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SERVICEMAN'S LOG
The aircon that nearly made me lose my cool
Like other appliances, air-conditioners won't
last forever. But spending a bit more can
sometimes leave you with a longer lasting
and better made device. However, all good
things must come to an end, as our 15 year
old aircon started to take flight.
I think I’ve mentioned I’m involved
in a renovation project; I’ve been working on it whenever I can for the last
five months so it does tend to come up
in conversation. For example:
Friend: “How’s the renovation
project going?”
Me: “$#<at>$%#!!!”
Sprucing up a house from the
ground up is not easy at the best of
times, let alone in the middle of a harsh
Christchurch winter. On the bright
side, the project is excellent training
for a multitude of DIY disciplines. In
the two years
since we moved out, the tenant had
run it down – a lot. One expects natural
wear and tear but dug up lawns, cutdown trees, damaged paintwork and
greasy surfaces are beyond the pale.
It was while I was cleaning some
of their old junk from the side of the
house that one of the two outside compressor units for the house’s air-conditioning system burst into life, making
such a terrible squealing noise that I
just about had a coronary.
We’d installed these units some 14
years earlier so they’d done plenty of
work, and while they were now well
out of warranty (by about four years),
we hadn’t had a problem with them
until now. The noise this compressor
unit was making now was something else though.
Flashback: before the
quakes
When I called my acquaintance in the air-conditioning industry all those years
ago for a quote, he recommended a Daikin system as
they had a good reputation
and an excellent (10-year)
warranty. Admittedly, they
were more expensive than
other brands, but we’ve always gone by the philosophy that spending more at
the beginning often saves
money in the long run.
In other words, don’t be
penny wise but pound foolish! This strategy has usually paid off, well, most of
the time anyway. But that’s
another story!
siliconchip.com.au
Australia’s electronics magazine
Dave Thompson*
Items Covered This Month
•
•
•
•
Air-conditioner repair
One smoking radar
Yamaha RX V450 receiver repair
Car fob repair
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
When I said earlier that we had
installed the air-conditioning units,
it was actually our professional acquaintance that I have mentioned who
did the installation. Having had a look
at our place, he decided that the outside units should go at what he called
the back of the house, which is actually the side, where a narrow strip of
wasted land and a fence separates us
from the neighbour’s property.
That sounded fine to me and we
signed off on the quote he sent us.
However, a few weeks later, on the day
of installation, I arrived home from
work to discover the installers had put
the compressor units literally on the
back of the house, facing our grassed
backyard and the patio/BBQ area.
They’d made an impressive and very
clean job of routing the gas and power
lines through walls, over the roof and
under the house to the various components, but the blasts of frigid air being
chucked out over the patio meant it
would be winter there all year round!
I was also surprised by the sheer size
of the compressor units which now
took up a large portion of our patio.
This simply wouldn’t do!
My wife almost had a coronary
when she saw them, but by that time
I’d called my mate and asked him
why the compressors had been placed
there, thinking that perhaps the installers had hit some snags that meant they
couldn’t be installed on the side of the
house, where they could blow cold air
onto the paling fence and drain water
into the unused grass strip.
September 2018 61
Do you have any good servicing stories that you would like to share in The Serviceman column? If so, why not send those stories in to us?
We pay for all contributions published but please note that your material must
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Please be sure to include your full name and address details.
was stolen from the wreckage of a
building by gang members doing
demolition working, while the owner
watched, kept away by police and
army security who held him behind
the cordons for his own safety. This
POS system turned up installed in a
backwater pub somewhere up north.
Nobody was ever prosecuted for
this blatant looting and there were
many, many other instances of this
happening. We’d paid a fortune to
have the heat pumps installed before the quakes, so why leave them?
Insurance wouldn’t cover the costs,
as most insurance companies were
being hammered senseless by quake
claims (some obviously fraudulent),
to the point some required government bailouts.
Of course, aircon systems are supposed to be professionally removed,
with the gas recovered properly to
avoid pollution, but the fact that the
gas lines had been ripped out of the
compressor units and were left dangling in mid-air meant there was no gas
to recover. So I had no qualms about
removing everything myself.
I didn’t know whether they could
be used again but I wasn’t about to let
someone nick them and profit from
my loss. I was therefore very pleased
when Clary looked at my pile of components and told me that he could reinstall them, and for a fraction of the
cost of either getting new/refurbished
units or the cost of hiring an aircon
company to come and do it.
And so it was Clary I called when
I heard the noise this older unit was
making. Given the current state of affairs where appliances seem to be considered “consumables”, designed for
replacement rather than repair, I was
fully prepared for the fact the motor
might not be available. But in that case,
I’d either try to replace the bearings,
or ask Clary about re-purposing a different motor for this unit.
Surely, given the similarity between
different aircon models, it wouldn’t
be too hard to locate a similar motor
that would fit.
While neither of these solutions
would be ideal, shelling out for a second-hand compressor unit wouldn’t
be much chop either, so I sent him a
PXT (Multimedia Messaging Service)
of the label on the side of the compressor and hoped for the best. Within a
few hours, he’d called to say he could
get a new motor assembly for a trifling
Australia’s electronics magazine
siliconchip.com.au
He let out a stream of expletives
(some of which I’d heard before, while
others must have been aircon industry specific) and said he’d be around
to check it out. Sure enough, he soon
rolled up with the two navvies who
actually did the job and made profuse
apologies for his employees’ lack of
apparent intelligence, for mistakenly putting them on the actual back of
the house.
I was going to point out that he had
written “back of the house” on the
quote but given the circumstances (and
his extensive vocabulary), thought
better of it.
He promised to make things right
and a few days later the guys were
back, with a couple of others to assist
and had soon relocated the compressors to their current location, with
power and gas lines re-routed and
any old holes nicely filled in and even
painted. And there they have lived
and worked happily for nearly fifteen
years, until the day I was moving rubbish and the fan started up and just
about caused an underwear change.
Back to the present problem
The noise was like a jet taking off,
winding up to a very shrill level. I immediately flicked the outside isolation
switch off and the fan ground its way
to a stop. How the tenants had put up
with this awful noise, given that one
of their bedroom windows was almost
directly above this thing, was astonishing. Even more concerning, how did
the neighbours put up with the noise
without complaint?
Admittedly, there was a driveway
separating the neighbour’s house from
the paling fence but as the crow flies,
it was only about four meters to their
living room. With the air-conditioning
running in our house, the noise must
have been truly annoying in theirs!
No prizes for all you diagnosticians
correctly guessing the cause of the
noise; any serviceman (or enthusiast)
worth his or her salt will be shouting:
fan-motor bearings! Well, that’s what I
thought, so my first job was to call my
new air-conditioning specialist Clary,
who had installed heat pumps in our
new place.
My knowledgeable assistant
I’d met Clary through a builder
friend and when I discovered that he
could install heat pumps for us at our
new home, I was sold. We already had
the heat pumps as we’d stripped them
from our quake-damaged workshop
rather than leave them for the vultures that were picking over the broken bones of Christchurch businesses
at the time and selling their swag in
pub car-parks around the country.
As an example, a multi-thousand
dollar customised café POS system
Servicing Stories Wanted
62
Silicon Chip
$120 plus tax and shipping, which
sounded like a pretty good deal.
In the meantime, even though it was
below zero most mornings I went to
work on the house, I avoided using
the heat pump, not because it might
get damaged further but because I was
embarrassed about the noise, and I
didn’t really want any trouble with
the neighbours.
It took a few weeks for the motor to
arrive and Clary messaged me when it
did, asking if I wanted him to install it,
or do it myself. I asked him the likely
cost of him doing it and he reminded
me that I’d looked at a circuit board
for him about a year previously, and
because I hadn’t charged him for repairing it, he would change the motor
over for me for nothing.
What a surprise, as I’d forgotten
about doing that little job for him, and
just goes to show what a little karmic
investment can reap. I pledged to help
him though, partly out of a sense of duty
and partly out of professional interest,
because I’d never seen the internal
workings of one of these units before.
Getting to the motor
He arrived early one clear-but-bitterly-cold morning and we set about
swapping out the motor. He first fired
the thing up and we chatted as we
waited for the compressor to kick in
and the fan to start. When it did, we
weren’t disappointed and Clary immediately agreed with my diagnosis
that the fan motor bearings were almost certainly the cause of the noise.
Getting things apart on the compressor unit looked quite straightforward, with just a few sheet-metal
screws holding the exterior panels on. I
thought this job would be a cinch; talk
about your famous last words!
Clary started on one screw with a
large Phillips head screwdriver and
immediately it became clear that the
screws were a little tight. I grabbed another, smaller screwdriver and started
with other screws, while he braced
himself and cranked harder on his
stubborn fastener.
You can imagine the grunting and
swearing, and Clary was the same, especially when his screw head sheared
off, leaving the screw’s threads fused
to both the panels and the rivnut-type
threaded insert.
While most of the screws had combined Phillips/7mm hexagonal heads,
suitable for a socket or crescent wrench
siliconchip.com.au
(shifter for you Australians), as the
screw had failed using just a screwdriver, I expected it would shear even
more easily using a socket wrench.
I had no luck at with any of the other
screws with my smaller driver either,
so we resorted to a liberal application
of penetrating oil spray on all visible,
to-be-removed screws. While the oil
did its work, we did manage to remove the plastic front shroud, which
used beefier, coarser-threaded screws.
After the four shroud screws are
removed, the panel slides upwards
and this releases several plastic clips
holding it to the front of the compressor unit. Without knowing this trick,
I would likely have resorted to levers
and prying to release it, so almost
straight away Clary’s knowledge and
experience made things easier.
Removal of the shroud cover exposed the fan, a large-diameter, threebladed plastic unit. I was surprised at
how small the now-visible motor was,
given the size of the blades.
Once again, Clary’s experience
showed as he mentioned that the fan
nut, a nylock-type, might use a lefthand thread. As it happened, it didn’t,
and we discovered that because the
nut was quite loose.
Clary had a socket for this task, assuming it would also be tight, but he
found when he applied the socket
that he could actually spin the nut
off by hand.
He’d mentioned that sometimes the
fans can be a real pain to remove from
the motor shaft, but in this case, the
nut spun off the usual way and the fan
came off just as easily, revealing the
motor and mounts behind.
By this time, we hoped the penetrating oil had done its job, as it was obvious we’d have to remove the top, front
and one side panel in order to unplug
the old motor’s lead from the controller board. This sat inverted near the
top of the case in a water-tight plastic
box. Having removed that, we would
need to route the new motor’s cable
and plug it back in.
They certainly could have designed
this a bit better, given that the cable on
the motor needed to be about one metre long in order to snake around the
plastic PCB case to reach the buried
socket on the opposite side!
The next screw we tried to remove
also failed but this time it took the
threaded parts with it, leaving a larger hole than before. On viewing it, I
Australia’s electronics magazine
September 2018 63
theorised that dissimilar metal corrosion had, over time, welded the screw,
panel and insert together; whatever the
actual cause, it was certainly stuck fast.
We got half the case screws out
without damage but the motor screws,
which are a smooth-shafted bolt with
a small threaded piece on one end,
all sheared off in the pressed, sheetmetal mount. What fun this job was
becoming!
In the end, we just went for it and
whatever screws we had to drill or
wind out with pliers we coped with.
Fortunately, none of the fasteners
were critical, except perhaps the motor mounting bolts which pass through
and tighten onto rubber mounts to keep
vibrations to a minimum. For those,
we just drilled out the jiggered holes
and re-threaded them for the slightly
larger threads of some new bolts that
Clary had in his bits boxes.
It helps to have good tools
Whilst helping him to find new
screws, I couldn’t help but admire the
contents of his work van. Talk about
tool porn! He had tools and gas-fitting
stuff I never knew existed and his van
had just about any tool or device you’d
need for installing heat pumps.
While it can be difficult to justify the
outlay for some of these tools, given
you might only use them once in a
blue moon, it’s a fact that when you
need a specific tool for a specific job,
and nothing else will do, then you’d
be glad you bought it. Well, that’s my
theory anyway, and is what I usually
try to tell the wife when I want to
buy some new widget or tool for my
workshop!
That said, it does get to a point
where even a workshop isn’t big
64
Silicon Chip
enough, so there must be a line there
somewhere, I just haven’t found it yet.
The job changing the fan motor was
not overly difficult but it wasn’t simple
either. The old motor growled when
the shaft was manually turned and the
new fan was almost completely silent
when we fired it up, so that was definitely the problem.
Hopefully, the neighbours appreciate their newfound peace and quiet.
I doubt they realise how much work
went into achieving it!
A smoking radar transformer
R. E., was responsible for repairing large radar systems – not a job for
the faint-hearted! Some years ago, he
found an unexpected fault while performing the first six-month service
on a newly installed radar. Here's his
story...
This new radar system had replaced
an older unit that had been in service
for many years. It was a 250kW unit,
one of many similar radars operated
by this particular government department. It comprised a transmitter/receiver unit and associated scanner
control gear, all located in an equipment room on the ground floor of the
building, except for the scanner itself
which was mounted on the secondstorey roof.
The scanner was connected to the
equipment room via a rather long and
convoluted waveguide, with bundles
of cabling carrying power and control data, both of which I had helped
to install.
By this stage, I had the service on
this type of radar down to a fine art,
which included greasing of the mechanical gear trains in the elevation
and azimuth system, removal of the
Australia’s electronics magazine
slip ring brushes and cleaning of the
slip rings that carry the power to, and
data from, the elevation part of the radar scanner.
I also checked all power supply voltages and ran checks on and tuned up
the radar transmitter and receiver. This
ensured that the transmitter was both
on frequency and putting out the correct power and that the receiver was
tuned correctly and had the specified
sensitivity.
The mechanical service, while
messy, was simpler on this radar than
on the older unit that it replaced, as
the previous radar had two large oilfilled gearboxes for the azimuth drives
(one high speed and one low speed)
plus an elevation gearbox, all of which
had to be drained and refilled every
six months. There were various points
where I had to inject fresh grease, too.
The service on this new radar initially went well, as you would hope and
expect with a new radar. The entire
process took two days, with breaks for
operational requirements, as at times
it had to actually be used for the purpose for which it was installed, during
which I busied myself with work on
other equipment at the station.
I was finished with the radar itself
around lunchtime on Friday, which
was good since I had a 400km return
trip to get home for the weekend. Just
one check remained – I had to test
the station's backup generator, which
had only been installed just prior to
my visit. It had been tested off-load
by the contractors who had installed
it but they had left by the time I was
ready to load test it.
So, having warned the station staff,
I went out to the station meter box and
switched off the three-phase supply to
the site. After a short delay, the generator started and I checked that the oil
pressure and other readings were OK,
then wandered back into the office to
make sure all the equipment was still
working properly.
When I stepped back in, the first
thing I noticed was a burning smell,
which did not initially alarm me as
the station staff often produced odd
smells when they were cooking. But
as I walked into the radar equipment
room, I was horrified to see smoke
pouring out of the radar control rack
and hurriedly switched off all power
to the radar.
I could hear a crackling sound coming from the back of the radar interface
siliconchip.com.au
and as the smoke slowly cleared, I saw
a toroidal transformer that had clearly
cooked up.
This was odd as it surely couldn't be
a coincidence that this happened right
when the generator fired up, but the
only thing that had changed was the
power source. A quick check showed
that every other piece of equipment
that was in the office, and on-site, was
operating perfectly well.
I checked the power coming from
the generator but each phase was close
to 240V, as expected, and I couldn't
find any other issues using the equipment I had on hand.
Anyway, clearly, I would have to replace the transformer which was now
the extra-crispy type. To start with, I
would have to remove the radar interface, which connected the control
computer to the rest of the radar, to
get a closer look at the burnt transformer. I was relieved to find that we
had a spare transformer available so I
at least had a chance of fixing the radar that afternoon.
I started by drawing a diagram showing which connectors went where at
the rear of the interface. I had learnt
the hard way not to rely on my memory of what goes where, as many of the
cables were not labelled.
Since it was a new design and only
recently put into operation, I knew
nothing at all about this system and
was more than a little hesitant about
working on it. But I really didn't have
a choice at this stage.
Access to the components was by
undoing numerous screws on the top
panel and flipping the large lid over to
reveal the components all mounted underneath that top panel on solder tag
strips, none of which were labelled, and
all connected via hook up wire, most
of which was the one colour – pink.
AZ synchro
18TRX6
Radar
scanner
synchros
18TRX6
EL synchro
After refitting the upper board, remounting the interface in the rack, and
then reconnecting the myriad of cables
to the rear of the unit, I was ready to
power it up.
At this stage, the generator was still
providing the mains power. I decided
to risk powering the radar back up
while still on generator power since
it was the only way that I could think
of to prove whether the generator was
the root of the problem.
I crossed my fingers and flicked the
breakers. The radar initially seemed
fine but after about 30 seconds, I could
once again hear the crackling sound
of overheating insulation and a quick
glance at the interface showed that the
replacement transformer was starting
to cook. And the fuse had not blown.
This was not totally unexpected and
suggested that the fault was not in the
radar itself, but something to do with
the generator. I had no option but to
once again power down the radar and
ponder what to do.
Clearly, the radar could not be operated like this. Even if I had a second
spare transformer, I could hardly fit it
and leave since if the mains dropped
out and the generator came on, that
would be the end of the radar again
and could possibly result in a fire. In
fact, it was lucky that this was the first
time the generator had been used.
Well, if these toroidal transformers
would not work on the generator power, perhaps a different type would. Certainly, the rest of the transformers in
the radar, and other equipment on site,
was handling it without a problem.
I realised that the 95VAC required
for the synchros was similar to the
110VAC used for American mains.
There was a very good chance that the
local Dick Smith (remember them?)
might have a step-down transformer
meant for powering American equipToroidal
240V from
transformer
ment in Australia and that could be
mains or generator
95V
suitable for this job.
50 cycles
By this stage, it was getting close
REF
to 4.30pm, so I jumped in the car and
S1 S2 S3
tore down to the store before they
AZ synchro closed and was rewarded with a small
step-down transformer complete with
to digital
converter
mains lead and plug. Its 100V output was not exactly as specified but
I figured the worst that could happen
EL synchro was that the synchros might run a little warmer.
to digital
converter
I wired this in place of the toroidal
transformer. The result was not pretty
A diagram showing how the toroidal
S1 S2 S3
but I was pleased to see that turning
transformer drove the "synchros" in the radar.
siliconchip.com.au
All I could do was use my multimeter to figure out which connection
went where. Then when I was finished,
I would need put it all back together, laboriously re-connecting all the
plugs, wait for the radar's five-minute
warm up-timer to finish, then apply
high voltage and see if it was working.
If not, I would have to start the whole
tedious process again.
At least the interface on this new radar was less complicated and easier to
access than the old one. So, I dug into
it, removing all connectors, undoing
the interface rack mounting screws and
dragging it out on top of a trolley, where
I could work on it. During this process,
I labelled the connectors and sockets
so I would have a reasonable chance
of putting it back together properly.
I could now see the damaged transformer and the fact that it had gotten
quite hot was obvious, with melted
plastic insulation and other signs of
heat stress.
My circuit diagram showed that the
purpose of this transformer was to supply 95VAC to the radar synchro receivers. These are small devices somewhat
like motors except that they are used
to determine the rotational position
of the radar.
I checked the resistance across the
transformer load and got a reading
about half that which I measured from
a spare synchro; I had expected this as
the transformer drove two synchros.
This suggested that it was not a short
circuit at the output which had caused
the transformer to burn out.
I swapped in the spare transformer
and added a temporary unofficial modification: an inline fuse holder and fuse
in the secondary of the transformer, on
the cable powering the synchros, just
in case I was wrong about the transformer load being the problem.
Australia’s electronics magazine
September 2018 65
66
Silicon Chip
Mentioning this problem to the main
workshop further south seemed to provoke some disbelief until later the following year they encountered the same
problem at an identical new radar installation, whereupon they contacted
me to let me know that the same thing
had happened to them!
is used to switch power to the main
transformer.
The circuit operation was difficult
to understand at first. Current from the
mains Active flows through a 22nF capacitor and 2.2kW resistor to a 10V zener diode and this arrangement then
feeds a 9.3V rail via diode D4 to power
a 4013B flip-flop which drives the gate
of Mosfet Q1.
Q1 switches current through a small
transformer, T1, via bridge rectifier D1
and this transformer provides a 12V
standby rail for the main PCB.
I hooked up the sub power PCB to the
mains via an isolation transformer. The
voltage across Z1 was only 6.4V, not
10V as I expected. The circuit seemed
to work to some degree as there was
8V across C2.
I decided to remove C1 and measure its value as the coupling capacitor in this type of circuit has proven
to be a problem before. C1 measured
only 10nF, not 22nF as it should be.
I replaced it with a mains-rated (X2
class) 22nF capacitor and powered up
the board again. I then observed 10V
across Z1 and 12V across C2.
The voltage across C2 slowly
dropped under load until it fell low
enough to make the optoisolator Q2
turn off. This allowed Q1 to turn on
for a short time to top up C2. So the
circuit was designed to save power by
only running transformer T1 when it
A
N was required.
Yamaha RX V450
5.1ch receiver repair
J. W., of Hillarys, WA, decided to
help a friend out by repairing a cherished Yamaha surround sound receiver. He was rewarded for his generosity
in liquid form...
A friend asked me to look at his
Yamaha RX V450 5.1-channel receiver.
It was quite a few years old and had
recently become difficult to switch
on. Sometimes it would power up but
other times would take a number of
presses of the power button. Now it
would not power on at all.
I removed the cover and found that
the incoming mains supply went to a
small PCB. This seemed like a good
place to start. I removed the PCB and examined it through my magnifying lamp
but couldn't see anything unusual.
At this point I decided to try to find
a circuit diagram on the net, I located
the one shown here. The small PCB
was called the sub power board and
was responsible for providing power
to the main PCB to run the infrared
receiver and the coil of a relay which
R1
2k2
Yamaha PSV sub-board circuit
C1
0.022
D1
Q1
U1A
4013B
3
6
4
D
CLK
SET
RST
VDD
14
R4 1M0
5
VSS
R3 220k
Q
Q
1
T1
R2
220k
2
7
D2
9.3 V
Z2
U2
R5 2k4
D4
C2
50uF
9.1 V
RELAY
Z1
10 V
R6
C3
50uF
2k2
Q2
TO MAIN POWER
TRANSFORMER
6
5
4
3
2
1
the radar on again resulted in full operation and no burning smell. I hung
around for an hour or so monitoring
the operation to ensure that nothing
untoward happened with this new
transformer in circuit, then took off
for the day.
Of course, this was not a permanent
solution, but it did get the gear back
on the air, which was most important,
and would allow me to return home
the following day, once I had checked
the operation again in the morning to
confirm that all was still going well.
Back in the workshop the following
Monday, I ordered both a replacement
toroidal transformer for the unit and a
spare for the spares cupboard. I then
contacted the contractor responsible
for the supply of the generator to let
them know that something was amiss
and that the generator installation was
not acceptable.
I also contacted a transformer manufacturer to chat with them and they
told me that a “shorted turn” that can
occur with toroidal transformers, depending on how they are mounted.
This sounded very much like the
problem that I had seen, though how
it occurred was something of a mystery to me.
I should mention that toroidal transformers were pretty new technology
back then and I didn't yet understand
them all that well. Almost all the previous equipment that I had worked
on used the older-style E-I core transformers.
The contractor replied sometime later that week that they had found that
the office earthing had not been done
correctly at the generator but that it
had now been rectified.
My theory is that the Neutral from
the station was tied directly to the
Earth at the generator, which somehow caused a shorted turn effect via
the metal mounting bolt and plate that
was holding the transformer to the
earthed metal base plate. But truth be
told, I really do not know for sure and
now that the radar was completely operational again, I had other things to
think about.
Once the replacement toroidal transformers turned up, at the next possible opportunity I returned to the
station and fitted the specified transformer and a test run with the generator showed that the radar would now
run off the generator with no problem,
which was a significant relief to me.
P1
TO MAIN PCB
Australia’s electronics magazine
siliconchip.com.au
I reassembled the receiver and ran it
for a few days. The difficulty switching
on had disappeared so I gave it back to
my friend, who now has his surround
sound system working again. He generously came around with a bottle of
scotch for my efforts.
Editor's note: failed X2-class capacitors have become a theme in our
Serviceman contributions. We think
it must be due to their "self-healing"
properties, where damaged sections
of the metal plating will burn away
so that the capacitor does not short
the mains.
But this results in their value dropping and eventually, it will drop far
enough to cause the device to malfunction.
What causes the damage in the first
place? It may be that the capacitors
are poorly manufactured and simply
degrade over time but it seems more
likely that it's due to voltage spikes
in the mains, from thunderstorms
and such.
This type of circuit for reducing the
receiver's standby power was used for
many years in Yamaha products. They
were one of the earliest manufacturers to reduce standby power of their
appliances.
The resulting standby power figures
are impressive, at around 100mW. This
is made possible by switching mains
across the transformer periodically,
minimising the average magnetising
current.
Car remote repair
R. W., of Lakes Entrance, Vic, found
that even a simple repair job can be satisfying and can save quite a bit of money too – especially when the item that's
being repaired is in the automotive
realm. Replacement electronic parts
for cars can be surprisingly expensive
so fixing them is often worthwhile...
Cars and oil are usually a good combination but this time, it lead to an unusual service challenge. My daughter
now owns my father's old Nissan Pulsar and it was one of the early models
that adopted remote locking, boot release and a panic button (which sets
off the alarm). It has been a very reliable runabout.
But after spending a week or two in
Melbourne and borrowing the car on
numerous occasions, I became aware
the remote locking fob was not reliable and while the lock button would
always work, unlock often did not.
siliconchip.com.au
These things are notoriously expensive to replace so a repair was definitely worth a try.
Using a coin, I cracked the fob open
and found a large button cell in good
condition. I bought a new cell and replaced it but no luck; it made no improvement.
Having to think a bit harder, I inspected the fob and prised the PCB
out of silicone insert which held it
in place and also formed the rubbery
buttons that poked out the other side.
To my surprise, the whole thing was
covered with a greenish goo. At first
it looked like corrosion, but the the
silicone cup was actually full of oil.
It looked like clean engine oil and it
was everywhere. My daughter assured
me she knew nothing about it so I am
guessing the key fob's oil soaking had
happened before she started driving
the car.
While there was no evidence of corrosion affecting the operation of the
remote, the oil had been there long
enough to stiffen and gum up the
switches. Strangely, there was no oil
at all on the battery side of the fob.
Perhaps the silicone part had formed
a gasket, stopping it from getting into
the back of the remote.
I washed the oil off the PCB and
silicone by applying turpentine and
Australia’s electronics magazine
scrubbing it with an old toothbrush.
The brushing must have been overly
vigorous though, as one of the metalbodied SMD tactile switches was left
with only one leg out of four still attached. Using my finest soldering tip,
I re-soldered the three detached pins
on one switch and refreshed the solder on all the other switches.
Then, using a fine hair brush, I
dabbed fresh turpentine on each
switch in turn and using a metal probe,
quickly pressed the switches off and
on many times. This action released
goo from inside the switches that I
then wiped away. Cycling around the
switches in turn, washing and clicking gradually flushed all the goo out,
giving a satisfying click when each
was pressed.
I repeated this over and over until
I was happy the turpentine was clear.
I then used methylated spirits to give
the PCB a final clean, to remove any
turpentine residue.
My daughter and I were both pleased
to find the clean new fob worked properly again. While literally a small job,
it was a most satisfying challenge and
my father would have surely been
pleased too. He was of the conviction
that nothing could be thrown out unless it had been repaired at least two
times already!
SC
September 2018 67
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