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SERVICEMAN'S LOG
The Serviceman's Curse
I reckon servicemen are cursed. I don’t mean
that people swear at us a lot (though they
might!), I mean that we bear the Curse of the
Serviceman. This means that when anything
breaks down, we always consider the repair
option first. It doesn’t really matter what has
broken or whether we usually repair or service
these things in our day jobs, it’s just that we
simply can’t help ourselves from wanting to fix
something that’s broken.
This is mostly fine if we just have
ourselves and our own household to
think about, but for some, it also means
that when any of our friends, acquaintances or colleagues break something,
we are often expected to fix their stuff
as well, just because we are servicemen! As if being our own go-to repair
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guy isn’t enough. This is what I mean
by a Serviceman’s Curse.
While the more prosperous servicemen among us may have learned
to suppress the curse and are able to
chuck away the broken device and go
out and buy a replacement instead, for
me and many others, that is a difficult
Celebrating 30 Years
Dave Thompson*
Items Covered This Month
•
•
•
•
Car battery charger
CIG Transmig 200 welder
Compaq CQ61 laptop R&R
MR16 LED downlight repair
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
decision to make and we would have
to force ourselves to even consider it.
When something in my household
breaks, my first instinct is to weigh up
all possible options to repair it myself,
with the very last option being to buy
another one. Perhaps if I won big on
the lottery, or inherited a few gazillion
May 2018 63
bucks, this attitude might change – I’d
sure like to test that theory! But in the
meantime, I always consider repair before replacement.
I know plenty of people who think
the other way. They replace anything
that breaks with the latest and greatest new version, regardless of whether
it was repairable or not, but not many
of these people are servicemen. I can’t
really blame them; after all, they don’t
bear the curse!
Of course, there are exceptions; if a
repair isn’t feasible or economically
sensible, such as a dropped dinner
plate or wine glass then the curse
doesn’t really apply. Having said that,
I have been known to glue people’s favourite plates or porcelain figurines
back together. But if the broken article is even remotely within my skillsphere, then the curse awakens.
My neighbour invokes the
curse
A recent example involves a neighbour who tried to start his car the
other day while he still had a battery
charger connected. He subsequently
discovered that the charger no longer
worked.
I’ve done this myself in the past and
perhaps due to dumb luck, I’ve had no
problems, though it stands to reason
that one probably shouldn’t leave anything connected when cranking the
engine unless it’s designed to handle it.
This is especially true if the car battery is dead flat to begin with and we
are essentially relying on the output
of the charger alone to supply enough
grunt to fire up the motor. In such situations, the current draw through the
leads and internal components of the
charger can be considerable, and when
the car starts there is even more current introduced into the circuit by the
alternator’s output.
Many car battery chargers are simply
not designed to withstand this kind of
punishment.
Ordinarily, a guy would just think
the charger was dead, chuck it in the
bin and go out and buy another one
– especially given the current (hah!)
prices of chargers these days. In this
case, the sticky wicket was that my
neighbour had borrowed the charger
from a friend, and while it was by no
means new, it looked to him to be a
reasonably flash model as far as car
battery chargers go. He didn’t relish
the thought of having to cough up to
replace it.
He brought it over to my workshop
in a bit of a panic and asked if I could
have a look at it, at least to see whether
it was repairable. If not, he’d be chowing down on a large crow sandwich
and splashing out for a new charger.
I promised to see what I could do,
mindful of the fact that this would
probably end up being one of those
“pro bono” jobs all servicemen get saddled with and would more than likely
take up time I could ill afford to spare.
That said, I couldn’t refuse a neighbour
in need, especially as it was highly
likely that I could fix the charger. The
Serviceman’s Curse strikes again!
The charger was about as simple as
any electronic device can get. A mains
cable enters the plastic case through a
cheap-but-effective clamping arrangement and connects via a fuse to the
primary of a reasonably heavy-duty
transformer. The secondary is wired
to a small PCB with a glass thermal
cut-off switch, a couple of carelesslyplaced diodes and three LEDs.
Attached to that board are a couple of cables which then exit the case
through a rubberised grommet with
comically-large alligator clips on each
end; one red and one black. He might
have thought it flash but I disagreed;
it was a bog-standard battery charger.
The battery connector cables looked
to me to be a little on the light side,
considering the size of the transformer
and the cables that make up your average set of jumper leads. But I suppose
these modern-style, piddly-thin wires
would have the advantage of being
self-limiting and besides, they’d ordinarily only have to cope with a few
amps at the most for relatively short
periods anyway.
Servicing Stories Wanted
Do you have any good servicing stories that you would like to share in The Serviceman
column? If so, why not send those stories in to us?
We pay for all contributions published but please note that your material must
be original. Send your contribution by email to: editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
64
Silicon Chip
Celebrating 30 Years
The LED indicators were mounted
inside the case but shone to the outside world by way of clear plastic
light tubes.
I’ve seen this method used before,
especially in devices like amplifiers,
radios and laptops and it tends to work
fine for them. But the inside of this
charger gets hot then cools down, over
and over, and this, when combined
with the natural ageing process, causes
the plastic to go opaque.
Because of this, the amount of
light reaching the user would likely
be pretty low. I’d wager these indicators would be barely visible during
the day, especially in bright sunlight.
I’d confirm that theory once I’d fixed
the thing…
Testing the charger
I plugged the charger into my lightbulb based load box and flicked the
box’s socket switch to on. I’ve gotten
into the habit of using this load box,
largely because it is set up on my workbench permanently and this makes
it the handiest power socket for any
mains-powered devices that cross my
desk. It can’t hurt, regardless of whether
I really need it or not.
The neighbour told me he’d plugged
the charger in and got no indication of
power, and with no specific mention
of fuses blowing or circuit-breakers
popping, it was unlikely that a shortcircuit was present. However, the test
rig socket is right there, so I used it.
The load box consists of two 250W
incandescent bulbs (remember them?)
mounted in a couple of lamp sockets
screwed to the top of a suitably-sized,
plastic hobby box.
The lamps are wired in series with
the Active wire and all three mains
wires are then terminated into a standard dual, switched mains socket on the
front of the box. The box is powered
from a wall socket.
I generally power any mains-powered equipment under test into the protected socket on the load box. If there
is an internal short or other, similarlynasty electrical fault present, the lights
glow to let me know while they limit
the voltage applied to the load, giving
me time to switch everything off safely
without the drama of blowing fuses or
the guts of the device under test flying
across the workbench.
I also have an adjustable auto-transformer (generally known as a Variac,
but mine isn’t Variac-branded) and I
siliconchip.com.au
use that for similar jobs, especially
those where it is more prudent to
slowly bring up the voltage than apply it all at once. I mostly use the lightbulb load box for mains-powered stuff
though, especially valve amps and
similar devices.
Both methods save replacing fuses
and reduce the risk of damaging other equipment on the same circuit, and
both are invaluable to the serviceman
who needs to work with mains-powered devices and they are well worth
the effort of building or purchasing.
As expected, the battery charger
did nothing on switch-on. No bright
lights on the load box and nothing
on the front panel of the charger. For
all intents and purposes, it was as if I
hadn’t plugged it in.
Delving into its innards
My first thought was a blown fuse.
There must be one, and while some
chargers have a fuse socket accessible
from the outside, this model didn’t,
so it had to be inside. Getting in was
easy enough, with only four long, PKstyle screws holding the case together
at each corner.
It is refreshing to be able to open up
something without having to resort to
cruder methods of removing those ridiculous and unnecessary “security”
fasteners that seem to be all the rage
these days.
It’s also getting increasingly rare to
find the screws out in the open and easily accessible to normal tools, instead
of being buried inside deep channels
or concealed under rubber feet, plastic bungs or warranty seals.
Once the screws were out, the case
split apart easily and the various components were laid bare. There indeed
was a fuse, in line with the Active lead
and right next to the cable clamp. The
fuse was obviously intact as I could
see it clearly, but I popped it from its
holder and checked it with my meter
anyway.
If it was dead, it wouldn’t be the first
time a fuse appeared undamaged but
was, in fact, open-circuit; a classic beginner’s trap. In this case, though, the
fuse rang out OK. On to the next component in the troubleshooting queue:
the transformer.
This also looked OK but then again,
something would have had to fail catastrophically for it to appear otherwise.
I measured the secondary windings
and got around 0.5W on my analog
siliconchip.com.au
multimeter; probably not that accurate
a reading but at least it had continuity.
When I measured the primary though,
it appeared to be open circuit.
A current surge might have burned
out the windings but I could see no
darkening of the yellow tape they
typically use to bind transformer coils
with and there wasn’t even the faintest
whiff of that distinctive burnt-enamel
smell that almost always goes handin-hand with high-current component
failures. I’d have to dig further.
After making a note of what went
where, I desoldered the transformer’s
wires and removed the four screws going down through the laminations and
holding it to the bottom of the case. I
do like these simple-to-disassemble
devices.
With the tranny out and sitting on
the bench, I re-measured the windings
with another meter just to be thorough
but got the same result; the primary
side was definitely open-circuit. Ordinarily, this is where most servicemen/repairmen would start looking
for a replacement transformer but as
I’ve already made clear, I hate throwing
things away (that curse again).
Anyway, without having any part
numbers or any other information
written on the component, I’d have
to either take an educated guess as to
its specifications or assess other, similar chargers to determine or approximate the voltages and ratings of their
transformers.
Either method would likely lead
me to a replacement component that
would be close enough for rock and
roll – it’s a car battery charger after all
– but that’s a bit too wishy-washy for
my liking. Besides, I wasn’t finished
with this dead transformer yet.
Fixing it the hard way
I started by removing as much of the
yellow tape that bound the windings
as possible, a task made difficult by
the way the E-I core kept getting in the
way. I got out one of my craft knives
and slid the edge of the blade between two of the hundreds of tightlylaminated shaped metal shims that
make up the core.
It went in relatively easily, meaning the laminations weren’t potted or
bonded together with varnish, as some
are. I removed the transformer’s folded
heavy-metal outer cover by bending
four metal locking tabs on the base out
of the way and lifting it clear.
Celebrating 30 Years
With the core now totally exposed,
I used a sharpened flat screwdriver
to carefully pry free a couple of the
E and I-shaped laminations from one
side. Now loosened, I could ease out
the rest of the laminations one by one
until there was a large pile of them lying on the bench.
What remained was a hard, white
plastic bobbin that held the primary
and secondary windings, and it was a
simple matter to strip the remaining
yellow tape away from the primary
side. Once gone, I could see nestled
at the very top of the now-exposed
windings a black, rectangular, twolegged component that I assumed to
be a thermal fuse, wired in series with
the primary winding.
I already knew it would be open circuit, as the clean state of the windings
showed nothing had burned out but
I measured it anyway. It was dead as
John Cleese’s parrot. I unsoldered it
and measured the windings beyond
it. My meter made it around 50W and
whether that was about right or not
I’ll leave to the mathematicians; all
I needed to know was that it seemed
about right to me.
I located another thermal fuse in
my parts store, which according to the
data sheets I downloaded from the web
was a suitable substitute for the original. Once soldered in, I re-bound the
primary windings with similar tape
and set about re-assembling the core,
a grubby job as each one is coated in
an anti-corrosion substance that if not
May 2018 65
actually oil, has very much the consistency and feel of it.
However, after I’d stuffed as many
of the laminations back into the bobbin as I could, I still had about a dozen “E”s and “I”s left over. No biggie,
or so I thought.
After a quick megger check to make
sure my insulation was good, I temporarily rigged up a mains cable to the
primary and used my auto-transformer
to power it up slowly. My multimeter
showed the secondary voltage rising
as expected as I wound up the power,
but then it happened; the transformer
started to buzz.
Above about 150VAC, the transformer was buzzing very loudly; I
guess I was going to need those extra
laminations after all! By using some
wood-workers’ clamps and a lot of
very colourful language, I managed
to shoe-horn all the remaining laminations back into the core. It was then
thankfully buzz-free.
That just left the simple matter of
reassembling everything, giving it another insulation test and trying it out.
It worked as well as it did before and
while those LEDs were barely visible,
my neighbour was hugely relieved and
grateful. He offered to pay, but I declined; it was the neighbourly thing
to do. Darn this Serviceman’s Curse!
CIG Transmig 200 welder repair
Sometimes it doesn't take a large
fault to stop equipment worth thousands of dollars from working. G. S.,
of Castle Hill, NSW, recently saved a
heavy-duty welder from the boneyard
and here is how...
My ex-neighbour Paul is into old
Ford Falcons from the 1960s. He restored a '64 ute some three years ago
and has two 1964 2-door coupes awaiting restoration. He also recently acquired a '63 Falcon station-wagon that
he's working on at the moment.
Sitting in his garage among that lot
is a real gem – a 1967 Ford Mustang
coupe that's currently a body shell and
a pile of parts. So why is he mucking
around with the Falcon station-wagon and not putting all his effort into
the Mustang restoration? I dunno but
he'll come up with all sorts of excuses
if pressed on the matter!
Vehicle restoration projects invariably require rust repairs and so, about
eight years ago, Paul acquired a second-hand CIG Transmig 200 welder.
This is a large 3-phase machine and
66
Silicon Chip
The faulty
contactor shown
inside the welder.
is mounted on a sturdy metal trolley
that can be trundled around in his
garage. It probably cost around $3000
new but had been acquired for a pittance by one of Paul's mates when a
business shut up shop.
Having no real use for it, the mate
eventually passed it on to Paul for an
even lesser pittance and he subsequently used it while restoring the ute.
It then sat unloved at the back of Paul's
garage for three years until he got his
station wagon restoration underway.
It wasn't long before the welder
was needed for this project and so the
machine was duly trundled out and
hooked up to the garage's 3-phase power
outlet.
Paul then pressed the trigger on the
wire-feed nozzle to check its operation
but no wire fed through. Instead, the
3-phase circuit breaker in the household fuse-box tripped out.
Puzzled by this, Paul reset the breaker and pressed the wire-feed trigger a
second time. The circuit breaker immediately tripped out again and it did
so a third time after he had reset it.
At that stage, Paul decided to ask my
brother, who is a licensed electrician,
to take a look at the machine for him.
I went along for the ride and when we
got there, we found that Paul had already removed the side panels from
the machine.
It took my brother just a few minutes to diagnose a faulty contactor.
This normally pulls in and powers up
a large transformer and various other
parts in the machine when the wireCelebrating 30 Years
feed trigger is pressed.
Our snap diagnosis was that the
contactor was probably full of gunk
and this conclusion was reinforced
when my brother demonstrated that
the machine could be powered up by
manually assisting the contactor to
“pull in” by pressing on it with an insulated probe.
Even then, the wire-feed mechanism
still wasn't working, so it looked like
this welder had two separate faults:
(1) a faulty contactor and (2) a fault in
the wire feed mechanism or in the circuitry that controls the wire feed motor (or perhaps even a faulty motor).
There was no point trying to diagnose the wire-feed problem until the
contactor problem had been resolved,
so it was up to Paul, an electrical fitter by trade, to take things from there.
He's not a man to let the grass grow
under his feet and so, the very next day,
he carefully labelled all the relevant
connections, then pulled the contactor out and cleaned it to within a millimetre of its life.
It did indeed prove to have a lot of
gunk inside and when it was refitted,
he was gratified to find that it now
pulled in when the wire-feed trigger
was pressed without tripping the circuit breaker. So that solved problem
number one.
Now for problem number two. With
no access to a manual, circuit diagrams
or spare parts, Paul figured that his
next best step was to seek professional
help to get the wire feed mechanism
working.
siliconchip.com.au
The faulty tantalum capacitor on
the control board was replaced
with a similar electrolytic
capacitor, with the adjacent 7812
regulator circled in red.
As a result, he loaded the machine
onto a trailer and carted it off to a specialist welder repair shop. They duly
called back a week later to say that both
the wire-feed mechanism and motor
were OK and that they had diagnosed
a faulty control board.
Unfortunately, given the age of the
machine (it's probably late 1980s or
early 1990s vintage), replacement control boards were no longer available.
And as far as they were concerned,
without a replacement control board,
the machine wasn't repairable.
Never one to give up, Paul now figured that he would try to get the control board fixed. And that's when he
flicked the problem my way.
I suggested that the best approach
would be to remove the board from
the machine and drop it around to me.
That way, I could inspect the board for
dodgy solder joints and test the various
semiconductors, electrolytic capacitors
and other parts at my leisure.
Having made the suggestion, I
thought he might drop the board off
in a week or two but as I said, he's not
a man to let the grass grow under his
feet. He turned up at my house within
the hour, clutching his faulty control
board with the external wiring leads
all carefully labelled.
I took a look at it the next day. Despite its age, it was still in good condition with no signs of corrosion. Its
main parts included a couple of 555
timer ICs, an LM3900 quad amplifier IC, several transistors, a relay, two
stud-mount SCRs and a stud-mount
siliconchip.com.au
diode. The external leads ran off to a
couple of pots and some spade clips.
So had one of the semiconductors
failed? Or was it a faulty relay, a dodgy
capacitor or a dry solder joint? If it
wasn't the latter, the easiest approach
might be to simply blanket-replace the
ICs and transistors and check out the
SCRs, the diode and the relay.
It didn't come to that though, because I quickly spotted what was almost certainly the cause of the problem. There were five 10µF 16V tantalum capacitors on the PCB, two of
them in the timing circuits of the 555
timers. Four of these tantalums were
dark blue but the fifth had turned a
pale blue colour with a greenish band
across it.
Surely it wasn't going to be this ridiculously easy? I stuck a multimeter
across the capacitor and it registered a
dead short! I then traced the PCB tracks
from the capacitor and found that it
was across the output of an adjacent
LM340T-12 12V regulator.
This device is mounted on a small
heatsink in one corner of the board
and provides a regulated 12V rail to
the 555 timers and the quad amplifier
(and possibly also the relay).
I removed the capacitor and the
short across the regulator's output
disappeared. I then replaced it with
a 10µF 16V electrolytic that I had on
hand. Two other 10µF bypass tantalums on the PCB were also replaced
with electrolytics, while those in the
timing circuits of the 555 timers were
left in place.
In theory, the LM340T-12 should
have survived since these devices
are short-circuit proof. However, I
replaced it with an equivalent 7812
regulator as a precaution, along with
an adjacent electrolytic capacitor for
good measure.
At that stage, it was tempting to apply power to the circuit and check the
operation of the 555 timers. However,
not having a circuit diagram (no luck
with Google), I was afraid that this
might risk damaging something, especially if two of those external leads
shorted together.
The best bet would be to test the control board in the welder itself. I called
Paul and told him what I had found.
He was on my doorstep some 25 minutes later, collected the part and shot
back home to refit it.
I was cautiously hopeful that it
would now work and I didn't have
Celebrating 30 Years
to wait long to find out. An ecstatic
Paul was back on the phone an hour
later and he was floating somewhere
between his Mustang chassis and seventh heaven. “You're a genius”, he
exclaimed. “The welder is working
perfectly!”
There's nothing like a bit of flattery
to massage the ego but at the end of
the day, this was really a joint effort.
My brother diagnosed the faulty contactor, Paul fixed the contactor, the
service centre correctly diagnosed a
faulty control board and yours truly
fixed the control board.
So a part costing less than a dollar
was all that prevented this valuable
welder from working. It's since been
used to weld some fresh sheet metal
into that old Falcon station wagon
but it's the Mustang restoration that I
reckon he should be getting stuck into.
Editor’s note: older Tantalum capacitors seem to go short circuit more often than you might expect so it’s well
worth taking a good look at any such
capacitors first when repairing something made before the year 2000 or so.
Compaq CQ61 laptop repair and
refurbishment
B. P., of Dundathu, Qld, spent quite
some time refurbishing and repairing
an old laptop for his wife to use. In the
process, he discovered and fixed some
classic laptop hardware problems and
also ran into some time-consuming
software pitfalls...
Our daughter has just started university. After five years of intensive use,
her old laptop was well and truly the
worse for wear, so she bought herself
a new laptop and she gave us her old
one when she came home during her
mid-year break.
When I assessed the old laptop, it
was in a rather dilapidated condition.
The keyboard had one key cap missing on the numeric keypad and most
of the top row of keys (numbers and
symbols) no longer worked.
The top silver layer of the touchpad was also worn off in places, revealing the black base colour, the keyboard surround had a lot of the black
paint worn off it and the lid hinges
were loose. Although the laptop still
worked, it was certainly beat up.
I started the repair by removing the
old keyboard, by undoing the securing screws on the bottom of the laptop.
I ordered a new keyboard and while
waiting for it to arrive, decided to conMay 2018 67
tinue working on it by plugging in a
USB keyboard.
This allowed me to do a factory reset
so that we could start with a fresh copy
of Windows 7. After that was done, I
uninstalled all the trial software and
I installed some additional programs
that were needed. Then I partitioned
the 500GB hard drive into two separate partitions so that data could be
stored on the D:\ drive, separate from
the operating system on C:\.
I noticed some issues with the Compaq factory version of Windows 7 that
I wasn't happy with, so I decided to
do a fresh install of Windows 7 from
an OEM disc (ie, one purchased from
Microsoft) instead.
This all went well, but then I noticed that the webcam driver was not
installed in Device Manager; it was
showing up as an unknown device. I
tried to locate the correct driver for the
webcam on the internet, however, this
proved difficult. I did eventually find
the driver and installed it but when I
went to test it with Skype, Skype said
that it was already in use by another
program. It wasn’t, though.
I thought I would try uninstalling
the webcam driver in Device Manager and then scanning for new hardware. This did not work, as the webcam then showed up as an unknown
device again. I decided to do another
factory reset to try to get the webcam
working correctly but because I'd altered the hard drive partitioning, the
restore partition was no longer present.
I still had the set of three restore
discs that we'd made when the laptop was new, so I decided I would
just use those.
I set about restoring the laptop from
those discs, but when I got to disc
three, it had a read error, so the factory reset failed. This left me with a
blank hard drive. That meant using
the OEM disc to reinstall Windows
7 again. So I was back to square one,
with the webcam still showing up as
an unknown device.
I then realised that we had a related Compaq laptop model, a CQ42,
that uses the same HP-101 webcam.
I checked what driver the webcam
used and it was a standard Windows
driver. I'd recently installed Windows
7 on the CQ42 without any issues and
Windows had found and installed the
webcam, so I wondered why I was having so many problems with the CQ61's
webcam.
68
Silicon Chip
I then tried to tell Windows to use
the driver that it should be using, but
this idea didn't work out and I was
still in the position of not having the
webcam working. At this point, I decided to give the laptop a rest and do
something else.
I went to my shed to look for something and when I opened a box to
check inside it, I discovered another
Compaq CQ61 that I'd been given
some time ago that I'd forgotten about.
This CQ61 was a cheaper variant with
much lower specifications than the
one I was working on, so I would use
it for parts.
I started dismantling it with the intention of using the top case half to
replace the well-worn top case half
on the one I was fixing. The touchpad
still had its original silver colour and
the keyboard surround was still in asnew condition.
These new parts would make a huge
difference to the original one. Unfortunately, the keyboard on this laptop
was also faulty and unusable.
After unscrewing a multitude of
screws, I had the donor laptop fully
dismantled and I retrieved the parts
that I wanted to use for the refurbishment. Then I turned my attention to
the laptop I was working on and I dismantled it. I was now ready to reassemble it, using the better parts from
both laptops.
Before proceeding further, I decided
to give the interior a good clean because there was a considerable amount
of dust inside it from the many years
of heavy use. I used a small paintbrush with natural bristles in order
not to generate static electricity while
brushing the dust off the motherboard
components.
When I got to the heatsink, I removed the fan for cleaning and I noticed that there was a thick layer of
dust on the inside of the heatsink's
fins, where the fan had been blowing air through it.
This dust was removed and
the fan was then thoroughly
cleaned, before being refitted.
This is a very common problem with older laptops and
often causes them to overheat and either lose performance or become unstable.
It was fortunate that I had
stumbled across the other
laptop and as a result, decided to take apart the one I was
Celebrating 30 Years
working on because if I hadn’t done
so and cleaned it out, chances are I
would have run into some of these
problems later.
At this point, I decided to also
transfer the lid assembly from the donor laptop (including the display and
webcam) because it was in slightly better condition than the original lid. By
this time, I was also suspecting that
the original webcam may be faulty,
so this was the perfect opportunity to
test this theory.
With the laptop partly assembled,
I propped the lid against a box, so
that I could connect it up and test the
screen and the webcam. Once booted, I
checked Device Manager and the webcam was now installed. I loaded Skype
and tested it and it now worked, indicating that the original webcam had
been faulty all along.
I then noticed that there was a problem with the replacement screen, as
it had several dead pixels in the lower right-hand section of the screen.
This blemish was not that bad and it
would not make a huge difference to
the laptop, but seeing that the original screen was in better order, I would
swap them over.
I dismantled the lid and fitted the
original screen to it and then I reassembled it and continued with reassembling the laptop. It's very important to
take particular note of which screws
go where when reassembling a laptop.
There are around five different
length screws in some laptops and
each screw must be used in the correct location to prevent damage (when
putting a long screw in where a short
one should go).
siliconchip.com.au
After a bit more work, the laptop
was reassembled and back in working
order again, except for the keyboard. I
was still waiting for the replacement.
In the meantime, my wife could just
use the laptop with the USB keyboard.
Eventually, the replacement keyboard
arrived and I fitted it; the laptop was
then fully refurbished and it has a new
lease on life.
This laptop is now around seven
years old and it would be classified as
being quite outdated. But it's still quite
suitable for light duty work, such as
web browsing, emailing, letter writing
and other general duties.
For a bit of work and less than $20
for the replacement keyboard, it's as
good as new. That’s a lot cheaper than
buying a new laptop, even a basic
one, and it’s still perfectly adequate
for most jobs and uses less electricity
than a desktop computer.
Having the donor laptop on hand
certainly saved me quite a bit on replacement parts and resulted in a more
cosmetically appealing end result with
the new top case shell to replacing the
well-worn old one.
This was my first major laptop repair and I was surprised that it was
nowhere near a difficult as I had imagined it would be. It's simply a matter
of proceeding with caution and paying
close attention to details.
There are also plenty of videos on
YouTube which go into considerable
detail about laptop repairs but I managed to do the refurbishment without
referring to any.
MR16 LED downlight repair
D. M., of Toorak, Vic, had a 12V
MR16 LED downlight fail far short of
its claimed 20,000+ hour lifespan. It
would have been cheaper to just buy
a new one but he wanted to know
what had gone wrong so set to taking
it apart…
I wanted to know what had failed
inside the MR16 LED lamp as I find
the claims for LED downlight life expectancy, typically of 20,000 to 50,000
hours, quite unlikely.
At eight hours per day, that would
amount to a service life of 7-17 years.
Although LED downlights have not
been available for 17 years, in my experience, most such lamps don’t even
last seven years.
My particular light was a Muller-Licht (house brand) Reflektor rated at 320
lumens and 5W. I carefully examined
siliconchip.com.au
the light to determine how it might be
disassembled without damage.
I found I could gently pry the top retaining ring off the body with a knife
which also caused the release of the
light diffuser, revealing the LEDs and
their heatsink.
Two Phillips-head screws could
then be removed from the heatsink,
allowing the separation of the top and
base portions of the light assembly (see
photos at right).
LED lights typically contain a driver which delivers a constant current
to the LEDs. I quickly determined
that it was the driver that had failed
as when power was applied directly
to the LEDs, they lit up. I decided to
obtain and install a suitable replacement driver.
I found one online that was rated at
the same current as the LEDs, 650mA
and only cost about $2.50. This driver has pins attached with the correct
size and spacing to plug into an MR16
socket.
So these could be used to replace the
existing pins on the lamp body, or alternatively, they could be desoldered
from the driver if necessary for other
applications.
The driver utilises a PT4115 chip.
The website where I bought it has details of the circuit; see siliconchip.
com.au/link/aajr
I removed the old driver from the
LED body and then the old MR16 pins.
Be careful removing the old pins as it
is easy to break the plastic body. In this
lamp, the pins were hollow.
You may be able to cut them and
then drill through to remove them
(with a very small diameter drill). I
tried twisting them with pliers which
ended up cracking the body of the case.
Alternatively, it might be easier to
leave the pins in place and desolder
the old driver, then solder them to
the new driver board. The driver is
housed in the otherwise empty “well”
in the base of the lamp, just above the
pins.
Having soldered the new driver in
place, I glued the ends to ensure the
pins would not move. Make sure any
conductive parts that might contact
each other to cause a short circuit are
appropriately insulated. The lamp
worked fine after that and so I put it
back into service.
This particular lamp replaced an existing halogen downlight and is driven
by an old-style iron core transformer
Celebrating 30 Years
Prying off the cover revealed the
retaining ring, diffuser, LEDs and
their heatsinks.
After removing two screws the LED
enclosure could be separated showing
two leads attached to a driver PCB.
The LED driver shown above is the
replacement one and is mounted
differently to the old driver.
Left: the replacement MR16 driver.
Right: the failed MR16 driver.
supplying 12VAC. These transformers are not as efficient as more modern
electronic ones but they do work with
LED replacement lamps.
Some modern electronic “transformers” designed for use with halogen lamps will not work with LED
replacements as they do not draw
enough current (or perhaps it’s because
they’re a non-resistive load).
There are many different designs of
LED downlight. Some such as the one
described here might be relatively easy
to disassemble, others might be more
difficult or impossible. Note that type
of repair is not very economical, especially if you include your time in the
calculation but I found the job to be
both fun and educational.
SC
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