was fixed by
“dressing” it with a fine file.
I knew the rear bearing would be
under $10, so it was worth taking a
risk and replacing it. As it turned out,
it cost less than $5 from a local supplier. Once I got it home, I set about
re-assembling the vacuum cleaner and
when I had the motor back together
and in place, I decided to give it a run
before re-fitting the cover.
When I turned it on, it ran smoothly
without the rumbling noise but there
was considerable arcing from the
brushes. I was begining to think that the
motor might be on the way out when it
suddenly picked up speed. At the same
time, the whine it made increased in
pitch and it sounded “smoother”.
When I looked at it, I immediately
noticed that there was no further arcing
from the brushes and it was running
nicely. I can only assume that the initial arcing had been caused while the
brushes “bedded in” again.
Who knows how much longer it will
continue working but while ever I can
continue to repair it and keep it going, I
will do so. This repair cost less than $5
siliconchip.com.au
and saved yet another defective piece
of equipment from going unnecessarily into landfill.
Of course, this type of repair would
not have been taken on by a service
agency. The cost of the labour alone
would have comfortably exceeded the
price of a new vacuum cleaner. It’s really handy to be able to do this type of
repair myself and save our family quite
a bit of cash in the process.
Faulty guitar tuner
A. C. of Clarement, Tasmania recently repaired an ancient guitar tuner that
had no less than three faults. Here’s
how he got it going again . . .
One of the challenges of being someone who “knows about” electronics
is that all your friends and associates
know you’re the guy to send their paraphernalia to for a quick check-over
when it’s not working.
Recently, I was handed a cheap
guitar tuner from my wife’s employer
(“your husband can fix stuff, right?”)
with the highly-detailed diagnosis that
it was dead. The unit turned out to be
a Zen-on Justina Quartz Guitar Tuner,
with a 3-position switch to power the
unit and check the battery level, a 6-position switch to select one of six string
pitches, a moving coil meter to indicate the battery level and tuning of the
guitar, a built-in mic to allow tuning
acoustic instruments and a 1/4-inch
socket on the side to accept a connection from an electric instrument.
The case was made of plastic in a garish 1970s orange colour but despite its
apparent age, it looked to be in pretty
good shape. In fact, the Justina reminded me of my first guitar tuner which
had been given to me for Christmas
about 25 years prior. Its familiar control layout suggested that it was some
kind of generic design that had been
produced over the years as a budget
alternative to the more expensive tuners made by companies such as Boss
and Peterson.
After sliding off the 9V battery cover it was a no-brainer to work out why
Servicing Stories Wanted
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We pay for all contributions published but please note that your material must
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Please be sure to include your full name and address details.
the unit was dead. The battery clip was
missing, with only the red and black
wire entrails hanging out of the compartment. This was going to be easy!
I rifled through my parts drawers
and extracted a 9V battery clip of a
vintage that complemented the retro
orange duco, de-soldered the two wires
from the PCB and refitted the new clip
in their place. I then managed to find
a 9V battery with enough zing in it to
pass the lick test and clipped it into
the tuner.
Flipping the unit back over, I moved
the first switch to the BAT position and
was encouraged to see the needle rising
to the lower end of the “Good” mark
on the meter. I then slid the switch to
the ON position, selected the A-string
pitch and did my best impersonation
of a chorister at what I thought was
about 440Hz, but the meter’s pointer
failed to rise off the lefthand end-stop.
My first reaction was that the tuner
was simply being judgemental about
my dulcet tones, so I tried a few different pitches on the pitch selector
switch, again with no success. I then
connected a guitar to the 1/4-inch input socket but this also failed to elicit
a response and after confirming that
both the cable and the guitar were
OK on a known-good tuner, I realised
that it wasn’t my singing that was the
problem!
I opened the case again and had a
careful look for any dry solder joints.
This quickly revealed a fractured joint
on the 1/4-inch socket and I surmised
that both the microphone and guitar
signals passed through this socket,
with the microphone signal being bypassed when a guitar was connected.
After re-soldering this joint, I turned
the unit back on and checked the response with my voice and a guitar but
the meter still refused to move.
Disassembling the tuner for a third
time, I re-inspected the PCB for any further dry joints that I may have missed.
I found a couple of narrowly-spaced
pads near the new battery clip pads
that looked a little frosty but I didn’t
think they were bad enough to cause
trouble. Even so, I re-flowed these pads
with fresh solder as well.
Curious to know what was on the
other side of the board, I flipped it over
and had a look at the device connected to the pads I had just re-flowed. It
turned out to be a 78L05 5V regulator
but there appeared to be some kind of
strange mark on the front of its body.
On taking a closer look, I realised that
the mark was in fact a crack that had
split the regulator right down the middle.
I duly replaced the damaged regulator and reassembled the guitar tuner for
what I hoped would be the last time.
And that was it – this time, when I connected a guitar, I was at last rewarded
with the pointer springing up to the
middle of the dial when I ran the pitch
tests. A quick whistle test confirmed
that the microphone also worked. It
also confirmed that my initial assessment of my vocal abilities wasn’t too
far off the mark.
I can’t imagine what caused the
78L05 to fail in such a spectacular way
considering that the highest voltage applied to it would have only been from
a 9V battery. As can be imagined, the
owner was grateful to have the tuner
SC
back in working order.
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March 2016 59
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