This is only a preview of the November 2016 issue of Silicon Chip. You can view 42 of the 104 pages in the full issue, including the advertisments. For full access, purchase the issue for $10.00 or subscribe for access to the latest issues. Items relevant to "50A Battery Charger Controller":
Items relevant to "Passive Line To Phono Input Converter":
Articles in this series:
Items relevant to "Micromite Plus LCD BackPack":
Items relevant to "WiFi Controlled Switch Using A Raspberry Pi & Smartphone":
Purchase a printed copy of this issue for $10.00. |
SERVICEMAN'S LOG
Odd happenings in my new house
You never know what problems are going
to crop up when you move into an old
house and start renovating. In my case, we
encountered some decidedly dilapidated
electrical wiring but after tidying it up, we
were hit with a puzzling power outage.
I reckon that the house we’ve just
moved into is cursed in some way.
Weird things have been happening
from the day we started renovations
but there’s no evidence of an old crone
ever living here and I’m reasonably
sure that the house isn’t built over an
old burial ground. So perhaps all the
odd things that have happened can be
put down to plain old bad luck or to
my seemingly ever-present companion, Murphy.
The first “peculiar” event concerned
our mains power. During the course of
our renovations, we had the walls and
ceilings stripped naked and so had a
golden opportunity to check out the
wiring, much of which was showing its
age. The main part of the house went
up 1966 and it was mainly this area
that we were renovating. This meant
that we were dealing with the original
60s-era building materials and wiring.
In one case, I had removed a light
fitting from the ceiling and after undoing all the screws and pulling it down,
much of the exposed insulation on the
wires fell away in small, brittle fragments. This left about 40mm of exposed copper wiring looking very dan-
40 Silicon Chip
gerous and in obvious need of replacement. My reaction at the time was that
if the rest of the wiring was anything
like that, we were going to have some
real problems.
This section of the house was built
just like most other houses in this
country at the time. It was all quite
basic, with no fancy extras such as
under-floor, wall or ceiling insulation.
And with typically only one notoriously inefficient open fireplace located
in the family room to heat the whole
house, residents were obviously expected to weather the savage Christchurch winters with nothing more than
Dave Thompson*
Items Covered This Month
•
•
•
•
•
Gremlins in Dave’s new house
Bosch BSG82030AU/01
vacuum cleaner
Sharp microwave oven repair
Fuses can be deceptive
Merlin Powerlift garage door
opener
grim fortitude and a pioneering spirit!
During our renovations, we took the
opportunity to rectify that situation by
adding decent insulation and the difference it made was remarkable.
Because the majority of the downstairs wiring was still original, it was
replaced wherever it was possible to
access it. To be honest, the wiring was
a mess due to circuits being added over
the years. Some circuits disappeared
off with no apparent destination, or at
least none that we could trace.
There was also an outside light
mounted on a faux Victorian lighting standard that was never used because the previous owners didn’t know
where the switch was or even if it existed. We borrowed some nifty electronic
tracking tools from a sparky friend that
allowed us to map out the fuses and
switchboard to the various power and
lighting circuits around the house. In
the process, we located several power
feeds that didn’t go anywhere at all,
disappearing at various locations into
the joinery and back out but not terminating in any outlets or switches. These
were stripped out to avoid confusion.
To accomplish this as safely as possible, we removed the pole fuse, which
was a large ceramic-bodied, bayonetfitting fuse arrangement mounted (confusingly) on the edge of the roof. It connected the house wiring to the mains
feed coming in from the street. According to my electrician friend, it was
rated at 65A and was easily removed
by turning it 90° anti-clockwise until
it dropped free.
With the pole fuse removed, the
siliconchip.com.au
house is theoretically isolated from the
grid. Even so, I ran all my mains-detection devices over the switchboard before going anywhere near it, wary that
some cowboy may have wired things
up badly at some stage in the past and
that this could catch out amateurs
like myself. For those concerned readers, I can assure you that our friendly
sparky – who but for very recent surgery would have been doing more of
the physical work himself – oversaw
every stage of the process. In fact, I ran
everything by him (before and after) to
make sure it was up to code and to ensure I wouldn’t be killed in the process!
In the end, we examined all the wiring we could access and removed any
that looked even slightly dodgy. In the
process, we found one circuit in the
80s extension where four power sockets had been cabled in using wire intended for lighting circuits. We removed all of it right back to the switchboard and replaced it with new wiring
with the correct specification.
Most of the wire used by the original
electricians was a flat, twin-core type
with a plain copper earth wire buried
down the middle of the insulation.
Anything utilising this type of cable
was replaced with modern triple-core
flex with a separate (and properly-insulated) multi-strand earth wire. In addition, every socket and light switch was
replaced with new, modern plates and
switches and any sockets used in wet
areas included inbuilt RCDs.
Over the years, the switchboard had
become a bit of a rat’s nest, with what
seemed like a separate circuit and fuse
for every individual socket and light
switch. We ended up replacing two of
the buss bars due to the old ones being full to the brim with wiring and
because both also had several stripped
connectors, meaning those particular
holes could no longer be used.
Because there was literally no room
left in the switchboard, we had to cull
some of the circuits and combine others where possible so that we could
add some heavy-gauge cabling and
breakers for new heat pumps and a
new oven. As a final upgrade, we replaced the old ceramic and wire fuses
with circuit breakers. This was a reasonably expensive job given the price
of the circuit breakers but one well
worth doing.
In the end, we did a lot of electrical
work and I thoroughly enjoyed doing it under my friend’s supervision,
acquiring a few new skills and some
good knowledge along the way. (Editor’s note: unlike Australians, New
Zealanders are legally entitled to do
house wiring but it must conform to
AS/NZS 3000 standards and must be
inspected and signed off by a licensed
electrician).
While the floors were up in various
places, we decided to overhaul the
plumbing system by replacing all the
rusting old galvanised water pipes we
had access to with butylene equivalents. However, this impacted on our
electrical system because many older homes utilise the metal plumbing
structures for mains earth purposes.
This means that removing old metal
pipework can leave the house in a potentially dangerous state.
To rectify this, my sparky overseer
stated that as we didn’t appear to have a
dedicated earth point for the house, we
had to add one. To this end, we sourced
the required 2-metre-long earth rod
from a local supplier and drove it the
regulation 1.8 metres into the ground
right beside the house. After attaching
a new earth cable to it (and the mandatory plastic tags warning about removing it), the wire was run through the
house’s framework and terminated at
tel: 08 8240 2244
Standard and modified
diecast aluminium, metal
and plastic enclosures
www.hammondmfg.com
siliconchip.com.au
November 2016 41
Serr v ice
Se
ceman’s
man’s Log – continued
The Vacuum Cleaner With No Suck
A vacuum cleaner that doesn’t suck
sucks. S. G. of Brookvale, NSW got this
one sucking again . . .
Lesley’s vacuum cleaner, an 8-year
old Bosch BSG82030AU/01 unit with
variable suction control, was sucking
up the dust quite nicely one day when
suddenly its “suck” disappeared. It was
so sick that it could hardly vacuum up
fluff from a tiled floor, while on carpet
it was completely useless.
The first thing Lesley did was poke
a flexible hose through the wand assembly and the floor nozzle to clear
any possible obstructions. They proved
to be clear, so Lesley replaced both
the collection bag and the motor protection filter that sits behind this bag,
in front of the motor intake. The socalled “HEPA” filter that sits in the exhaust outlet was also inspected but it
appeared to be clean and was left in
place (HEPA is an acronym for “high
efficiency particulate arrestance”, in
case you’re wondering).
The collection bag and motor protection filter replacements failed to
cure the problem and so, after inspecting the hose/wand assembly for damage, Lesley threw her non-sucking
vacuum cleaner into her car and took
it to an appliance repair centre. When
she collected it several days later, they
told her that the problem had been
fixed by installing a new HEPA filter
and billed her accordingly.
Well guess what; the new HEPA
filter made no difference although in
fairness to the service centre, it was
easy to be misled as the machine appeared to have reasonable suction at
the hose connection socket.
At that point, I offered to take a look
at it and Lesley demonstrated the fault
to me before handing the machine
over. During this process, we discovered that the motor speed could be
varied only up to about half-way. Moving the suction control over the top
half of the range had no further
effect, the motor speed remaining constant.
My initial thoughts were that if
the motor speed could be varied
over the first half of its range, then
there probably wasn’t much, if anything, wrong with the motor control
module. Perhaps it was nothing
more than a faulty pot on the
the switchboard’s ground bus.
The thing is, without a professional electrician guiding me, I likely
wouldn’t have even considered the
ramifications of changing the plumbing. And that’s precisely why DIY/cowboy electricians and plumbers can be
so darned dangerous. Electrical and
plumbing work should both be left to
those who know what they are doing!
As another example, during the
quakes we dealt with so many prolonged power outages that a lot of residents purchased petrol-driven generators to keep their essentials running
(myself included). However, I heard
of several instances of people receiving severe electric shocks due to near
neighbours connecting generators to
their household supply and thus to
42 Silicon Chip
control module or a simple mechanical
fault in the speed control mechanism?
Google to the rescue
Now I’m no vacuum cleaner repairman, so the first problem was to figure out how to remove the top cover
from the rear half of the unit, so that I
could get at the speed control assembly and motor control board. Lifting up
the cover above the dust collection
bag revealed two self-tapping screws
that clearly had to be removed, while
another two were hidden deep down
in wells under the HEPA filter cover.
However, even with all four screws
undone (and the collection bag and
filters removed), the top cover stubbornly refused to budge. I searched
for extra screws on top but there were
none, so I looked at the base of the
unit. There were no screws visible
there either, so were they hidden under the steerable wheels and if so, how
did the wheels come off?
That’s where Google came to my
rescue. A quick search on dismantling this unit revealed that you have
to prise off the two rear wheels using
a flat-blade screwdriver. This then reveals plastic clips on either side of the
unit and releasing these allows the
top cover of the machine to be lifted
clear (after pulling the power cord part
way out).
With the top cover out of the way, I
took a look at the speed control drive
mechanism. This is nothing more than
a plastic spindle with a curved blade
which runs between the two fingers of
a Nylon slider bracket. As this bracket
is slid one way or the other along its
mounting rail, the spindle rotates and
drives a potentiometer on the control board.
Basically, it’s a very simple gear
mechanism that converts a linear control action into a rotary control action
to drive the pot.
As it turned out, the problem was
the grid because an isolating switch
wasn’t used.
In the process, they inadvertently
“livened up” neighbouring properties
where the householder had assumed
the power was off-line. A few discovered that their wiring was in fact live
the wrong way and it’s indeed fortunate that no-one was killed.
I’ll now get to the main point of this
siliconchip.com.au
The speed control (left) rotates a curved spindle which in turn rotates a pot on
the motor control PCB. The photo at right shows the partly-cleaned intake blades.
staring me right in the face – the Nylon
slider bracket had somehow become
detached from the curved blade on the
spindle. All I had to do to re-engage it
was slide the Nylon bracket off its rail
at the low-speed end, then slide it back
on again with the spindle’s blade positioned between the bracket’s fingers.
Once it was on, I applied power and
gingerly varied the slide control, all
the time taking great care to keep my
hands well clear of the control board
which operates at mains potential. And
that was it – the motor speed could
now be varied right across the control
range and the motor could now be run
at its top speed.
Job done, I thought, so I reassembled the machine, gave it a quick test
and returned it to its owner.
My triumph turned out to be shortlived. Lesley subsequently reported
that although the machine was now
working reasonably well, it still wasn’t
performing at its full potential. Apparently, at the maximum setting, it
should suck an elephant through the
nozzle (OK, a slight exaggeration)
but it was still nowhere near capable
of doing that.
And so I faced up to Lesley’s baulky
Bosch for round two. I began by carefully examining the hose and wand
assembly, looking for blockages and
air leaks. This revealed nothing, so I
dismantled and cleaned the floor nozzle but again found nothing that would
cause loss of suction.
The suction control was still correctly varying the motor speed over
its full range, so that indicated that the
control module itself was OK. It was
beginning to look like there might be a
blockage or a restriction near the motor somewhere.
I dismantled the machine once
more, unclipped the top cover from
the motor housing and lifted the motor clear. Once again, the problem
was staring me in the face; the intake
blades at the front of the motor were
badly covered with a build-up of hair,
dust and fluff (see photo). It was so
bad, it was a wonder that the machine
ran as well as it did.
Fairly obviously, this problem had
been building up for some time but
because the loss of performance had
been gradual, it largely went unnoticed until the speed control mechanism went haywire.
I removed the fluff from the intake
blades using a flat-blade screwdriver
and a soft brush, then used my own
vacuum cleaner to suck out any remaining debris. The reassembled machine then really did have lots of “suck”
and has many years of life left in it yet.
story (it’s been a long time coming, I
admit). Anyway, half-way through the
renovation process, we’d plugged the
pole fuse back in so that we could test
some of the lights and switches we’d
installed. However, while we were
checking things out, the power suddenly went off.
This was rather odd as we weren’t
really doing anything at the time. And
while we still had some un-terminated
live cables hanging out of the walls,
everything was well-insulated with
tape, so I was reasonably certain that
we hadn’t caused the outage.
We initially went outside and check
ed the pole fuse, half expecting it to be
fried, but it was intact. A quick check
with a neighbour then confirmed that
there wasn’t a general power outage, so
Round 2
siliconchip.com.au
there was definitely something wrong
with our mains supply. All we had to
do was find out what the problem was.
Over the previous few days, we’d
been installing LED lights in the kitchen, laundry and bathroom and I’d noticed that they sometimes flickered
when they were on. At the time, I
thought that this was probably due to
the fact that we still had a lot of connections to tidy up in the switchbox
and my electrician friend agreed with
this, as some connections can loosen
with age,
As it turned out, a lot of the connections on the switchboard fuseholders
required at least two screw turns to
fully tighten them. Unfortunately,
although this reduced the flickering
somewhat, it still remained right up
until the power completely failed.
Tracking it down
With full access to a range of electrician’s tools and gadgets, I was confident we’d be able to quickly track down
the cause. I began by climbing back up
the ladder to the pole fuse. We’d been
mucking around with this, so it was a
natural place to start. My contact-less
mains detector showed power flowing in from the street and up to where
it entered the ceramic pole fuse housing. From that point on though, I was
unable to detect anything, so it had to
be the fuse, didn’t it?
I removed the fuse and had a good
look at it under a magnifying lamp. Its
contacts, though aged and a bit corroded here and there, appeared fine
and the fuse checked out OK on my
multimeter. I then used my diamond
contact shaping file and some fine-grit
sandpaper to clean up both the holder and the fuse contacts but this made
no difference; we still had no power.
Next, I took a closer look at the mains
feed where it entered the fuseholder
and discovered that the insulation
had bubbled and discoloured – obvious signs of overheating. This could
certainly have something to do with
the problem but I wasn’t going there.
I’d made (and was obeying) a self-imposed rule of touching nothing on the
incoming side of the pole fuse and in
any case, I wasn’t authorised to do so.
Nor did I have the knowledge or the
courage to muck around with a live
mains feed.
My sparky mate confirmed that we’d
have to get hold of the power company
to go any further and they had a guy out
November 2016 43
Serr v ice
Se
ceman’s
man’s Log – continued
to my house within a couple of hours.
I was straight up with him about what
we’d been doing and accepted that if
the fault was down to me, I would be
up for the cost of the repairs (the standard operating practice for most utility
companies).
As expected, the linesman had all
the right tools; a proper wooden extension ladder, a heavy-duty safety
apron and rubberised gauntlets (or long
gloves). After listening to my theory
about the dodgy-looking feed wire, he
checked the meter box before climbing up to the pole fuse. He did what
I’d done to test it, with the same result,
and agreed that the signs of overheating were a concern.
And then, as soon he touched the
wire, it dropped clear of the pole fuse.
“There’s your problem,” he commented dryly! On closer inspection, it had
corroded through, probably over many
years, heating up as each strand gave
way and less wire carried more current until it picked this moment to
finally let go.
His initial plan was to simply re
attach the cable to the pole fuse, tidy
it up and carry on but one of the two
brass screws that fastened the cable
into the ceramic holder sheared off as
he tried to release the burned-off end.
This triggered a chain of events that entailed a new pole fuse being installed
and even a whole new pole!
The reason for this is that new pole
fuses need to be mounted at a certain
height but our old pole was too short
to comply. That meant that a new one
had to be installed.
In the end, it was a different and a
much more modern arrangement. Best
of all it finally restored power to the
house so we could carry on with our
renovations.
Sharp microwave oven repair
Microwave ovens are now so cheap
that most people immediately replace
a faulty unit with a new one. Not so
J. N. of Tauranga, NZ. When the display on his microwave oven failed,
he fixed it instead of consigning it to
landfill . . .
We’ve owned a Sharp Carousel microwave oven for some time now and
it has suited our purposes admirably.
Unfortunately, its display suddenly
disappeared one day but all the other
functions were still fine.
As a semi-retired electrical/electronics technician, I like to do any repairs on our home appliances myself
and this Sharp microwave was no exception. I began my investigation by
dismantling its front panel and found
a single PCB mounted behind the display. I then downloaded the matching
circuit diagram from Sharp’s website.
It didn’t take me long to realise
that the combined display/processor
IC had simply given up powering the
display. I then contacted a Sharp parts
supplier but they couldn’t supply the
PCB alone, instead quoting for a complete front panel and PCB for NZ$199 +
GST. I declined; for that sort of money,
I could buy a new microwave!
I was not about to give up that easily, however. I had the Sharp part number for just the PCB, so I surfed the net
for a replacement. Amazingly, I came
across the exact replacement on eBay,
complete with the front panel, for an
outlay of just NZ$49 landed in NZ.
When it arrived, I swapped over the
power supply transformer from our
old unit in keeping with our 230VAC
mains input, since the US transformer it came with was for 120VAC. After reassembly, the microwave worked
perfectly again and I was feeling very
pleased with myself until I realised
that the clock was running at the wrong
speed. This also meant that the timer
would be way out.
And then the penny dropped! After
checking the circuit diagram, I realised
that the oscillator running the proces-
Servicing Stories Wanted
Do you have any good servicing stories that you would like to share in The Serviceman column? If so, why not send those stories in to us?
We pay for all contributions published but please note that your material must
be original. Send your contribution by email to: editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
44 Silicon Chip
sor was locked to the mains frequency
and this new unit needed 60Hz instead
50Hz to operate correctly.
Determined not to be beaten, I isolated the now 50Hz pulse to the processor at its INTPO terminal. I then
delved into my spare parts box where I
was lucky enough to find an MM5369
oscillator IC and a 3.579MHz crystal.
Armed with these parts, plus a few passive components, I then constructed
a pulse unit on Veroboard which produced a nice 60Hz output.
The next step was to “steal” some
power from the processor’s DC supply
to power this add-on board. The output
from the MM5369 was then connected
to the processor’s INTPO terminal and
the board secured in position.
The timebase conversion proved to
be a success and our old Sharp microwave is still soldiering on, with a nice
clear display.
Fuses can be deceptive
There’s only one sure way to check
a fuse and that’s with a meter, as
L. W. of Logan, Qld found out when he
tackled a faulty AC/DC fridge. Here’s
what happened . . .
On our new caravan’s maiden voyage, I noticed that the 3-way fridge
didn’t seem to hold up too well when
operating on the 12V setting. It worked
fine on either 230VAC or the gas setting but seemed to defrost rather quickly when 12V operation was selected.
For those unfamiliar with these devices, 12V operation is intended to
only keep an already cold fridge cool;
it definitely does not have the capacity
to chill from scratch. As a result, this
setting is usually only selected while
in transit, when 230VAC is obviously
not available (unless using an inverter) and running off gas is not recommended for safety reasons.
The 12V supply is usually provided by the towing vehicle’s battery and
should be set up so that it powers the
fridge only while the vehicle’s battery
is being charged from the alternator.
Nominal heater resistance is in the
vicinity of 1Ω, so a battery voltage of
12.5V at the fridge results in a current
of 12.5A and this would flatten the
battery in a short time if it wasn’t being recharged.
We made several trips during which
the fridge quickly defrosted (ie, when
powered from 12V) before I finally decided that something had to be done.
After some thought, I decided to have
siliconchip.com.au
Merlin Powerlift Garage Door Opener
Remote-controlled garage door
openers are great except when they
don’t work. The electronic gremlins
recently got into a controller belonging to A. D. of Naremburn, NSW
while he was overseas but he managed to evict them and get it working again . . .
Many years ago, I built a garage
from a kit and fitted a power-operated Merlin Powerlift roller door
opener. It was quite easy to fit and
it was subsequently used for many
years without problems.
Several months ago, I went overseas and, following my usual practice, I disconnected the power to
the door-opening mechanism before leaving. However, when I subsequently returned after a couple of
months and plugged it in again, the
remote control wouldn’t open the
door. I tried the manual button on
the controller housing and it worked
fine but it stubbornly refused to work
with the remote transmitter.
I rang the company that I purchased the unit from and explained
my problem. She quickly told me
that it was probably the remote control itself and informed me that she
a look at it myself rather than take the
caravan to the dealer. The installation manual conveniently provided
a wiring diagram and it showed that
the circuit was quite simple: a heating element in series with a 25A fuse,
in turn connected through the mode
switch to the 12V supply. So how hard
could it be?
The first hurdle came when I removed the outside vent covers to access the rear of the fridge. Only the 12V
connection point and one end of the
heater wiring were visible; there was
no fuse to be seen. This meant that I
couldn’t test the heater element or the
fuse independently for continuity.
At that point, I connected my voltmeter across the 12V connections and,
with the towing vehicle connected and
its engine running, measured a healthy
14V with the fridge switched to the off
position. Switching the fridge to 12V
operation had no effect on this voltage
reading, so I then decided to check the
current. Just as I suspected, this gave
a reading of 0A, indicating that there
siliconchip.com.au
could sell me a replacement. When
I suggested that it may not be that
and asked what I should do if it still
didn’t work, she had no reply other
than to suggest buying another complete unit at a cost of $770.
Unfortunately, she wasn’t able
to provide any schematics and so I
found a company which sold and repaired such doors. The guy I spoke
to told me it was so old they didn’t
have spares but he’d check it out for
$282, which included the price of
another main electronic unit. Since
I had paid only $375 for the whole
thing originally, I didn’t think that
was worthwhile and thought that
a simple solution would be to wire
a remote switch (as sold by Oatley
Electronics) across the manual button contacts, thereby completely bypassing the original remote control
circuitry. In fact, I use just such an
Oatley remote switch to control my
home-made gate opener and I figured
that I could use a spare button on the
existing gate transmitter to trigger the
garage door controller.
Before doing this though, I decided
to have a look at the garage controller and its remote to see if I could
was an open circuit somewhere.
There was nothing for it; the fridge
would have to be completely removed
in order to gain better access to its rear.
An hour later and with the back of the
fridge now exposed, there was still no
sign of a fuse. The problem was that
both the 230VAC and the 12V DC wiring from the heaters disappeared under a thin metal cover which covered
most of the top of the fridge.
Fortunately, this was easily removed
by undoing four screws and at last there
were two fuses visible. I was also able
to see where the 12V heater element
connected to its fuse and switch assembly. Being a 25A fuse, it was easy
to “see” that it hadn’t blown, so I decided to check the heater element for
continuity. It measured just under 1Ω
on the multimeter, which is normal.
I was getting a bit frustrated by now
because that left only the switch as a
suspect. And as it was a multi-pole
switch that contained four sets of contacts, I really didn’t fancy dismantling
it to find out what the trouble was.
find the fault. The LED on the remote
still came on when the button was
pressed, so I looked at the controller
itself. On examining the main PCB,
the first thing I noticed was a blackened resistor and a small 3-terminal
device which appeared to have overheated. Fortunately, I could just read
some of the writing on it and it appeared to be a 6V regulator.
One of the legs on this device was
burnt where it entered the PCB and
the track had been damaged. I didn’t
have a 6V regulator but I did have a
5V regulator in my parts drawer, so I
wired in some resistors in the usual
fashion to increase its output voltage,
replaced the faulty resistor and repaired the damaged PCB track using
some tinned copper wire and solder.
That was it; as soon as I reassembled it and applied power, I was
rewarded with a perfectly working
garage door opener again.
I have no idea what caused the
original regulator to blow, since I
had disconnected the mains supply
from the controller before I went
away. However, judging by the burnt
tracks, it was obviously something
fairly drastic and it almost certainly
occurred when the unit was powered
up on my return.
It was then that I recalled some advice that I was taught way back during
my training days: “always test a fuse
with your meter. It may look OK but
you won’t know for sure unless you
see that needle move over to read zero
ohms” (no digital meters in those days).
And so, with no better ideas at this
stage, I removed the fuse and tested it
on the low ohms scale of the multimeter. It measured open circuit! I tested
it several more times because I just
couldn’t believe what the meter was
saying. After all, it was a 25A fuse and
it appeared to be intact.
Replacing this fuse restored the
fridge to 12V operation for the first time
in its life. All that was left then was to
replace the metal cover and reinstall
the fridge in its cabinet.
Several days later, I hit the ends of
the faulty fuse with a hot soldering
iron and as one end was heating up, its
metal cap moved very slightly inwards.
From then on, it read OK on the meter
and so, just as I suspected, it had been
SC
faulty from new.
November 2016 45
|