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SERVICEMAN'S LOG
When spare parts aren’t around
Some things just aren’t made like they
used to be. When tools break you would
expect that it would be cheaper for the
manufacturer to supply spare parts than
expect the consumer to buy a new tool.
Some of my earliest and happiest
memories are of being in my father’s
workshops. I say workshops, because
like many engineering types, he had
several different shops over the course
of his working life. The first I remember was literally on the “other side of
the tracks” in an area that was considered a little bit, well, industrial.
At that time, Dad was making materials for a fishing rod manufacturer.
He’d designed and built a machine –
his lifelong specialty – that took multiple threads of glass fibre from huge
spools and pulled them through a
heated mould. Depending on which
mould was being used, either a solid or tubular fiberglass rod magically
emerged from the other end.
This machine almost certainly dictated the type of workshop required
due to its bulk, and was why this particular location worked out so well.
He also did a lot of other work from
that workshop. For as long as I can remember he was the neighbourhood’s
go-to guy for fixing everything from
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TVs to talking dolls. These were the
days, the mid-sixties, when people actually held onto the stuff they had, as
opposed to just chucking it away and
buying a new one.
Mind you, manufacturers back then
had a different philosophy as well, to
make the best possible product and to
make it last, even while making spare
parts widely available should the
worst happen. It made a lot of sense for
owners to repair rather than replace,
and while that meant the cost of buying new was dollar for dollar more
prohibitive than it is today, products
lasted much longer.
This all meant that Dad had an almost never-ending stream of jobs
across his workbench and it was always littered with a variety of gadgets and the specialised tools he sometimes made to fix them. The nannystate’s health and safety police of
today would likely have a fit if they
could have seen this workshop, with
Dave Thompson*
Items Covered This Month
•
•
•
•
Nail gun – replace or repair?
Medion computer
Roberts DAB radio
Toyota RAV4 speedo fault
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
the holes in the floor, exposed whirring and spinning machinery and the
constant smell of hot fibreglass resin
but I loved it and recall being very sad
when Dad moved on from that venture
to something else.
Fast-forward ten years, and his
workshop was then almost exclusively
electronics. This was during the CBradio craze of the mid-seventies and
Dad was manufacturing a CB radio
called the Telstat Minicom.
My interest in electronics was getting more serious and this workshop
was like a little slice of heaven for
me. Given it was only a few kilometres from home, I ran there every day
after school under the guise of “training” for athletics but my motives
were ulterior. I would spend an hour
or so with Dad and his then business
January 2017 43
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partner, sometimes helping stuffing
circuit boards, punching holes in chassis or simply watching and learning.
Sadly, once the CB fad wound down,
so did that business and Dad moved
on to a home-based business, which
meant his home workshop, which was
already quite well appointed, gained
some new specialised machinery and
tools such as rotational moulders and
vacuum formers.
Eventually, I picked up that mantle of the local repair guy and I’m still
asked to repair home stereos or old
radios and the like, mainly because
the particular device holds sentimental value.
However, dare I say it, I think the art
of repair is disappearing, thanks to this
replacement culture, and manufacturers have a lot to do with it, with many
changing their manufacturing methodology to reflect that culture. These
days, even if the owner wants some44 Silicon Chip
thing repaired, it often can’t be, due
to the non-availability of spare parts.
Just the other day I had to break the
news to a neighbour that their 1992era, 3-CD player cannot be repaired
because I just can’t find any suitable
parts for it. Such is “progress” in the
modern age.
Another example of this “no repair”
culture is illustrated in something that
happened to me recently. It is nonelectronic but the situation has many
parallels in the field as well.
A few months ago, I purchased a
name-brand, 2-in-1 pneumatic stapler and brad nail gun from a large
Australian-based hardware emporium who have several stores here in
Christchurch.
This tool cost $99, which I thought
a sensible price for a quality tool made
by a well-known tool manufacturer. I
especially like the bright-green plastic fittings, a trademark colour scheme
this company uses on all their tools.
The nail gun came with 250 18 gauge
staples and 250 18-gauge brad nails
and I bought it specifically to tack
building paper onto the walls while
renovating my latest workshop.
With this pneumatic staple gun,
the job went very well, however even
before I’d used up all the staples that
came with it, the hard-plastic ‘bumper’ that clips onto the end of the barrel of the stapler broke in two and fell
off the gun. This plastic piece offers
some protection to the surface of the
material you are stapling or nailing
and assists in spreading the pressure
applied when you push against the
work, which you must do in order to
activate the trigger mechanism and fire
in the staple.
Without the plastic bumper on
there, the end is quite small and being metal, easily marks timber or other
softer surfaces. Indeed, when I tried
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it without the bumper, the bared end
tore the building paper on two out of
five staple attempts, meaning I could
no longer use it for this job.
I consider myself reasonably good
with tools, that is, I don’t habitually
thrash them or put them under any
more duress than they are designed for.
This is the line I took as part of an
explanation email to the support and
spare parts departments of this company in an effort to obtain a replacement plastic bumper.
Surely I couldn’t be the first one
this had happened to? I thought that
this must happen often enough to warrant a healthy store of spare bumpers,
made available through the retailer or website parts department. But
no, the bumpers aren’t available as a
spare part.
I had to email back to make sure. Did
no one else ever have this happen? I
mean, the tip is plastic and takes a lot
of hammering and once broken, the
tool is a lot less functional, especially on surfaces we don’t want marked.
I’d pretty much have to junk the tool
if I couldn’t find an alternative solution. Then again, I shouldn’t have to
do that at all…
The first thing I did is what any
self-respecting serviceman would do;
I tried to repair it. After cleaning the
two plastic pieces with isopropyl alcohol to remove any oils and grease,
I applied a liberal amount of 24-hour
epoxy resin and taped the cover together.
I left it for two days to be sure the
epoxy had completely set. It lasted all
of ten staples before falling apart along
the same fault line. Disappointed but
undeterred, I went to the same local
hardware emporium and bought the
strongest two-part glue I could find.
I also tasked the tool guys there
about the bumper only to be told the
same story.
This time I glued the piece in place,
using a U-shaped piece of copper shim
material formed to bridge the gap at the
top and being careful not to get glue
into any of the workings of the gun. To
hold it all together, I added another layer of glue to the outside and wrapped
the whole thing in a couple of layers
of heavy-duty electrician’s tape, pulling it as tightly as I could to squeeze
the glue without breaking the tape.
As it dried, I periodically worked
the staple mechanism to ensure it
wasn’t going to end up stuck together.
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After another 48 hours, I trimmed the
tape back with a scalpel and carefully
cleaned off any dried glue that would
foul the end of the bumper. Since then,
I’ve pumped at least 4,000 staples and
brads of various sizes through the gun
and it is still going strong.
However, the story didn’t end there.
After that initial email stating there
was no such spare part, I wrote another email in response saying how
disappointed I was that such a fragile
and necessary part was not available
and that the tool was virtually useless
to me without it.
I said that I expected more from this
particular company and considered it
unfair that after paying over the odds
for a better-quality tool, I actually ended up using it for less than a fraction
of the time it should have lasted me.
I told them I’d intended to use it for
woodworking and joinery after the
building paper job but that now looked
to be out of the question.
It was about this time I decided to
try and repair it, and since I ended
up with a working nail gun, I considered it a win, no matter the company’s
response.
A few days later, I got a call from
an Australian customer support representative. She asked for my postal
address, which I gave, and she assured
me the matter would be resolved. I
thought they’d scraped up some bumpers after all and were sending them
over, though it was a bit moot now I’d
glued mine on.
However, that repair wouldn’t last
forever, so I’d at least have another
bumper to replace it with. A few days
later, a courier arrived with a large box,
and I immediately thought this was a
ridiculous amount of packaging for a
couple of tiny plastic parts. Perhaps
they sent a hundred of them!
When I opened the package, they
had sent me a whole new nail gun! I’m
extremely grateful for the amazing customer service but I can’t help feeling
they could simply make spare bumpers available and save themselves
shelling out a lot of extra nail guns!
Medion computer repair
B. P., of Dundathu, Qld locked horns
with a faulty Medion desktop computer. It was a time-consuming exercise
but he eventually got it going again . . .
I was recently given a Medion computer by a friend, after they bought a
new computer. At the time, I was told
that it no longer worked and that they
would dump it if I didn’t want it.
When I first saw it, I immediately
noticed that the card reader door on
the front panel was missing, as it had
been accidentally broken off some time
ago. However, the computer did have a
Windows 7 license, making it a suitable candidate for repair, so I grabbed it.
When I got the computer home, I
immediately decided to check to see
what was wrong with it. I began by removing the side panel and unplugging
all non-essential items from the motherboard. I then removed the RAM and
cleaned the contacts before refitting it
and turning the machine on.
It initially started up but then halted with a CMOS error. As a result, I
got into the BIOS set-up, altered some
of the settings and rebooted it. That
didn’t fix it, unfortunately. Instead, it
was now completely dead.
All further attempts to get it working, including replacing the RAM with
known good RAM, failed and it was
now clear that the motherboard would
have to be replaced. I then checked
the hard drive on another computer.
It was also dead, so something major
must have happened to the computer
to cause all these hardware failures.
Before going any further, I next decided to look into replacing the missing front-panel door. After all, there
would be no point doing anything
else to the computer with the front of
it looking the way it was.
Much to my frustration though, the
front panel proved difficult to remove,
because the optical drive was blocking access to one of the retaining clips.
However, by using a thin knife, I was
able to pop the clip and then remove
the panel.
I knew I had another Medion computer stashed in my shed and after
some searching, I was able to locate
it. This machine was considerably
older than the one I wanted to repair
and had a different front-panel layout.
The case was also badly rusted at the
back and the front power button was
missing, so I didn’t mind wrecking it
for parts.
I removed the front panel from the
older case, retrieved the door panel
and door and compared it with the
door panel from the newer case. It
was significantly different, being some
6mm deeper than newer unit, so I completely dismantled the replacement
door panel and trimmed it down to
January 2017 45
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size. I then reassembled it and fitted
it to the newer panel.
This worked out well and in fact,
the front of the computer looked completely original.
My next step was to see if I had a
motherboard that could be used as a
replacement. As it turned out, I had a
very similar AMD-based motherboard
that looked like a suitable candidate.
This was a Gigabyte GA-880GM-USB3
Rev 3.1 motherboard with an Athlon
II Quad Core 3.0GHz CPU, whereas
the original motherboard contained
an Athlon II dual-core 3.1GHz CPU.
Provided I could get the replacement
board working, it would have a bit
more fire-power than the original unit.
I then rummaged through my box
of DDR-3 RAM and managed to find
four Kingston 2GB modules. I installed
these in the replacement motherboard,
fitted the board inside the case and ran
Memtest 86+. It all passed with flying
colours, so that was the RAM sorted.
I then cleaned and swapped over
the original heatsink and fan from
the faulty motherboard, as both were
slightly larger than the stock AMD
units on the replacement board. The
fan was also fitted with a clip-on trumpet and this actually lined up better
with the holes in the side panel than
the original trumpet.
I also had a spare 500GB Seagate
hard drive, so I installed that and then
went about installing Windows 7 on
the computer. Once finished, Windows 7 booted up without complaint
and when I checked, I had 30 days left
to activate it.
I then installed the drivers for the
motherboard and the inbuilt WiFi
card, which is located behind the
front panel. After a few days of testing to make sure everything was OK,
I then activated Windows so that the
machine was now ready for use.
However, there was now a further
problem. The original motherboard
carried two internal USB 3.0 ports and
there were two cables plugged into
these: one running to a front-panel
USB 3.0 socket and the other to a USB3
back-up drive connector on the top of
the case. Unfortunately, these internal
ports were lacking on the replacement
motherboard.
I wanted to be able to use a USB 3.0
port on the front of the computer, so
46 Silicon Chip
I had to think of some way of to connect it up (the back-up drive connector was less important). A search on
eBay soon turned up a USB 3.0 PCIe x1 card with two external rear USB
3.0 ports and an internal 19-pin header
at the front of the card. This would be
ideal, as I had already previously seen
a 19-pin USB 3.0 plug to two USB 3.0
ports adaptor on eBay.
In the end, I ordered two adaptors
and two cards and I waited for them
to arrive. Once the parts arrived, I installed one of the cards and plugged in
a 19-pin to two USB 3.0 ports adaptor
and connected the two USB 3.0 cables.
I then turned on the computer and
grabbed the card’s driver CD.
Unfortunately, finding the correct
driver on the CD proved to be anything
but straightforward. The CD contained
several drivers, so it was a trial and
error process until I found the correct
one. Once that had been done, the two
extra USB 3.0 ports were fully functional and ready for use.
Unfortunately, after about a week,
the computer suddenly stopped working. I soon found that the replacement
motherboard had failed completely,
which was a real blow after all the
work I’d put into it.
I had another look through my shed
and this time I found an old rusty case
with a Windows XP license. It also had
a Gigabyte GA-880GM-USB3 motherboard, so I thought I would use this.
I then noticed that even though
it was exactly the same model, this
was a Rev1 board, whereas the one in
the Medion was a Rev3.1 board. The
main difference was a slightly different layout near the RAM slots, with
the Rev1 board also having one IDE
connector and one floppy drive connector, whereas the Rev3.1 board did
not have these additional connectors.
Other than that, the two motherboards were almost identical, with the
same number of SATA ports.
However, why do a simple swap
when there’s an opportunity to complicate things! I knew I had another
Rev3.1 motherboard in another computer that I’d just upgraded, so I decided to remove it from that computer
and use it in the Medion
The Rev1 motherboard could
then be slotted into the donor computer. This would be a more practical arrangement because the
donor computer had a moulded floppy
drive slot in its front panel. By substituting the Rev1 motherboard, I could
then connect the floppy drive again.
The motherboard swap went
smoothly and both computers were
soon back in operation again, each
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Roberts DAB Radio Repair
Fixing a simple fault can sometimes involve a lot of disassembly
work, as G. C. of North Ryde, NSW
found out when he tackled a friend’s
DAB radio. There’s always the risk of
breaking something in the process.
I was recently asked by a friend
to have a look at a 5-year old DAB
radio which, after daily use in the
bathroom, was refusing to switch
on. The radio in question was a Roberts Ecologic 4 mains/battery set. Its
owner said that it was a good performer and that he would like to
have it fixed, if possible.
Working on modern electronic appliances is not my favourite
pastime, as I much prefer restoring valve equipment. Despite this,
I agreed to have a look at it as a favour owed.
Given that this is a digital set, my
initial guess was that the fault was in
the push-on/push-off power switch
itself or with the associated logic. If
it were the latter, then I was hoping
the requisite part would be readily obtainable. Roberts is a British
company, although the radio itself
is clearly made in China.
Before spending time on the radio, I decided to Google the symptoms and found that this was a very
common fault, with many disgruntled owners saying that the response
from Roberts was to send the radio
back to them for repair, along with
the specified fee.
I couldn’t find a service manual online so I emailed the Roberts
Technical Department, requesting
an explanation of the notoriously
common fault to help me fast-track
a local fix. They replied that I should
send the radio to them for repair.
It was patently obvious I wasn’t
going to get any leg-up from the
manufacturer.
At this stage, I decided to open
up the set. This involved the usual
routine of removing a dozen or so
deeply-buried screws using a smalldiameter, long-shafted screwdriver.
The screws were of assorted gauges and lengths, so I made a note of
which went where.
With the case split in half, I was
confronted by a power supply board
in the rear section, adjacent to the
battery compartment, from which
a number of wires ran across to two
main PCBs: one for the radio function and its associated knobs and
pushbuttons and the other for the
stereo amplifier function.
These two boards are mounted
back to back, with an insulating
sheet sandwiched between them.
This sheet consists of a piece of aluminium foil covered on both sides
with its original CPU and RAM. However, I did have to reinstall the USB 3.0
driver in the donor computer, because
the Rev1 motherboard has a different
USB 3.0 chip. Apart from that, all the
other drivers for both motherboards
were identical and there were no complaints from Windows about the motherboards being changed.
Although this had all been a somewhat time-consuming exercise, the
end result is a refurbished, reasonably-modern computer that would have
otherwise gone to scrap.
It may not be up to gaming but it’s
perfectly adequate for internet browsing, emailing and other similar activities. And because I got it for nothing
and I used mainly recycled components for the refurbishment, it cost
me much less than the price of a new
computer.
Nothing to RAV on about
B. C. of Dungog, NSW recently
turned auto-electrician when he took
Servicing Stories Wanted
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by black insulating material.
The upper PCB is made of fibreglass and contains mainly SMD components. By contrast, the lower PCB
is phenolic and contains throughhole components. A plethora of
wires run between these boards
and to the stereo speakers. As well
as those unpluggable cables, there
were three wires soldered to metal
inserts in the case which presumably provide shielding.
It’s not what I’d call an elegant, optimised design by any means.
The on/off control is a 6 x 6mm
pushbutton switch which is soldered to the upper PCB. Without
further disassembly I was able to get
my DMM across its terminals and
confirm that it was functional, so
the problem lay elsewhere.
Further Googling found just one
technical reference to the fault and
it laid the blame on a 4013 dual-D
flipflop. That made sense, given that
a momentary on/off switch needs a
memory of its last switched state.
And a dual-D flipflop is a typical
way to accomplish that.
A small dental mirror allowed me
to see that there was a SOIC chip soldered adjacent to the power switch,
so I proceeded to remove the PCB
sandwich from the case, layer by
layer. Removing the lower PCB and
the insulating layer was comparatively easy.
continued next page
on an aging Toyota RAV4 with speedo,
tacho and air-conditioning faults.
A friend’s daughter has owned the
Toyota RAV4 (a late 1996 model) for a
number of years now. Unfortunately,
due to its age (20 years) and high mileage, various problems have needed attention in recent times.
Recently, I was asked if I would look
at problems with the speedometer, tachometer and the air-conditioning/
heating system. And so, on a recent
visit to her parent’s place, I took the
opportunity to examine the vehicle.
By this time, the speedo had completely failed and she was using the
GPS function on a smart-phone to
monitor the road speed!
Fortunately, the Nippon Denso instrument panel is relatively easy to remove from this vehicle. I then retreated
with the faulty unit to my workshop,
January 2017 47
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However, removing the upper
PCB involved detaching the fascia
from the case in order to reach three
screws hidden underneath it. Unclipping the fascia without breaking
it was a real chore but I was eventually able to reach the PCB.
A quick check with a DMM revealed a short between pins 7 & 14
of the 4013. Fortunately, it’s a fairly common chip costing around 50
cents and a mate with an SMD reflow
station kindly replaced it for me in
a 60-second manoeuvre.
With the new chip installed, I reconnected everything on the bench,
applied power to the system and
pressed the power switch. Bingo! –
placed it face-down on a towel and
removed the speedo and tacho heads
from the main PCB assembly. Each
head in turn had a small PCB soldered
to its rear containing a meter movement with two coils.
The speedo head (PCB – 0680) carried a 24-pin ND SE236 DIL IC but
that wasn’t the cause of the problem.
Instead, there was a dry solder joint
on one of the four coil pins (two pins
per coil). The same problem was evident on the tachometer head PCB. This
board carried a 16-pin D056956-0240
DIL IC and it too had a bad solder joint
on one of its four coil pins!
Since these failures were due to vibration, I decided to blanket solder
all the joints on both the speedo and
tacho PCBs to ensure future reliability.
It was then just a matter of reassembling the instrument panel, taking it
48 Silicon Chip
the LCD displayed “ABC Radio connecting . . .” and a second or two later, sound came through the speakers.
As I reinstalled the PCBs inside
the case and wrestled once again
with the fascia, I began thinking
that this hadn’t been too painful a
job after all. And then it happened!
The on/off button itself was attached to the upper part of the case
by a flimsy web of plastic, about
1mm across, which acted as a sort
of spring.
As the switch’s own button was
only about 2mm high, the on/off
button activated it by way of an integral plastic shaft about 15mm long.
Unfortunately, as I attempted to
back to my friend’s house and refitting
it to the vehicle. A subsequent road test
then showed that both the speedo and
tacho now worked perfectly.
It was now time to troubleshoot
the air conditioning/heating system!
Switching the fan speed to each position (with the ignition turned on),
revealed that the blower fan motor
wasn’t running at all.
Removing the glove box and some
trim items gave access to a subcontrol panel and the blower fan
motor assembly.
A quick check with a DMM then
indicated that +12V was present at
the blower fan input connector, so it
wasn’t a supply problem.
I unplugged the unit and connected
a 12V 7Ah gel battery directly to the
motor input connector via some suitable test leads but there was still no
line the button up with the switch,
while simultaneously keeping the
fascia in place, both the plastic web
and the shaft disintegrated. There
was nothing left to salvage or glue.
Not happy, Jan!
After the customary string of
choice words, I thought about my
options. As there was little chance
of reconstructing the original plastic shaft and spring arrangement, I
decided to fit a new tactile switch
with its own long shaft.
Fortunately, I was able to source
one with a 17mm-long shaft (or actuator) and that was long enough to poke
up through the hole where the on/off
button resides. And so, once again,
I had to remove the PCBs in order
to solder in the replacement switch.
The next task was to gently ream
out the button itself and fill the inside with Knead-It, a fast-setting
epoxy putty. Once it had set, I then
used a slow drill to make an indentation into the putty just deep enough
to accommodate the top of the
switch’s shaft, while ensuring that
the on/off button was at the correct
height to remain in place in its hole.
I then proceeded to once again
wrestle with the fascia and this
time it all went together without
any drama.
The new switch has a more positive feel about it, and my friend was
very happy to have the radio back in
working order.
response. As there were only three PK
screws securing the blower motor assembly in place, it was easily dropped
out for closer examination. Removing
a small air vent cover then allowed access to the rear of the motor.
Close examination of the motor with
the aid of a LED torch subsequently
revealed that the brushes and commutator were both badly worn. And
that meant that a replacement blower
motor assembly would have to be obtained and fitted.
A search on eBay uncovered two
locally-available secondhand units,
both at a reasonable price. One of
these was ordered and I bench-tested
it before fitting it to the RAV4 during
my next visit. This replacement unit
completely restored the vehicle’s airconditioning and heating system to
normal operation.
SC
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