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SERVICEMAN'S LOG
When a GPS loses its way
GPS satnav systems are widely used in cars,
boats and for personal navigation when
walking in country but it is safe to say that most
of these would be discarded when they stop
working. That is probably the most practical
approach but what if you were using GPS
tracking collars which are fitted to wildlife?
These are much more expensive units that are
quite costly to replace if they fail.
I am certainly getting a variety of
work these days and I can no longer
complain about doing the same “boring” sorts of repairs. I get all sorts of
jobs and I wonder if it is because the
servicing game has changed so much
here in New Zealand. So many repair
business have closed or maybe just
given up. . .
I’ll bet a lot of service businesses
here looked at the silver lining when
the quakes struck Christchurch, with
many taking the seemingly God-given
opportunity to close with dignity.
There are few other explanations as
to why so many of these businesses
never re-opened. Some of us have kept
going though...
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73 S
ilicon Chip
A client from “down south” recently
visited Christchurch and found me
working on my new workshop. He’d
heard that I fixed GPS units and asked
if I was interested in looking at his. I
told him that I’d repaired a few in the
past few years as word got around that
despite many industry claims, they
might actually be fixable.
This guy was a typical kiwi “southerner” and I say that with a lot of respect. I mean that he is one of those
characters that spends much of his life
in the far south of the country, where
bush is thick, the terrain harsh and the
weather beyond inclement. There are
still uncharted areas down there, and
this is my client’s backyard.
Dave Thompson*
Items Covered This Month
•
•
•
•
Garmin GPS animal trackers
Cambridge CD player repair
Fixing a useless machine
A Pony 3 mobility scooter that
just wouldn’t scoot
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
Having the GPS working properly
could be the difference between coming home safe or spending a night (or
longer) out in the boonies, so they are
an important piece of kit.
What he wanted me to check over
was a Garmin hand-held GPS unit and
three Garmin Alpha T5 tracking collars, the sort you might fit to a lion or
a bear in order to keep tabs on their
whereabouts. They are certainly not
the dainty “domestic” types sold by
the likes of AliExpress for pet owners
to monitor Snuggles’ nocturnal antics.
My client uses these collars, together
with the hand-held GPS, to monitor
animals in the wild and gather information about their movements so that
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Se
ceman’s
man’s Log – continued
programs can be devised to ensure
their continued survival.
The collars are made using heavyduty synthetics, hard rubber and some
metal parts for the clasp arrangement,
all of which have to be robust enough
to withstand natural hazards and the
animal’s efforts to rid itself of the annoyance.
Apparently, all of these collars had
failed with the same symptoms; they
no longer acquired satellites and were
thus useless for tracking.
Due to the cost of replacement, the
guy thought he’d ask around to see
if anyone fixed them and for some
reason, my name popped up. However, there was a snag (isn’t there
always?). Garmin made these collars
to withstand the rigours of extreme
conditions; to that end, they are built
like the proverbial masonry ablutions
block.
The external connections are wellsealed with some formerly-liquid armour and the GPS module – which is
housed a separate small plastic “box”
along the collar from the main electronics case and connected by a shielded cable – is completely enclosed in
a case with clear potting compound
and thus completely isolated from the
environment – and potential
repairmen.
74 Silicon Chip
The main box of electronics goodies is three times the size of the GPS
module and is home to the battery,
charging ports and a small, doublesided PCB stuffed with surface-mounted components and edged with tiny,
multi-colour LEDs that indicate what’s
happening with the unit.
At least this board is accessible
after removing half a dozen long, finethreaded screws and prying the lid
away from the seal that (supposedly)
keeps the contents safe and dry.
The guy mentioned that he, and others with the same issue, thought the
problem was the shielded cable from
the GPS module and commented that
it was often under some strain, so they
thought all it needed was re-terminating into the main module. Or at least
that’s what YouTubers and posters in
online forums reckoned.
Just by looking at it, I doubted this
was the issue. The cable was embedded in the plastic collar and appeared
well-connected, with all the strain relief necessary. And given that it really
didn’t flex or move that much when
the collar was worn, I found it difficult
to accept that this was the problem.
We’d see though; I’ve been known to
be wrong before.
The first thing I did was try the collars out. Two of them had flat
batteries since they’d been
sitting on the shelf for
ages after failing and so
they were non-starters.
The third one gave a
healthy series of beeps
on button-push and the
middle of three LEDs
flashed solemnly every
few seconds.
This informs the user
when enough satellites are acquired for accurate operation; one flash
is no satellites;
two flashes indicates two satellites and three
flashes indicates
at least three satellites are acquired
and this will provide
the most accurate positioning.
The problem with this collar was
that it wasn’t acquiring any satellites
at all; the LED only blinked once every
few seconds.
My initial thought was that perhaps
the guys were right in thinking that the
GPS module’s lead had come adrift. It
would certainly explain the lack of satellite acquisition. This would be well
worth checking out anyway, if not to
confirm the diagnosis, then at least to
rule it out.
I decided to start with the one that
powered up; I could use that battery to
check the others as the client neglected
to bring the specialised charging dock
for the collars. Once I had the battery
out I could use my bench supply to
top it up if necessary.
I started by removing the six screws
holding the main module together.
Two of those screws hold a smaller,
separate cover and another, smaller
machine screw and two tiny PK-type
screws beneath that held the GPS
module’s connection harness to the
main module.
With those smaller screws removed,
the end of the collar and the embedded
GPS module’s shielded cable could be
pulled away from the main module.
But not very far; the portal where the
shielded cable enters the main module is heavily potted and the material
is somewhat elastic, but very tough.
The VHF antenna, which is about
350mm long and follows the contour
of the collar due to it feeding through
various holders, is basically a chunk
of heavy gauge, multi-strand steel cable with a basic crimp terminal at the
module end and a red, plastic antenna
tip at the other. This connects to the
main module via a relatively large machine screw but this isn’t potted in and
is easily removed.
With all the screws and bits removed, I used a small flathead screwdriver to gently pry the metal frame
out of the main module’s thick plastic
body. It fits very tightly and aside from
a few animal hairs and some dried
mud, it came out cleanly, revealing two
plugs from the board; one to the battery
and one to the charge port, which were
screwed and moulded into the main
plastic housing respectively.
Once unplugged, the PCB came
away with the metal base, and I could
see the PCB was attached to the base
with a few more of those tiny PK
screws and stuck with potting compound in several places.
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The first thing I noticed was a lot of
grub between the VHF antenna terminal and its connector into the module.
As I said, that end of the antenna is not
potted in and only has an unsealed,
thin plastic cover over it in the wild,
allowing moisture and other debris to
work its way in.
I cleaned the terminal with some
isopropyl alcohol on a rag and used
my 30-year-old contact-cleaning diamond file to clean the face that contacted with the one in the module.
The module side of things was a little
dirty but looks to be nicely polished or
even chromed steel, so I didn’t file that.
Instead, I used my fibre-glass-bristled
PCB cleaning brush to spruce it up.
Looking further onto the PCB, I
could see that moisture had gotten
into this one. There is a rubber O-ring
type seal between the metal base and
the plastic body of the main module
and it looked to be intact, so I’m not
sure how the moisture got in, but it had
started to corrode some of the solder
joints on the board.
Once again, I used my PCB brush to
clean the board and with a very fine tip
in my soldering iron, I went through
and tidied up every dodgy-looking
connection on the board before setting that aside and checking out the
GPS module.
The GPS module had a plastic bottom, which was held on with four
small screws. Once removed, the base
came away easily, revealing a completely potted PCB board taking up
the whole interior space. The connecting cable exited via a purpose-made
channel in the collar and entered the
potting material, which was clear, so I
could see the cable gently curl around
and end up soldered to the PCB.
This cable was also heavily potted in at the main-module end, so it
wasn’t easily accessible for ringing out.
It needed to be tested for continuity
though, if only to prove or disprove the
client’s theory that it was the problem.
The easiest way to do this was to
drill a small hole through the potting
material down to the joints on the
PCB. I used a standard 1.5mm “jobber” drill to start with, drilling slowly
down by hand with a pin chuck until
I was nearly to the joint, a distance of
about 5 or 6mm.
I finished off with the same-sized
drill, but with the bevels ground off,
making it flat-bottomed. This I twisted
in until it just touched the soldered
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joint. Luckily, the refracted light didn’t
throw me off the mark, as it certainly
looked odd from certain angles as the
drill went in.
I then used my dentists’ pick to clear
the way for one of my multimeter leads
and after touching one lead on that,
went to the main module’s board and
used the other lead to “ring” out the
shielded cable.
Although the main board end was
also potted over, I could touch various parts of the board and get readings, and on the grounded side, could
make a one-to-one contact with earth
points on the main board, even when
twisting and manipulating the cable
at either end, so that confirmed to me
that this cable was not the problem
with this collar.
I refilled the holes I’d drilled in
the potting compound with 5-minute epoxy and though probably not
as tough or hard as the original, for
filling a 1.5mm x 6mm hole it was
sufficient for air and moisture protection.
I assembled the VHF antenna and
plugged in the battery – which by this
time I’d removed from the housing –
pushed the ON button and took the
whole caboodle outside and sat it on
the rag top of my car. Within about 30
seconds, it was double-flashing and by
one minute, was flashing three times,
indicating that at least three satellites
had been acquired.
When I fired up the handset and
selected one of the dogs listed, two
didn’t show any data, though the third
indicated a stationary distance of two
metres, and when I moved the collar
to the end of the driveway, twenty metres. That was good enough for me, so
I reassembled everything bar joining
the main housing and metal base together; I’d need the battery for testing
the others.
The second collar was pretty much
a replay of the first; cleaning up all the
connections resulted in another working collar. The client was well pleased,
and at this stage mentioned there was
a YouTube video of a guy fixing one
of these collars with the same symptoms as ours. I had a look, and that
guy simply replaced the GPS module
with a new part, which was overkill
in my opinion.
The third collar defeated my attempts at basic repair and I think the
GPS module has really gone in that
one. I’m currently stripping the potting
compound out of it. After all, I’ve nothing to lose by doing that and I think I
can pick up a suitable module for a lot
less than the YouTube guy paid. We’ll
have to see.
Repair to Cambridge Audio
640C CD player
D. R., is a tinkerer living in a small
country town, who sometimes gets
asked to look at various non-operational devices...
A friend recently asked me to look
at her CD player. I have had a few CD
players requiring a lens clean, but as
the front panel showed that it was reading the info off the disc, that wasn’t the
case here. There was a signal at the
digital output socket, but nothing at
the analog audio output sockets.
I found a circuit diagrams on the
web which showed that there was a
relay which could mute the output.
There was no “mute” button on the
unit or the remote control so it wasn’t
going to be that easy.
The relay was a 5V DC coil unit
and checking around, I found a mute
connection (CN4) on the board near
the relay. This had either five or zero
volts on it depending on whether play
or pause/stop was pressed. I (stupidly)
jumped to the conclusion that the relay
coil must be open. I ordered a suitable
replacement, but of course replacing
the relay made no difference.
Searching around on the board, I
noticed that four capacitors appeared
to have leaked brown gunge onto the
board. I could only get higher voltage
rated versions so one of them had to
be fitted horizontally on long leads. I
half-hoped this might make a difference to the voltages, but the relay was
still not operating.
Servicing Stories Wanted
Do you have any good servicing stories that you would like to share in The Serviceman
column? If so, why not send those stories in to us?
We pay for all contributions published but please note that your material must
be original. Send your contribution by email to: editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
September 2017 75
Partial circuit diagram for the Cambridge Audio 640C CD player showing the
output mute control, as described in the text.
The diagram showed a circuit with
four transistors associated with the
mute relay. I tested these and they all
appeared OK.
To try and work out what was going on, I soldered a few flying leads
around these transistors so that I
could monitor voltages while the unit
was operating. I realised (a bit late)
that the mute 5V signal was present
when the relay should be off and zero
when it should be on.
This meant that the circuit must invert the mute voltage. I finally traced
the fault to R11 which was difficult to
find as it was covered in brown gunge
from one of the capacitors. It was difficult to test in circuit as it effectively
had a large capacitance in parallel, but
it was open.
I did not have a 2.2kW resistor handy
but a 1kW and 1.2kW in series worked
as a replacement. This fixed the problem and it was reassuring to hear the
relay click on and off and get audio
via the sockets on the back.
After removing my flying leads and
reassembling, I checked that all was
still operating. My friend was very
happy to have her music back, but
since I had deprived her of it for so
long (waiting for parts to arrive and
putting it aside out of frustration), I
felt I couldn’t charge her anything.
I might have saved time and frustration if I had done some better testing
at the start and applied (correct) logic.
Pony 3 mobility scooter
J. W., of Aspendale, WA, was recently asked if he could repair a connector on his friend’s mobility scooter
so naturally he agreed to have a look
at the machine. . .
My friend said that the scooter was
not going as fast as it used to. He had
76 Silicon Chip
been fault-finding the problem over
a period of time and had isolated the
fault to a 2-pin Molex connector. So he
delivered the scooter and we set it up
in the workshop. I removed the cover
from the controller and checked the
“faulty” connector. It seemed to be OK
but I gave it a clean anyway.
With the scooter out of gear, we
were able to hear that the motor was
still not revving fast enough, although
at one stage it did rev up for a short
period. I traced the wiring from the
2-pin connector and found that all it
did was connect the ignition switch
to the controller PCB. So it seemed
highly unlikely that this would have
any effect on the speed of the scooter.
I suggested that he leave the
scooter with me and I would
investigate further. I could not
find any service information on the ‘net so decided
to check the obvious and
hope to find a cure.
The speed was controlled by two potentiometers: a throttle
control with levers for
forward and reverse and
a speed control potentiometer which set the
maximum speed.
I disconnected and
removed the throttle
controller which looks
like a rectangular potentiometer. I found
on the ‘net that
this was called
a wig-wag controller with a
self-centring
position that
was supposed
to give a resist-
ance of half the total. The wig-wag
controller was marked as 5kW and it
measured 5kW between the two outside terminals.
I then checked between the outside terminals and the centre one.
The reading showed a variation of approximately 2.5kW when the controller shaft was moved in each direction.
I assumed that this was OK so put it
back in circuit.
I then unsoldered the speed controller pot and checked it with a multimeter. The pot was marked 20kW and
started at a reading of 20kW at the low
speed end of its travel.
The resistance reduced as I turned
it to a higher speed position but as it
reached about ¾ of the travel, the reading reverted to 20kW and stayed there.
So with the pot turned up to maximum
speed it was giving a resistance associated with low speed and not the zero
ohms I was expecting.
I only had a 50kW pot on hand so
I connected it up and found that the
motor now started at low revs and increased to quite a high speed with the
pot turned to zero ohms, the maximum
speed position.
So it was off to my local parts supplier to get the correct replacement
for just $2. Once it was installed and
everything put back together, I did a
few laps of the garden to prove it was
siliconchip.com.au
all OK. My friend was delighted as he
had been quoted over $200 to have it
looked at by the supplier.
Fixing a useless machine
J. G., of Princes Hill, Victoria is having fun in his retirement, reliving those
halcyon days when he made model
planes and played around with electronics. He takes up the story. . .
My most recent project has been to
make a “useless machine”, invented by
Marvin Minsky at MIT in Boston. The
first prototype seems to have been built
in the 1950s by Claude Shannon, the
pioneer of information theory.
A useless machine consists of a box
with an on/off toggle switch on top.
When it is turned on, a hand emerges
and turns it off. That’s all it does. You
can buy useless machines from Jaycar,
but I wanted to make one that is even
more useless! It would be more creepy
if the hand emerged very slowly but
snapped back into its box the moment
it hits the switch.
Servo motors used to control model
planes are ideal for this purpose. They
consist of a small brush motor and a
set of reduction gears which actuate
a “control horn” linked to the rudder
or ailerons.
The servo is controlled by a stream
of pulses, the width of which sets the
position of the control horn. Typically,
a pulse width of 1.5ms sets the horn at
a midway position; a pulse of 1.0ms
moves it to one extreme and 2.0ms to
the other extreme.
It was relatively simple to devise a
circuit using a CMOS version of the
ubiquitous 555 timer IC, where the
pulse width is smoothly increased
by a slowly rising voltage on the control pin, causing the hand to emerge
slowly, followed by a sudden return to
a short pulse, putting the hand back
into the box.
Preliminary testing without the motor connected showed that the circuit
worked well, but the best laid schemes
o’ mice an’ men gang aft agley. With the
servo connected, the hand oscillated
wildly and randomly back and forth.
This problem is well known in the
radio-controlled plane fraternity, and
is known as “servo chatter”. It didn’t
take long to confirm that it was caused
by noise from sparking motor brushes.
Somehow the motor noise was getting
into the control circuit but a variety of
measures including ferrite beads in the
motor wires and a 2000µF capacitor
siliconchip.com.au
across the battery made no difference.
Old-timers will remember a common problem that used to affect valve
radios, aptly known as “motor-boating”; characterised by a loud put-putput-put in the speaker. These days
it is sometimes seen in valve guitar
amplifiers.
Motor boating is caused by feedback
between the power output stage and
earlier voltage amplifier stages via the
high voltage supply line. Badly designed circuits can be prone to motor
boating but it is typically caused by a
faulty electro.
Motor boating is commonly prevented in the design stage by decoupling
the early stages from the power stages,
by using a simple RC filter in the high
voltage line to prevent fluctuations in
the supply line feeding back into the
high gain voltage amplifier stages.
Could decoupling solve my problem
with servo chatter?
The motor and the control circuit
were fed from a 6V battery. Measurements showed that the servo motor
drew a wildly fluctuating current with
peaks of well over an amp and the
scope confirmed that the supply voltage jumped up and down randomly
when the motor moved. The control
circuit only consumed 2mA. How
about decoupling?
All it took was a 220W resistor followed by a 1µF MKT capacitor to
earth. The control circuit still worked
perfectly with less than half a volt
drop in supply voltage, but the servo
chatter disappeared completely. Now
when the hand moves out slowly and
creepily, and snaps back instantly, it
always provokes fits of laughter in
young and old.
Incidentally, while the labelling on
the switch in the accompanying picture may look incorrect, it is not. The
switch is pictured in the ON position.
The hand pushes the switch to the
OFF position. In the “resting” situation, the servo arm presses against
an invisible microswitch, keeping it
in the OFF state. The microswitch is
in parallel with the visible switch but
is not seen in the photo, such that no
power is delivered to the electronics
or the motor.
The hand is activated by moving
the switch to the ON position. This
supplies power to the electronics and
the motor.
The hand slowly moves forward,
such that the microswitch is now
turned on. The hand moves out of the
box, pushing up the lid, and pushes
the visible switch to the OFF position.
The hand then moves quickly back to
the inside of the box, where a hidden
protrusion presses on the microswitch
and turns the power off.
There’s more to it than meets the
SC
eye!
A useless machine is a functional device that serves no useful purpose. This
example was designed such that when switched on, a hand will come out and
turn the switch off; using a servo to provide the hand with a variable speed.
September 2017 77
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