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SERVICEMAN'S LOG
Rangehood repair full of red herrings
Dave Thompson*
No matter how good you are or how much experience you might have,
sometimes servicing just comes down to luck. That can mean good luck,
where you take apart a monstrously complex device and immediately
spot the simple problem which is preventing it from operating. Or bad
luck, when you are trying to repair the simplest device and nothing you
try seems to help. This is the second kind of story.
I've had some brilliant successes
but more than once, and especially
lately, I’ve completely misread clues
and then made assumptions that
steered me away from the true cause
of a problem.
Once, I stripped a lawn mower motor down to the block, looking for all
manner of non-existent faults, when
all I needed to do was change the
spark-plug; something even the least-
experienced DIY enthusiast knows is
the first thing to check!
Another time, I stripped every nut
and bolt from a vacuum cleaner in
order to disassemble it when just a
few screws held it all together — I
just didn’t twist it the right way to
pull it apart.
We've pretty much all had this kind
of experience and while you just have
to chalk it up to experience and learn
from your mistakes, it's still incredibly frustrating.
So I'd like to play a game
with you, dear reader. I'll
describe the symptoms
of a very real problem we
had with our just one-year-old range
hood and see whether you can guess
what was wrong while you're reading through all the trouble-shooting I
did, which only served to demonstrate
what wasn't wrong with it.
The appliance in question is a Robin
Hood Range Hood, model RWV3CL6G.
It was installed almost exactly one year
ago, having been purchased brand new
from a local big-box store. It wasn't
even at the age of a toddler yet but was
already starting to spit the dummy.
This particular model has five illuminated buttons along the front panel
(called "sophisticated electronic controls" in the user manual) to control
the fan and the two 24V, 1.5W LED
downlights in the front corners. The
buttons turn a function on with one
press, and off with another, each time
accompanied by a soft beep.
A blue LED backlight indicates the
button’s state; illuminated when on
and dark when off. The buttons are
positive, tactile and worked well, and
the three-stage fan and LED lights were
both powerful and efficient.
We use this appliance frequently.
It sits directly over a gas hob in the
kitchen and is vented to the outside
world through the wall, via a short
piece of steel ducting.
Items Covered This Month
•
•
A rangehood of repairs
MIG welder repair
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
siliconchip.com.au
Celebrating 30 Years
November 2017 61
All is not well in the
serviceman's abode
A few weeks ago, while cooking,
and with the fan and lights on, the
LEDs flickered in unison before coming back to full brightness. I switched
them on and off a few times and they
still operated normally, being flickerfree for the next few days. I put that
event down to a one-off power issue
and forgot all about it.
Less than a week later, though, the
same thing happened again, with both
lamps dimming to a dull glow before
coming right. The following day, I
switched the lights on and halfway
through cooking our meal, they dulled
down and then went dark altogether.
Of course, this had to happen just a
few weeks after the (rather short) warranty ended. Like many others, I suspect companies choose their components very carefully so as to maximise
the chance this sort of thing happening, so you have to run out and buy another one... and another... and another.
Many of my own customers have
often joked that computer manufacturers must install a timer into their machines so they fail just out of warranty.
All joking aside, though, it does seem
awfully coincidental and convenient
for the manufacturer…
So, both LEDs were not working.
Pressing the light control button still
resulted in a beep and the blue LED
lit up but there was no light output.
Occasionally, when switching on, the
LEDs would flash at full brightness but
almost instantly go dark again. This
always happened to both lamps at the
same time but after this, for the most
part, there was no output at all.
So here's the fun part. What do you
think? What would you have done,
which parts would you have blamed
from such a fault? See if you can outsmart the serviceman and figure it out
before the end of the story.
Given these symptoms, I suspected
the LED driver. One lamp behaving
badly might be a failing LED, but both
behaving in an identical manner? And
anyway, surely LEDs would last longer
than this, while drivers can fail quite
early due to dodgy electrolytic capacitors, voltage spikes on the power lines
or various other woes.
access issues. I disabled power to it at
the breaker board before removing the
lamp assemblies. These were held in
using clip springs and simply needed
to be prised out with something flat
and thin.
Once out of the housing, the LED
units hung on their respective power
cables. The lens and reflector assemblies were held together in a bayonetstyle fitting; a quick twist anti-clockwise separated the lens, reflector and
the brushed-aluminium trim ring, revealing a G4-type LED.
The heavy-duty lamps were virtually all aluminium heatsink, with the
LED die itself set into the very end.
Rated as being equivalent to a 15W
incandescent bulb but drawing just
1.5W, I was reasonably sure that they
were bulletproof, and with no signs of
overheating, I set them both aside and
dug further into the hood’s internals.
Removing the aluminium filter
from underneath gave both better
access and more light, so I could at least
see what was going on. This model
range hood has a thick, curved glass
canopy, which is held onto the body of
the appliance with four large set screws.
To get to these screws, I had to remove the stainless-steel chimney,
which is a three-sided cover that
conceals the fan, output ducting and
electronics.
It is simple enough to remove the
two small PK screws holding it in place
but awfully fiddly to get free due to it
being right at the ceiling and with me
not wanting to stand on the benchtop
or gas hob.
A bit of wiggling around (and cursing) got it free, but I wasn’t looking
forward to having to get it back up
there; we’d had issues lining it all up
when we first installed it, and there
were two of us on the job back then.
Still, I’d cross that bridge when I got
to it; all I could do now was carry on
and find out why these lamps weren’t
working.
With the panels and canopy off, I
had a clearer view of the internals. The
front switch panel was connected with
a ribbon cable to a controller circuit
board further back in the guts of the
range hood somewhere. To get to the
board, I’d have to dig deeper. However,
right in front of me, mounted on the
shoulder of the main frame, was the
LED power supply/driver.
This unit was smaller than I expected, being only about 30 x 30mm
and around 20mm thick. It had a twopin terminal block for mains power
input and a similar terminal block
that the dangling LED holders were
wired into. It only had to deliver 3W
in total, so I guess it didn’t need to
be very large.
Much wasted effort later
Pulling the thing apart was relatively
simple but the fact it is stuck to the
wall above the hob introduced some
62
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Celebrating 30 Years
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Celebrating 30 Years
November 2017 63
With the driver nicely accessible, I
broke out my multimeter and, ensuring all the wiring was in a relatively
safe state, restored power. I pushed
the light switch, saw that the blue
LED lit up and with my meter sitting
on the kitchen benchtop, I carefully
measured across the input terminals
of the driver. The meter read around
230VAC on the 250V scale, which was
close enough for me.
Add cornflour to plot,
stir until it thickens
I use an analog meter for this type
of work, as it is easier for me to read a
meter needle position than having to
read and understand a numerical value. So after adjusting the meter range,
I measured across the driver’s output.
Hmm, I got 24V; I was expecting nothing, or thereabouts. Still, it might be
intermittent so I switched it on and off
a few times, checking each time. getting a stable 24 volt output. Curious.
After powering things down, I reinstalled the bulbs into their respective holders. This time, when I pushed
the light switch, for a brief moment,
both bulbs lit up to full brightness
before going dark again. What was
going on here? With the light switch
on, I set about wiggling and measuring
in equal amounts, but aside from the
briefest of dull glows, they remained
stubbornly dark.
Somewhat puzzled, a notion was
beginning to poke its way through to
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Silicon Chip
the front of my mind; after all, despite
the appearances of the LEDs, there
could only be one explanation, given
the results of these tests.
To confirm my diagnosis, I took
out the LEDs again and departed to
my workshop, where I broke out my
benchtop power supply. After carefully setting the output to 24V and
limiting the current to about 100mA,
I connected each LED up to the supply using small, alligator-style clips.
As had slowly dawned on me, neither
bulb showed any sign of life.
Actually, that’s not quite true; once
or twice, as power was applied, I saw
the briefest of glow from the LEDs.
If I interrupted the supply by touching and releasing one leg of the LED,
I could very infrequently get a fullbrightness flash, almost like a flashgun, from one of the bulbs. In laymans’
terms, they were both poked.
How could I be so thick? A simple
bulb failure, and here I am with the
range hood lying all over the kitchen
bench. Both bulbs gone, failed at exactly the same time and exhibiting (for
all intents and purposes) exactly the
same symptoms. Apparently, failed
LEDs can show full brilliance for short
periods of time. I know this seems unbelievable, even unlikely, but I assure
you I’ve described things exactly as
they happened.
If only one bulb had failed and had
flickered from full brightness to a dull
glow, I would have assumed that bulb
Celebrating 30 Years
had failed and simply replaced it; a
five-minute job (if that) which doesn’t
involve disassembling the range hood
into component parts. To my mind,
both LEDs exhibiting exactly the same
behaviour as they failed beggars belief.
Surely, the driver had something to
do with this? Perhaps it surged and
took the LEDs out, fooling me into
thinking it had failed instead. To determine if this was the case, I removed
the two screws holding the driver to
the frame and took it out to the workshop, where I proceeded to connect
some strip LEDs I had on the bench
and powered them up using mains
power input, just as it would be in the
range hood.
I ran the strips for about an hour at
full power, monitoring the voltage output and current, and everything was as
stable as could be expected. Annoying
to say the least but at least I know the
driver likely had nothing to do with
anything, and it is just a LED failure,
pure and simple.
An easy fix. Or is it?
Well, this one really got me good.
Hopefully, I’ll be a bit more aware
in the future but the way these LEDs
failed is a new one on me.
Now all I had to do was find some
replacement LEDs and get the range
hood reassembled. But finding replacement LEDs turned out to be
tougher than putting the range hood
back together.
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The only G4 LEDs I could find locally (and when I say locally I mean
within New Zealand) were listed on a
campervan manufacturer’s website at
a whopping $43 each! Needless to say,
I wasn’t paying those daylight robbers
anything like that for a LED. After a few
more wild goose chases, with similar
results price-wise, I decided to try my
luck over at AliExpress.
Sure enough, there were hundreds
of listings of G4-type LEDs, the vast
majority being replacement lamps for
chandeliers and cove lighting. But
they would likely be suitable for our
needs as well.
The LEDs I ended up buying have
a 12-24V AC/DC input range and are
rated at 3W each. The cost was just
US$7.80 for a pack of six. While they
might be a little over the top for a range
hood, there was nothing with a lower
power rating that I could find with a
G4-style connector.
We put up with not having lights
in the range hood until the new LEDs
arrived. They are actually rather impressive in the flesh. For a start, they
are quite large; at 15 x 45mm they are
about 10% larger than the originals,
and therefore barely fit into the receptacles in the range hood.
However, they are also flexible, being made out of some kind of amazingly-clear and pliable silicone material,
so a bit of fettling got them fitting OK.
However, it appears I didn’t choose
well, as the driver won’t power up
the new LEDs.
All I get with one LED plugged in
is the LED flashing at full brightness
at about two hertz. I didn't want to try
plugging both LEDs into the driver
since that would be a 6W load and
as far as I know, it's only designed to
handle the original 3W worth of lamps.
I tried powering the new LEDs with
my benchtop supply, thinking perhaps
I’d purchased blinking LEDs by mistake but I found that even at 10V and
20mA, they easily lit up. So perhaps
there is something awry with that
driver after all.
That said, it did test out OK, powering up the strip lighting with no apparent problems, so it is more likely just
a mismatch between it and the new
LEDs that leaves it unable to power
them properly.
Regardless, I’ll have to either replace
the LEDs or find another driver. After
another quick look on AliExpress, I
found a new driver that should do the
siliconchip.com.au
job. While a little bit larger physically,
it will still easily fit in the space for
it within the range hood, and with an
output of 12V and 2A, it has more than
enough grunt to drive these two LEDs
at full noise all day long.
At just US$4.50 with free shipping,
it is also affordable and, I think, a reasonable upgrade to the range hood. It is
yet to arrive, but I have no doubt it will
be the answer to this whole problem.
So once again it seems I overthought what turned out to be a stupidly-simple fault. In my defence, given
the symptoms and the fact that both
bulbs failed at exactly the same time,
I didn’t even consider the LEDs could
be the issue.
I expect LEDs to last a lot longer than
a comparable halogen or incandescent
bulb of similar output, as per all the
marketing hype, and to have them fail
at just over a year with very little actual
use is a big disappointment.
I would guesstimate that, on average, they haven’t been used for more
than a couple of hours a week over
that year, resulting in a lifespan of only
around 100 hours.
And I consider a replacement price
after such a paltry life of 40 plus bucks
each a huge rip off. The pair of halogen
bulbs in our previous kitchen’s range
hood only needed to be replaced twice
each in 10 years and likely had more
Celebrating 30 Years
use than the LEDs in the range hood at
this house, so either we got unlucky,
or we got burned. Time will likely tell
which it is.
Well, I hope you enjoyed playing
"outsmart the serviceman" and I'm sure
many of you made better guesses than I
did initially. At least I'm on the way to
having this one sorted but really, you'd
think that replacing a lamp would be
an easy job for an old hand like me.
Metal inert gas (MIG) welder repair
The next story is from M. H., of
Albury, NSW who had to first reassemble and clean out what was left
of a MIG welder before he could even
have a go at fixing the fault which left
it in this sorry state. His story is as
follows:
My friend’s mate gave him a MIG
welder that was not working and he
asked me to fix it. When I first looked
at the beast, it appeared that lots of
different people had previously had
a crack at getting it going again.
The handover ceremony involved
the presentation of an ice-cream container of assorted parts along with the
statement "It's beyond us, Mike. If you
can get it going, it is yours!"
I own a handbag-sized IGBT welder
with rod and TIG options and at the
time, had developed just enough skill
for backyard, weekend-warrior type
November 2017 65
The control knob is connected to a stepped rotary encoder
on the front display PCB. The mounting pins were repaired
and copper wires added to provide anchoring.
welding. I had observed professional
welders using a good MIG unit, but
when I investigated the cost, I decided
I really did not need one. Well, this
was my opportunity to gain a working
MIG unit as well as further my skills
at saving stuff from the landfill.
The broken unit I was given is a
BOC Smootharc 180 MIG Welder. MIG
stands for metal inert gas and it works
by feeding a wire out of the handset
end to maintain the arc and also provide the metal for welding. A gas is
simultaneously discharged under the
hood around the arc to exclude oxygen, which would prevent a proper
weld from forming.
You can also use "gasless" wire that
contains a material which vaporises,
providing the same oxygen displacement protection as the inert gas would.
This has the advantage that you don’t
need to rent a gas bottle, lug it around
or have it periodically re-filled.
Anyway, having decided to fix it,
I placed the unit on the bench in my
workshop and attacked the obvious
faults first. No need to remove the
cover; it was already in the ice-cream
container.
I cleaned out all the bent and melted
tips from the wire feed compartment.
It seemed that this side of the unit
At a glance everything in the power section of the welder
looked like it would work OK, until it was switched on. The
fault lay on the main PCB.
has been used as dumping ground for
busted parts.
I then checked the action of the motor drive for the wire feed by manually turning the motor parts and all
seemed okay. The other half of the
casing contains the main circuit board
and it was lined with dirt and dust and
metal shavings from years of grinding
near the unit.
Evidence of attempted repair action was everywhere. The main heat
sinks were floating free off the board.
The IGBT drivers were floating free
and there were broken wires on the
gas solenoid. Transistor clamps had
also been removed and a heat-sensing
thermistor had been torn from the
mountings.
What a mess! It was going take a lot
of work to put everything back in place
before this baby got mains power connected again.
The front of the unit housed a control knob to vary settings on the display, which was broken and wobbling
free. It was connected to a stepped
rotary encoder. The shaft retaining
pins were broken and it required
some restoration work and wire strips
added over the base unit to give it
strength.
With all the obvious faults restored,
Servicing Stories Wanted
Do you have any good servicing stories that you would like to share in The Serviceman
column? If so, why not send those stories in to us?
We pay for all contributions published but please note that your material must
be original. Send your contribution by email to: editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
66
Silicon Chip
Celebrating 30 Years
it was time to review what this thing
was actually capable of doing. 15A
mains power passes through a toughlooking mains filter to keep the noise
inside the box from getting out on the
mains and then immediately through
two large bridge rectifier blocks and
then off to the main board via oversized red and black wires.
A thick cable runs from a very large
heatsink to a lug terminal secured by
a 10mm bolt, to connect the welding
cable to the front of the unit. The other work cable passes though a large
toroidal coil and then through what
looked like a final filter. I assumed this
section basically operated as a “buck”
step-down converter, but that’s unimportant at this point.
Since all was looking good and
clean, and everything appeared to
be in place, it was time to "light this
thing up". So with mains on, the fans
were running and display on. Good.
The knob varied the display numbers.
Pressing the wire feed button caused
the wire to spool out. All was looking great.
I pulled the trigger on the handset
and tapped the work clamp with no
result; no sparks, no action. I now had
the original fault to chase.
What should have happened when
I pulled the trigger was that the wire
feed motor should have started.
When the wire hits the workpiece,
this should cause the current to flow,
creating the welding arc. But tapping
the wire to the workpiece produced
nothing. It was time to visit the main
board and inspect it further.
I am always pleased to see designsiliconchip.com.au
This interior shot of the MIG welder shows the main control The wire feed motor is mounted at the opposite end of the
PCB and the power supply filter board above it. The failed
case. One of the symptoms of the fault was that it did not
component is at lower left; see the close-up image below.
operate when expected.
ers of equipment using LEDs on the
boards to indicate conditions. A LED
blinked when I tapped the wire to the
work, so clearly it was detecting this
action. But nothing happened when
the trigger was pulled.
I then investigated if there was a
fault in the trigger or handset. Using
my old faithful Dick Smith analog
multimeter it was easy to prove the
trigger signal arrived at the main
board.
Near the connector for the trigger
was a cluster of resistors, a transistor
and a few diodes to form what looked
like a trigger detection circuit. Its output was fed to an opto-isolator.
I powered the unit up again and
measured the voltage across the input
side of the opto-isolator, which revealed 14V when closer to 1V should
have been present, ie, the forward voltage of its internal infrared LED.
So this LED must be open circuit. A
quick Google search showed that the
opto-isolator was nothing special and
just had the typical transistor output.
As I am a “throw nothing out” sort of
guy, a quick search in the junk pile
revealed a replacement. I used a heat
gun to de-solder the SMD opto and the
replacement was soon in place.
At last, I was ready to apply mains
again. The fans ran, the LED displays
came on and the unit seemed ready.
So to test it I tapped the wire to the
work and pulled the trigger.
Sparks flew everywhere and red
dots dashed about on the floor. The
carpet mat at my feet was smoking
with burn holes. Wire was feeding out
of the handset. It was like Christmas
siliconchip.com.au
on Black Saturday and my workshop
filled with smoke. I decided that perhaps I should control the situation a
little better before the next strike on
the work clamp.
To control the wire feed, I removed
the drive clamp. This will allow the
motor to drive without feeding wire
out of the handset. I then pulled the
trigger and viewed the main controller
board. Lots of LEDs blinked, indicating
the IGBT driver section was operating
and output was present. When the
trigger was pulled, the output floated
about 20V.
It was now time to move outdoors
to make more smoke and try melting
stuff. It all seemed to do what it should,
so I was convinced it was time to visit
a friend that has a proper MIG to compare with my now-working unit.
It compared well, so the conclusion
is that this wonderful beast had been
brought crashing down by the failure
of a 20¢ opto-isolator and was almost
relegated to the dump because my
mates tried to fix it by "just undoing
stuff" with no real idea of what the
fault may be.
Luckily I managed to rescue it! SC
The faulty opto-isolator is near the top of the photo (U16), while the hand trigger
switch connectors are at lower left (CON3). Both solder joints had blown for
some reason or another.
Celebrating 30 Years
November 2017 67
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