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SERVICEMAN'S LOG
Travelling makes me go cuckoo
Finally back from a long trip overseas, I
had the expectation of a holiday from my
holiday, but it wasn’t to be. One of the tacky
souvenirs I brought back as a gift was faulty
and of course it needed someone to fix it.
While most people would throw it away, this
was a gift and so I couldn’t help myself and
went straight to work.
On slow days, most of us day-dream
of relaxing in some exotic location,
with nothing better to do but to chill in
the sun and sample the local delights.
Unfortunately, modern travel has
put a wet blanket on those dreams for
me. After far too many hours standing
in queues, lounging about in airports
the size of small cities waiting for connecting flights and being crammed into
aeroplanes packed to the winglets with
irritable travellers, we couldn’t wait to
get to where we were going – whether
far away or back home.
I’ve concluded that this baggageclass travel lark is for other people;
next time it will be business class or
bust!
In theory, technology exists to make
life better but I saw plenty of evidence
to the contrary on my trip. For example, those body scanners at airports.
Not only are they personally invasive
but they are actually slower than the
traditional pat down and metal-detector approach!
On the way out, all the women passengers were diverted from the queue
into and through the scanner, and on
the way back, all the men were. For
those who haven’t had the pleasure,
you walk into a large, walk-in wardrobe-sized metal and glass booth, plant
your feet on two painted footprints
on the floor and hold your hands up
as if surrendering – which of course,
you are.
A back-and-front scanner laterally
rotates around 180° and back before an
image is displayed for the perennially
Dave Thompson*
Items Covered This Month
•
•
•
Fixing a cuckoo clock
Vintage army computer repair
Westminster chimes in Oz
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
grumpy operator to view. (Wouldn't
you be grumpy too if your job was to
stare at images of tired travellers' saggy
appendages all day?)
While there is a display outside
the booth that the passenger can view
on stepping out, the security person
barked out orders for me to move forward so sharply that I didn’t have a
chance to see what it looked like before I got a full pat-down anyway. So
what’s the point of these scanners?
For another example, smartphones
are everywhere now. In many parts
of Europe, you can pay for parking,
petrol, souvenirs, groceries or pretty
much anything else just by using an
app, texting a number or holding your
phone near a terminal.
In the airport, you can use smartphones to display online boarding
passes at express check-in terminals
and to pass through the departure and
boarding gates. The express check-in is
great, and a real time-saver, unless (like
us) you have bags you can barely lift
that need to be checked in manually.
However, using the phone for boarding takes longer than when the ground
crew check each boarding pass the oldfashioned way, so where’s the benefit
here to the weary traveller?
On more than one occasion, a passenger couldn’t get the phone to wake
up or the scanner to read it correctly,
holding up those waiting to board even
more. Progress? I’m not so sure.
Enough grumbling. . . for now
Anyway, after two gruelling days
of travel, we were happy to be home,
58
Silicon Chip
Australia’s electronics magazine
siliconchip.com.au
and then came all the unpacking. We’d
brought a few souvenirs with us for
friends and family, as one does, and
we’d packed them very carefully to
prevent them from being damaged.
YouTube is full of videos of baggage-handling staff at airports around
the globe casually kicking or dropping
suitcases 15 metres to the ground,
or chucking bags from the hold onto
the trolleys – and sometimes missing. I have no doubt that most airport workers are diligent but even
with our hard-shell cases, we suffered
some damage.
It’s annoying but there it is; we knew
the risks. It is even more annoying
when you unpack something you purchased for someone else, only to find
it doesn’t actually work.
We have an informal but long-standing competition with one couple we
know to bring back the cheesiest souvenir for each other from whatever
country either of us goes to. In this
case, we brought back a small and very
cheap and nasty souvenir cuckoo clock
purchased from a tacky tourist shop at
a famous beer hall in Munich.
This is ostensibly a miniature representation of one of the many cathedrals
dotted around southern Germany that
boast a “glockenspiel”, a mechanical
automaton-style display built into the
clock tower that comes to life on the
hour, every hour and performs sometimes-complex routines in time with
pealing and tolling bells.
We saw quite a few of these displays
from tourist-packed town squares, but
none we saw resembled this souvenir
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version, which includes a tiny, watchsized working clock movement and
a pendulum underneath that swings
back and forward – or at least, is supposed to.
It all looked fine from the outside,
but when I opened the flimsy cardboard box and inserted the two hearing-aid style batteries that came with
it, nothing much happened.
The second hand did advance as expected and the clock ticked away as
cheap movements often do, but after 10
minutes, the hour and minute hands
hadn’t moved at all and the pendulum stayed stubbornly on one side, no
matter how much I helped it to swing.
We couldn’t give this thing away
like it was; no matter how cheap and
cheesy it is, it should at least work. I
had to try to get it going.
But how can one rationalise spending any real time on fixing a $10 trinket? The Serviceman’s Curse strikes
again, of course!
Delving into the clock
Working on it was a bit of a challenge because it is small and oddlyshaped and there is no flat face at the
front on which to lie it down, so I sat
it on a sponge.
The back half is just a plastic frame
but the main body of it is sculpted,
painted plaster with tiny figures inside it, making it relatively fragile. So
I'd have to be careful handling it during the repair.
There are four small neodymium
magnets set into the rear moulding to
hold it to a fridge. These are mounted
Australia’s electronics magazine
on the rear corners of the plastic housing. Inside this plastic frame, I could
see the clear plastic case of the actual
clock mechanism, a very typical cheap
movement likely manufactured by the
millions in some Chinese factory.
Getting to it meant breaking the glue
holding the magnet housing to the
plaster body and this was achieved
with the aid of a craft-knife blade and
a little force. With that housing out of
the way, I had access to the four tiny
screws that held the clock movement
together.
The time-adjusting handle stuck out
from the back of this housing and for
those wondering, I’d already played
around with that in order to get the
hands moving.
While I could manipulate the hands
with the adjuster, they wouldn’t move
under their own steam. It is one of
those systems where you pull on the
adjuster to engage it and twist it either way to move the hands forward
or back, to the correct time.
My thinking was that perhaps the
adjustment mechanism wasn’t clearing the gears when pushed back in and
thus preventing them from moving. No
such luck; even after twiddling the adjuster through the entire range, there
was no hand movement at all. The second hand still ticked away happily but
the time never advanced.
As I had to remove the plastic frame
first, and this housed the pendulum assembly, I decided to check that next.
The pendulum appeared to be moved
by some type of electromagnetic system, an elaborate set-up for such a
cheap device.
The pendulum is simply a painted,
heart-shaped plaster weight moulded
to a short length of silver wire, pivoting at the very top of the plastic frame
and running through a plastic “C” core
which must house coils of wire used
to create the alternating magnetic field.
The problem was that the pendulum
was very stiff, so it stayed where it was
no matter where in the stroke I put it.
I soon saw the problem; the injectionmoulded plastic ‘bearing’ the pendulum pivoted on had come out of its
housing and was sitting slightly askew.
I tried to pop it back in, but it kept
falling back into the misaligned position. I used a bit of pressure to spread
the plastic housing apart and removed
the pendulum assembly entirely from
its mounts and had a closer look at
the pivots.
December 2018 59
Either it hadn’t been made properly
during manufacture, or it had suffered
a catastrophic event in transit, because
one of the tiny pivot pins had mashed
to one side and when I attempted to
straighten it, it broke off completely.
Excellent! This plastic pin looked to
be about half a millimetre in diameter
and about 1.5mm long, so replacing it
would be tricky.
However, I’ve worked on smaller
stuff before, so it was out with the microscope and dad’s old box of teenyweeny drills. I was fortunate to inherit
these drills and blanks when dad broke
down his workshop.
Repairs in miniature
He’d sourced them when he was
making miniature jet engines for model aircraft, using modified car turbochargers for impellers because the
bearings could cope with the expected
100,000 RPM shaft speeds.
He’d needed to make tiny fuel tubes,
mostly from (if memory serves) 1-2mm
diameter brass or copper pipes, which I
think he also made. He’d needed these
drills to bore a series of holes along the
sides of the tube; a tricky task for any
engineer, but he managed to do it.
As different sized holes would
change the engine’s performance, he
drilled many holes in many tubes and
did a lot of experimenting. He’d needed many different-sized drills for this
task and had kept a lot of the blanks
from having the drills made.
These drills were really tiny, some
so small you couldn’t even make out
the flutes until you got them under
a good magnifying glass. They make
my Jaycar set of PCB drills look like
monsters!
I broke out my micrometer and
found one the same diameter as the
remaining plastic pivot pin (0.45mm
diameter) and after trimming off the
remainder of the old, damaged pin
and squaring off the surface with a
craft knife, I used a pin vice with my
smallest chuck to manually drill the
hole where the old pin was.
After going into the plastic block as
far as I dared (probably only a couple of
millimetres), I simply cut the drill off
using a pair of old side-cutters, forming
a new pivot pin. I used a Dremel and
a small cutting disc to very carefully
round off the sharp end of the cut drill,
barely touching it to avoid heating it.
When done, I re-assembled the pendulum into the housing and tried it; it
60
Silicon Chip
now sat square and freely moved back
and forth. Hopefully, the clock mechanism would be as easily fixed.
Onto the next job
I removed the four tiny screws that
held the back of the clock on and it
came off with the adjuster handle
mounted in it. A simple spring arrangement holds the adjuster clear of
the clock’s gears until pulled out to
move the hands. As mentioned, while
the hands do move when adjusted using this method, they just won’t move
any other way.
My guess is there must be something
not making proper contact somewhere
in the movement’s gearbox; a gear must
have slipped out of position or something like that.
The clock movement is a simple
quartz type, with a tiny stepper motor
and a small gear train that moves the
hands. The gears appear to be injection-moulded Nylon, and reasonably
well-made; that is, they are clean and
clearly defined, unlike many cheap
injection-moulded parts.
Individually, they all seem to move
without binding, as demonstrated by
being able to adjust the hands manually, but the problem of why the hands
didn’t move became evident when I
dug in further.
One gear near the start of the train
had several teeth missing, perhaps
faulty from manufacture or more likely eaten off due to the clock running
with the hands stuck or the adjuster
preventing gear movement.
When I advanced the gear to where
there were some teeth, the hands
moved as expected, but soon stopped
again when the gear came around again.
This was the worst-case scenario, as
while I have a parts bin full of gears
and small cogs recovered from old
clocks, printers, scanners, video recorders and various other contraptions
over the years, I had nothing remotely
like this gear in there. To repair this
clock, I’d either need another suitable
clock mechanism to replace this one,
or a 3D printer and a plan of the gear;
none of which I have.
I hate being beaten by anything, let
alone something as seemingly insignificant as this but it happens all the time,
at least in my serviceman’s world; perhaps I should have paid more attention at school.
There are always jobs where I discover there are no circuits or parts
Australia’s electronics magazine
available, or the manufacturer has intentionally obfuscated components,
making them next-to-impossible to
identify and replace, yet every time
it happens it is still a bitter pill to
swallow.
There is nothing worse than a run
of jobs that don’t have positive outcomes, and it transpires that this one
will stay broken as well. It’s a shame
that after all this we can’t give it to our
friends, so after gluing it back together, it now hangs on our fridge. We had
to give them another cheesy souvenir
that we had (luckily) also purchased
when overseas.
At least the clock sounds like it is
working and the pendulum goes back
and forth. That is a fix that I am quite
proud of. I’ll take the win no matter
how ridiculous it was to do it.
Even though the clock doesn’t work,
at least it shows the correct time twice
a day!
Military computer repair
These days, if you have a problem
with your computer hardware, there
are all sorts of diagnostic tools to help
you figure out what is wrong.
That wasn’t true back in the 70s
though; most computers were too expensive and specialised. G. C., of Briar
Hill, worked for the Australian Army
when he ran into the dreaded intermittent fault with a computer they were
evaluating...
In the late 1960s, the Australian
Army was investigating the possibility
of using a computer system to quickly
and accurately calculate the angles required to aim artillery guns.
A “paper evaluation” concluded
that a British Army computer had features more suitable for the Australian
Army than those of a similar computer
used by the American Army.
So an arrangement was made for one
of the British computers to be evaluated by the Australian Army.
Rather than sending out a British
Army technician to look after the computer while it was in Australia, it was
cheaper to send an Australian Army
technician to England, to be trained
on the equipment.
I believe the arrangement was between the Australian Government and
the manufacturer, Elliott Automation;
the system that came to Australia didn’t
belong to the British Army.
In 1969, I was selected to go to England to do the three-month course on
siliconchip.com.au
the maintenance of the Field Artillery
Computer Equipment (FACE) at the
British Army’s School of Electrical
and Mechanical Engineering (SEME).
The equipment, along with diagnostic equipment and many spare parts,
arrived in Australia in 1970. I then
became intimately associated with
the system, working with it for more
than a year.
The system comprised six major
pieces with many interconnecting
cables. These pieces were: the operator’s console, the computer, a program
loading unit, a teleprinter, a DC-to-AC
inverter (to power the commercial
teleprinter) and a power distribution
module.
Due to the short length of one specific cable, the computer was mounted
upside-down on the trolley which was
built to hold the lot.
A team of Australian Army Artillery personnel had been trained in
the use of the system and it was then
taken all around Australia, to various
Artillery units, to show it off and to
have its usefulness evaluated. I went
along with the system, to make sure it
kept working.
It worked flawlessly for about six
months, then it developed an intermittent fault.
The fault showed up as an error code
displayed on the console and the code
(9000 from memory) indicated that it
was a fault in the computer, but not
what the fault was.
The computer was an Elliott 920B,
which was a lighter weight but ruggedised version of their 920A computer.
This was used, among other purposes,
to control traffic lights.
As I had been trained on the test
equipment, I figured that I could easily find the fault. The main piece of
diagnostic equipment was the computer test set.
All I had to do was undo some of the
cables going to the computer module,
connect other cables to the computer
test set and start the test.
A slight hiccup: some of the points
the test set needed to monitor didn’t
appear on any of the pins of any of the
external sockets of the computer, so it
had to be opened up and two smaller
cables then connected to the internal
points. Simple, except that there was
the main cover to be removed then an
internal electromagnetic shield.
The cover was no problem, only
20 large screws to undo. The shield,
though, had 64 screws holding it in
place. And this was in the days before
we had electric screwdrivers. It took
about half an hour just to get the test
set connected.
Once the cover and shield were removed, two printed electronic circuit
(PEC) cards had to be pulled out and
re-installed using extender PECs. The
two smaller cables were then connected to sockets on the extender PECs.
The testing with the computer test
set was all logical; it tested computer
functions (circuits), in a specific order,
and then used the tested functions to
extend the testing.
It had many rotary switches and
these had to be switched in specific
sequences. At each step I compared
the results, shown on nixie tubes, to
values in a table in the repair manual.
The complete test took about an hour.
The first time I did this test to find
what the 9000 error code was actually about, the test set indicated that
no fault was found. I reckon that I repeated the test about six times and it
didn’t find any problems.
I disconnected the test set, put the
shield and cover back on and re-connected the system. Everything worked
correctly; no error code appeared on
the console.
The system worked for another
month or so, then it did it again. I
repeated the test and still, no fault
showed up. This happened once or
twice again and each time, some sequence in the testing seemed to clear
the fault before it could be detected.
Then the fault started to occur more
regularly and I was getting a “bit of
stick” from the operators for not being able to fix the equipment.
I was beginning to think it was a heat
related problem, and that by opening
the computer up, the cooling cured
the problem. To prove this, when the
error code next appeared, I closed the
system down and left it overnight to
cool down.
The photo above shows the teleprinter at left and operator’s console being used, with a labelled diagram at right. This
computer used a ferrite core system for memory with a total capacity of 147,456-bits. Refer back to the article in Silicon
Chip, March 2014, for an explanation of core memory (siliconchip.com.au/Article/6937).
siliconchip.com.au
Australia’s electronics magazine
December 2018 61
The Field Artillery Computer Equipment,
with the Elliott 920B in the foreground.
The next morning, the error code
showed up immediately the system
was switched on. Only running the test
sequence cleared the problem.
So, I tried to overheat the system to
get the unit to fail completely. With
the computer opened and the test set
hooked up, I had a vertical bank of
two-bar electric radiators pouring heat
into the computer; still, it didn’t miss
a beat on the test set.
Finally, the error stayed and going
through the test sequences with the
test set didn’t cure it. But worse, the
test set didn’t identify what the problem was.
I got permission from the Australian
agents of Elliott Automation to contact
their head office, in Britain, directly.
The quickest way to make contact, in
1970, was to use the Defence messaging system. This was a teletype system.
Elliott Automation had a British
Army message centre on their premises, so I could compose a message directly to them.
I would write out what the problem
was and what I had done and submit
the message to an Australian Army
message centre. They typed it up on
their teletype system and sent it over
the submarine cable to Britain.
Due to the time difference, I usu-
ally had an answer back when I got to
work the next day. This was kept up
for about a week, with their engineer
telling me what to try next.
I’d write up the results I’d found in
another message before leaving work
for the day and have a reply by the next
morning. Most of their suggestions involved exchanging various PECs in the
computer with a spare.
The people at Elliott Automation
must have sensed that this slight problem may be about to put the kybosh
on the sale of the FACE systems to the
Australian Army.
The engineer asked me, by message,
did I have a home telephone that he
could call me on? No, I didn’t, and the
Army unit where I worked had closed
for the day by the time the engineer
was at work in England, so I couldn’t
stay back to talk to him. What I did
have, though, were parents-in-law
who had a home telephone.
I arranged for the engineer to call
their number at about 8:00pm Australian time and I’d be there to talk to
him. This we did for about three days
and nothing he could think of worked.
“I’m coming out,” he said, and he was
there in Sydney in about three days.
He observed the fault first hand and
stepped through the test procedure,
many times, getting the same result
as I had. The test set was not finding
the fault. His analysis was that it was
a fault in the computer memory. This
was the only item for which a spare
hadn’t been sent out with the system.
The computer memory was a ferrite core system, with 147,456 ferrite
doughnuts being the storage medium.
Its capacity was 8192 18-bit “words”.
The engineer then brought out the
“big gun” from his luggage, a computer programming keyboard. We
hooked it up directly to the computer;
the keyboard had its own display. Because I had been taught the computer
“language”, its instruction set, on the
course that I had attended, he told me
to write a program to test each bit of
each word of the memory.
So, I tried writing all 1s to each bit
Westminster chime clock repair
Do you have any good servicing stories that you would like to share in The Serviceman column? If so, why not send those stories in to us?
We pay for all contributions published but please note that your material must
be original. Send your contribution by email to: editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
J. H., of Nathan, Qld, ran into his
own clock problems, with a custom
part being faulty. However, his story
turned out better than expected...
As children growing up in the 40s,
both my wife and I lived in households
which had a Westminster chimes mantle clock. So as a special gift for my
wife’s birthday I presented her with a
Napoleon’s Hat Westminster Chimes
clock. The clock has given wonderful
performances for twenty years. The
quartz movement gains so little time
that the clock does not need resetting
between battery changes.
However, just recently, the clock
lost its chime function and because of
the sentimental value attached to this
clock, I thought I should try to repair it.
The clock consists of two sections
– the quartz movement powered by
a 1.5V alkaline cell and the chimes
section, independently powered by
Australia’s electronics magazine
siliconchip.com.au
Servicing Stories Wanted
62
and reading the bit back straight away.
All good. Then I tried all 0s, still good.
Then he suggested a chequer-board
pattern, writing “10101...” (18 bits) to a
location and test it straight away, then,
if good, write “01010...” to the same
location, read it back and, if good, go
on to the next location.
Well, that did it! Finally, the fault
showed up as one bit that didn’t
change to the appropriate magnetic
state when it was being programmed.
The fast changing of the magnetic
state of that one ferrite core with the
chequer-board program identified the
problem. The computer test set didn’t
perform such a test.
A hasty message was sent back to
Elliott Automation and a new memory unit was dispatched and it was in
Sydney within a week. “These memory units never fail, that’s why there
was no spare sent out with the equipment,” the engineer told me, “they are
ultra-reliable.”
They were also very expensive. The
cost of all the other spare parts sent
with the computer was insignificant
as compared to the cost of one ferrite
core memory unit.
The evaluation of the FACE system
continued, once the new memory unit
was installed, and the Army went on
to buy many of these systems.
A representative of Elliott Automation told me later that the ferrite core
in the memory unit that failed had a
microscopic crack through it.
Silicon Chip
two 1.5V alkaline cells in series. Two
wires run from the movement to the
chimes section and, on the hour, the
movement shorts these two wires
which then triggers the chimes section to start the hourly chiming and
tolling sequence.
The faulty chimes unit consists of
an epoxy-encapsulated IC about the
size of a 10¢ coin which drives a tiny
4cm speaker.
The speaker tested OK but there was
no way that the epoxy covered IC could
be repaired. An internet search for a
possible replacement revealed that
they cost about $US30, with about as
much again for postage.
One clock company in the USA had
a replacement for about $US8 but the
postage was a secret. I emailed them
three times for the total cost including postage but never once received
a reply.
Determined not to be beaten, I had to
fall back on my own resources to effect
a repair. Surely, I thought, it wouldn’t
be too hard to get a microprocessor to
play the simple Westminster Chimes
tune and then add the appropriate
number of tolls. There are only four
or five notes involved.
I had some older mark 1 Micromites
on hand so I used one of the pulse
width modulation (PWM) outputs to
generate the required frequencies and
experimented with the duration and
pausing between notes until I had a
respectable melody.
I used the two wires from the movement signalling the hour to wake the
microprocessor from sleep mode,
whereupon it would play the chime
and toll and then go back to sleep. For
good battery life, not only did I use
sleep mode but I also set the CPU to
run at its slowest possible speed. Also,
I set the chimes to cease at 10pm and
resume at 7am – as much as I like a
chiming clock, the friendship ceases
at 10pm.
The new circuit was able to fit (just)
into the space vacated by the original IC and as I assembled the clock, I
thought I had solved the problem. But
it was not to be. After a few hours listening to the chimes, I realised they
weren’t Westminster chimes at all!
Where were the bells? The square wave
PWM output was just so mechanical
and un-musical.
Well, I thought, maybe I could make
the sound more interesting by adding
a second PWM channel with a note
siliconchip.com.au
separation of about 8Hz from the first
to create a vibrato effect on the note.
This did make the sound more interesting but it still sounded like the Westminster Chimes played on bagpipes!
So I put the clock back together
again with its bagpipe sound but I
knew this wasn’t the end. Maybe I
would get a reply on that unit from
the USA?
It was sometime later that I came
across the DFPlayer Mini. This device is a 16-pin miniature MP3 player
module measuring about 20 x 20mm.
With its own 3W audio output stage, it
can be configured to play MP3 tracks
stored on a microSD card either by a set
of momentary contact switches or by
commands sent from a microcontroller via a serial port (see the El Cheapo
Modules article on page 74 for details
on this module).
I had already seen websites from
which the full set of Westminster
chimes could be downloaded in MP3
format. I had played some of these on
my computer and they sounded impressive. So here was the solution to
my problem. A ménage à trois of the
DFPlayer, a set of MP3 chimes on an
SD card and a Micromite.
It took four weeks for the DFPlayer
Mini to arrive from China but in that
time, I was able to build a circuit on
Veroboard, ready for the module to be
dropped in.
I also prepared and tested a suitable
program for the Micromite. The original clock only chimed on the hour
but not on the half or quarter hours.
As mentioned previously, the hourly
chime was synchronised by the two
leads from the clock being shorted
together.
But now that I had a full set of
chimes, I decided to make my program
Australia’s electronics magazine
incorporate the half and quarter hour
chimes also.
The hour chime is fully synchronised to the quartz clock but the half
and quarter chimes would have to rely
on the Micromite’s internal clock. As
the Micromite’s internal clock is not
very accurate over the long term, it is
reset by the program to correct time
on the hour as determined by the
quartz clock.
The DFPlayer finally arrived and all
was ready to go when disaster struck!
As I was unsoldering the previous set
of leads from the clock’s tiny loudspeaker, to connect it to the DFPlayer
outputs, the loudspeaker’s terminal
connection pad completely separated
from the frame.
A quick examination of the fine
leads going to the loudspeakers coil
verified that repair would be impossible. I had some small 6cm speakers
salvaged from old computers but they
were too big for the allocated space in
the clock. So to test the new chimes
circuit, I pressed into service a larger
12cm speaker. This speaker is the type
usually seen in a car’s audio system on
the rear parcel shelf.
And what a surprise – with this new
bigger and better speaker the clock
sounded like Big Ben itself! It wasn’t
a disaster after all. I decided to mount
the speaker on the rear of the clock – it
just fitted neatly but I would now have
to remove it every time the clock’s battery needed changing.
Also, the power requirements meant
that the chimes could no longer be
powered from a 3V battery source. I
had to use a 5V plugpack supply instead. But this was a small price to pay
for such a fantastic outcome. Gone are
the tinny sounding chimes and gone is
the bagpipe wielding Scotsman. SC
December 2018 63
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