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SERVICEMAN'S LOG
Video trials and tribulations
Dave Thompson*
What did we do before USB flash drives became available. They certainly
simplify the playback of digital content but even though they are not
mechanical, I have found some unexpected reliability problems. We have
become so used to the innate reliability of electronics equipment and
it now it seem that can no longer be taken for granted. Still, if you are
prepared to delve into these problems, the repairs can be quite simple.
Long-time readers of this column
may recall the trials and tribulations
I experienced when we purchased a
new home-theatre system a few years
back.
My main gripe was with disc region
codes; after years of playing discs from
all regions in our old, all-zones player, this new Blu-ray capable system
would only play Zone 4 discs.
For those unfamiliar, powerful entertainment-industry lobbyists forced
major manufacturers to implement a
region coding system for DVDs, which
meant, for example, discs produced for
the American market wouldn’t play
on a system designed for the
Australasian market.
This was apparently done to protect
the industry from loss of income due
to them not having control of when
and where movies are released.
But what it really does is impose
price-fixing and monopolising practices onto consumers, which is why
there is barely any legal basis for disc
zoning in most countries.
Thankfully, some manufacturers
ignored these directives and consequently most of us had relatively easy
access to region-free DVD players, at
least we did until Blu-ray came along.
Once again, consumers on this side
of the world are forced to buy inflatedpriced discs long after northern-hemisphere buyers get
to enjoy them, while they
also have a larger variety
of titles at subsidisedby-us prices.
Some good news
is that there is a
huge, quasi-underground network
of dedicated reverse-engineer
types working
to provide
region-free firmware for all brands of
consumer disc players.
Except that back then, there was no
firmware available for our particular
player, and while there might be something now, we’ve long-since worked
around the issue.
For starters, we don’t play Blu-ray
discs, and most of the material we
watch is digital content stored on
USB media, so it isn’t such a big deal
any more.
The biggest blow back then was the
fact we couldn’t play any of the dozens of European (Zone 2) discs we’d
picked up on our travels, including
many titles that were never released
on DVD in this region.
How these corporate bullies still
get away with dictating what we can
watch and when (if at all) escapes me,
which is why I enjoy undermining
their efforts to beat me down. Note that
I’m not advocating ripping off studios
or creators, I’m talking only about legally-acquired media.
When I discovered this LG system
was region-locked, I very nearly returned it and likely would have, until I learned there were no region-free
Blu-ray home-theatre systems on the
market here yet to swap it with. Such
is technological progress.
USB is the answer
This means the main way we watch
content on our system these days is
via a USB flash drive. The system is
network capable, and “internet ready”
but the proprietary WiFi dongle it requires is so ridiculously overpriced I
refuse to buy it.
Running a permanent cable is not
feasible either, given the location of
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Celebrating 30 Years
siliconchip.com.au
Items Covered This Month
•
•
•
Blu-ray player and HandyCam
360° passive infrared sensor
repair
Fuse blows, stove goes
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
the system and the distance from the
nearest network switch.
It’s not really a bother; we simply
load up what we want to watch on a
flash drive and put it into the single
USB port in the front of the player;
after a few seconds we have a basic
file-system we can surf around using
the remote and choose the file to play.
However, of late, we’ve had a few
problems with the drives. Initially, I
thought we might have worn out one
of them, as it would "drop out" once or
twice and we’d have to re-insert it and
fiddle about to try and find where we
left off. This was annoying but with it
only happening every now and then,
not a show-stopper.
Eventually I bought a couple of
higher-capacity flash drives and was
mildly peeved to find one sporadically
not being recognised by the system.
Eventually, it got to the point where
none of the drives would register until we plugged and re-plugged the
drive and even then only with
significant wiggling around;
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obviously there was something amiss.
Like all servicemen, I’m always
ready to drop everything and head to
the workshop. This particular night
we were hyped to watch a particularly
good show and the air was rendered
blue when we discovered that none of
the flash drives would "play".
After unplugging the raft of cables
and plugs connecting the base unit
to the speakers and peripherals, I repaired to the workshop to do some,
er, repairs.
Opening the thing up was simplicity itself. Six small screws held the
metal "top-hat" style metal case onto
the base. The shape of the cover required me to splay the bottom edges
out to lift it straight up and away to
reveal the interior.
The USB socket was in plain sight,
though due to the way it was situated,
the soldered connections were underneath the board. So another half a dozen screws needed to be removed and
a few flying leads and plugs removed
before I could flip the PCB over.
Immediately I could see the problem: every one of the socket’s four
solder joints had a tell-tale dark ring
around the lead coming through the
board. Flexing the socket widened
these rings on one side and compressed them on the other, indicating
that all were fractured and would only
electrically connect when the socket
was pressured this way or that.
No wonder the programs were dropping out and it was hard to get the
drive initialised in the first
place. In fact, I was surprised it worked at all,
given the gaps in the
solder joints.
By this time my
soldering station
was well up to
temp and a quick
application of heat
and a press of the
button on my Goot
solder sucker soon
had each pad on
the PCB and the
socket’s leads
clear of old, dry
solder.
I sweated in
each joint with a
fresh pool of solder and flipped
the board over to
check it had gotten
Celebrating 30 Years
right through to the opposite side as
well. It all looked good and within 10
minutes the screws were back in and
I was in the lounge plugging all those
cables back in.
From that point to this, any flash
drive inserted registers almost instantly and is ready to go within seconds.
Interestingly, I never recalled it being
that good before, so perhaps it had
been defective right from the word go.
There was certainly very little solder on those connections and a lot
less that it has now. I guess this is the
price we pay for lower-cost electronics
in general but surely a bit more solder
all-‘round wouldn’t break the bank.
HandyCam challenge
Another challenge I faced recently
was with my Sony HandyCam. While
this is now about 10 years old, it is
still a pretty good little camera and
since I need a decent camera for my
new YouTube venture, it was, as the
Americans say, a "no-brainer" to dust it
off and charge it up, ready for testing.
Over the years, I’ve taken a lot of
video and stills with this camera. The
4-megapixel sensor might be a bit lame
compared to what’s available now but
back then it was the business.
However, since in all those years I’d
never dumped many of the photos or
videos I’d taken from the 40-gigabyte
hard disc, it was pretty full.
I recently recorded a couple of test
clips with it and while only HD rated
(720p), it will do me fine, until I can
afford to shell out for a mirrorless,
DSLR FHD camera that can do 1080p
at 60 frames a second. Best tools for
the job, right?
And therein lies my problem; the
display shows a mere 18 minutes of
hard-disc space remaining if I continued filming at the current resolution.
To do anything serious, I’d need to
December 2017 61
dump the data on the camera’s drive
to one of my computers to free up a
bit of space.
To accomplish this, Sony deemed
it necessary to provide just one way
of getting the files from the camera to
a computer. Actually, there were two,
possibly three ways, but I’ll talk about
that in a minute.
The problem was that in the shift
to this new house, I’ve misplaced the
supplied USB docking station the
camera requires for a computer connection.
A quick look on the local auction
sites didn’t show any of the correct
model for sale and according to references I found in forum posts regarding the subject, Sony have long-since
stopped making and selling them. I also
tried the usual Chinese online sources
but there was nothing there either.
Convinced the docking station must
be packed away in one of the dozens
of boxes we still hadn’t un-packed, I
spent an entire weekend opening and
sorting through so much extraneous
rubbish that I was almost ready to
dump it all straight into a skip.
I don’t consider myself a hoarder
and it isn’t like I have to sleep standing up because every square metre of
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Silicon Chip
floor space is packed to the ceiling with
swag but I do appear to have a lot of
stuff I could well do without.
How I ever accumulated it all is a
mystery. I can’t recall buying a lot of it
but it’s there so I must have acquired
it at some stage! Annoyingly, though,
the docking station was nowhere to
be found.
It was time to get creative. I blew the
dust off my eBay account and hit the
international auction sites to try and
find one. The model I was after is the
DCRA-171, made especially for my
camera and a handful of other models. I found a couple, and was quite
excited until I saw they were asking
as much as US$95! That seemed a little steep, but I guess the price reflected just how hard to find these things
were becoming.
After a bit more digging, I found one
listed on the UK eBay site, for a much
more reasonable £12, roughly NZ$25.
I placed a bid after discovering they
shipped overseas and even with shipping included, I’d be looking at about
fifty bucks, still a bit high but realistically a much more reasonable amount.
The day of the auction came and
went; when checked I discovered it
had been purchased by someone else
Celebrating 30 Years
after a small bidding war for £35! This
was getting tiresome.
It was about this time I noticed the
camera also has a memory card slot. It
is tucked away under the fold-out LCD
screen and I’d never really noticed it
before. This could be the solution. If I
could still get a memory card to fit it,
perhaps I could transfer the files from
the camera’s hard disc to the flash media and transfer them to the computer using a card reader. That sounded
much more feasible.
I checked AliExpress and the MSDuo cards the camera took were as
cheap as, er, chips and it was no big
deal if I had to wait a little while for it.
However, before I committed myself, I checked the camera’s user manual and believe it or not, there is no way
to transfer files from the hard drive to
the memory card. I could do it the other way, from the flash drive to the hard
disc, but not the way I needed. Darnit!
However, while I was looking on
AliExpress, a camera caught my eye; it
was one of those "action cameras" with
all the cases, mounts and trimmings
for just US$45. Cheaper than a docking
station and with claims of 4K video at
25 frames per second, this seemed an
ideal solution to my problem.
The only extra hardware this camera required was a microSD card and
as I already had a couple on hand, I
wouldn’t need to buy anything else.
Sadly, I put the Sony back in the
drawer while I waited for this one to arrive. I had plenty else to do in the meantime so I went on with that instead.
The camera duly arrived and I was
impressed. It came with a clear, water-proof housing and a dozen other
adaptors and mounts for helmets, handlebars and tripods. I mounted it onto
my tripod and set about testing it out.
The first thing I discovered was that
when set to 4K recording, it could only
manage about one or two frames per
second; a long way away from the 25
FPS claimed. No real harm; I wouldn’t
record in 4K anyway, so it was moot.
However, after further trials, I discovered the camera could only manage a maximum of 23 FPS at 720p and
while truthfully I had no right to expect a 4K, 25 FPS capable camera for
that money, I still felt burned.
And then there is the audio quality;
the on-board mic level was poor and
while this was to be expected when
mounted inside the water-proof case,
even when sitting outside the case the
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audio capture wasn’t great. If I did use
the camera, the cover could be handy
as at times it would be working in a
dusty workshop environment.
As a potential workaround, I carefully bored a 2mm hole through the
plastic case adjacent to the mic aperture in the camera’s case – after all, it
wouldn’t be going under water. While
this improved things a bit, it wasn’t
enough to allow me to record without an external mic, which the camera doesn’t have facilities for anyway.
Boy, this YouTube stuff is difficult!
With that camera a dead duck, I
returned to the Sony and the web. I
eventually stumbled upon a schematic someone had drawn up depicting
the DCRA-171 docking station’s proprietary USB connections. This was
more like it; this might enable me to
solder a cable or connector directly
to the camera’s PCB.
Though heartened, I was reluctant
to pull the camera apart. I remembered last time I repaired it, how complex it was and this time I would need
to strip it down even further, right to
the bottom of the camera.
I took my time and after careful
parts removal, finally reached the
socket. To my dismay, the connector
markings bore no resemblance to the
diagram. Nothing tallied and the two
components seemed miles apart, with
nothing referencing the other.
There were no pin numbers visible and though I had a good go with
a multimeter, trying to ‘ring out’ the
ground, +5V and data + and - leads
and match anything at all to the diagram, it was to no avail. Annoyed, I
reassembled the camera, wondering
where to go from here.
Then, I got lucky. As if on cue, an
email notification popped up saying a keyword search I’d set up on a
local on-line auction site had a hit.
I immediately went online found a
guy selling a DCRA-171 docking station for $20 plus shipping; I bought
it on the spot.
It arrived a few days later and I
hoped like hell I’d not caused more
problems mucking around with the
socket. I needn’t have worried. The
USB connected straight away and I
cleared the files from the drive. Now:
lights, camera, action!
360° PIR Sensor Repair
When something breaks, usually the
worst case is that you have to replace
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it with a new one. B. P., of Dundathu,
Qld did just that, only to find that not
only was the brand new unit broken
and would need to be fixed, it also had
to be modified to fit where the old one
had been mounted! Here is the story
as he tells it…
When we built our new house in
the early 1990s, I installed a 360° PIR
(passive infrared) sensor underneath
the front verandah, near the outside
edge, to operate two coach lights on
the front wall of the house (either side
of the front door) automatically whenever someone approached.
The sensor only worked for a short
time. I wondered why it had failed
when it was still nearly new, so I removed it and inspected it. I found that
the circuit consisted of a 270Ω 0.5W
resistor in series with an X2 capacitor, followed by a bridge rectifier, zener diode and electrolytic capacitor
to supply the low voltage to operate
the unit. This is the same arrangement
used in many low-power mains-connected devices.
It was the inrush current limiting
resistor that had burned out. Luckily,
the resistor had burned out in such a
way that I could still read the value.
I replaced the resistor with the same
type and as a precaution, I wrote its
value on the PCB, just in case it ever
needed replacing again. The unit then
worked again for a short time, before
failing yet again and it was the same
resistor that had burned out yet again.
I could see that this was going to
be an ongoing problem, so I decided
to replace the resistor with something
more substantial. I looked through my
stock and decided to use two 150Ω 1W
resistors in series, as that was the closest I could find at short notice. The total was 300Ω, but it should work OK.
Well, that was obviously the right
thing to do as the unit then worked
for over 20 years with no issues, until
one day when my wife said that it had
stopped again. I took the plastic cover
off and it promptly disintegrated in my
hand due to its old age. So clearly, I
needed to replace the whole thing, no
matter what was wrong with it.
A couple of days later, we were in
Bunnings so I headed to the electrical department and we soon spotted a
similar unit on the display wall. However, when we checked the shelf, there
were none in stock.
In a stroke of luck, the company rep
for that brand was in the store doing
Celebrating 30 Years
December 2017 63
a stock-take, so she grabbed a ladder
to scan the unit on the wall to check
the stock. On her way up the ladder,
she spotted a box at the back of the top
shelf, with the last remaining 360° PIR
sensor, so we bought it.
Later, when I went to fit it, I checked
the light switch for the old sensor and
it was off, so it's possible that the old
sensor was still in working order.
The problem had been that a storm
one night, some time back, kept tripping the sensor and turning on the
coach lights, which are near our bedroom, so it had been turned off and
we then forgot to turn it back on later.
Note to self: next time, check that
the unit is switched on before taking
it apart to fix it!
Anyway, I got set to fit the new sensor and the first problem was that I
needed to drill new holes in the Villaboard ceiling because the new sensor had a different mounting arrangement to the old one. I screwed the base
to the ceiling with the idea being that
the PIR sensor itself would then clip
into the base.
But when I grabbed the unit itself,
I could see that there was a problem
because the three-wire terminal block
protruded and would foul the ceiling.
That would mean I would have to
drill a large clearance hole in the Villaboard, which I did not want to do.
I can’t say I was very impressed with
the design at that stage.
However, I was able to cut the terminal block into three individual terminals with a Stanley Knife so that the
terminals could lie flat and therefore
fit in the recess in the back of the unit.
Problem solved.
As I proceeded with the installation,
I thought I would set the three adjustments: LUX (light threshold), SENS
(movement sensitivity) and TIME
(light on-time) to the values I wanted.
I set SENS to maximum and LUX to
a daylight level so I could test the unit
after installation. But when I went to
set the time to the minimum, the small
adjusting knob kept turning and did
not stop.
Something was obviously wrong
there, so I took the unit down and
opened it up. The two sections of the
case are held together by four clips
around the edge of the unit, so I was
able to separate them without too
much trouble.
A closer look revealed that someone
had tried to adjust this unit on a previous occasion and turned the adjuster
hard against the stop and broken off
the small square plastic extension of
the knob that sits inside the pre-set pot.
What to do? I could not take the unit
back for exchange because it was the
only one in stock and besides that,
I had already modified the terminal
block. There were three choices: bin
the unit, put it up with the broken part
or try to repair it. I quickly ruled out
the first two, so I had to work out a
way to repair this small plastic knob.
I needed to think of something to
add a new square extension to it, in
order to restore it. I tried to think of
something of the right size with a
square cross-section to replace the
broken piece of plastic with and then
I realised a matchstick would do the
job. I cut the head off a match and compared it to the broken piece; it was an
almost perfect match.
So I removed the knob and very carefully drilled a hole where the stop had
broken off, using my cordless drill at
minimum speed, while holding the
knob in my fingers. I started with a
1/16-inch drill, then a 5/64-inch drill,
then a 3/32-inch drill. The resulting
hole was a tight fit for the matchstick
shaft, so I glued it into the hole using
a drop of super glue.
I then trimmed the match to length
carefully with a fine-tooth hacksaw
blade and reassembled the unit. This
somewhat unusual repair resulted in
the restoration of the sensor to “good
as new” condition and saved it from
the bin. Unfortunately, these days,
things are not made to be repaired,
so you often have to be crafty when it
comes to repairs.
I was then able to adjust the delay
time to just above the minimum set-
Servicing Stories Wanted
Do you have any good servicing stories that you would like to share in The Serviceman
column? If so, why not send those stories in to us?
We pay for all contributions published but please note that your material must
be original. Send your contribution by email to: editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
64
Silicon Chip
Celebrating 30 Years
ting and soon had the unit mounted in
place. Job done. I turned the power and
light switch back on and went outside.
The lights were on, but they stayed on
for over a minute, so I started thinking
that maybe there was a fault with the
unit. Then the lights went out.
That was a relief as it just meant that
the TIME adjustment was set too high.
I set it to the minimum and stepped
aside. The lights stayed on for eight
seconds, so that was too short. I advanced the setting small amount and
this resulted in a 15-second delay before the lights went off.
I was aiming for 20 seconds, so I adjusted the setting by a hair and stood
aside. The lights then stayed on for
well over a minute, which was far
too long.
I set the adjustment back by a hair
and this resulted in a 15-second delay
again. This adjustment was far too sensitive, so I just settled for the 15-second delay. I then set the LUX setting
to a suitable level for night-only activation and the job was done.
Exploding circuit board
in my stove!
R. B., of Kambah, ACT was cooking
a stir fry when his induction cook-top
abruptly gave up the ghost. Luckily,
the repair was reasonably straightforward and economical, considering the
high purchase price of the unit...
Recently, I was cooking the evening
meal on my Belling stove which has
an induction cook-top. About halfway
through cooking, the stove went BANG
and the cook-top stopped working. I
rushed around and found a portable
butane cooker to complete the stir-fry.
After dinner I searched out the warranty and purchase documents for
the stove; it had a 2-year warranty
but the purchase was three years ago.
Not good.
Knowing that the induction cooktop was the most expensive part of
the stove, I was thinking this problem
was going to be expensive. With this
in mind I was keen to investigate the
problem and possibly repair it. To this
end I began to dismantle the stove.
It was not too hard to remove the
glass top as a unit, before which I had
pulled the fuse on the stove circuit.
To remove the top required removing
four screws at the back and disconnecting the power supply to the induction top and also unplugging the
signal wire connections to each of the
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control knobs on the front of the stove.
Laying the stove-top upside down, I
was able to remove the screws around
an aluminium tray which held the induction unit under the glass top. Turning the tray over it, was a simple matter to click out the induction coils and
unscrew their cable connections to a
circuit board.
The coils had to be removed to get
to the Torx screws which held a plastic
tray to the aluminium tray. This tray
has three circuit boards clipped into
it. Once the plastic tray was free it was
a simple matter to clip out the circuit
boards after marking and disconnecting the power cables and digital cable
connecting to a small control board.
Looking for the cause of the BANG,
on removing a power filter board I
found that underneath was a large
black soot and vapourised copper
splatter on the board and in the plastic tray.
After scrubbing all of the splatter
off the board it was clear what had
happened. This board had a narrow
track, with slots punched each side,
designed to be the fuse. To support this
analysis, on top of the board paralleling this track is provision to install a
proper 240VAC-rated fuse.
Therefore to make the repair I installed an appropriately-rated glass
mains fuse. There was another similar fuse on the other edge of the board
which I also replaced with a glass fuse
and then cut the copper track. Having
repaired the fuse I had to then determine the reason for the fuse blowing.
On the induction heating coil driver
board, there is a power transistor and
large capacitor for each cook plate.
Checking the large transistors with an
ohmmeter, I found that one transistor
was clearly fused (zero ohms between
all leads).
On looking at the board markings
the three leads on the transistor were
marked C, E and G – odd; I have not
seen a transistor marked this way. Using a solder sucker I unsoldered this
transistor, and to remove its heatsink
I was able to use a long clamp to pull
the clip sideways to cause it to pop
out of the groove; I did not want to
deform the spring in the clip so that
it could be reused.
Once the transistor was out I
could read the markings “TOSHIBA
40RR21”. Finding the datasheet on the
internet, it is an Insulated Gate Bipolar Transistor (IGBT) and “Dedicated
siliconchip.com.au
The underside of the stove-stop which shows the various induction coils and
their cable connections to the circuit board below. These coils were removed so
the aluminium tray could be unseated and the circuit board freed.
to Voltage-Resonant Inverter Switching Applications”. The resonant circuit appears to be formed with a large
capacitor and the induction coil for
each hot plate.
Being a specialised device I was not
so confident I would be able to find
a replacement. However, a Google
search found a replacement at www.
aliexpress.com
My stove cook-top is now working
as before, except next time I should not
have to clean up all the spatter and a
fuse blow-out will be safer.
SC
One of the power transistors on the induction heating coil driver board had
fused and needed to be replaced.
Celebrating 30 Years
December 2017 65
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