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SERVICEMAN'S LOG
Getting sucked in by a vacuum cleaner
A recent vacuum cleaner repair had me asking
myself the rhetorical question: How much of an
imbecile am I? Sometimes repairs don’t quite go
the way they should, and in this case it might
not have even needed a repair! In my defence,
I’d never worked on one of these particular
models before, so it was very much a trial and
error process.
The housekeeping duties in our
home are shared equally between Mrs
Serviceman and myself. When anyone
asks me for relationship advice (you’d
be surprised how many people ask me
how I’m able to spend so much time
in my workshop without my marriage
breaking down), I tell them this: helping out with the housework beats any
bouquet of flowers or diamond ring.
Nothing says “I love
you” more than
doing dishes,
68 Silicon Chip
doing the vacuuming or cleaning the
toilet!
My point, as usual an age in coming, is that the other day I was doing
the floors with one of our four vacuum cleaners, a battery-powered Bissell Air Ram (if I’m doing the floors, I
need the best tools for the job, right?)
when the machine suddenly made an
alarming and nasty sound before stopping dead. This was accompanied by
a very brief, high-pitched whine and
the usually green battery-status LEDs
suddenly started flashing red.
I promptly hit the off switch and recalled the instruction manual (yes, I
do read manuals) stating that if something got caught in the workings, the
motor would automatically shut down
and the LEDs would flash red as
a warning. The manual also
mentioned that once the
jam was cleared and the
lights stopped flashing, the device could
be restarted.
However, while
the LEDs did stop
flashing, any attempt to switch
the cleaner back
on resulted in
the lights flashing again, indicating something else must
be happening.
I flipped the cleaner
over and checked out
the air intake and powered roller brushes but
Dave Thompson*
Items Covered This Month
•
•
•
Vacuum cleaner repair
Faulty capacitors in Behringer
active PA speaker
CHIMEI LCD monitor
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
couldn’t see anything obvious. As
nothing else is visible from the outside, the only option was to dismantle
the machine in order to get a proper
look inside.
Most battery-powered vacuum
cleaners are underpowered and thus
have the suction of an asthmatic
mouse. This unit is powered by a 22V
Li-Ion battery and has all the moving
parts packed into the compact “head”
of the cleaner down near the floor.
The only thing in the handle is the
battery, making the cleaner lightweight, manoeuvrable and very
efficient, as it only has to suck the
dust and dirt about 50mm into the
dust collectors.
The only complaint I would have
with it is that the two dust reservoirs
are small and fill quickly, meaning
it has to be emptied frequently for it
to perform at its best. I’d obviously
sucked something disagreeable into
the thing because the noise it made
sounded terrible. I actually thought a
fan might have come loose or perhaps
it had run a bearing.
Being a serviceman, this presented
no real problem other than the fact I’d
never had one of these apart before
and so I wasn’t sure exactly what I’d
find once I got in there, or even how
to get in there!
As usual, there was nothing remotely useful or service-manual-ish on the
internet. I assumed only dealers and
repair agents would be privy to that
information. All I could do was grab
my trusty screwdriver and set about
stripping it down.
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I took what I like to call the “shotgun” approach to stripping this machine down. That is, I started by undoing every screw I could find, simply because they all appeared to be
holding the vacuum cleaner together.
There are about two-dozen visible fasteners dotted around the outside of
the case and as it is constructed from
high-quality plastics, all the screws
are classic PK types.
However, instead of using straight
blade or Phillips-style heads, the
screws were all T10-sized Torx-style
splined heads. Fortunately, a long time
ago I invested in one of those multibit sets that included all these oddball types, along with a decent-sized
driver handle. As such, I have yet to
encounter a screw I cannot remove.
Regular readers will be aware of my
feelings towards those horrible antitamper or security type fasteners, however, Torx screws are growing beyond
that use and have become quite popular among builders and constructors.
One feature of Torx screws I find very
useful is that the bits fit tightly into the
heads of the screws and hold fast, making one-handed installation a breeze.
This also means you can get away
with not having to use a magnetictipped screwdriver because once engaged, the screw hangs on to the bit until you physically pull it off. Disassembly is also less stressful as I don’t have
to mess around, fishing out screws that
have been loosened but have fallen
back into the screw cavity.
After removing all the screws in the
business end of the cleaner, I could
only get a couple of small panels off;
siliconchip.com.au
one on the left side front and one opposite that on the right. Nothing else
would give, no matter how I pushed
or prodded it.
These two panels provided
access and anchor points for the
rotating brushes at the front bottom
of the cleaner. With the machine running, these brushes would turn briskly
and sweep anything in the way rearwards into the path of the suction
intake. On most cleaners I’ve seen, these
rolling brushes are one-piece, beltdriven devices spanning the head of
the cleaner.
This model has two shorter rollers,
one each on the left and right sides,
driven by a centrally-mounted gearbox, like the differential on a car. When
the side panels came off, the brushes
came off with them, leaving the square
metal drive-shafts exposed in the centre. Mounted in the side panels were
bronze bushes for the rollers’ axles
to run in.
They looked very dry which
wouldn’t help things but the axles
still turned easily in them. While each
roller brush had what appeared to be
multiple hairs and threads wrapped
tightly around it, none of these would
have caught or choked the machine to
a standstill.
It took a good half-hour with a knife
and tweezers to remove those threads
from the rollers; no doubt after a few
hours of use they will be just as bound
up again.
The bushes appeared to be oil-infused bronze types. I don’t possess a
vacuum chamber, so there was no way
to re-infuse them properly so I soaked
them overnight in a cap of “3-in-1”
oil, hoping they’d absorb enough to be
lubricated for a while longer at least.
Then it was back to stripping the
head unit down. I could see the two
rear side panels had clips on the bottom but the screws holding them on
at the top were buried in behind lots
of plastic, which meant the centre assembly would have to come out before
I could undo those screws.
Based on this, and a couple of other
buried screws I could just see down
inside if the viewing angle and light
was right, I concluded there must be
another way in.
Perhaps there was something in the
moulding that the handle mounts onto
that was holding this centre piece in?
After popping out the battery in the
lower half of the handle, four screws
were exposed.
Once these were removed, the handle’s cover split apart and with that
out of the way, I could see a couple of
larger screws below the battery connector assembly that might be connected to something further down inside the body of the cleaner.
Holding the handle just so, I had
clearance enough to remove the top
left screw. Twisting the handle back
the other way, I similarly exposed the
right-hand side screw and removed it.
As I did, something inside the head
let go with a loud click and a spring
fell out - never a good sign! The centre assembly still didn’t move; it was
as if I’d not removed any screws at all!
This was becoming frustrating and as I
now had to get in to re-fix that spring
onto whatever mechanism it had fallen off from, I was past the point of
no return. Tricky stuff, these vacuum
cleaner repairs!
Servicing Stories Wanted
Do you have any good servicing stories that you would like to share in The Serviceman
column? If so, why not send those stories in to us?
We pay for all contributions published but please note that your material must
be original. Send your contribution by email to: editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
May 2017 69
Serr v ice
Se
ceman’s
man’s Log – continued
I then concluded there must be fasteners hidden behind the two closelyfitting plastic wheels. All I had to do
was figure out how to remove them.
There were covers over the entire
surface of the wheel and I could see
they were held on by two wide plastic
clips mounted 180° apart. A thin metal spudger was strong enough to ease
the clip off one side and this allowed
me to lift that side up. I did the same
on the other side and with a bit more
persuasion, the hub cap came off.
(So what’s a spudger? It is one of
those plastic or metal tools one uses
to pry open a smartphone or tablet. I
have several different types and I have
to say they are bloody handy things;
I use mine for cleaning fingernails,
scraping glue or paint off items and
even for prying the wheel covers from
Bissell Air Ram vacuum cleaners!)
Underneath was a circlip holding
the 90mm diameter plastic wheel
onto a 12mm metal axle. I dusted off
my circlip pliers – the first time I have
used these in a very long time – and
removed the clip. The wheel lifted
off and a bigger bronze bush and steel
washer came off along with it; I soaked
these bushes along with the others.
Sure enough, partially hidden behind the wheel was one very large
stepped screw and one smaller screw.
The smaller screw, when undone,
wouldn’t come out but just wound
around with apparently nothing on the
other end. The corresponding screw
on the other side did the same thing.
As you can probably already guess,
this made absolutely no difference
to the centre assembly’s coming out.
(These screws turned out to be holding
simple cable clamps that didn’t have to
be removed at all.) I felt sure the larger, stepped and specially-machined
screws would, however, be holding
this assembly in place; after all, it made
sense that the larger screws would be
doing the job and besides, I couldn’t
see any other screws left to remove!
I was confident the centre piece
would fall out onto the bench once I
took out these screws so I was extra
careful to make sure everything was
supported as I removed them.
Once they were out, everything
came apart. Well, when I say everything, I mean the handle mount separated from the head of the cleaner,
70 Silicon Chip
leaving it dangling by a couple of
wires from the battery enclosure. As
for the centre assembly, it remained
fixed in place!
I just couldn’t see what was holding this darned thing on. At this point,
I was starting to feel a bit of the “red
mist”descending, so I walked away
and spent an hour or so tidying up
the workshop; nothing’s worth losing
one’s cool over!
On my return, refreshed and relaxed, I sat the unit on the bench and
just looked at it. I concluded there was
only one possible way it could go, and
that was straight up. There seemed to
be nothing mechanical holding it that
I could see, and as no one part could
come off before another, there could
be no other way.
I found a couple of large screwdrivers and found a leverage point on each
side that could take a bit of pressure
and gently started applying upwards
force, testing to see what would give.
As I put on a little more pressure, I
could feel something starting to shift
and with even more pressure applied,
the centre assembly slowly worked
free of the base unit. Vindicated, I
silently heaved a sigh of relief;
I really didn’t know where I
was going to go if that hadn’t
worked!
It turns out that the centre
assembly is held by just
six small screws, meaning I didn’t have to take
any of this other stuff
apart at all. It was a
classic waste of time
and effort, due to lack
of talent.
A large, moulded
electrical plug on the
bottom of the vacuum unit pressed
into a corresponding socket in the base
of the cleaner, and this transferred battery power to the motor buried in the
vacuum unit. The brushed electric motor, very similar to those used in electric model aircraft, is only 30mm in
diameter and 60mm long and powers
an 80mm hard-plastic impeller within
a clear moulded air duct system.
A shaft connected to the armature
of the motor drives the two rotating
front brushes through a differential
system and I could see everything was
designed for the most efficient use of
the motor’s power. I could also now
see what had jammed the impeller; a
half-burnt incense stick had been ingested and had hit the fan at just the
wrong angle, stopping it and causing
the built-in circuit-protection system
to activate.
I’m glad they included such a system as I’m guessing that 22V Li-Ion
battery could deliver some serious
juice if put to the test and this would
easily burn out the wiring or the motor if not disconnected.
Splitting the vacuum assembly apart
was a simple matter of removing two
siliconchip.com.au
Faulty capacitors in Behringer active PA speaker
G. D., of Mill Park, in Victoria,
managed to find a suitable circuit
diagram for a PWM power supply
to help him repair a pair of active
PA speakers. He writes . . .
I was recently asked if I could
have look at my mate’s daughter’s
speaker systems. The power LED
and clip LEDs were flashing briefly
but no sound would come out when
her guitar was connected. Her diagnosis was that the fuse had failed,
so could I help?
So two “Behringer Eurolive
B115D Active 1000W PA speakers
with wireless option and integrated
mixer”, both with the same fault,
were loaded into the ute to make
the journey to the workshop. After
removing numerous screws, the
power module was lifted clear of the
speaker box and once the speaker
connections were released, it was
laid on the bench.
Another six screws needed to be
removed and the lid of the aluminium box housing the electronics
could then be opened, only to reveal more screws holding the circuit
board in place, plus several clamps
that held the various active devices to the case which also acted as
a heatsink.
It was a messy task, with a copious
quantity of the heatsink compound
making its way to my fingers.
The operator’s handbook was
with the speakers but it contained
no information about the actual
construction and definitely no
circuit diagram, so I was on my own.
A search on the internet revealed a
number of other people had experienced the same fault but offered
no solution.
However, I did find a circuit for a
Eurolive B215D that I downloaded;
my thinking being that there would
be some commonality but once I
started to compare the diagram with
the actual circuit board, all hope
vanished. Nothing seemed to be in
common except the brand name.
A visual examination of the faulty
circuit board showed all solder
joints to be good and there were no
signs of any distress in any components. The board comprise three
sections: the mains input to a rectifier via a common mode input filter,
a PWM controller to derive the DC
output voltages and an amplifier section that has two class-D amplifiers,
one for the bass speaker and the second for the tweeter.
So now what? A discussion with
the workshop owner determined
that the PWM chip (NCP1271) or one
of its associated components was the
most likely problem. A packet of 10
NCP1271 devices could be had for
five dollars (including postage), so
I placed an order and while waiting
I noted down all the active component numbers and went looking for
their datasheets.
When the PWM chips arrived I
swapped it but the fault persisted.
I now concentrated my attention to
long-ish screws and cutting through
some clear tape sealing each top and
bottom join.
Once done, the stick fell out easily and to rub some salt in, if I had
known what this looked like before
this happened, I could probably have
extracted it from outside using a pair
of long-nosed pliers without taking
out a single screw. Imbecile indeed!
I reassembled the impeller assembly, replacing the cut tape and plugged
everything together in order to test
run the motor. After rigging up the
battery, I pushed the button only to
find the LEDs still flashing red. Concerned that the jam had burnt something out, I made sure the impeller
was free to turn.
I dragged one of my bench power supplies out and dialled in about
12V and set the current limit to about
half (2A) before connecting the motor
directly to it.
siliconchip.com.au
the NCP1271 datasheet and noted
the example circuit shown on page
18. It matched what I was seeing on
the Behringer circuit board.
A note in the “operating description” section of the datasheet, under
fault conditions, detailed a requirement for a 130ms time to allow a
feedback signal to be received, or
else a fault condition will be recognised and the PWM will not start.
The example circuit shows two
100µF capacitors across pin 6
(VCC) but in the Behringer circuit
they were 47µF and although they
showed no signs of distress, they
measured less than 20µF, with the
worst being only 5µF.
I had some 50µF caps handy and
replaced them and with the power
applied, the circuit responded in the
correct manner. So I began the task
of reassembly, trying to keep contact with that sticky white stuff to
a minimum.
Once the box was assembled
with power on and a microphone
was connected, a healthy amplified sound was produced. Since the
second unit had the same fault the
repair took only a few minutes, plus
the hour and a bit getting it apart and
back together.
The example circuit
diagram in the
NCP1271 datasheet
that is similar to the
Behringer circuit
board.
The motor powered up fine, which
was a relief, but why then was the protection circuit still activated? The only
visible component (I assumed the rest
of the electronics were up in the handle behind the LEDs) was a 1N400x series diode across the motor terminals,
which I assumed to be a snubber diode
to limit back-EMF from the motor. A
quick in-circuit measurement with my
Peak semiconductor checker showed
the diode to be a dead short.
May 2017 71
Serr v ice
Se
ceman’s
man’s Log – continued
No problem; I have a box full of
these and I soon had it replaced. This
time at switch on, the LEDs showed
two greens out of four, indicating the
battery was down to about half capacity. Even so the motor spun up at an
alarming rate.
Now all I had to do was reassemble
all the bits I’d unnecessarily removed,
including the two cable clamps and the
spring-loaded detent for the handle
assembly, which is where the spring
sprang from during disassembly. The
silver lining is that I now know a lot
more about this device, so if I ever
need to repair it again, I’ll be prepared.
Job done!
By the way, there is a good 3D look
at the cleaner in question at: www.
bissell.co.nz/air-ram
Three different faults in a
CHIMEI LCD monitor
Sometimes you have to go back
three times before the repair sticks, as
A. C., from Sunnyvale in New Zealand
experienced during a long saga with
a CHIMEI CMV T38D LCD monitor.
I recently acquired a 20-inch LCD
monitor with a fault description that
sounded like it could be due to bad
capacitors: “takes several tries to turn
on and is getting worse”.
The prospect of a cheap 20-inch
LCD was rather enticing and since I
had repaired other equipment before
simply by replacing dead electrolytic
capacitors, I figured this would be just
as easy. How wrong I was!
This particular monitor is delight-
fully easy to disassemble. A plastic
shroud covers the stand hinge and
mount, held in place by some plastic
clips and this just pops off with little
effort, by pulling on it from its bottom edge.
This reveals the stand mount, held
on with four screws in a standard
50mm VESA arrangement. There
are just three screws left for the back
cover, which comes off almost as easily (watch out for two clips in slots at
the bottom – use a flat screwdriver). In
retrospect, I wish all monitors were as
easy to open.
The overall structural design is
basic but quite clever. The stand is
attached to the back of a rigid metal
cover which protects the circuitry and
in turn, screws onto the back of the
LCD panel assembly. The plastic case
and frame are actually all clipped onto
and held up by the panel assembly.
I removed the metal circuitry
cover plus the threaded hex bolts for
the VGA and DVI input connectors
and was greeted by the familiar sight
of electrolytic capacitors bulging and
leaking throughout the power supply.
Ah-ha, I thought.
I removed the lot, except for the
primary filter capacitor (these generally last far longer). As I went, I noted
down their capacitance, voltage and
reference designators, as well as the
brands and series in a spreadsheet.
It’s also usually quite important to
note down the diameter and height
of the capacitors, as in a lot of equipment, space is at a premium and not
Some of the electrolytic capacitors had begun leaking onto the power supply PCB.
However, this wasn’t the only fault that was found in this particular monitor.
72 Silicon Chip
all replacements will be the same size.
Having all the data also means you
don’t mix the values up, and makes
ordering new capacitors easy, as well
as a future reference which (hopefully) doesn’t require opening the equipment again.
In my monitor, all the blown capacitors were CapXon brand, although
there were a couple of Taicons in the
PSU as well. Interestingly enough,
the Taicons both looked and tested
OK on my ESR meter, while even the
CapXons which looked physically fine
tested just as poorly as their bulging
and leaking companions.
This just goes to show that for the
same thermal conditions and age,
some brands of capacitor just cannot
stand the heat.
Next, I looked up the datasheets
for the capacitors I had removed.
They were standard low-ESR types.
Replacements should have the same
ESR or lower – not too low, as significantly lowering ESR can affect circuit
operation, especially in a switchmode
power supply (SMPS).
The Ripple Current Rating (RCR)
is like voltage – choose the same, or
higher. Make sure the datasheets both
specify ESR at the same frequency.
Low ESR type capacitors typically
specify it for 100kHz, while general
purpose capacitors specify it at 60Hz,
or not at all.
Some quick work with element14’s
parametric search and I soon had suitable replacements lined up (all high
quality Japanese brands – Panasonic/
Nichicon etc). Upon receiving the new
capacitors, I soldered them in and it
was time to test the monitor.
I plugged it in, turned it on, and
was instantly greeted by a nice crisp
image which stayed on the screen. It
was then pressed into service as my
primary computer display.
But a mere three months later, more
trouble emerged from the otherwise
pixel-perfect paradise. This time all
the control buttons stopped working, except the auto-adjust button. I
immediately jumped to horrible conclusions about blown inputs on the
main control chip (as one does),
though as in all other respects the
monitor was working just fine.
Once again I disassembled the monitor and found that the buttons reside
on a separate board, connected by a
flat-flex ribbon cable. Unplugging this
and running continuity checks on the
siliconchip.com.au
button board showed that none of the
switches were faulty. This meant the
fault had to be on the scalar board
somewhere.
The input handling for the buttons
is a pretty simple affair. Each button
is pulled up to the +3.3V VCPU rail via
a 10kW resistor and inductor in series,
bypassed with a small capacitor to
ground. The output signal is tapped
off between the resistor and inductor,
then fed to the input of the main processor, so there’s not much which can
go wrong.
I started checking voltages at the
buttons, and discovered that the auto-adjust button had a much lower
voltage (0.86V) across it than all the
rest (3.3V).
My first guess was that the resistor
had gone high in value but the resistors
and capacitors in question are all part
of two four-way SMD arrays. I managed to remove the RP1 resistor array
with a flood-and-wipe method, tested
it as OK, and managed to eventually
get it back on the board without completely destroying the pads. I didn’t
like the idea of trying to remove anything else, so I started probing around
some more instead.
It soon became apparent that the
auto-adjust button line was also showing a low resistance to ground and this
didn’t change even with the button
board disconnected. Clearly, something was shorted to GND, either the
debounce capacitor or the processor
input itself.
Given the difficulty of working on
the resistor array, I didn’t want to
attempt removing the capacitor
array, as I could see myself lifting
pads. Besides, even if I had a safe and
easy way to replace it, I didn’t know
its value. I saw no sense in risking
damage. The monitor still worked, and
I didn’t really need to use the buttons
anyway, so I reassembled and continued using it.
Unfortunately, the poor thing died
completely a few months later, simply
shutting down without warning and
refusing to power up again; not even
the power LED worked. This time I
was not sure where to start, disheartened by the fact that the power LED is
driven by the scalar board, and I felt as
if my fears about the processor failing
were confirmed.
But I eventually got around to it, and
for the third time, had it open on the
workbench. The first thing to do was
siliconchip.com.au
figure out which board the fault lay on.
A dead scalar board could explain the
lack of a power LED but so too could a
dead power supply. I removed the PSU
and started with a visual inspection.
There had been no noise when the
monitor shut off, so I did not expect
a blown switching transistor or such
but I carefully eyeballed all the power semiconductors anyway. Nothing
was obvious; no burnt parts or bad
solder joints.
I put the PSU back in the monitor and firmly screwed it back in, as I
didn’t want the possibility of a mainspowered board scooting around the
workbench while trying to test it.
I first measured the voltage across
the mains filter capacitor, and found
it correct and steady at around 340V
DC, so at least I knew the fuse and capacitor etc were OK. I went on to the
secondary side.
Despite having no schematic, the
voltage rails were at least labelled, although they were supplied to the scalar board by a right-angled dual-row
0.1-inch pitch pin header, which was
not easy to probe with a multimeter.
I got creative. This involved plugging an old floppy drive cable onto the
header, which basically broke out the
connections to a convenient socket.
I was then able to clip one multimeter probe to chassis ground, follow the
connections to the other end of the cable, poke a short piece of wire into each
socket position in turn, and measure
the voltages there.
I found that the +12V rail seemed
OK but what was supposed to be a +5V
rail was bouncing up and down around
2.4V. It certainly seemed as if the power supply was bad, but I didn’t want to
assume anything straight away. I know
some SMPSs do not run correctly without a load, and I wanted to be sure the
scalar board still worked anyway.
I tried the reverse approach, taking a standard ATX computer PSU
and connected it to the scalar board.
Upon powering it up, I was pleasantly
greeted by a green power LED on the
monitor, and a “No Signal” message
on the screen. The scalar board was
clearly still working, and this proved
the PSU was at fault.
Since I was getting something out
of the PSU, it seemed then that the
primary side was fine, and thus I focused my search on the secondary
side. I decided to check all the output
rectifiers first. These often fail open-
circuit, shorted, or leaky, so they’re a
good place to start.
Some quick in-circuit testing
revealed that D101 was a dead short
and this was obviously putting the
PSU into a protection shutdown-andretry loop, hence the fluctuating +5V
rail. I’m glad the PSU controller was
smart enough to do this – some supplies simply blow up when faced with
a short on the output.
D101 is an SB20200FCT dualschottky rectifier in a TO-220 package
and the easily-obtained MBR20100CT
from Jaycar was a suitable replacement, although I had to add an insulating thermal pad and washer as the
original rectifier was an ITO-220AB
insulated variant. With the new rectifier, the PSU sprang back to life with
all rails steady and correct.
Of course, while the monitor was
now powering on again, the buttons
were still not functioning. I decided
to revisit that fault, armed with better
tools, including a hot air rework station. I also got lucky with a schematic,
by searching the PCB code (A190A2-HS1) on Google and discovered the same
scalar board (and probably PSU) are
also used in a Viewsonic VA1912w-1/
VA1912wb-1, for which I found the
service manual easily.
The shorted capacitor array, CP7,
was listed as a 100pF 50V 0603*4 part.
(As I later found out, this package is
referred to as 0612, and is the same
physical size as a 1206 component. For
array components, it seems the dimensions are simply written swapped).
The magic of hot air and tweezers
made short work of removing the old
array, and a quick test proved one of
the capacitors in the array was indeed
shorted. I was also able to confirm that
the other three were about 100pF, as
per the schematic. Another order later and I soon had some new capacitor
arrays ready and waiting.
After cleaning up the pads with solder wick and alcohol, I used tweezers
to dab some tiny spots of solder paste
onto them, before placing a new capacitor array on top and re-flowing the
whole lot with hot air. I must say, it’s a
marvellous thing to watch solder paste
melt effortlessly before one’s eyes, instead of struggling with an oversized
iron and solder wire.
But the upshot of this long and
arduous story? The monitor and all
its buttons have been working ever
SC
since!
May 2017 73
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