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SERVICEMAN'S LOG
How I got trapped inside my MG
There are enough hassles when it comes to
moving house without freezing because your
car’s driver-side power window is stuck halfway down. Even worse is getting trapped
inside a car that’s full of stuff and having to
be rescued.
Things have been rather unsettled
in the Serviceman’s world recently.
We’ve been moving house (and workshops) and it really is a wonder just
how much (let’s be frank) “rubbish”
two people can accumulate during 15
years of living together in one place.
Like my electronics-enthusiast uncle
in Melbourne and to a slightly lesser
extent my Dad, I like to hold onto any
stuff that comes my way, just in case I
might need it one day. Some call this
hoarding but I am a long way removed
from those poor unfortunates who have
to sleep standing up in a corner of their
laundry, because every other room
in the house has been stacked floorto-ceiling with old tat and random
salvage. I can certainly relate in some
small way to those folks and my heart
goes out to them. However, I do know
where to draw the line, although my
wife may disagree somewhat.
It’s not hard to understand why.
After making at least a dozen trips to
our new house with cars and trailers
packed full of stuff, the contents of our
old house and workshop still looked
to be untouched! That’s not only terribly demoralising but also makes it
impossible to deny that I/we have
accumulated far too much junk.
It’s at times like this that I could just
as easily have had a skip parked next
to the trailer and filled both with equal
enthusiasm. I really need to ask myself:
“do I really need this?” If the answer
is “no”, then out it goes. It’s the only
way to shed some of the extra tat we
really don’t need.
While we didn’t have a skip on hand,
Dave Thompson*
Items Covered This Month
•
•
•
•
Dave’s moving house saga
Three switchmode power
supplies
Healing satellite TV box
Exorcising the gremlins from a
mains electricity supply
a lot of stuff did actually make it to
either the recycle station, the clothing
bin or the refuse-collector’s compactor.
And to be honest, there’s a lot more that
can go yet, now that we’ve finished
renovating the new house and can
turn our now-jaded renovator’s eyes
towards the garage and workshop.
Shifting house is difficult enough
at the best of times; renovating the
house before moving into it should
be classified as a form of madness. We
kept postponing the actual moving-in
date, much to the dismay of the friend
who was moving into the house we
were vacating, mainly because various
tradies hadn’t finished within their
quoted time-frames. There was always
some excuse as to why but if you take
whatever time-frame they give you and
double it, you’ll generally be closer to
the mark!
Power window problem
I was hoping that things would at
least go smoothly during the move but
then an unexpected problem cropped
up. On one of the last trips over to the
new place, my MG filled to the brim
with whatever stuff I could cram into
it, I pressed the button to lower the
driver’s-side window to let in a bit of
air. Half-way down, the drive motor
suddenly loaded up, let out a loud,
nasty-sounding “bang” and stopped
dead in its tracks.
“Oh great, just what I need”, I
thought. Fortunately, the weather was
clear but it was very cold and the wind
carried the freezing bite of snow falling
somewhere to the south of us. I was on
a high-speed ring road at the time and
despite juggling the switch, it quickly
66 Silicon Chip
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became obvious that it was going to be
open for the rest of the journey.
No worries, Kiwis are made of pretty
tough stuff and a little cold never hurt
anyone.
Once I got to our new place and had
unloaded the stuff, I had a look at it
to see if I could at least close the window, as the sky was threatening rain
(or worse) and I didn’t fancy driving
back across town with it stuck down.
First, I gave it a good heft and managed to move it in the track a little. I
then pushed the switch and, with a bit
of help from me, the motor strained
and whirred away until the window
eventually reached the top. I wasn’t
prepared to try opening it again and
simply drove the car back to our old
place, where I’d be spending another
few nights before finally changing
locations.
The next day, with the car once again
piled high with more of our earthly
possessions, I headed off to the new
house. However, when I got there and
went to open the door to get out, the
handle felt unusually stiff. I pulled
on it a little harder than usual and
following a loud internal “thunk”, the
handle suddenly became very loose.
Obviously, the cable that actuated the
door latch had parted company with
the handle mechanism somewhere.
With a sinking feeling, I recalled
that the previous day, while helping
the window into place, I’d felt (and
heard) something “give” inside the
door. At the time though, I assumed
that it was something related to the
window’s scissor mechanism. Now
it appeared to be more to do with the
door opening mechanism!
Whatever it was, this presented
me with a bit of a problem. I couldn’t
lower the window, I couldn’t open
the driver-side door and the passenger
compartment was jammed full of bags
and boxes. I can report that the air was
turning bluer by the second!
At that moment, a builder friend
who has been helping with the renovations drove up in his van. Saved! I
shouted out the problem and he tried
to open the door from the outside but
without success. The exterior handle
apparently wasn’t attached to anything
inside the door either. More blue air
followed but no matter; he could at
least unload the gear from the passenger side and I could clamber out
that way.
And that’s eventually how I extrisiliconchip.com.au
cated myself from my MG. It wasn’t
very elegant but at least I was out!
After dealing with the stuff I’d
brought over, I set about looking at the
door. Problem number one was how
to open it. Neither handle worked,
the window didn’t want to move and
I couldn’t remove any panels from
the inside of the door unless the door
was open. This was turning into a real
chicken-and-egg scenario.
My builder friend and I tried some
of the more obscure methods of opening the door but nothing worked. We
even tried the old hand-saw trick;
something I’d seen done many years
before and had actually pulled off once
on a Nissan van I’d owned. However,
while it might work for unlocking
doors to retrieve locked-in keys, it certainly wasn’t about to open this door!
Still, we had a van that was loaded
with tools and a temporary computerservicing workshop that was also full
of tools; surely we had something that
would help us open this door!
The problem was that the mechanism to unlatch the door needed to be
actuated, yet all approaches to it were
obscured or simply not an option. By
now feeling quite frustrated, I sug-
gested cutting a hole in the internal
door panel (I have a spare set) but my
friend’s calmer mind prevailed and
after a lot of jiggery-pokery, we eventually managed to move the window
down in its track. This involved him
leaning on it different ways while I
operated the switch and bit-by-bit we
moved it, very choppily and noisily,
most of the way down. Apart from everything else, something was also very
wrong with this window mechanism!
With the window down, we now
had access through the top of the
door and could see the door-latch
assembly a lot more clearly. All we
had to do was figure out how it operated. Eventually, after a lot of poking
and prodding, we discovered that the
part that is actuated by a cable when
either handle is toggled had popped
out of its plastic housing. Usually, it
was clipped securely in place but the
Nylon bushing had come apart and so
it wasn’t holding onto anything at all.
All I had to do was get something
onto that mechanism and actuate it
to open the door but that was a lot
easier said than done! Finally, I made
up a tool from a 700mm length of thin
aluminium tube I’d salvaged from a
Servicing Stories Wanted
Do you have any good servicing stories that you would like to share in The Serviceman column in SILICON CHIP? If so, why not send those stories in to us? In doesn’t
matter what the story is about as long as it’s in some way related to the electronics
or electrical industries, to computers or even to car electronics.
We pay for all contributions published but please note that your material must
be original. Send your contribution by email to: editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
October 2016 67
Serr v ice
Se
ceman’s
man’s Log – continued
Three switchmode power supplies
Faults in switchmode power supplies can sometimes be
difficult to track down. R. L. of Oatley, NSW recently tackled
completely different faults in three switchmode power supplies,
each with complete success. Here’s how he did it . . .
I retired some years ago after working as an electronics
engineer in the aviation industry. However, friends still ask
for my assistance and advice when their electronic gadgets,
radios and toys, etc fail.
Recently, I was asked to look at three totally different devices
that had failed: a docking station, a washing machine and a
DVD/VCR machine.
The first item was a Phillips AJ7260D/79 clock/charging
station which was completely dead. I removed the bottom
cover and found a brown stain on the inside beneath the power
supply. As there appeared to be no external spillage from the
top, I guessed that something in the supply itself had failed.
On removing the supply, it was obvious that the main capacitor (EC1) had exploded. So was this due to something
else failing or was this the only fault? I checked along the
input path from the 230VAC connection and found that fuse
F1 had gone open circuit and that thermistor RT1 had cracked
from overheating.
Further checking showed that the rectifier was OK and that
switching transistor Q1 had no signs of heat stress. I obtained
the replacement parts, reassembled the unit and powered it
up. It functioned perfectly.
The second item, a Simpson EZISET 550 washing machine,
was apparently working OK one day and dead the next.
After dismantling the top control panel, I checked that all
the switches were functioning correctly and that power was
getting to the control module, which it was, so it looked like
the module itself was faulty. As a result, I removed the control
module and took it back to the workshop.
After prising the circuit board out of its plastic cover, I discovered that the LNK306 power supply switching module (U1)
skip somewhere (see, I knew it would
come in handy!) and an Allen wrench
which was taped half inside one end.
This was carefully eased through the
window gap and then, bit by bit, a
slight curve was formed in the tube
until I got the Allen key onto the latch.
Once it was in-place, it was almost an
anti-climax as to just how easily the
door popped open when I pressed on
the mechanism. What a palaver!
With the door open, it was a simple
matter of removing the door panel to
reveal the goings-on inside. Straight
away, I could see where the window’s
scissor mechanism had come apart.
Two separate steel levers formed a
stamped and spot-welded “X” section
and this created a fixed-point around
which the mechanism pivoted. I was
68 Silicon Chip
had a crack in it and that the surrounding jelly-like coating had
blackened. I checked all the other components between the
230VAC connections and U1 and they were OK.
I ordered a replacement LNK306 (U1) on-line and installed
it as soon as it arrived. The machine then ran flawlessly.
The third item, an LG RC689D DVD/VCR, had suffered a
substantial power surge. I disassembled the unit and removed
the power supply board. It was immediately obvious that there
was some major damage.
I set about tracing out the circuit with the aid of an application circuit for the STR-W6200D switching IC that I’d found
on the internet. The input diode bridge, the filter capacitor, the
limiting resistor, two zener diodes and the switching IC (but
not the input fuse) had all been destroyed, so I ordered the
appropriate parts and waited.
Once these new parts had been installed, the unit powered
up and everything worked fine, hopefully for many more years.
going to need a new scissor mechanism
but in the meantime, I fudged it back
together by drilling a hole through both
pieces and using a short bolt, nut and
washer to secure them.
The window then worked, although
not very well and not through its full
travel. But at least I could open and
close it a bit.
The handle mechanism problem
was quite different. A right-angled
piece of steel rod on the end of a short
cable was supposed to hook into the
door actuator assembly, with a Nylon
clip preventing it from pulling away.
However, this clip had broken. In fact,
the assembly appeared to have been
caught in the window scissor mechanism while I had been manhandling it
the previous day. This had pulled the
cable away from the latch and broken
the clip.
The nylon clip obviously had to
be replaced but in the meantime, I
needed to be able to enter and exit the
car without clambering through the
passenger door! I tried putting the clip
back together and gluing it with epoxy
but it simply pulled apart when the
handle was pulled. It was obvious that
the clip wasn’t going to hold together,
so I scrounged through my parts boxes
and found a nylock-style nut that was
slightly smaller than the diameter of
the steel rod on the end of the cable.
My aim was to thread the end of the
rod and use the nut to hold it onto the
latch, rather than rely on the plastic
clip. To make things easier, I removed
the latch mechanism from the door
siliconchip.com.au
so I could work on it outside the car.
Using a socket, I forced the nut onto
the rod and with a drop of machine
oil to lubricate it, used it as a crude
die to cut a thread. Eventually, I managed to get it on far enough so that it
was secured by the nylock section, so
it wasn’t going to come off in a hurry.
In the end, it worked so well that I
don’t think I’ll bother trying to source
a new clip for it. Besides, now that
the end of the rod has been threaded,
it would probably tear out the inside
of a replacement plastic clip anyway.
Collateral damage
Another instance of collateral damage during the move involved my
headphones. I usually have a reasonably good set of speakers connected
to my computer but in the interests
of domestic harmony, I also use a nice
set of headphones when the situation
requires it.
These aren’t fancy, expensive headphones but they are good, cover-theear types that don’t give me a headache. Many larger style headphones
don’t work well with people who wear
glasses, such as myself, as they press
on the arms and cause discomfort.
However, these ones are just right and
I was a bit annoyed when they started
behaving badly after the move, with
audible crackling and the audio cutting out on the righthand side.
I discovered that I could affect the
sound by flexing the cable where it
entered the left headphone cup, so it
appeared something had come adrift
inside. From memory, these headphones only cost about $12, so most
people would just bin them and buy
another set. However, as a serviceman,
that goes against the grain and so it
was out to the workshop with them.
After a rummage around to find the
necessary tools to strip them down, I
set about finding out what was going
on. Most headphones come apart the
same way; popping off the ear cushion
reveals screws that hold the cup together. Once these have been removed,
the ear plate comes away, usually with
a speaker attached, and with trailing
wires leading off to the rest of the set.
In this case, there was a small circuit
board which was held on with a couple
of screws at the base of the left ear-cup.
Flying leads then ran from this board
to the lefthand speaker and via the
headband to the righthand speaker.
What was rather odd was that a 3.5mm
stereo socket was mounted on this PCB
and the audio cable terminated into
it via a standard 3.5mm stereo plug.
It’s really a good idea, as it makes it
easy to change the lead, should that
be required. What wasn’t such a good
idea was the long, stripped speaker
wires that were touching each other
and other pads on the PCB. Flexing the
cable where it entered the cup moved
the PCB and wires slightly and this
caused the audio interruptions.
The repair simply involved shortening the wires and re-terminating them
with heatshrink insulation installed.
The audio was then once again cracklefree and achieved without needlessly
throwing away a perfectly good set of
headphones.
Healing satellite TV box
N. G. of Gymea recently struck
problems with a Healing satellite TV
receiver that conked out each time he
tried to point the motorised receiving
dish in a new direction. Here’s how he
tracked the problem down . . .
I was a self-employed TV serviceman for most of my working life and
still maintain a keen interest in hobby
electronics, thanks largely to SILICON
CHIP and its predecessors. My main
lounge-room amplifier (still in daily
use) is a Twin 17 Watt Ultra Linear
Valve design, published by John Moyle
in Radio TV and Hobbies and built
while I was a student in 1959.
My wife and I were never able to
find one that sounded better but I guess
that’s another story!
Several years ago, while heading
for retirement and with more time
to pursue the fun stuff in electronics, I decided to have a go at satellite
technology. This was done with the
help of Geoff, my first apprentice and
still a good friend. He rounded up a
secondhand dish and LNB (low-noise
block)and suggested that to make full
use of what was available, a dish motor
would be a very worthwhile addition.
This has proved to be every bit the
case, as the free-to-air stations available in Eastern Australia that are worth
having are well and truly scattered
across four different Ku-band satellite
locations.
Of the hundreds of un-encrypted
channels which can be viewed, I filter
out 40 or so which are of some interest
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October 2016 69
Serr v ice
Se
ceman’s
man’s Log – continued
The gremlins really had fun with
the electricity supply at A.L’s home
in Turramurra, NSW. At odd times,
the power would switch off for no
apparent reason and it took months
to find the cause . . .
“There’s no power dad – can you
fix it?” That was the question from
a family member some months back
when our internet router went down,
along with the dishwasher, the kettle and all sorts of sundry chargers,
lamps and printers etc. It was just
the usual family excess use of all
the available power outlets.
“OK, that should be easy”, was my
answer (famous last words). I soon
discovered that a circuit breaker (in
combination with an RCD) in the
fusebox had flicked off. However,
before switching the power back
on, I switched off all the chargers,
desk-lamps and other items, including the kettle.
The power was then restored
without incident and all was normal
for about the next two weeks. And
then one evening, the same thing
happened again, just as the dishwasher was in the middle of a wash
cycle but without much else on.
Aha! – now was the time to see
which utensil was causing the prob-
lem! I removed everything, restored
power and then plugged things in
one-by-one to make it easy to establish the culprit. Wrong! Nothing
seemed to trip the circuit breaker
or RCD and even when I switched
everything on, the power remained
intact.
At that stage, I put it down to a
possible surge from the mains because our voltage is relatively high. I
measured it at 251V RMS at the time
it cut out (off peak) and assumed
(incorrectly) that any slight surge
may be sufficient to flick the circuit
breaker off.
All then went well for about two
months and then it started to happen
again, usually when the dishwasher
was on. It got to the stage where my
wife was insisting that everything
be turned off (including the router)
when she wanted to use the dishwasher and so I began checking the
prices of new dishwashers, fearing
that the one we had might “blow
up” for good!
After a while though, nothing
seemed to make sense, as the power
seemed to cut out intermittently at
any time of the day regardless of
which appliances were being used.
What’s more, none of the appliances
had any apparent faults!
I also checked the wiring with an
RCD tester, fearing that there may be
some kind of problem like a short circuit or leakage to earth. However, the
system responded perfectly and only
turned off at the specified 30mA and
was OK at 10mA and 20mA. What’s
more, a static current measurement
using a clamp ammeter showed no
measurable residual leakage at all!
Then one day there was a “hallelujah moment” when my wife shouted
“I’ve discovered the problem, it’s the
microwave oven!” She had switched
it on at the power point and the circuit breaker had cut out at the exact
instant. We quarantined the microwave oven but left it sitting on the
kitchen bench while we celebrated
our apparent victory.
Alas, two weeks later, while we
were watching a movie, the power
failed again! So it wasn’t the microwave after all; it had just been
coincidence.
I ventured out to the fusebox in
the darkness and rain to switch the
circuit breaker back on yet again but
this time I noticed a distinct smell
coming from it. It was also warm to
the touch! “Wow”, I thought, “there
must be a lot of current through it to
do that”. Either that or perhaps there
was a problem with the internal
working components of the circuit
breaker itself.
It was a 20-year-old unit (a Clipsal 4BE216/30) and it now became
the main suspect in the mystery. I
and save them as favourites. There are
many very useful programs that are not
normally seen in Australia, even with
pay TV. The satellite FTA choice seems
to be definitely improving (perhaps
being spurred on by all the free TV on
the internet?).
The time shifting that is in effect
provided by the ABC and SBS due to
Australia’s different time zones can
also be very useful.
An FTA standard-definition (SD)
satellite receiver was part of the original package (Strong SRT 4663X) and
was good enough for a while. However,
with increasing numbers of channels
being only available in HD with MPEG4, I eventually decided to buy a new
Healing HHS242 satellite receiver.
This HD FTA receiver performs
remarkably well for its size and price
and incorporates Disec 1.2, giving full
control of the dish motor (a Sadoun
DG-280) via the single RG6 connecting
cable. It all worked perfectly for the
first 18 months or so, the motor drive
always moving the dish to the exact
location required in very little time.
At the end of this period, it suddenly
ran into problems, with a “No Signal”
message displayed on the TV screen.
When I checked the problem out, I
noticed that the dish was pointing
much too far to the west. However, I
was able to perform a motor reset to
the north reference point and it then
operated normally again – for a while!
This same problem was subsequent
ly repeated several times, so I searched
the internet for clues. This threw no
light on my particular problem but I
did discover that a firmware upgrade
was available for the HHS242 receiver,
mainly to deal with a sound issue. I
held out a vague hope that installing
this upgrade might improve things but
no such luck; the problem was every
bit as bad after the upgrade and, in fact,
was becoming more frequent.
The problem subsequently progress
ed to the point where I was unable to
even perform the motor reset, the dish
remaining stuck pointing too far to the
west. When I attempted to use the remote control to move towards the east,
the notation on the screen was exactly
as you would expect – a little flashing
arrow indicating movement to the left
but with no actual physical change in
the direction of the motor itself.
Exorcising the gremlins from
a mains electricity supply
70 Silicon Chip
siliconchip.com.au
This photo shows the obvious signs
of the heat generated on the output
terminal of the RCD due to a loose
wire.
subsequently had it replaced and
all returned to normal.
As it turned out, it was not really
the fault of the Clipsal unit itself. If
you look at the accompanying photo,
you will see that one of the screw
connectors had come loose, possibly
because it had not been sufficiently
tightened, and this had caused a hot
spot as it was not making a good connection to the outgoing Active wire.
And because it was on the bottom of
the unit, the rising heat was causing
the circuit breaker, which is tripped
by heat, to turn off.
It’s probable also that vibration
caused by constantly opening and
closing the fusebox and operating
the switch exacerbated the loose
connection. In fact, subsequent
checks revealed that there was nothing wrong with the Clipsal device
and except for a slightly burnt terminal, it still works as specified. It was
replaced for good measure anyway.
I connected a meter to the receiver’s
LNB input socket and this gave readings of 13.5V DC when the receiver
was tuned to vertically polarised
transponders and 18.4V for horizontally polarised ones. This was exactly
what you would expect and made
me inclined to suspect the dish motor rather than the receiver. I then
wired up a temporary RG6 adaptor
lead which allowed me to measure
the output voltages with the LNB and
motor connected together. This time,
the reading was 0.56V regardless as
to where the receiver was tuned, so
obviously the LNB and motor would
be unable to function.
So was the dish motor placing an
unduly heavy load on the receiver and
causing it to effectively shut down?
siliconchip.com.au
Or was it the LNB that was causing
the problem? Or was the fault in the
receiver?
I have learned over many years of
involvement with electronics to be
very careful about what I throw out
(much to the annoyance of my wife).
And fortunately, I’d had the good sense
not to dispose of my old SD satellite
receiver. This was now reconnected
so that I could check the LNB and
dish motor without the Healing HD
receiver. I was a little surprised to find
that the motor and LNB now operated
perfectly; in fact all of the original satellite locations were still remembered!
When I reconnected the Healing
receiver, I got another surprise. It was
now doing a perfect job of receiving
all of the usual channels on Optus C1/
D3. I then realised that this just happened to be where the dish had been
left pointing when I disconnected the
SD box after testing. The receiver now
appeared to be fully operational for C1/
D3 but it shut down instantly when I
tried to receive a channel from a different satellite.
Clearly, it was sheer luck that the
HD receiver happened to be tuned to
the C1/D3 channel when I first reconnected it, which coincided with the
dish position. This indicated that most
of the receiver was working normally
but it would shut down each time I attempted to move the dish to a different
location. The receiver was thus able to
operate normally with DC power provided just for the LNB but was unable
to provide the extra “grunt” necessary
to turn the motor and drive the dish to
a new location.
This indicated that the receiver’s
13V and 18V supply rails were unable
to cope with the dish motor when
needed. On the other hand, these
supply rails must still be present,
otherwise it would not have been
possible to receive any channels from
the LNB. So how hard could a power
supply problem be to track down? It
was definitely worth a shot.
When I opened the box, I found a
finely detailed double-sided PCB with
numerous plated through connections. Unfortunately, the component
labelling was sparse and there was no
separate power supply board; everything was bundled together. Indeed,
it appeared that this device was not
made to be repaired.
I thought that the logical place to
start was with the electrolytics, so I
used my trusty SILICON CHIP ESR tester
to check all 11 of them. This didn’t
reveal anything unusual and after taking into account the young age of the
unit, the fact that all the electros were
105° types and the plated-through connections, I decided to do a bit more
checking before replacing any of them.
The distributor was unable to provide a circuit diagram, so I did an internet search for any technical details
using the various letters and numbers
on the PCB. This led to nothing of use
so I then tried to make some sort of
sense of what the circuit was doing.
The main power supply itself appeared to produce just two outputs,
nominally 5V and 12V, both of which
measured OK. So where did the 18.3V
and 13.5V for the dish motor come
from? There would have to be a switching voltage convertor of some kind
involved near the LNB input side of
things, so I decided to start with the
electros in that area. Because replacement would not be easy (due to the
plated through PCB holes), I initially
tried bridging the electros in that area
of the PCB but to no avail.
I then carried on bridging the electros in what looked like the main
power supply area itself and that’s
when I struck pay dirt! Capacitor EC3,
a 220µF 25V electrolytic across the
12V rail, was the culprit and bridging
it with a similar value immediately
restored the ability of the unit to rotate
the dish motor without the receiver
shutting down. When removed from
the board and tested again, its ESR was
certainly too high at 5.6Ω but when it
was in-circuit, it was well under 1Ω.
This would not be the first time
that removing an electro was the only
sure way of testing its ESR but I must
say that the symptoms displayed by
the unit were rather strange. It’s several months now since the repair and
there’s been no hint of further trouble.
Finally, I can’t help pondering what
I would have done if the Healing HD
receiver had been tuned to a different
channel to the SD receiver when I
reconnected it. In that case, it would
have immediately tried to initiate dish
movement and would have shut down,
leaving me unaware that it was still
capable of receiving channels.
And that may well have dampened
my enthusiasm for proceeding further with this repair. So I was lucky
– Murphy must have been on holiday
SC
at the time!
October 2016 71
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