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SERVICEMAN'S LOG
Two devices what failed th’idiot test
Dave Thompson
Murphy’s Law (the real one) says: it’s impossible to make anything idiotproof because idiots are so ingenious. Or to put it another way, you make
it idiot-proof and then they make a better idiot.
This seems to be the case with both
the items I repaired this month. In each
case, the user (or one of their family
members) managed to break it by doing something you’d think it would be
designed to cope with.
A while ago, a customer picking up
her PC from my workshop noticed a
few of my electronic bits and bobs lying around.
She asked me if I knew anything
about blood glucose monitoring devices. I immediately responded that since
customers bring them in all the time, I
was an expert at repairing them, and I
knew them inside and out.
Actually, sorry, that’s a lie. What I
really said was no. While I had seen a
few from afar, I had never played with
them to see what made them tick. I decided to gloss over this technicality,
though, and instead asked what the
problem was.
She said that as a diabetic, she
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needed such a machine to check her
blood sugar levels. While her older,
basic model still worked fine, she had
shelled out a considerable amount of
cash on a new, more sophisticated version, which she couldn’t get to work
correctly.
Perhaps I could have a look at it and
see what I could do. Well, you know
me, I had to at least have a go...
When she brought it in, I was a little shocked at what she reportedly
paid for the monitor. Though it looked
like a quality, well-made unit, and
came in a very nice travel case, there
just wasn’t that much to it to justify
the huge price tag. Having said
that, if it worked as intended,
it would be an ideal tool for
managing her diabetes.
The blood sugar monitor is a small, hand-held
unit about the size of a
pocket watch, with a
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large, clear liquid-crystal display taking up most of the front face.
On the top edge of the case is a receptacle for removable test strips. On
the right-hand side of the case is a
small sculpted gap, which looks like
a socket for some kind of expansion
module, and on the bottom edge is a
mini USB port.
That’s pretty much it; there are no
switches or any other features to complicate things.
This unit can connect via Bluetooth to a smartphone (or Bluetoothequipped laptop/PC), or to a PC via
the USB socket. The smartphone app
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Items Covered This Month
•
•
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Two faulty Blood sugar
monitors
Olympus camera with a
smashed viewfinder
iPhone 5S battery replacement
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
and the downloadable software for
the computer (both accessible via a
QR code included in the package) do
pretty much the same thing, ie, save
a record of all readings gathered by
the device and present it in a graphical format.
This enables the user to track their
blood sugars, to see at-a-glance what’s
happening, making things a bit easier
to manage. It is a clever little device.
But it didn’t work, and as it was purchased over a year ago, it was out of
warranty.
Most of these monitors operate in
much the same way. The test strips
look like a small rectangle of plasticcoated PCB material with exposed
contacts at one end and a sensor track
running down the middle. One is inserted into the slot at the top of the
device and this action powers the
machine on.
A drop of blood from a pricked finger is presented to the tip of the test
strip, and this is drawn down the centre track by capillary action.
After a short countdown, a blood
sugar reading is shown on the display.
Usually, the monitor loses this information when the strip is removed and
the device powers off, though with
this model that data can be shared to
a phone or PC.
A lucrative business model
Some of these machines can read
both glucose and ketones levels. As
these tests use different test strips,
there has to be a way of telling the machine which strip is being used. The
way they accomplish this is by plugging in a module, which looks very
much like a USB dongle for a wireless keyboard or mouse, into that PCB
socket I mentioned above.
When a customer buys a container
of test strips, a module is included
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that is designed to work only with that
particular monitor and set of strips.
This is how the machine knows what
it is measuring, and in this way, the
manufacturer can guarantee reasonable accuracy.
Each batch of strips and the module
carry a unique identification number,
and as long as these all match, the
monitor readings will be as accurate
as a home-use machine can get. So
you can use one strip and module to
measure blood glucose, then swap
the module and the strip and test for
ketones.
Mind you, quality test strips aren’t
cheap. I get the feeling that manufacturers of blood monitors took a leaf
from the inkjet printer manufacturers’ playbook; they must make most of
their money from sales of the consumables. And just like an inkjet printer,
you can’t use test strips or modules
from company A in the monitor made
by company B.
Clearly, there is big money to be
made in health products, and all power
to the people who design and market
this stuff. But diabetics (here in New
Zealand, at least) are offered little to
no government subsidies for medical
appointments, or any of the kit they
need. It seems rather unfortunate that
they charge as much as they do.
But regardless of cost, no device is
any good if it doesn’t work. In this case,
the customer reported that it powered
on when a test strip was inserted,
but did not detect the strip module.
The monitor was not detected when
plugged into a PC via the USB cable
either. I suspected that these two problems would have the same cause.
The first thing I did was check the
battery. There have been many times
I’ve swapped cells out of a unit, to
check whether it just needed a fresh
battery, only to find that the cells I put
in were already dead!
Convenient though this solution
may have been, both of the CR2032type lithium batteries (20mm diame-
ter, 3.2mm thick) measured a healthy
3.1V on my analog multimeter; more
than enough to fire it up.
Opening it up was easy enough; a
couple of tiny screws hidden beneath
rubber ‘feet’ hold one end of the back
cover while a clip arrangement holds
the other. Once open, I could see a potential problem straight away. Of the
four pins for the removable test-strip
module, which is simply a set of exposed pins, two were bent.
With the module in place, these pins
weren’t making contact. The alignment of the module depends on how
it is inserted into the cavity in the side
of the case. Like a USB connector, it
can only go one way. But given the lack
of an actual socket frame or guide the
module should line up with, it is easy
to insert it cock-eyed.
It looked to me that this is what happened. If it were forced in the wrong
way around, that would explain the
bent pins and lack of function. You’d
think the manufacturer would have
considered that and offered some protection against such a simple mistake
‘bricking’ the device.
Luckily, straightening the pins was
no real problem. I just had to be super-careful not to bend them too many
times; this type of material is easily
work-hardened, and it will break if
pushed too far.
I prefer to use tweezers for this sort
of job because they prevent me from
exerting too much pressure on the
metal. I try to flex the pins only far
enough to line them back up, and take
great care not to overshoot and have to
bend them back the other way. That is
a sure-fire way to snap something off.
This was a simple straightening
job, and when finished, I immediately
plugged in the module and made sure
everything worked before buttoning it
back up again.
When I described what I found to
the client, she recalled her teenage
son had assembled the monitor when
she first got it, and it was most likely
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Australia’s electronics magazine
December 2019 77
he who had first inserted the test-strip
module incorrectly.
It was relatively simple to download the app into her phone, and I
installed the PC program and drivers
from the links provided, so I could
check that the machines all talked to
each other. To my knowledge, she is
still using it and has reported no further problems.
Repairs always come in twos
I’m no stranger to odd coincidences.
Back when I was a poor apprentice, my
tooth broke. Later that day, I discovered enough money to cover the bill to
fix it in a jacket pocket I hadn’t worn
for years! Other times, I’ve thought
of clients I haven’t heard of for years,
then they call the next day, wanting
work done.
I’m busy figuring out how to capture and bottle this phenomenon and
when I do, you’ll find me kicking back
on Easy Street!
So, not a week after that last repair,
another client asked me about fixing a
water-damaged blood sugar monitor. I
thought it strange I’d never fixed one
before and now, within a week, I have
two coming through the workshop.
This monitor was a very basic model, slightly older than the previous one,
with fewer features and predominantly used for measuring ketones in the
blood. This is useful for those on a socalled ketogenic diet – a high-fat, low
carb diet which is used to get the body
to burn ketones for energy instead of
carbohydrates. The things we learn as
servicemen!
In order to know if the diet is working, many people turn to electronic
blood monitors that can give reasonably accurate readings of blood ketone levels. If these numbers are maintained, fat loss (and the weight-loss
that goes with it) is the typical result.
This customer was standing near
the kitchen sink with their monitor
and had accidentally dropped it into
the dishwater, whereupon it immediately ceased working. Despite putting
it straight into the hot-water cupboard
and leaving it for the past month, it
still didn’t work.
Liquid-damaged electronics are
tough to diagnose. Sometimes everything starts working again after
they dry out; other times, the device
remains dead forever, regardless of
whether a bag of rice, a hair-dryer or
some other method is used to dry it
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out. Two identical devices could be
submerged in the same circumstances
with different outcomes.
I typically explain this to the client and let them make the call as to
how we deal with it. Given that you
can pick up very cheap blood monitors out of China, it makes no sense to
throw a whole lot of money at repairing an older, faulty one. So we have to
decide how much effort (and money)
it’s worth expending on a repair before we pull the plug and chuck it in
favour of a new one.
The customer had a new box of 100
test strips made specifically for this device, so it made sense to put a nominal amount of cash into at least trying
to repairing it.
Another easy fix
Opening it was very similar to the
last monitor, except this model used
four small screws to hold the cover on.
Once the back was off, I took the board
out and checked under a microscope
for obvious signs of water ingress.
Though this was a relatively inexpensive model, they sure packed a lot
onto the PCB. It was made with almost
all surface-mounted components on a
double-sided circuit board.
Water under any of these components could cause it to malfunction,
and getting any residue out could be
a major headache. But it was surprisingly dry inside, and I couldn’t see
any evidence of water ingress. So why
didn’t it work?
I started at the beginning, or at
least the electrical beginning, with
the contacts at the top where the test
strip connects. On closer inspection,
these looked very oxidised and patchy.
While they appeared to be gold-coated,
I guessed the actual gold content is a
little lower than contacts in a higherquality monitor.
Whatever other compounds were
mixed in with it had tarnished. I used
isopropyl alcohol and a light rub with
my fibreglass-bristled cleaning pen to
bring them back to the gold standard.
I also checked the module pins – the
module was still in place, and these
too had a look of intermittency about
them.
Cleaning that was a little tricky, especially the contacts inside the module, but a few strips of alcohol-soaked
tissue flossed carefully among the various pins and contacts had them looking better.
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I installed new cells and broke out
a fresh test strip. This time when I
put it in, the display powered up. It
looked a little blotchy, but it worked
and displayed legible characters, so
that was a lot more than what it was
doing before. I pricked my finger and
fed the test strip; apparently, I wasn’t
in “ketosis”, but I didn’t expect to
be, so the reading was most likely
accurate.
To be thorough, I removed the cells
and module and put everything in a
bag of rice in the airing cupboard for
a week, in the hope of leeching any
remaining moisture out of the parts
before returning it to the customer.
As far as I know, he is still using
it, working his way through the test
strips he has left. If he still wants a
new monitor after that, he won’t feel
so bad about wasting the money spent
on strips.
Olympus camera smashed
viewfinder
B. W., of Sydney, NSW, had that
dreaded moment where he accidentally dropped the bag containing some
delicate electronics and heard a nasty crunch. Luckily, he had a piece of
donor equipment and the patient survived the operation...
It all started when I was hurrying
along a Melbourne train platform with
my lovely old Olympus C8080W in its
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carry bag, the strap over my shoulder.
The strap slipped off my shoulder and
down it went onto the pavement. My
first thought was that the glass in the
wide-angle lens could have smashed
on impact.
On opening the bag, I could see
that the digital viewfinder glass was
cracked and the LCD screen behind
it was showing tell-tale black areas
where the liquid crystal had leaked
out.
While the bag is padded to handle
short drops and other impacts, unfortunately, the lens cap had been pressed
into the viewfinder, resulting in this
damage.
The camera has a second internal
viewfinder but while this worked in
playback mode, it no longer worked
when I tried to take a photo. Perhaps
the damage was shorting something
out. Regardless, I would have to fix
the smashed screen.
I had another identical camera
which no longer worked but the screen
was intact, so I decided that this would
become a donor.
My pal Dick from the Yahoo Olympus Camera Group sent me a pictorial
breakdown PDF of the camera internals so that I could see the disassembly
steps required. I would need a set of
tiny screwdrivers, tweezers, close-up
eyeglasses, good lighting and a cautious approach to succeed.
I started to take the camera apart
and it all went well. Finally, I had
the LCD screen out of the articulated
holder but still connected to the feeder PCB hiding just inside the holder,
with two flat ribbon cables still firmly attached.
The next step was the most delicate;
if I made a mistake by forcing any of
these fragile and tiny components,
the whole repair and the future of this
camera could be in jeopardy.
The ribbon cables were sensibly attached to connectors on the partly hidden PCB, still inside the articulated
carrier. I gently nudged them as best I
could but they would not budge and
there was nothing obvious to pull or
push on the sockets to remove the cables. I had to turn to the internet for
answers.
I found the following YouTube video from a German guy who was doing just what I needed to do, on the
same model of camera. His lighting
was poor and the camera angle was
not great but just once, he showed a
pull of a locking black bar across the
top of the socket and the ribbon cable
then came free! See: http://youtu.be/
uyCVRY9Z1h0
So that was it! Now with confidence
and armed with a dentist’s hooked
tool, I ventured into the hidden cave
of the PCB and hey presto, the socket
opened up, allowing the ribbons to
slide out and the donor ones to go into
place with ease. I then re-locked the
ribbons into the sockets, re-assembled
the camera, inserted the battery and
switched it on. Hooray, the viewfinder
was operational!
I then just had to clean the display,
re-fit the protective glass panel and
then make some changes to my carry
case so this sort of damage will never
happen again.
the back and sides of the phone. It all
felt “squishy”, so I suspected that the
battery had become swollen and was
pushing the screen out.
My wife had also remarked that
the battery was tending to run down
quickly, which strengthened the swollen battery hypothesis.
A swollen lithium-ion battery is a
fire risk, so until a new battery could
be fitted, I found a large Pyrex bowl
that we could put the phone in while
it charged, to prevent it from igniting
anything else if it caught fire.
The Apple store charges $119 to replace the battery in this model, which
is more than the phone is worth, and
it probably couldn’t be done while
we waited.
There are various phone repair stalls
in arcades and shopping centres, and
they charge about $35 to replace an
iPhone battery, but I decided to have
a go at it myself first.
Despite some misgivings, I bought a
new battery from eBay which was advertised as “brand new genuine original”. It cost just under $18 delivered,
including a full set of tools and the allimportant adhesive strips, and I had
it in less than two days. I was pleasantly surprised at the quality of what
I received.
The iFixIt.com guide for iPhone 5S
battery replacement estimates it will
take between 30 minutes and an hour.
It took me closer to two hours, but
that’s because I read every single comment that individual fixers had made
iPhone 5S battery replacement
A. P., of Concord, NSW obviously
loves a challenge because he had the
option to pay someone else a small
fee to fix his wife’s phone but decided to do it himself anyway. Luckily, it
worked out well in the end...
My wife recently told me that her
iPhone 5S was showing “rainbow
colours” wherever her finger touched
the screen.
I took the phone out of its protective case and observed that the bottom
edge of the screen was pushed slightly
out of the aluminium shell that forms
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Australia’s electronics magazine
December 2019 79
on every single step; I’m glad I did, as
they almost certainly saved me from
breaking something.
The first step when the battery is
swollen is to discharge the phone’s
battery to no more than 25%, to minimise the risk of the battery catching fire if ruptured. The phone was
at 83% charge when I started, so I set
the screen to full brightness, turned
on the torch function, and set AutoLock to “Never”.
I used the time while the phone battery was discharging to read through
some of the steps of the repair and the
associated comments, but after half an
hour and with the battery still at over
50% charge, I became impatient and
powered the phone down, ready for
the dismantling process.
The iPhone 5S case consists of
a one-piece aluminium tray which
forms the back and edges of the phone.
The front panel squeezes into the tray
and consists of the display, its narrow
plastic bezel, and metal clips which
grip the inside edges of the tray. The
tray holds most of the electronics and
hardware of the phone, including the
battery.
There are some flat cables near the
top of the phone that connect the display and front camera and sensors to
the motherboard. There is almost no
slack in these cables, but the display
can be pivoted up 90° with these cables
still connected, giving pretty good access to the interior of the phone.
There is one other flat cable, near the
bottom of the phone, that connects the
home button/Touch ID sensor to the
motherboard. There is enough slack
in this cable to allow the bottom of the
display to be lifted a couple of centimetres away from the tray, which gives
sufficient access to disconnect the cable from the motherboard.
To start with, I removed the two pentalobe screws at the bottom, on either
side of the lightning socket.
The home button cable is particularly prone to being torn in this model because the front panel is meant to
be quite a tight fit in the tray and can
come away suddenly. If you damage
the cable, you have to replace the home
button, but only the original home button is “keyed” to the motherboard so
you’ll lose the Touch ID feature.
As I started pulling the two halves
apart, I noticed that the display was
separating from the metal clips.
The iFixIt crowd-advice for this sit80
Silicon Chip
uation is to ease the metal clips out of
the tray using two plastic tools shaped
like guitar picks.
These were supplied with the new
battery, and I found that by using a
combination of fingernails to do the
pulling and inserting the picks into
the gaps to prevent them from closing
up, I was able to ease the bottom of the
front panel up out of the tray without
too much trouble.
The next step was to remove the clip
that secures the home button cable’s
plug in its socket on the motherboard.
Having removed the cable, I discarded the clip as I realised that it would
be awkward and risky to reinstall it.
I read comments from those who had
done likewise and found that the cable
nevertheless remained secure.
I then popped the home button cable off the motherboard using the corner of a spudger and was able to lift
up the bottom of the front panel, with
the remaining flat cables at the top of
the phone bending like a hinge.
The battery was now fully exposed,
and I could both see and feel its swelling. The new battery, by way of comparison, was perfectly rectilinear.
At this point, iFixIt guides you to
remove the display, touchscreen and
camera/sensor cables from the motherboard, thereby separating the front
panel from the phone.
This would have required dealing
with another four tiny screws in three
different sizes (1.2mm, 1.3mm and
1.7mm) that must all be put back in
the correct holes during reassembly,
or else risking permanent damage to
the motherboard. I felt that I had good
enough access to remove and replace
the battery without bothering to disconnect these cables, so I skipped
ahead to the battery removal.
The battery connector is secured by
a screwed-down clip. This was easy
to remove, and I then used a spudger
to pop the battery connector off the
motherboard.
Even this apparently easy step has
a gotcha: it is difficult to see whether
you have inserted the spudger between
the battery connector and its socket,
or between the socket and the motherboard. Prying too hard when the
spudger is under the socket is liable
to damage the motherboard.
The next step is to remove the old
battery, without using sharp metal
tools that could puncture it. The battery is secured to the tray by a couple
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of double-sided adhesive strips. These
strips emerge from the lower end of
the battery and join to a pull-tab that
is usually tucked into the space at the
lower edge of the battery.
You pull slowly on the tab and the
adhesive strip narrows and pulls away
from the space between the battery
and the tray. To make removal of the
adhesive strips in this phone easier,
iFixIt suggests putting the phone on
something warm to soften them first.
I microwaved a damp face flannel
in a plastic bag and laid the phone on
top, then teased the pull-tab out from
the gap at the lower end of the battery. There is a small hole in the tab,
and the tiny Philips head screwdriver that came with the battery let me
pull it out far enough to be grasped
in my fingers.
Then I pulled gently on the tab, just
enough to see the two white adhesive
strips start to come out from under the
battery. At this point, I snipped the tab
in two using nail scissors so that there
was a separate tab for each of the two
strips – this lets you deal with each
strip separately.
Next, I pulled a little bit more firmly on one of the tabs. The trick is to
pull firmly and constantly, but to be
patient. It also helps to continually
work your fingers along the strip towards the battery as the strip stretches, as this minimises the chance of the
strip breaking.
In my case, both strips snapped before they were completely out, so I was
left with the unenviable prospect of
levering out the battery while avoiding bending it too much lest it rupture
and catch fire.
To do this, I used a plastic spudger
and used the same principle of firm,
constant pressure and patience. By applying not quite enough force to perceptibly move the battery, and waiting,
the battery came free without being
deformed. Once the battery was out,
I was able to clean up the remains of
the adhesive strips.
The replacement strips have blue
protective film on the side that is to
be installed facing the tray, and pink
film on the side that faces the battery.
After sticking the new battery into
the case, reassembly was straightforward and the front panel now fit precisely. The phone works fine with
its new battery, and the rainbow colours surrounding fingers touching the
screen are gone.
SC
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