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SERVICEMAN'S LOG
A laptop, spilled tea and a crack
The vast majority of my ‘bread-and-butter’ work
is mundane to the point of being drop-dead
boring. Most of it wouldn’t even pass muster as
a footnote to more interesting stories. If I wrote
a column solely about these jobs, you’d probably
unsubscribe in disgust. However, occasionally a
job will come along that is worth mentioning.
One such job that comes to mind is
something I tackled a little while ago.
A customer brought in a laptop that
wouldn’t boot.
It had been working well until recently; I’d given it a thorough service
about six months ago. But while cleaning a shelf above the computer desk,
the owner had dislodged a decorative,
over-sized tea mug and this had fallen
onto the laptop, landing square in the
middle of the keyboard.
The machine wasn’t running at the
time, but when she tried to power it
up after the event, the lights were on
but nobody was home. She called and
asked for advice, and my recommendation was that she bring it in so I could
assess it, see what’s going on and then
we could go from there.
It seems to be the way things often
work out that the customer was in the
middle of an assignment that was due
in a few weeks and her main concern
was losing her data. I told her on the
phone that while it was very likely
her data was intact, I wouldn’t know
for sure until I got my hands on the
machine.
The fact the laptop wasn’t running
at the time, and the likelihood of the
hard disk being mounted some distance away from ground zero, meant
that it would probably be OK.
When I opened the lid, the first thing
I noticed was a slight bulge in the centre
of the keyboard, which she confirmed
was the area of impact. While barely
perceptible, it was readily apparent in
the right light. That sort of thing never
bodes well, given the lack of room available in most laptops; something must
have given way under there.
siliconchip.com.au
I whipped the back plate off and
removed the hard disk, which I then
plugged into a workshop computer
using a USB-to-SATA bridge adapter.
I ascertained that her data was still
where it should be and informed her
that while I’d need to run a few tests
over the drive, the fact it spooled up
and could be trawled without complaint meant I could be reasonably
sure it would be all right.
Dave Thompson
Items Covered This Month
•
•
•
Repairing a beaten laptop
Cleaning PC motherboards
Philips air fryer repair
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
A stern lesson on
backups
The customer was
understandably relieved to hear this
good news, and I
took the opportunity to give her my
standard backing-up pep talk.
Like most people, she had a
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April 2019 53
backup system installed and set up,
but after the first initial backups done
many months ago, she just never got
around to running it again.
Given that people’s data can change
radically within days, a regular backup
is never a waste of time. While a lot
of today’s technology users rely on the
“cloud” retaining backups of all their
data, many have no idea where that
data actually is or even how to go about
retrieving it should disaster strike.
They’ve either been told that once
they set up their phone or computer
that all their data will automatically
be backed up to a cloud account, or
they’ve misunderstood what backing
up to the cloud really entails.
Easily-overlooked details such as
needing to have an active iCloud,
OneDrive, Google Drive or similar account in place and the fact there is often a need to actively manage the files
that are supposed to be backed up to
remote locations leaves users vulnerable to data loss.
It is also worth remembering that in
the past, services such as Google, Amazon and Yahoo have lost vast swathes
of users’ data with no recovery or compensation. Users with years of email
history, documents, photos and other
irreplaceable files had to write it all off
and start over from scratch.
That’s a tough pill for anyone to
swallow, yet these sites offer precious
little information on how to go about
backing up that cloud data, requiring
end users to deal with it instead.
Editor’s note: if you use Google services and are concerned about this,
check out http://takeout.google.com
which allows you to download most
of your data hosted by Google, easily.
I’m not saying don’t use such services – I make good use of the OneDrive
system that comes with later versions
of Windows. I’m just saying that these
companies typically encourage endusers to forgo local data storage and
hard-copies in favour of using their
all-singing/all-dancing online services. Many users aren’t even aware that
these services can fail, so it is essen-
tial that backups are made and kept
up-to-date.
If that isn’t bad enough, many new
customers of mine are horrified to discover they are not backing up what
they thought they were backing up.
I’ve seen plenty of external drive ‘backups’ with only desktop icons, empty
folders or thumbnail files instead of
original photos copied over.
I try to remedy these situations by
installing and setting up a backup program that takes just three mouse-clicks
to get up and running.
However, while it can be scheduled
to run automatically, there is usually
still some manual input required, such
as plugging in an external hard drive
or flash drive on which to copy the
backed-up data, and people being people, this is the point we usually forget
or simply flag it, convincing ourselves
it’ll be OK for one more day.
If only I had a dollar for every time
I heard that mentioned after a hard
disk failure!
We now resume our regular
service(man)
Back to the bulging laptop. I removed
the screws holding the keyboard in
place (typically hidden under panels
around the back of the machine) and
carefully released the retaining clips to
prise the keyboard out. Surprisingly, no
keys had broken or popped off, some-
Getting to the root cause
Do you have any good servicing stories that you would like to share in The Serviceman column? If so, why not send those stories in to us?
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Please be sure to include your full name and address details.
The connector is similar to a PCB
stacking connector, and a quick browse
on the usual-suspects component sites
revealed that they are available for
only about five bucks.
The problem is that while I could
probably fluff about and fluke soldering one of these things on, getting the
old one off without a lot of collateral
damage would be a real mission.
I know this because I have attempted
Australia’s electronics magazine
siliconchip.com.au
Servicing Stories Wanted
54
thing that often happens when a heavy
object is dropped on a laptop keyboard.
Repairing those little cantilever
plastic ‘springs’ under the keys is
a royal pain, so thank goodness for
small mercies.
Underneath, I could see areas of the
motherboard and the usual peripheral-connecting ribbons poking through
open sections in the top frame. I could
also see where the cup had impacted;
there was a nice dent in the thin metal
chassis. Beside that was a multi-pin
plug that had popped off its socket;
the plug’s leads disappeared off to
the screen, so this explained the lack
of video. It also explained the keyboard hump.
This could be an easier fix than I
thought; all I had to do was panelbeat the bent section of the case back
into its original shape, plug that big
connector back in and it should work.
But you know it’s never going to
be that easy! When I tried to replace
the popped plug, it wouldn’t re-seat,
and on closer inspection, I could see
that the socket mounted on the motherboard was cracked right through,
making each end kinked slightly offline and preventing the plug from going in. Excellent! Of all the places on
this motherboard, the cup had to fall
onto this point.
Before going any further, I had to
remove everything from the case so
that I could straighten the bent chassis properly, and that entailed taking
out the motherboard assembly.
There was nothing special to it, just
a lot of screwdriver time making sure
all the screws were removed (even
the one hidden under the hard disk
and the three tiny ones along the edge
hidden by the CD-ROM drive) before
separating the clips holding the two
halves of the case. I soon had the case
bent back into shape, but I was more
concerned about this 40-odd pin micro-socket with the crack in it.
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stuff like this in the past, and at the risk
of being labelled a man who blames
his tools, I blame my lack of proper
SMD desoldering tools – and the talent to make the best use of the ones I
do have. If this was my motherboard,
I’d likely have a go, but for a paying
customer, I draw the line.
Removing an 8-pin SMD is one
thing, taking off a bonded 40-pin socket like this is another game entirely, especially when it is on a tightly-packed
motherboard.
So I thought I’d check it under a microscope before deciding what to do
next. I could see that all the legs were
still securely soldered and nothing was
really out of place, except for the misalignment of the now-separated hard
resin body of the socket.
The crack went right through it, and
if I pressed in the right places using
some repurposed dental tools, I could
close the crack right up and straighten the socket, likely enough to put
the plug back onto it. But as soon as
I released the pressure on it, it would
open up again.
I made a vague attempt to close the
socket and while holding it closed,
replace the plug with my third hand,
but while it did close with a bit of
pressure, it wouldn’t hold, and without some extra tweaking I knew this
wasn’t going to fly.
Back under the microscope, I could
see the majority of the socket’s pins
siliconchip.com.au
were still straight, with only a couple
on each side adjacent to the crack itself bent out of line.
All the pins were holding the two
halves of the socket tightly, if apart.
I reckoned that if I could straighten
those bent pins, this would relieve the
stress holding the break open, and it
would let me get some glue in there
to close the crack.
I would then just need to hold it
long enough for the glue to cure, and
in theory, I would be able to re-connect
the plug and it “should” work. That’s
a whole lot of “ifs” though…
The biggest problem I faced is that
one drop of glue in the wrong place
and I’d be right in the litter box; the
connector would never go back onto
the socket and if it did, the chances are
that one or more pins wouldn’t make
proper contact.
Considering the size of the component, and the consistency of most of
the glues I have access to that could
bond this type of resin with any
strength, I would have trouble getting
enough glue into the crack without
spilling any over into the surrounding areas. I would also only get one
shot with this method and if it didn’t
work, it would be game over.
After much wringing of hands and
gnashing of teeth, I considered my
only feasible option would be to juggle things enough so I could dry-fit
the plug to the socket, make sure it
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April 2019 55
worked and then spread glue over the
entire plug and socket assembly so it
couldn’t move.
With this method, the elephant in
the workshop is the trouble I would
be in if it ever became necessary to
get it apart again, ie, if something else
should go wrong with the laptop.
Once the plug was potted, it
wouldn’t be coming off again and,
due to the way the connected cable
interacts with other removable parts
of the laptop, that would make disassembling the machine again virtually
impossible.
I decided to put these issues to the
client, who had already been half-resigned to getting a new machine anyway, given she thought this one was
dead.
I called her and told her what I’d
found, and after discussing the options, she was happy for me to go
ahead and try to repair this one, with
the full knowledge that it might not
work anyway, and even if it did our
future repair options would be severely compromised.
Repair time!
With the go-ahead given, the first
thing I did was straighten the pins
out. While I have plenty of microtools for this kind of work, I always
gravitate back to using my array of
dentists’ tools.
These picks, probes, burs and scalers are excellent for electronics work
because they are strong, resilient to
fluxes and solders and very hard. I use
them for everything from mixing glue
to cleaning circuit boards.
Don’t be afraid to ask your dentist
for old ones – they chuck theirs away
regularly, usually regardless of condition because they get brittle with
repeated sterilisation (among other
things) and become a bit dangerous
to use. My dentist has a carton of old
tools and I never leave empty handed
(it is also nice to get something, other
than working teeth, for all that money
dropped there!).
The tools are usually cleaned in the
autoclave before being disposed of anyway, so there are no worries about them
being dirty. I had to promise my dentist
that I wouldn’t use them on my or anyone else’s teeth, and surprisingly, that’s
not a tough promise to keep!
The extremely sharp probes that typically strike fear into the hearts (and
mouths) of patients are ideal for this
56
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pin-straightening business. I used one
to gently coerce the dodgy pins back
into line. This worked better than I
expected and all the pins were equally-spaced and still well-connected
to the motherboard once I’d finished
probing.
The crack in the resin part of the
socket now looked to be just a hairline and the plug fitted back onto the
socket relatively securely. I assembled
the laptop parts on the bench and sat
the battery onto the motherboard’s battery connector.
When I pushed the power button,
the screen lit up and the machine tried
to boot, but because I had no hard drive
in it, I merely got the usual “no system
disk” message.
With that working, I removed the
battery and other bits and tried the
plug again; it was still too easy to disconnect. Usually, it is held quite firmly by friction, but now it wasn’t even
holding stable with the plug pushed
on as firmly as it would go. I taped it
down, mixed up some epoxy resin
and ‘tagged’ it with a good-sized blob
at each corner.
When set, the plug was held in so
it wouldn’t come out, yet was accessible enough so that if I needed to remove it again, I could break the glue.
I reassembled the laptop, and with
everything attached, it booted into
the operating system and worked as
expected.
The keyboard no longer had the
hump, and there was still some wiggle-room should we need to get it apart
Australia’s electronics magazine
again. The owner was happy, I was
happy this fix would last, and everybody wins. Sometimes it is worth having a go anyway, even if the outcome
looks bleak.
Cleaning motherboards
B. W., of Warriewood, NSW lives
near the coast, and a common problem
with electronics (and especially computers) in these humid areas is corrosion and a build-up of dust and other
gunk on the circuit boards.
This eventually interferes with the
operation enough to cause failures.
The solution is to give them a good
old clean and check them over for any
other problems while you’re at it...
I have five PCs making up a broadcast HD editing system. The oldest, a
2003 model with a Gigabyte motherboard and an 8-slot NAS with 16TB
of storage has worked flawlessly for
12+ years, but recently it started getting slower and slower.
Finally, it refused to switch off; then
when I forced it off, it wouldn’t power
back on. While all the power supply
output voltages seemed OK, the motherboard lacked 12V in some locations.
It was time to bite the bullet and
pull out the motherboard. Living on
the coast, many times over the years
various bits of electronic gear have
chucked a wobbly or just stopped and
the reason is usually dust, fluff, hair
and other fine debris that gets deposited on the PCBs, stuck down with a
salt-laden conductive deposit from the
sea breezes we often get.
siliconchip.com.au
Before and after cleaning the PC motherboard; note a few of the ICs had not been re-seated yet.
With the narrow pin spacing of modern ICs, the worst thing you could organise is dumping a conductive matting over and between the tracks and
the pins of the ICs and surface mount
parts.
Many bits of gear are thrown out
just because they have been used in
this environment for several years and
then simply quit working. They usually wind up in the council cleanup.
The simple cure is the get out the
methylated spirits, some old toothbrushes, small art painting brushes,
clean rags, old newspapers, magnifying glasses, a fine bladed scalpel, and
ensure no ignition sources exist.
Pour a small amount of metho into
a lid or other container, and use the
tools to wash/scrub down the PCB
with all the sluiced-off waste going
onto the newspaper.
Use the scalpel and toothbrushes to
very carefully clear between the fine
pins of the ICs. Mop up any leftover
metho with a tissue or a rag; you can
even use a hair dryer to dry it off, ensuring that no metho hides under the
ICs or other components.
Re-assemble the equipment, and
that’s it. While cleaning up this PC using the above method, I discovered a
bloated 3300µF capacitor, so I replaced
that too. Then pow, up it came first go,
and I’m typing this tale on it.
So before you throw any gear out,
give it the big clean; you may be surprised just how well it works, and just
how easy it is!
to fix them but this raises the possibility that these designs are not rugged
enough for our electrical grid...
This problem may be of interest to
your readers as it appears to be a common fault with Philips HR2940 Air
Fryers. I have two units which were
both dead, having no display.
The first problem was removing the
top cover to get to the power board.
You need a long T20 screwdriver as
the screws are deeply recessed. My
photo shows the unit after the cover
is removed, with the power supply
board visible.
The power supply board uses the
ST Microelectronics Viper16 8-pin DIP
flyback switching regulator IC. This
has an internal high voltage (700V)
FET which failed and destroyed the
two 30W resistors feeding it. The fuse
survived(!) It seems that these ICs are
not able to handle the high voltages
they can be exposed to.
Replacement ICs are available from
RS components. I also found that C6
(10µF 50 V) was shorted out on both
Air Fryer power boards. Replacing
the regulators, 30W resistors and 10µF
capacitors got the units back up and
running. Note that the power board
will not produce any output unless
it is connected to the control/display
board.
While I had the units open, I also
added a metal oxide varistor (MOV;
blue disc) across the 30W protection
resistors at the IC’s high voltage inputs. It should reduce voltage spikes
getting to the Viper16 IC. I am hoping
that this will prevent similar failures
in the future.
There is a similar problem with
some Toshiba TV power supply
boards. These use a similar high voltage 8-pin DIP IC (ICE3B0365) for the
5V standby power supply. These are
also made by ST Microelectronics. I
have three boards where the same IC
SC
has failed.
Philips air fryer repair
R. S., of Fig Tree Pocket, Qld has
multiple failed power supply boards
exhibiting the same fault. He was able
siliconchip.com.au
Close-up of the power supply board used in the Philips HR2940 air fryer.
The only IC (a Viper16) in the unit had failed due to high voltages.
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April 2019 57
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