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SERVICEMAN'S LOG
Roped into fixing a friend's dishwasher
Dishwashers are ostensibly quite simple
mechanical appliances with pumps, solenoids,
a timer and a little thing called a “wax motor”.
What's a wax motor? I hear you ask? I didn't
know the answer either and this was my
introduction to fixing a friend's dishwasher.
Fortunately, I did not have to fix it before we
had dinner.
I was invited to the dinner by an engineer acquaintance I hadn’t seen for a
while, which was a pleasant surprise.
Over dinner, the conversation veered
toward work. Then my host asked if
I knew anything about dishwashers.
Sensing the loaded question, I informed him that I didn’t know much
about them, never having had one apart.
When I asked the reason, he told
me his dishwasher was just out of
warranty (of course) and had started
misbehaving. The powder dispenser
was no longer opening, meaning the
wash cycle was completing without
any powder or rinse-aid being introduced. Could I perhaps take a look?
I wonder if mechanics who visit their friends get asked to replace
a leaky head gasket after dinner. Or
whether doctors out for a nice evening of food and wine with acquaintances end up getting roped into doing a quick surgical procedure on the
dinner table. But I digress...
I had a quick look at the dishwasher,
checking the patently obvious, ie, that
the powder/tablet dispenser’s door
could indeed open and close freely.
Beyond that, we were into (for me at
least) a technical grey area.
While I’d have thought nothing of
opening the appliance up there and
then, some serious shade was being
thrown my way by the other half, reminding me that we’d come for dinner, not to work!
I arranged a time to go and have a
proper look, secretly relieved as I never did like going into anything blind,
especially with someone looking over
my shoulder.
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At least I’d now have time to look
into dishwasher operations and potential problems and solutions before
committing to a repair.
Dishwashers for dummies
These appliances turn out to be a
very simple idea cleverly implemented. Essentially, they are just a watertight box with trays that hold dishes
at different levels while heated water
is sprayed around by (usually) waterpressure powered rotary nozzles.
At a certain time in the wash cycle, the powder drawer is opened
and the cleaning agents are introduced. There is then
a rinse cycle or two
– with or without rinse-aid
added – be-
Australia’s electronics magazine
Dave Thompson*
Items Covered This Month
•
•
•
•
Dishwashers for dummies
Ants on the drive
Earth leakage fault
Heat pump repair
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
fore the water is pumped away and the
dishes gradually dry off in the warmed
cupboard.
Some models may also automatically pop the door ajar during the final,
drying phase to aid moisture evaporation; some also use ultra-violet light as
an anti-bacterial "sterilisation" feature.
While that all sounds pretty straightforward, as with all appliances there
are many potential things to go wrong.
Leaks, blockages or electrical-mechanical faults can cause mayhem if the cycle gets out of whack.
August 2018 57
In a worst-case scenario, we could
end up with a shed-load of water all
over the kitchen floor, something I can
tell you from experience is what you
don’t want happening.
The majority of my kitchen furniture is made from melamine-coated
particle board and while the sides and
edge-banded areas may be watertight,
the bare edges of all the cabinets sitting on the floor act like a sponge to
any moisture they are exposed to, so
a few centimetres of standing water
doesn’t do them much good!
If exposed to too much moisture,
the edges swell up like the half a digestive biscuit I always drop into my
mug of tea, causing drawers and cupboard doors to stick and, in more serious cases, entire cabinets to sag and
bow. I know this because it happened
to us and repairing that kind of damage is difficult and expensive.
Modern dishwashers utilise various sensors and onboard computers
to control all the various functions,
while some older or less-expensive
types use mechanically-operated timers and actuators instead.
Some early models used bi-metallic
strips to regulate water flow or open
the dispenser when the right water
temperature was encountered, while
newer or more sophisticated units
use electronic temperature sensors or
electrical and thermally-operated solenoids called “wax motors” to achieve
the same thing.
Other older types used mechanical
timers to pop the powder drawer at a
certain point in the cycle so there is
plenty of scope for variety.
The meat of the repair
The dishwasher in question, a Haier
branded unit, is regarded as a basic but
usually reliable unit if internet chatter is to be believed. This model has
a very simple control panel: an on/off
pushbutton, a half-load button and a
single dial on the right-hand side for
different cycle settings; no fancy bells
and whistles to complicate things (or
go wrong!).
According to my research, it utilises
a wax motor drawer-release mechanism and the problem was most likely
to be the heating coil for the wax motor going open-circuit (more on this
below). If not that, there is likely some
mechanical reason for the drawer not
opening. The only way to know for
sure was to open the thing up and get
58
Silicon Chip
probing with a set of eyeballs and a
multimeter.
Thankfully, this dishwasher manufacturer has its act together and everything to do with working on this unit
was a breeze. For starters, getting it out
was easy; the rear two support rollers slot into corresponding locating/
holding clips that are screwed to the
floor, while the front is supported by
wheels; an arrangement that prevents
the dishwasher moving around in any
direction once installed.
Grabbing the edges of the closed
door and pulling straight out was all it
took to roll the unit clear of the bench
cavity. The power cable was plugged
into a socket located on the wall up
behind the unit, while the water and
waste hoses fed through a sizeable hole
in the adjacent cabinet wall. There was
plenty of slack in all the leads and
hoses and getting behind it to disconnect or unplug them was no problem.
I removed the power plug but left
everything else in place; no point
tempting fate by needlessly disconnecting hoses and potentially introducing leaks if I didn’t have to.
There were no visible screws on the
outside of the cabinet but upon opening the door I could see everything I
might need to undo was easily accessible from the inside and along the edges
of the chassis. Hopefully it wouldn’t
come to that, but either way the door
front would have to come apart, as that
is where the powder-drawer dispenser
and actuator lives.
Like most white-ware, the thin steel
panels are held to the main frame using medium-to-large PK-style countersunk screws. The coarse thread pattern
on these fasteners is excellent for this
type of sheet-metal joinery. However,
due to their size and the screwdrivers
typically used to fit the screw heads,
they are very easy to over-torque during re-assembly.
This often leads to servicemen finding oddball-sized screws utilised,
as the original’s mounting holes are
stripped and ever-bigger fasteners are
used by over-enthusiastic re-assemblers. I’ve even found the odd large
wood-screw holding fridges or oven
panels together! Thankfully, it appeared I was the first serviceman into
this appliance, so no mismatched
screws to deal with here.
Half a dozen removed screws later,
the faux-enamelled front panel fell
away from the pressed-steel interior
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door section and sprung, tubular-steel
support frame, revealing some very
non-technical components.
Getting down to nuts & bolts
There were several sound and vibration-deadening carpet swatches stuffed into cavities, a couple of
purpose-shaped plastic foam packing pieces and multiple wiring looms
coming from beneath the bottom door
hinge and going off to points (for the
moment) unknown.
One small loom disappeared into
some sound-proofing material about
half-way up the door, to the barelyvisible, injection-moulded plastic dispenser assembly. While this was mostly buried in foam packing, I spotted the
wax motor mounted on the left-hand
side of the dispenser.
According to Wikipedia, a wax motor is “a linear actuator device that converts thermal energy into mechanical
energy by exploiting the phase-change
behaviour of waxes.”
It apparently contains a small tube
packed with wax and a piston; heating the tube at a certain time into the
wash cycle, usually electrically via a
thermistor, causes the wax to gradually
expand, forcing the piston to extend,
which pushes on a plastic bell-crank
and, via a lever arrangement, disengages a sear which then allows the
powder drawer to spring open.
It is a simple yet effective method
of opening the dispenser. In some
models, a secondary actuator allows
rinse-aid to enter the cabinet during
the rinse cycle.
The powder drawer itself sits opposite the wax motor assembly on the
other side (inside) of the door panel
and a rubber seal keeps any water from
entering the door cavity. As the drawer is opened by a spring and manually
shut once the powder or pellet is added, it doesn’t take much to release the
retaining sear and pop it open.
Once open, the drawer is usually
stopped by and rests under the top
dish tray, a position that helps guide
water into the dispenser to ensure
all the powder and/or rinse-aid is
washed out.
On many dishwashers, when you
open the door to remove the dishes,
you hear the dispenser door flick open
all the way, a somewhat disconcerting
sound if you haven’t heard it before.
However, in this case, the drawer
remained closed. Testing it in-situ
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would be a problem, as running the
appliance through a wash cycle is
both time-consuming and inconvenient, especially since I had the covers
off and it was sitting in the middle of
the kitchen floor.
What I needed to do was to see if
I could measure the resistance of the
thermistor which heated the wax to operate the wax motor; this would at least
tell me if the thing was still electrically
alive. If it was, the problem could lie
with the wiring, the controller board
or something mechanical.
I removed the leads from the motor
terminals and with my trusty analog
multimeter set to the 10W range, I
placed one probe on each of the terminals.
I measured roughly 2kW, which
according to Google (such a clever
chap!) is about average. I wasn’t too
concerned with the actual resistance
at this point, as long as it wasn’t at either extreme; I just wanted to know if
the motor had continuity, which it did.
The next step was to see if it actuated and to do that, I’d need to add
power. The problem with this is that
applying mains voltages to an in-place
component using a pair of flying leads
is a bit hairy.
Do you have any good servicing stories that you would like to share in The Serviceman column? If so, why not send those stories in to us?
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Please be sure to include your full name and address details.
which is usually supplied at the right
time in the cycle by the controller
board. For testing, I dialled in 240VAC
(indicated) on my non-Variac branded
variac and waited. After a short time,
the motor’s plunger slowly deployed,
moving the plastic lever system. However, the drawer remained closed.
From what I could see, the lever system didn’t move far enough to trip the
door mechanism. From this, I could
deduce we were likely looking at a
mechanical fault.
I removed mains power and while
the motor was still warm enough, manually moved the solenoid’s plunger
as far as it would go; while some of
the links go off to the rinse-aid dispenser, I could see the bell-crank and
cam arrangement that opens the dispenser door.
The plastic arm that trips the drawer release didn’t move far enough to
open it, though it did if I gave it some
extra help. I took a closer look and
could see the pivot pin on one of the
levers was out of whack. It was either
misaligned from new or slogged out, I
couldn’t tell which. As no individual
plastic parts are available for this dispenser, I would have to fix it if I was
to avoid buying a costly replacement.
The lever popped off easily enough
but it wasn’t repairable using the original pin, so I removed it altogether
and bored the linkage’s moulded pivot point out. I found a suitable cap
screw and self-tapped it well into the
base, tightening it down enough to
hold everything yet allow it to move
freely. Now, when I manipulated the
solenoid, the drawer popped open
every time.
I didn’t bother running another
heated simulation, as I was sure this
would work now. I’d spent a lot of time
on this, and as the owner assured me
he could reassemble everything, I left
him to it.
However, I received a text message
later that night saying that while the
dispenser now worked fine, the dishes were still not as clean as before. I
dropped by the next day to check it
out and discovered that while he’d had
everything apart, he removed the upper and lower rotating spraying arms
in order to better clean them, but had
re-assembled the bottom sprayer with
the holes pointing downwards!
After reversing them, a test wash
cycle proved everything was working
properly. Whew!
Australia’s electronics magazine
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Once bitten, twice shy
Many years ago, I vividly recall my
brother and me, who were just old
enough to get into trouble, messing
about in Dad’s workshop. My brother
had found and wired up a mains plug,
or perhaps just cut and stripped the
leads of an existing cable and plug,
while I watched over his shoulder.
We’d found a bulb after rummaging
amongst Dad’s bits boxes and were
keen to fire it up, the way we’d seen
him do it many times before – or so
we thought. What we had done is inadvertently created what olde-worlde
servicemen – in their typically dry
way – call a “suicide lead” or “death
cord”. In other words, a cord with a
mains plug at one end and bare wires
(or alligator clips) at the other.
I must admit to possessing such a
lead, which is typically used for testing valve-based equipment. But for obvious reasons, it makes me extremely
nervous. My modern version has a
crocodile clip to connect Active and
Neutral to the equipment I’m testing
but as kids back in the workshop, we
just used bare wires and I held the bulb
while we each applied one wire to one
of the bulb’s terminals.
It lit up, albeit extremely briefly
and with the shock of the brilliance
of it, I reacted and touched my lead
to my brother’s. Of course, this splattered and crackled and arced, scaring
the bejeebers out of us and temporarily blinding me as well; a situation
made worse by the fact the workshop
was now plunged into darkness as all
mains power went out.
Yikes! We were in for it now! I envisaged all manner of trouble was about
to befall us and to this day remember
the unusually stern talking to we both
received from Dad. Not only were we
told not to mess about in his workshop
with anything we didn’t understand,
we were especially not to go anywhere
near anything to do with mains-level
voltages.
He then showed us how he powered up bulbs with a battery and encouraged us to experiment with that
but not to mess about with anything
that plugged in.
He also demonstrated how easily
we could have killed ourselves by using his multimeter to demonstrate the
voltage from the mains socket. That
made me paranoid enough to still be
extremely wary of it today.
The moment of truth
I was going to use my suicide lead to
test the wax motor but not with direct
mains voltage. I’d brought my autotransformer along to use with it, and
while the output could still easily kill
me, I made darn sure the connections
to the wax motor were attached properly and well-insulated from anything
else before cranking up the juice.
In order for this wax motor to fully
actuate, it needs around 230-240VAC
Servicing Stories Wanted
60
Silicon Chip
Empire of the ants
J. R., of Woy Woy, NSW, recently
fought a pitched battle with a small
but numerous army of invasive critters which threatened to overheat and
gum up his electronic equipment. He
did not welcome these new insect
overlords and eventually banished
them from his domain. Here is how it
went down...
My "man-cave" is in our garage
which I share with my car. The walls
are bare single brick and although it
gets a bit nippy in the colder months,
the insulated ceiling helps a bit. I have
a desk, workbench and adjustable steel
shelving and I keep it all pretty neat.
We get a few mozzies and the odd
fly in the warmer months but they are
mostly dispatched with a very distinct
zap by my high-voltage bug killer with
UV attracting light. Ants are a different problem though.
Ants need food and shelter and it
seems they like to be warm. Wifey prefers a minimal amount of technological
stuff in the house so I keep my computer gear in the cave, including a couple
of hard drives, the NBN modem and a
router to network the house. Some of
my gear stays on 24/7 and has a nice,
stable temperature which is most attractive to insects, especially ants.
These industrious little beasts never
seem to tire and they are mostly very
good at staying out of sight as they
move about. One day I was happily
working away when a single black ant
sauntered past.
I brushed it to the floor and thought
no more of it until a while later when
I spotted another one that I imagined
might be looking for its mate. I thought
there might be more about so I decided
to look for their source.
I don't use the inbuilt keyboard or
screen on my laptop so it hardly ever
gets moved. I spotted a few more ants
walking along a cable and then disappearing down a gap in the screen's
hinge. Then I saw others leaving by
the same path. Alarm bells were now
ringing in my head and I immediately powered down the laptop and disconnected it.
There were probably a few alarm
bells ringing in the ants' heads too because more appeared from the screen
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hinge and the keyboard. Without closing the screen, I picked up the laptop
and took it outside to an old kitchen
table we use for potting. A quick brush
down of the tabletop and a strategically
placed towel made a good clean work
surface to open up the laptop.
Fortunately, I had a set of tiny Torx
drivers that I bought when I replaced
the hard drive with an SSD. More ants
were now starting to leave their hightech home and found themselves in a
strange, very exposed place.
I undid all the bottom cover screws
with the laptop sitting on the towel
like an A-frame. I did this because I
didn't want to squash any ants – the
acid inside them would affect the components and PCBs.
I removed the bottom panel and saw
what looked like millions of ants, their
eggs and larvae all packed into every
nook and cranny.
With the air now freely moving
around them and the internals cooling
down, it was every ant for itself! They
were swarming all over the table, with
many of them carrying an egg or larva.
I did not use any insect spray. I
quickly set up an old vacuum cleaner
I use in the garage and sucked most
of them up. It took over an hour before they stopped appearing. I wish I
had taken pictures whilst all this was
happening and still can't believe how
tightly packed they were.
What is more amazing is that there
was zero impact on the computer – it
had continued to function perfectly,
with no overheating or errors at all!
The ants must have been occupying
my laptop for days or maybe weeks before I spotted a couple of their scouts.
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I left the laptop out in the open for
another hour or so to give the last stragglers time to leave. Once it was apparently emptied of ants, I removed everything that could be removed and found
a few dozen more here and there. Some
compressed air blew out a few more
ants and eggs and eventually, I was satisfied that they were all gone.
I cleaned every surface I could with
a cloth very lightly soaked in CRC 2-26.
It is my weapon of choice against corrosion, moisture and electrical leakage and I feel sure the odour and the
oily film would discourage future ant
incursions. It doesn't go gooey either.
The only visible clue I could see left
behind by the ants were white marks
in tight places where the eggs had been
and some CRC 2-26 on a cotton bud
removed them almost totally. I left the
laptop on my workbench overnight
and reassembled it the next day. It
has been working perfectly ever since.
But this story does not end here. A
few weeks later I again noticed an ant
on my desk. My response was swift. I
whipped the laptop out of action and
checked it thoroughly, but no ants, not
even one – CRC 2-26 in action!
Nervously, I unplugged each item
one by one and moved them outside.
I saw no ants until I unplugged one
of my hard drives and lifted it up to
reveal a rectangular carpet of ants underneath. Yikes, not again!
Outside went the hard drive, onto
the table, to wait for the ants to depart of their own accord. Back inside I
quickly fired up the vacuum cleaner to
suck up all the ants now running every
which way on my desk. How had they
been getting to the drive?
August 2018 61
Well, the desk the drives are on is
screwed to the wall with a dress strip
making a nice dark tunnel out of the
mortar line and delivering the ants to
the hard drive. That strip is now gone.
I went back out to inspect the hard
drive and only a few ants were exploring the tabletop. I peered into the
drive's cooling vents and could see
ants, ants, and more ants! This time
they were not leaving, so using a few
impromptu spudging tools made from
scraps of fibreglass PCB and a screwdriver or two, I was able to carefully
remove the case without stirring up
the ants.
This time I took a couple of pictures
too (as shown above). It was the same
story as the laptop when it was opened
– legions of ants with their eggs and
larvae were now swarming all over
the table and the vacuum cleaner did
good once again.
It was then a simple matter to unclip
and remove a metal shield to inspect
around the hard drive and unplug the
tiny controller PCB. Hard drives have
dust-proof construction so no ants
could get into the mechanism. As before, compressed air removed the remaining eggs and CRC 2-26 was used
to clean up all contaminated surfaces
and generally protect everything.
Reassembly the next day was easy.
On testing the hard drive, I was relieved that the ants had caused no
damage and the drive has been running 24/7 ever since.
You may think that was the end of
it – no way!
62
Silicon Chip
Days later, more ants were observed
in the man-cave, just wandering about
looking for their next warm abode.
An extensive search eventually
found millions more living in the extruded aluminium frame of my one
and only window, right behind my
desk, with a few hundred extra ants
and eggs crammed into the little homemade headphone switch box which is
screwed to the side of my desk.
I tried various surface sprays in and
on the window frame and many days
and dead ants later, they were still in
evidence. Good grief, what does it take
to get rid of them? I don't like the idea
of long-lasting toxic chemicals being
sprayed copiously where I spend a fair
bit of my time.
After some trial and error, I eventually found that a Permethrin-based ant
and wasp powder in a puffer pack was
very effective and the safest way to go
(Permethrin is a synthetic version of
natural Pyrethrin). Result – no more
ants – yay!
An earth leakage fault
in the house
One morning, B. P.’s wife turned
on the light switch but nothing happened. He thought it was probably just
the globe that had failed but then another light could not be switched on...
The household appliances were still
operating, displaying clocks and so
on, so it obviously wasn’t a blackout. I
headed over to the laundry where our
sub-board is located to see what was
going on. The safety switch for the light
circuits had tripped. I tried to reset it
but it just tripped again, indicating a
serious earth leakage fault.
We have a modern house and our
electrical installation complies with
the latest Queensland electrical regulations. We have two safety switches,
one for the power circuits and one for
lights. Three power circuits and two
light circuits are protected by the safety switches.
Further investigations indicated
that there was a fault on light circuit
#1, which tripped the safety switch
when on but light circuit #2 did not.
So we could have light in part of the
house for the moment.
The wiring in our entire house had
been checked on three separate occasions by licensed electricians. The
first time was when we had the underground power connected to the
house, the second time was when we
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had the solar PVR system installed
and the third time was a safety check
following several electrocutions associated with the installation of foil
insulation in house ceilings. So this
was a new fault.
There was nothing for it but to head
up into the roof space and have a look
around and see if I could see anything.
There's been a lot of activity in our roof
over recent years, with the running of
cables, first for the ABG satellite internet, then the interim NBN satellite
internet, then again for telephone and
network cabling when we got ADSL.
Also, as we'd been unhappy with the
foil insulation that we had installed
(it didn't seem to be effective during
winter) we'd been putting “Earthwool”
insulation under the foil. It had to be
removed and re-installed on all of the
above occasions too.
So, could any of this activity have
caused the problem to occur? It seemed
unlikely as it had been several years
since anyone had done anything in the
roof space. The next thing I thought of
was rats in the roof. It's pretty common
to find rodents in your roof space, so
maybe a rat had eaten through a wire.
As I entered the roof space, I could
see evidence of rodents and nothing
stood out as problematic. However, I
decided to lift the insulation and inspect all the wiring anyway. I could
still find no problems. The wiring was
still in excellent order with no sign of
any damage whatsoever.
At this stage, I decided to give my
mate Ray a call. Ray is a licensed electrician and he lives in town, but he
often works in the Bay. Our place is
between, and as it happened, he was
just about to leave to do some work in
the Bay, so he said he'd call in on his
way past for a quick look.
When he arrived, he brought in his
“megger” and tested the circuit, which
gave a reading of 33kW. That’s way
too low and explained why the safety
switch was tripping. I checked with
my multimeter and I got a similar, but
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higher reading, so we knew that there
was an Active-to-Earth fault somewhere in the #1 light circuit. Now we
just had to find it.
The quest begins
Ray headed off and said he would
call in again on his way home when
he would have a bit of spare time, to
look into the matter further. When he
got back, I suggested that we could start
by disconnecting parts of the circuit
until we found where the fault was.
He agreed so we got started.
The #1 light circuit starts at the subboard and goes to the family room,
kitchen, dining room, lounge room,
entry, en-suite and master bedroom,
with branches going to the end of the
back verandah, the side verandah and
the front verandah. So by disconnecting the wiring along the way, we would
be able to isolate where the fault was.
We started in the family room, where
Ray disconnected the circuit at one of
the lights. This cleared the fault, so the
fault was further on. After reconnecting the wiring there, we moved to the
lounge room and did the same thing.
This again cleared the fault, so we
moved to the en-suite. This time, the
fault was not cleared, so it was between
the lounge room and the en-suite.
We'd skipped over the entry light, so
we headed there and Ray found that
the branch line from the light socket,
which took power to the light switch
near the front door, was where the fault
was. Ray then removed this power
wire at the light switch and tested the
wire, which showed the fault.
So for some reason, the Active wire
from the light socket in the entry to the
light switch near the front door had an
Earth fault. We would need to replace
this cable and I had a cable drum with
about 10m left in my shed. This was
the older-style grey cable with thicker insulation, compared to the newer
white slimline cable, so my left-over
cable would match the original wiring.
We both knew that running this cable would be difficult, so Ray said that
he would leave it with me and he'd call
in again tomorrow afternoon to connect it up, once I'd run it between the
two locations. In the meantime, he left
that branch disconnected, so we would
then have light in all the house except
for the entry and the front verandah.
The next morning, I tied the end of
the new cable to the old cable at the
light switch and went up in the roof
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to pull the cable through, while my
wife fed the cable up from the drum.
Our roof is 22.5° pitch, so while there's
enough room to get to the walls, it's a
tight squeeze.
I managed to get over to the front
wall with the aid of a plank set between the roof trusses which I could
lie on. The first thing I noticed was a
large snakeskin in the area where the
cable ran down the wall but there was
no damage to the cable at this point.
We often find snake skins around
the place. There are times when we
also find the owner of the skin, which
is typically a carpet python, luckily a
harmless type of reptile.
Occasionally, I have had to remove
snakes from the house or the back verandah as my wife doesn't like them
very much for some reason; I don't
have any problems with them, particularly as they help to keep the rodent
population under control. I usually
just re-locate them clear of the house.
Anyway, I pulled the new cable up
and ran it over to the light socket and
poked the end through the ceiling,
ready to be connected. I took the old
cable down with me so that I could
inspect it but initially, I couldn't see
anything obvious.
I'd been expecting to find some severe damage to the cable, but on a
quick glance, it looked like it was still
OK. This indicated that there must be
an internal fault in the cable itself.
I decided to rip the cable open to
look for an internal fault and while I
was doing this, I found the cause of
the problem. Around 10 years ago,
we'd been away for a few weeks and
when we got home, I found that termites had tracked across the front verandah in one of the joints in the concrete and eaten the pine panel under
the front door.
They were despatched quickly, but
in any case, they can't do any structural damage to our house as it has a
steel frame and is on a concrete slab.
It would appear that when these pests
had been present, they had actually
chewed a hole in the cable in the front
wall of the house.
As to why it had taken so long for
this fault to materialise, I suspect it
was because the weather has been exceptionally dry in this area for the last
decade and we'd experienced several
severe droughts during that time.
It's only last year that we've had unseasonal wet weather in spring, with
Australia’s electronics magazine
August 2018 63
very high rainfall and high humidity
levels. In fact, it was mentioned on
the weather report just recently that
this was the wettest spring in decades.
This must have caused any left-over
termite material in the small hole to absorb moisture and become conductive.
When Ray came back to re-connect
the wiring, I showed him the damaged
cable. He was amazed and he said that
he'd never seen anything like it in all
the time he'd been an electrician. I
told Ray that I'd previously seen wiring chewed by rodents, but I'd never
heard of termites attacking electrical
wires before.
Ray finished connecting the wiring
and we once again had all our lights
working. It was fortunate that we know
Ray and we often do favours for each
other, so that saved us quite a bit, compared to if we'd had to pay an electrician to locate and rectify the fault.
If we hadn't had the safety switch in
the circuit, it is possible that the current flowing between the conductors
could have caused it to overheat start
a fire. Fortunately, the safety switch
stopped it before it could escalate.
I had previously been wondering why there was a need for a safety switch on the light circuit, as it
would be difficult for anyone to come
in contact with a live wire, other than
through carelessness when changing
a light globe with the power still on. I
can now see a very good reason for it.
Heat pump repair
Have you ever called in a repair
technician, only to get the feeling that
you know more about troubleshooting
than they do? That must be how M. D.,
of Canberra, ACT, felt while dealing
with multiple parties, none of which
were able to find the fault in the household heating unit. He eventually managed to sort it out himself...
Our house is equipped with a reverse-cycle air-to-water heat pump.
It is a three-phase device with about
12kW heating/cooling capacity. It's
used for hydronic heating and cooling of the concrete slab in our house
and we have several hydronic fan-coil
units for conditioning the indoor air.
The heat pump is an imported Chinese model, rebranded and sold by a
local distributor. It appears to be well
built and has operated reliably for
eight years. But towards the end of
last summer, the unit began to intermittently trip. The system controller
64
Silicon Chip
reported “Power phase error”.
Throughout winter, this problem
arose frequently, but unpredictably. At
times, the unit would trip within minutes of starting, while at other times it
would run for many hours without any
problem. When the machine tripped,
it could only be restarted by cycling
mains power at the circuit breaker and
this was becoming tedious.
The electrical design is straightforward. The heat pump compressor is
switched by a contactor and this is
driven by a control PCB. The unit has
several safeguards such as a phase
fail relay, overcurrent protection (in
the contactor) and a system protection mechanism that monitors the heat
pump for faults such as low/high refrigerant pressure and excessive compressor discharge temperature.
Having tired of this fault, I called
the supplier. They suggested that the
heat pump might have lost its refrigerant and to get a heat pump specialist
to take a look at it. However, the lowpressure gauge was reading the correct
pressure during operation. I called a
heat pump technician. By connecting
pressure gauges to the high and lowpressure service ports, he declared the
system to be fine.
I then called an electrician. He
checked phase voltages and currents
and declared all to be in order. Without
any real diagnosis, he thought that the
phase failure relay would need to be
replaced. The phase failure relay trips
the main compressor contactor if the
phase-to-phase voltage is out by 15%
or if the phases are not in sequence.
This was an expensive guess and did
not fix the fault.
The electrician then sought to start
replacing every electrical component
upstream of the heat pump without
further diagnosis. I felt it was time to
take a more considered approach.
I called the supplier again. They
suggested that I bypass the compressor
safety switches to see whether that was
the problem. Although these switches
are low voltage inputs to the controller,
I was not comfortable in operating the
heat pump without these safeguards.
In any case, the heat pump reported a
power system fault.
The user manual is brief and offered
little guidance. As is often the case
with imported units, the English translation is ambiguous. The manual suggests that the heat pump is equipped
with a system protection PCB in adAustralia’s electronics magazine
dition to the main control PCB. The
circuit diagram in the door of the unit
also shows this PCB but it was not present in the hardware!
The error we were getting was supposedly coming from this protection
PCB, so I thought that the error message itself could have been in error.
I subsequently noticed that the
compressor heating band was in poor
condition with exposed wires where
rats had chewed away the insulation.
I disconnected the band, thinking that
it may be the cause of the fault, but the
unit still tripped intermittently.
It seemed to me that the control PCB
was deciding to switch the compressor
contactor off in response to an unexpected reading from some sensor. So
I decided to monitor the low-voltage
signals coming into the controller using a Maximite as a high-speed data
logger. The contactor provided an
auxiliary contact that I used to detect
when the unit tripped.
I monitored the low and high-pressure switches, the over-temperature
switch, the pump flow switch and the
phase failure relay at 20ms intervals.
Having observed several trip events,
I could see nothing that would cause
the unit to trip. I even powered the
control PCB from an external battery
to eliminate any power supply issues.
While checking voltages around the
control PCB, I noticed that the signal
from the over-temperature protection
switch was sitting at around 1V and
was unsteady. This was odd since all
the protection sensors were supposed
to be normally-closed switches. I had
configured the Maximite to read the
switches using digital inputs and so
this had remained undetected.
I reconfigured the Maximite to read
analog voltages and confirmed that the
“switch” was producing a varying voltage as if it had gone high-resistance.
Replacing the over-temperature cutout switch solved the problem. The
replacement cost about $5.
It was unsettling to witness lack
of proper diagnosis by the electrical
technician, the poor support offered
by the supplier and the poor level of
supporting documentation and the
misleading error messages reported
by the machine.
In the end, it turned out that I was
the only person able to properly troubleshoot this system! But it certainly
is a great relief to have heating back in
place for the Canberra winter.
SC
siliconchip.com.au
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