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SERVICEMAN'S LOG
Valve repairs are not for the inexperienced
The internet and YouTube are wonderful
sources of information for just about any
task but the ease of obtaining information
does not mean that you can fix the latest
Mercedes sedan or an old valve amplifier,
for that matter. Just because it looks easy
on YouTube does not make you a competent
serviceman.
Painting is one of those things that
most people think is as easy to do as
changing a light bulb or hanging a picture; anyone can do it. I don’t mean
painting as in creating the Mona Lisa
or Girl with a Pearl Earring, which requires a skill set very few people can
ever master.
I mean painting as in covering the
roof or walls of your house with paint.
The general consensus seems to be that
anyone with at least one working arm
and a pulse can paint a house.
However, they would be quite
wrong. Like anything, painting takes
knowledge, experience and skill to
siliconchip.com.au
pull off properly. To illustrate this,
here’s how a recent conversation between me and the paint-shop guy
went:
Me: I’d like to buy some paint please.
PSG: And what paint would Sir be
looking to buy today?
Me: Duck-Egg Blue please.
PSG: Would Sir be requiring oil or
water-based acrylic, latex or enamel
Duck-Egg Blue paint?
Me: Um...
And there’s the kicker; while anyone can wield a paint brush, only those
with the knowledge and experience
to have the right preparation, paint,
Australia’s electronics magazine
Dave Thompson*
Items Covered This Month
•
•
•
Repairing valve amplifiers
A problem safety switch
Neff oven repair
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
methodology and the skill to apply
it will get a decent result. The servicing industry is no different; many of
us will give fixing anything a go before admitting defeat and calling in a
professional.
I get the impression that many blokes
would do their own brain surgery, as
long as there was a video on YouTube
showing how to do it and someone to
hold the torch and mirror for them.
I once had a guy call me, asking
whether I could sell him a boot disk.
When I pressed him for more information, he said his computer wouldn’t
start up. He had an on-screen message
telling him to insert a boot disk, hence
the call asking if I could sell him one.
As politely as I could, I informed
him that even if he did have a boot
disk, it is doubtful he could get his
computer going as he’d have to know
what to do once he’d inserted it.
His reply was classic and one that
I bet a few computer-repair people
have heard: “If I come and get the
disk, could I call you back when I get
home and you can walk me through
what to do next?”
Well, no. When I first heard someone
suggest I walk them through repairing
their computer over the phone, I was
very polite in my response.
Yet as this became a more common
occurrence, I began turning it around
and asking people if they thought calling a mechanic and asking them to be
walked through repairing their car engine or calling an electrician to walk
them through fixing a dead circuit was
acceptable.
July 2018 43
When they inevitably answered
no, I then ask them why they think it
is OK to ask that of me. Most get all
bent out of shape and tell me that all
I have to do is push a couple of buttons anyway, so why would they bring
their computer in when I could simply
tell them what to do instead over the
phone. Some offer to pay; most don’t.
I point out that this is what I do for
a living, and that if I fixed everyone’s
computer this way I’d be broke, but
this doesn’t seem to wash as a valid
argument.
Typically, they either hang up or derisively inform me that they could find
out on the internet anyway, so I might
as well tell them now. At this point I
usually wish them good luck, sign off
and let them get on with it.
I coined a name for this type of person: a WOTAM, for Waste of Time and
Money. There’s also WOFTAM, for the
really annoying caller.
Historically, we ANZACs especially
are known for our genetic disposition
for DIY culture and I heartily applaud
us doing it ourselves, however most of
us have the wisdom and good sense
to draw the line when we are looking
like we are getting out of our depth.
Years ago, when my motorbike engine was in bits on the floor of my flat
and I wasn’t able to put it back together properly, I hired an engine guy to
help me with it.
When the power line coming into
our just-bought house from the street
44
Silicon Chip
started arcing, smoking and stinking
of burnt insulation, I was straight on
the phone to the power company before you can say CPR. I wonder how
many guys would just break out the
aluminium ladder and have a go at it.
The Darwin awards website is full
of stories of people who didn’t have
that common sense or if they did, they
chose to ignore it, eventually ending
up on an ever-growing list of headshaking anecdotes.
I mention this because recently I had
an old valve amplifier in the workshop
that someone had already had a go at
repairing and as in a lot of cases like
this, instead of helping, it made things
worse. Most people seem to know
somebody who is “good with computers’ and so naturally they farm all
their computer work out to this person.
In a similar vein, many of us know
somebody who is “good with mechanical or electrical things” in general, so
anything broken inevitably gets put
this person’s way for them to repair.
It is only if they can’t that the “professional” is commissioned to have
a look at it.
While this way of going about things
can be attributed to our DIY culture,
my guess is that it is more a case of
economics; getting stuff repaired costs
money, and sometimes a lot of money.
Call a plumber out on a Saturday
night to retrieve a stuffed toy from your
overflowing toilet bowl and you can
spend a week’s wages on it.
Australia’s electronics magazine
Calling a white-ware serviceman
out to discover why your fancy, justout-of-warranty washing machine is
throwing up an E09 error could mean
the kids going without new gym shoes
this term.
I get it; if we can get something fixed
cheaper, then we’re all for it. Unfortunately, as the old saying goes, we usually get what we pay for.
Repairing a non-working valve amplifier has a few “gotchas” for those
who don’t usually deal with tube gear.
For one, not many of today’s tinkerers
are familiar with valves and how they
work and two, these amps can kill you;
typically many times over.
While we all expect mains-level
voltages to be present in that vacuum
cleaner or toaster oven we have on the
work bench, we can add sometimes
200V or more to that floating around
valve amplifiers and that’s a funeral
waiting to happen. If one isn’t particularly wary of the potential danger, one
will almost certainly get bitten.
Then you get the type of hobbyist
who gets given an old valve amplifier or mantle radio to “have a look at”
and the first thing he does is plug it
in and try it out. Even before the fire
department has finished dampening
down the hot spots, he’s figured out
he probably should have checked it
over before turning it on.
Another problem is spare parts; it
isn’t like the “old days” when you
could go down to the corner store
with a bag of valves, plug them into
the tester and choose a new one from
the spares on the shelf when the go/
no go gauge told you your valve was
“weak” or “gassy”.
While good quality tubes are still
available, unless you are the member
of an antique radio club with access
to personal stocks or discounts, or
scored yourself a truckload of useful
NOS (New, Old Stock) valves cheap on
an auction site, you are probably going to get robbed by savvy, tube-selling vendors. Or you will buy a newly-manufactured, Chinese or Eastern
Bloc-made valve that may be excellent, mediocre or terrible, depending
on the individual tube.
Compared to say, the 1950s, practically nobody makes valves any more.
Fortunately for tube enthusiasts, the
relatively sudden advent of the transistor resulted in literally warehouses stacked full of now-unwanted and
unsold valves.
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Eventually, these found their way
into the hands of either recyclers or
people with enough vision to realise
they needed to be saved for future requirements. Sadly, many were lost to
landfills, but enough were saved to
keep the likes of amplifier manufacturers and tube enthusiasts in valves
for years to come.
Obviously, as this limited NOS
stockpile dwindles, the harder it becomes to obtain certain types of valves,
which pushes up the cost.
Matched-pairs of well-known audio
output valves can command eye-watering prices these days. You’d think
those very few valve manufacturers
still churning out tubes today would
fill this particular vacuum, ka-boom!
But sadly, the handful of factories
based in former Soviet republics and
China who still make valves don’t
make them with the same level of love
and attention that the likes of RCA,
Sylvania, Mullard or Philips made
them with back in the day.
Those well-known companies produced valves the old-fashioned way,
in huge factories using thousands of
skilled workers whose entire careers
consisted of making parts for, or assembling, valves.
Glassblowers, wire-makers, machinists, engineers, metallurgists, chemists, assemblers, fabricators and a myriad of other professionals depended on
the valve market to earn their crust. I’ll
bet the advent of the transistor didn’t
please everyone!
The majority of today’s tubes are
made on highly mechanised production lines with minimal human interaction, so modern valves are often
viewed with great mistrust and even
disdain by tube aficionados.
Repairing any valve device means
having access to replacement valves.
One can usually fudge one’s way
through a solid-state device repair using various other transistor or module types; doing this in an equivalent valve-powered device can be a
bit trickier.
And many of the peripheral components, such as bypass capacitors and
plate resistors, were chosen for a very
specific valve; simply plugging in another one that happens to fit the empty
socket is a recipe for disaster.
In the same way we used transistor
substitution books to find an equivalent transistor for one that has a weird
number (or no number at all), techsiliconchip.com.au
nicians of yesteryear relied on telephone-book-thick manuals for valve
substitutions.
You could cross-refer different
valves to see if a 12AX7 could be used
instead of the ECC83 specified in the
schematic (in this case you can; they’re
the same valve).
Most books also offered possible
equivalents, along with tweaks you’d
have to make to the circuitry in order
to use the suggested alternative.
If all else failed, you could look up
the tube’s specs and match it with
another candidate; as long as power
curves, plate and grid voltages and
current, amplification factor, mutual
conductance and a host of other values corresponded, or these could be
achieved with circuit tweaks, you were
good to go. Generally speaking, if the
book said it would work, it would.
This level of certainty was down to
the consistency of valves produced
back then. The same doesn’t hold true
today, where automated manufacturing creates differences between valves
even from the same production lot.
As these differences became more
of a problem, circuit design evolved
to cope, with the likes of variable biasing and adjustable feedback loops
incorporated in an effort to ‘balance’
performance.
A novice serviceman might get
caught out after replacing valves and
neglect to adjust biasing, which could
at best result in a bad-sounding amAustralia’s electronics magazine
plifier and at worst, result in output
transformer or tube failure. There are
a few traps for young players then,
but by far the biggest trap is the lethal
voltages present in most valve amplifiers and radios.
Even battery-powered devices have
the potential to hurt the unwary. Informal workshop rules were imposed
to keep people safe; putting one hand
in a pocket while working on a live
chassis meant it was less likely the
serviceman would get a shock through
the chest and across the heart, which
is potentially fatal.
One sore hand or arm from a highvoltage belt is God’s way of telling you
to be more careful!
Another rule is to avoid wearing
rings or other jewellery that could
short out something inside the case.
Gold chains around the neck are a really big no-no! Yet another rule advises
no fiddling with live hardware while
chemically altered, on the phone or
otherwise distracted. My own mantra
is that I suspect that every valve amp
is constantly trying to kill me. This
usually keeps me alert.
This amp in question is a 1970s
Fountain; a 10W, push-pull stereo
amplifier made in New Zealand using
common valves. However, it had been
sitting unused for a long time and the
“repair guy” had simply plugged it in
and turned it on to see if it would work.
It did, as a smoke generator! He pulled
the power as soon as he saw smoke
July 2018 45
but the damage had been done. Time
to call the professionals!
After removing the case and giving
the chassis a puff with compressed
air, I noted several power-supply capacitors were blackened - possibly the
source of the smoke. Capacitors “drying out” or otherwise degrading when
not being used are a major cause of
hardware failure, valve or solid-state.
While old caps can sometimes be
electrically recovered (see the Capacitor Reformer project in the August & September 2010 issues; www.
siliconchip.com.au/Series/10), I make
a practice of changing them on older
amps as a matter of course, especially the power smoothing and output
coupling capacitors. They are (usually) relatively cheap, readily available and easy to replace, so it makes
sense to do it.
With the caps replaced, I removed
the valves and plugged the amplifier in
to my light-load and auto-transformer,
gradually increasing the AC voltage.
No bright lights or smoke, so with supply input at 230VAC, I measured voltages at the usual points. While I had
a typical 6-ish volts AC for filaments,
I had only a fraction of the hundreds
of volts I expected on the plate pins
of the valve sockets.
Tracking back, I could see the power
supply’s transformer fed several carbon composition series dropping resistors adjusting voltage for each stage
of the amplifier, with the resistors bypassed to ground by now-replaced
dead capacitors. Though the resistors
looked OK, I suspected some might
have gone open-circuit.
I shut everything down and replaced
them all with new, 2W alternatives
from my parts boxes.
The valves, an ECC83, two EF86s and
four ECL86s, tested OK on my Valve
Heaven DIY tube tester (siliconchip.
com.au/link/aak5), and after plugging
them all back in and powering up,
a faint but gratifying hum gradually
sounded from my test speakers.
A signal injector clipped to each
input now confirmed everything else
worked as expected. The pots and
switches required a squirt of cleaner and a bit of working to settle them
down but once done we were up and
running and sounding great. Job done.
Tripping the RCD
A. L. S., of Turramurra, NSW, previously wrote of a problem with one of
the safety switches (RCDs) in his home.
He had to tackle another similar fault
about a year ago but this time, it had
a different cause...
There are two safety switches in
my household wiring and the repair
of the first one, which protected half
the power outlets in my house, was
described in Serviceman’s Log in the
October 2016 issue.
Imagine my surprise when the second one, which protects the front part
of my house, started to do the same
thing and cut out intermittently for
no apparent reason!
After the previous adventure, the first
thing I checked was the RCD itself but
it seemed perfectly fine and tripped exactly as it was supposed to with a leakage of 30mA (as confirmed with an RCD
tester). It was also cold to the touch so
I discounted it as being the culprit for
the time being. I would have to think
a little harder to figure out this one.
The RCD seemed to trip and cut the
power when I was in the downstairs
workshop which has many mainspowered test instruments, chargers,
powerpacks, computers, an air conditioner and even a freezer.
The first time it cut out I didn’t take
too much notice what was actually
plugged in and switched on but as a
precaution, I turned off all the power
outlets except for the freezer.
Returning to the workshop, I began
to turn things on one by one hoping it
would isolate the offending item but
it didn’t trip again. So I thought maybe the freezer was the problem and
it would only trip the RCD when the
thermostat cut its compressor back in.
So I waited patiently for its motor to
come on but when it did, still nothing happened.
Do you have any good servicing stories that you would like to share in The Serviceman column? If so, why not send those stories in to us?
We pay for all contributions published but please note that your material must
be original. Send your contribution by email to: editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
I put it down to a possible surge or
overvoltage and carried on regardless.
Then one day, I switched on my Audio Precision ATS-1 audio analyser to
do some tests on a subwoofer amplifier and the safety switch cut out about
five minutes later. Repeating the exercise, the same thing happened, so the
instrument was quarantined for later
investigation!
All went well for about a week but
then, 10 minutes after I switched on
my oscilloscope, the circuit cut out
again. I couldn’t believe it! Surely two
instruments which were normally very
reliable couldn’t go south at the same
time. I checked them both for possible earth leakage which could trip the
RCD but they seemed OK.
What I did notice that both instruments were plugged into the same
power board. This is a supposedly
good quality Jackson model PT8888
made in China and boasts EMI/RFI
filtering, surge protection and overload cut-out. It has eight outlets, two
of which are widely separated to fit
large plugpacks.
It is made of very strong metal and
was expensive when purchased from
a reputable electronics retailer. Fearing the culprit may be one of the eight
devices plugged in, I powered them on
one-by-one to see if the safety switch
would cut out but again, nothing happened.
Then one day, switching on another instrument, it tripped the RCD off
once again. This was another different
ATS-1 analyser which at first made me
think there may be a design flaw with
them but it was also plugged into the
Australia’s electronics magazine
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Servicing Stories Wanted
46
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Jackson power board. So I switched
off everything connected to the power
board and I also switched the power
board off, both at the wall and via its
onboard power switch.
Having quarantined everything on
that power board, the circuit was fine
for the next week. I then decided to
have another look at why those items
connected to that power board were
triggering the RCD.
I had to do it during the day when
everyone was at work because the TV
was on the same circuit and my family members complained loudly and
bitterly every time I cut the power during their favourite programs.
I started by plugging the Jackson
board back in and then plugging each
of the eight items in, one by one. After
a while, the safety switch cut out. Making this more difficult to diagnose was
the 5-15 minute delay between adding
a device and the power cut.
At this point, I tried switching the
board on and off with its own onboard
switch. At one stage, I had nothing
plugged in at all and upon switching
the board on, the RCD politely cut out
and therefore identified the Jackson
board to be the culprit at last!
The board looked very professional
but on closer inspections, had dubious approval markings and even had
a strange warning which read “AS/
NZS TESTING NOTE This device contains voltage limiting devices, test at
250V only”.
A continuity check indicated 409kW
between Active and Earth which was
suspect because any varistors it used
for surge protection would have a
much lower resistance at full mains
voltage and this would be enough to
leak more than 30mA to Earth.
Normally I would throw such a
board away but it was so expensive
and its metal case was really handy in
the workshop because it was so rugged.
Not only that but I had another one
exactly the same so I wanted to find
out the reason for the failure. I decided that a repair may be possible and
that the result may assist anyone else
who has a problem with this model or
similar models.
My first rather optimistic theory was
that a spider or insect had crawled into
a small gap between the metal panels
and was cooked and carbonized, creating a residual current between Active and Earth.
So I tried to undo the two small
siliconchip.com.au
Neff oven repair
J. B., of Melbourne, Vic, recently
had to delve into the innards of his
oven. What seemed like a simple
light bulb replacement turned into
a complex and technical repair...
I’m a self-taught radio technician
from the 60s and later became a black
and white TV valve jockey, eventually getting into colour TV and tape
recorder servicing.
For a day job, I am an aeronautical and mechanical design engineer
and I’ve retired as an airworthiness
regulator. I now repair aviation headsets and represent a US/UK Company using neural network synthesis
to find intermittent faults in cables,
connectors and chassis.
One day, as my wife and I were
preparing for the evening meal, we
turned on the light in our Neff oven
and it blew with a blinding flash. I
replaced the bulb but the new one
failed almost instantly. On inspection, the filament support wires inside the bulb had touched. This had
caused some kind of internal damage
to the oven so after removing what
was left of the failed bulb, I traced
its wiring to the Operations Module.
This module receives DC power
from a switchmode supply and signals from a switchboard. The Operations Module contains the microprocessor, driver integrated circuits and
numerous relays. The light circuit
had an SMD NTC thermistor in series with the relay coil (just a guess
as the device was a charred blob).
The PCB tracks had also been burnt
beyond recognition.
Whilst there was some separation
between the 230VAC light track and
adjacent low voltage control tracks,
the separation was insufficient for
this failure. The torching thermistor
burnt a PCB track which powered a
suite of relay coils and conducted
230VAC to the driver ICs. I repaired
the PCB and the burnt tracks and
soldered a 10W resistor where the
thermistor used to be.
On reassembly and power application, the oven went berserk; the
door lock mechanism continued to
cycle closed then open, the replacement oven light would go on but not
turn off and the circulating fan in the
heating space accelerated to take off
power and stayed there. So I decided
Australia’s electronics magazine
to pop the module back out and take
some voltage readings.
I found that when the microprocessor outputs went high, a hex Darlington switch with diode protection
turned on but not off. Four days had
passed since the lamp blew and my
wife was getting impatient. Plan B
was a replacement Operations Module; none in Australia, a few in Germany, an estimate of a one month
lead time and some $500.
Upon further investigation, I became more certain that there was
something wrong with the Darlington IC. Replacing one SMD in the
middle of a ‘farm’ was a challenge;
I’m not practised at this but the internet was very helpful.
I removed the immediately adjacent relay and wrapped the remainder of the components and tracks
first in paper and then in aluminium foil, leaving exposed only the
IC to be removed, along with a few
adjacent components. I cautiously
applied a heat gun to the IC and in
seconds, the parts were removed
whilst the masked components remained in place.
This was actually my second attempt as I first practised the technique on a disused board. I then tidied the PCB tracks and fitted the
replacement IC and other parts. The
original relay had a 9V DC coil but I
only had a 12V DC replacement on
hand, so I fitted that and ordered
some 9V relays to swap in later if
necessary. The oven was reassembled, power applied and all functions tested serviceable.
The roast lamb which followed
was delicious and I’ve banked some
brownie points for the future; I focussed on the time difference between repair and overseas supply,
definitely not the money saved!
Carefully measuring and recording
voltage readings in the unserviceable state then comparing these with
values expected from first principles
was the key to figuring this one out.
Impatience and a hasty dismissal of
what seemed to be zero voltage when
in fact there was some small residual
led me down a wrong path.
But most importantly, when replacing the lamp in your oven, make
sure the new one is designed for
high-temperature use.
July 2018 47
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Australia’s electronics magazine
screws underneath to have a quick
look. However, these proved to be of a
triangular design and none of the hundreds of bits in my toolkit would fit.
They were also countersunk so impossible to butcher with a grinder or
hacksaw.
The hardware shop didn’t have anything either but fortunately, the local
Turramurra cobbler (yep, the cobbler!)
was able to grind one up in about two
minutes and we had the back open just
a few minutes later.
Back in the workshop, I took a good
look at the innards. There was a small
PCB which had three varistors, type
14D147K (rated at 275VAC) across
each of the rails and one 100nF mainsrated capacitor. That was about it; so
much for the extravagant claims about
RFI/EMI protection!
It also had an integral 10A circuit
breaker and an onboard neon-lit mains
switch. It was perfectly clean and no
cremated insect or spider could be
seen!
So the PCB had to be removed because all the suspect components were
underneath. This was a real pain because it was held in place by a heap of
big soldered connections to the long
brass outlet rails and to the chassis
mounted switch.
After desoldering everything, the
chassis also had to be bent back 90°
to release the PCB-mounted circuit
breaker. Then I was able to remove
the components one-by-one and check
them for continuity. As luck would
have it, the last varistor I removed
proved to be the faulty one.
While the PCB was bare, I replaced
all three varistors with similar types
and put it all back together then stood
back and switched it on. It has given
no trouble since.
It does bring home the fact that components used for safety can sometimes
fail in strange ways and maybe cause
other problems like arcing or fire. I am
not sure why this one failed; it may
have been shock, vibration or humidity or a mains spike but I can never
be certain.
What is certain is that just about
all “surge protected” powerboards
use exactly the same components so
it’s something to look out for and it is
a good idea to switch power boards
with integral protection or filtering off
and/or unplug them when not in use,
to protect them from lightning damage and so on.
SC
siliconchip.com.au
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