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SERVICEMAN'S LOG
Chasing wild geese isn’t as fun as it sounds
I don’t know about other servicemen, but there
always seems to be something in my household
that needs fixing. I’m not just talking about
stuff I encounter in my day job, or even the
computers or phones in the office that get
messed up with updates or apps that don’t
work. I mean those domestic jobs that always
crop up that often need a serviceman’s touch.
For example, we were experiencing
an intermittent problem with some of
the devices in our home theatre system.
Now and then, we’d lose power and
while the TV still worked, the amplifier and disc player would go dark.
All the plugs were fully pushed into
a four-socket power board, except the
TV, which plugged in further along
the wall.
It didn’t take long to discover that
this power board suffered from the
same problems that I’ve seen readers
mention in several letters published
in Silicon Chip; in other words, it was
cheap, nasty rubbish. A tap with my
foot on one edge of the board resulted
in power dropping out. Another tap in
a different place restored it.
I couldn’t be bothered tearing it
apart to find the root cause; I’ve been
down that road before and there is typically nothing fixable inside anyway.
What really ailed it was poor design
and shoddy manufacturing.
siliconchip.com.au
I solved the problems by replacing
the power board with a new, betterquality model. While this issue was
easy enough to deal with, it still took
time and effort to track the fault down.
There was a more trying example
recently when we awoke to lukewarm
hot water and struggled to get in a couple of showers before the water was
too cold. This is unusual as we are on
a night-rate power plan; heating our
water overnight takes advantage of
the much cheaper off-peak electricity rates. While this usually works
out well, something appeared to have
gone awry.
As usual, my serviceman brain immediately kicked into gear, mentally
troubleshooting the possible causes.
But there were some “wild card” factors muddying the waters. Around
ten months ago, it was announced
the drinking water in Christchurch,
long prided on being the clearest and
cleanest in the world (if local lore is
to be believed), was to be chlorinated.
This caused quite the backlash from
the masses, including me, who strug-
Australia’s electronics magazine
Dave Thompson
Items Covered This Month
•
•
•
•
•
Cold showers in Christchurch
BWD 275 dual-range 36/72V
power supply repair
Static from a Codan X2 highfrequency transceiver
Cordless vacuum repair
A not so steamy kettle
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
gled with the reasoning behind it. Due
to a gastro outbreak in a city in the
North Island – the result of contaminated tap water – our local council got
spooked and decided that for the public good, chlorine must be introduced
immediately into our water supply.
What that outbreak had to do with
us, a whole island and a half away,
baffled me.
I suppose that any of the hundreds
of bores that tap vast aquifers deep under Christchurch might suffer the same
fate as those ‘up north’, requiring the
bore’s hardware (some of which dates
back almost a hundred years) to be replaced (no doubt at a huge cost to the
taxpayer). But adding chlorine to our
water just seems like a solution looking for a problem.
To placate the nay-sayers, the council claimed chlorination would only
be required for a short period, and
only in a few problem areas while all
the bore heads were tested and/or upgraded. It all sounds plausible, especially as the quakes might well have
had some impact on the state of these
aquifers and bores.
But the latest news is that the water could be chlorinated for years,
Christchurch-wide, which is just adding to everyone’s anxiety over the issue.
Anyway, the point to this backstory is that since this chlorination
program started, more than 2000 hot
January 2019 61
water tanks in homes around the city
have corroded through and been ruined, apparently by the chlorine in
the water. This number doesn’t take
into account the hundreds of plumbing leaks and pipe failures that are
also attributed to the chlorination of
the water supply.
Now I’m no plumber or water-tank
guru, so I can’t say for sure if this was
a just glitch in the matrix (ie, a coincidence) or merely a problem with some
older pipes and cylinders, of which
there are likely many still around
Christchurch.
Either way, it’s an unexpected boon
for water heater installers and manufacturers. The rest of us are mostly
just concerned about how our own
cylinders and pipes will fare in this
situation.
The game is afoot
Of course, chlorine-driven corrosion
sprang to mind as a possible cause for
our lack of water. The first thing I did
was to make sure that we didn’t have
a new indoor swimming pool beneath
the hot water tank.
The second thing was to check the
breaker at the switch-box to make sure
it hadn’t tripped. Everything looked
OK, so with those two causes ruled out,
I’d have to look further afield.
Now before I get flamed by those far
more knowledgeable than I am about
low-pressure home hot water systems,
let me qualify my troubleshooting process with the fact I know next to nothing about how it all works. I realised
there could only be a few possible
causes of no hot water, the most obvious of which would be the heating
element itself failing.
The element in our heater is a resistive immersion type, so its continuity
should be easily measurable, and the
wiring to, and within, the heater panel should ring out as well. I’d need a
multimeter for these tasks; I chose my
analog model as it is easier to read in
tight corners.
I then did what all servicemen love
to do; break out the tools and remove
whatever covers I could get off in the
hope I’d see something really obvious,
such as soot deposits, a broken wire
or a blown fuse. Maybe I’d get lucky!
The water heater looked to be relatively new and sits in a cupboard upstairs. I’m guessing it replaced the uninsulated, low-tech, late-fifties original
when the house’s second storey was
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added in the mid-nineties and everything was relocated from downstairs
to the upper level.
I removed the large, circular “biscuit-tin” lid that shields the wiring
and electrics. This is held on with
two diametrically-opposite PK style
screws, attaching it to a round housing that is spot-welded to the side of
the cylinder.
Once the screws were removed, it
was relatively easy to pry the cover
away with the edge of a screwdriver
(you could use your fingernails if they
are tough enough!).
As the shaft for the thermostat control protrudes through the cover, the
temperature-setting knob must also be
removed for the cover to come away
completely. In this case, the knob just
pulled off the pot shaft with a little
outward pressure. Once the cover is
off, the wiring to the element and thermostat is very easy to access.
Everything looked perfect, as if it
had been installed yesterday, so no obvious fault presented itself here. As I
was checking this during the day, theoretically there shouldn’t be any power
present on any of the terminals, but
while I might sometimes be an imbecile, I’m not insane, so I tripped the
breaker at the switchboard.
And though there is an isolating
switch on the wall of the hot water
cupboard, I wasn’t about to take it on
faith that it was wired correctly either.
Instead, I used my mains-detector tool
to check for mains-level voltage in the
wiring at all the points from the wallswitch to the element.
When the tool started screaming at
me, indicating voltage was present, I
considered my caution justified.
However, I know from experience
that this tool can sometimes be too
sensitive. I suspected it was picking up
stray emissions from a mains-wiring
loom that ran through the floor cavity just beneath the heater cupboard
on its way to the main switchboard
downstairs. In reality, I couldn’t get
anywhere in the cupboard without the
detector going off.
To be 100% sure whether mains
voltage was present, I’d have to measure it, so after removing the two retaining screws for the isolating switch
plate and dropping it clear of the wall,
I used my multimeter to ring out the
system.
I measured zero volts on all points,
regardless of the wall switch or therAustralia’s electronics magazine
mostat control’s position, so I was confident there was no power flowing to
the heater and that my detector was
indeed picking up stray emissions.
With everything now electrically
dead, I removed one of the Active leads
from one side of the element and with
my meter set to the ohms range, measured the element itself.
This type of element actually has
four terminals; I assume that there are
two separate-but-identical elements as
they were wired in parallel, with each
pair of terminals bound to the adjacent
pair with heavy brass links.
All I needed to do was put a lead
on each bus bar to measure the resistance. I got a reading of around 12W.
I didn’t know what it should be, but
that sounded about right.
At least it wasn’t open circuit, and
as the main breaker hadn’t blown, I
knew it was unlikely to be shorted
out. I also tested the thermostat and
it clicked in and out fine, with continuity from the power leads to the elements when it was on.
Since I had reasonable element resistance and all the wiring looked good
to and from the switch plate, and with
the switch properly isolating the mains
feed to the system, nothing appeared
untoward here. If there was no power
getting this far, there must be something else somewhere upstream preventing it from getting to this point.
Doing a sparky’s leg-work
I digress now to another back-story
that may have a bearing on this problem; when we renovated this house,
we replaced a lot of the ropey old wiring we found in the walls and ceilings
with new cables. I did most of this
work under the careful scrutiny of a
licensed electrician.
He’d just had surgery and couldn’t
do the monkey work, so I did it all
while he sat watching, drinking lots
of coffee, all the while telling yarns
and talking the usual tradie rubbish.
Once I finished each job, he’d hobble
over, check and sign off on whatever
I’d done.
When the water went cold, I had
a sudden thought that I might have
messed something up wiring-wise
and it had failed. While it wasn’t all
that likely, given we are now two
years down the road from doing all
that work, the possibility did cross
my mind.
With the fuse and wiring apparently
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OK, there wasn’t much left to check
on. What I did next was what I usually
do when I need to know something; I
phoned my friend, Google.
I searched for and found a link to
the New Zealand Standards for Storage Water Heaters, but after downloading the file and discovering it was
only a preview and that they wanted
$61.20 for the actual PDF, I widened
my search instead.
Fortunately, I found many installation brochures for heaters similar to
ours and most included schematics
and wiring diagrams for installers. Just
what I needed!
With my newly-acquired knowledge, I looked at the system again. It
seemed to me that if no power was getting to the switchboard, and then on to
the heater, there could be something
wrong with the ripple-control system,
part of which is located in the meter
box on the side of the house.
In the two years we’ve lived at this
address, this was only the second
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time I’d opened that box. The meter
was changed for a smart meter just as
we moved in (and had a wire fall off
the pole fuse, as described previously in Serviceman’s Log). Since then,
nobody has had cause to disturb the
contents.
The tone control blues
Sitting next to the meter in the box
is the ripple control relay. This heavyduty contactor controls when the hot
water is switched on, based on a signal superimposed on the mains power
waveform.
When the signal is received, the relay turns on or off as instructed. Clearly
if this was playing up, and failing to
switch on at the start of the off-peak
period, we’d get no water heating.
The trouble was, I couldn’t think of
any way to test it other than to check
whether there was power to the heater
element when there should be power
to it – ie, during the off-peak period.
But the point of the tone control sysAustralia’s electronics magazine
tem is that it can vary from day to day
(or more realistically, night to night).
Precisely when that should occur on
a given evening is anybody’s guess.
Ripple control has been used for
years in most big cities to prevent the
electrical system from being overloaded. If everyone in the neighbourhood
turned their water heaters on at the
same time, something would blow out
at the sub-station.
To avoid this, the ability to heat
water tanks on-demand was removed
from the consumer and instead, households would be assigned certain times
that their cylinder would be switched
on and off, all controlled by ‘the man’
somewhere out on the grid. In practice, this works very well, but it makes
things tricky when an amateur like me
wants to test the system.
Given that we’re on a night-rate
plan, I could stay up all night next
with a multimeter across the element,
waiting for signs of voltage as the ripple-control instructs it to switch on.
Or I could poke about the various terminals on the ripple control hardware
in the meter-box during the day to see
if (maybe) there was power going in,
ready to be switched to the cylinder,
or not.
However, neither of these options
seemed particularly attractive, especially given my reluctance to be electrocuted while playing around with
high-voltage hardware, about which I
know next to nothing. I closed the meter box and resigned myself to getting
my electrician friend to troubleshoot
the system for me.
This was bad news in many respects, not the least of which was the
fact we’d likely not be showering for at
least the next day while we waited for
the electrician to get his rear end into
gear, so it was with some reluctance
that I fired up my computer again to
find his number.
Getting to the bottom of it
However, shortly after my machine
woke up, an email alert popped up
advising me I had a communication
from my electricity provider.
When I downloaded and read the
email, all became clear. The message
was an apology, detailing how they’d
been having problems with their network and that some households would
not have water heating at the usual
times, or at all.
This was good news, as it meant that
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all we had to do was wait, and theoretically, it would all just work again
– as long as I hadn’t messed anything
up while stumbling around in the figurative darkness!
The next morning, it was gratifying
to feel the hot water back up to temperature. Typical serviceman that I am,
I just assumed something had to have
failed, or gone catastrophically wrong
for the system to have gone down and
that I had to get into it to find out why.
In the end, all I had to do was nothing.
The serviceman’s curse strikes again!
BWD Power supply repair
J. C., of Murrumbeena, Vic, loves a
challenge. He recently acquired two
BWD power supplies for free. That
sounds cheap but it was because neither of them worked! Here is how he
fixed the BWD model 275 power supply...
The BWD 275 would switch on but
did nothing else; the current and voltage controls didn’t do anything and
the output voltage was zero. I took the
covers off and had a look for clues of
which there were three: one transistor was missing (and all of the others on the circuit board had been replaced), two of the four screws holding the transformer down were missing and the ammeter pointer had been
repaired.
I found two suitable screws and
fixed the transformer securely. The
missing transistor was a JFET that the
circuit diagram said was a “Selected
Component”. It is used as a constant
current diode in the +16V section of
the auxiliary supply. I made a replacement +16V supply on a piece of Veroboard with an LM317 voltage regulator, two resistors and a trimpot.
To fit this, I had to remove two other transistors and two resistors from
the main board. Turning on the power supply revealed that the +16V rail
measured 0V.
Next, I checked the 30VAC output
from the transformer to the auxiliary supply. That measured zero too.
When I touched one of the wires,
it was loose, every strand broken. I
stripped it, tinned it and re-attached
it and then the power supply started
working again.
I don’t know why two transformer
mounting screws were missing. Maybe it was a botched repair attempt,
prompted by the failure of the JFET.
There were marks to show that they
siliconchip.com.au
were originally fitted and without
them, the transformer moved a little
bit every time the power supply was
picked up and put down. This caused
the short wires to flex at the circuit
board end and eventually break.
Because all of the other transistors
had been replaced, including two other “Selected component” JFETs, I had
to change one resistor to get the Vmax
for the 36 and 72V ranges set correctly. At the same time, I replaced the respective trimpots with 10-turn types.
The ammeter also required a resistor
change to allow accurate adjustment of
the two ranges. I had forgotten about
the repaired ammeter pointer. It broke
again when the pointer went full scale
very quickly.
I re-glued the broken pointer and
changed another resistor and was able
to adjust the maximum current ranges
such that the pointer won’t break itself
again (hopefully).
I later noticed that the Vmax settings
became intermittent and I suspected
that IC1 was the culprit; it contains six
transistors arranged as two differential
amplifiers. I pulled it out of its socket
and cleaned its legs with a glass fibre
brush, applied some contact cleaner
and re-installed it.
The problem went away. This is
why I’m not keen on IC sockets; they
tend to become intermittent after a
few decades.
I learned a few things during this
repair. The three JFETs in the circuit
marked as “Selected components”
were chosen at manufacturing time
based on the Vgs (gate-source voltage
switch-on threshold). Without knowing what this was and the Vgs of the
replacement FET, you will have to
change some resistor values to get the
circuit to work correctly.
Also, before setting the Terminal
Switch to “SET I”, it’s a good idea to
connect a 5-10W power resistor across
the output terminals and set the Terminal Switch to “USE”, to verify that
the current control does what it’s supposed to do. In the “SET I” position,
it connects a 0.1W resistor across the
output and if something is wrong, this
makes it easy to blow the fuse or even
the output transistors.
Cold weather Codan X2 HF
transceiver fault
R. M., of Sydney, NSW, got a bit of
a shock as he was driving along when
his HF transceiver decided to give him
Australia’s electronics magazine
January 2019 65
a blast of static for no particular reason. This very annoying fault would
have to be addressed so despite being
a relative amateur, he decided to have
a go at fixing it...
I’m not what you would call a technician but from a very young age, I’ve
had an interest in electronics. As a licensed amateur radio operator, I have
just enough electronics knowledge to
do simple repairs to my own equipment. For more complex repairs, I turn
to my friend for help, a very experienced technician.
So, when a strange intermittent
fault developed in my Codan X2 transceiver, I thought I might have a go at
tracking it down. The Codan X2 is a
25-year-old 10-channel commercially
made 100W HF transceiver which I
use with my amateur radio Automatic
Packet Reporting System (APRS). This
allows my family and friends to keep
track of my movements via the internet when I’m travelling.
I had to make a few minor modifications to the Codan X2 to interface
it with a Byonics Tiny Track 3 APRS
kit. When on the move, it turns the
X2 on, transmits a position information packet, then switches it off again.
This is an excellent arrangement as it
conserves my vehicle’s auxiliary battery, which powers other equipment.
I have been using this arrangement
for about two years. Most of the time
it works perfectly, however, the X2
always has had one strange fault that
caused it to intermittently break the
mute and open the speaker at full
volume. As is typical of intermittent
faults, it would never appear when the
X2 was on the bench.
I tried varying the supply voltage,
changing the antenna, transmitting,
turning it on and off, but they all had
no effect. The system would run perfectly for days just sitting on the bench.
Months would go by without the fault
appearing then suddenly there it was
again, the audio at full volume blaring away.
Every week I travel from Sydney
to the Southern Highlands of NSW
to work on my parents’ property. My
truck sits outside for a day or two, not
being used until my return journey to
Sydney. Over time, I noticed that the
fault would mainly appear on cold
winter mornings when I was leaving
the Highlands. At full volume, the
noise was so bad that I had to switch
the X2 off.
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By the time I had travelled 30km
and stopped for breakfast, on turning
the X2 back on, the fault had cleared
itself. This led me to believe that the
fault was temperature related.
On the suggestion of my technical
friend, I tried placing it in the refrigerator for an hour. But even that didn’t
activate the fault as, by the time I had
it set up on the bench, the unit had
warmed up again.
Reading the X2 service manual, I
was able to locate the TDA1020 audio
IC on the circuit diagram. My friend
had suggested that whatever was causing the fault would probably be associated with this IC.
The IC wasn’t difficult to find as the
audio board is mounted inside the face
panel of the unit. It was relatively easy
to remove the front panel to expose the
board and the unit could be run with
access to the IC. So I sprayed the IC
with a can of freezer spray to see what
would happen.
This produced a low-level hiss from
the speaker but it did not cause the
aforementioned fault to occur. Methodically spraying components associated with the IC finally reproduced
the fault. When I sprayed a 10µF electrolytic bypass capacitor, the mute
suddenly opened with the speaker at
full volume, which tapered off as it
warmed back up again.
The audio IC is riveted to a small
block of aluminium that serves as a
heatsink, which in turn is riveted to
the chassis. Drilling the rivet out and
removing the knobs allowed the audio
board to be lifted out of the front panel.
Carefully examining the underside
of the board revealed nothing unusual except for a bit of corrosion around
the pins of the audio IC. I removed the
corrosion with a toothbrush and some
methylated spirits and lightly re-soldered all the pins.
Using solder wick, I removed and
replaced all four of the ageing electrolytic capacitors on the board. After
reassembling, I again sprayed the section of the board which had caused the
problem to appear last time. All was
silent, as it should be.
Cordless vacuum repair
B. P., of Dundathu, Qld, had the
unfortunate experience of buying a
second-hand vacuum cleaner that
worked fine when initially tested but
then was found to be faulty when he
got it home. Luckily, he isn’t afraid of
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disassembling something right back to
its constituent parts and he managed
to get it going again...
After visiting our daughter and using her cordless vacuum cleaner, my
wife decided that she would like one
of her own. She looked on Gumtree
and found one locally, which we went
and examined.
It seemed to be working OK and we
got it for a reasonable price and headed off. When we tested it at home,
I noticed several problems with it.
For some reason, the three-position
switch was now jamming and the
brush wasn’t turning. This had not
happened when we first looked at the
unit, so they must have happened on
the way home. I decided to dismantle
the unit and try to fix it.
I started with the handle, which is
attached to the main body by a single
screw. The next thing was to dismantle the handle. This was achieved by
first pulling off the decorative covering, which revealed several screws,
which I then removed.
With the handle now apart, I could
see that the rotary switch operated a
lever which in turn operated a PCBmounted three-position slide switch,
which was supposed to be held on by
two screws.
Somehow, one of the plastic screw
holes had disintegrated and the screw
had fallen out and jammed the switch.
I removed the four broken plastic
pieces and the loose screw. Then I
screwed the PCB back on with the
remaining screw and fortunately,
this was enough to hold it securely,
so I reassembled the handle, with the
switch now working.
However, the brush still did not turn
when the switch was set appropriately,
so I would have to look further to find
why. I started by removing the bottom
cover of the cleaner head, where the
brush was.
This involved removing seven
screws and this would be routine for
cleaning the brush. Everything seemed
to be in order here, so with the brush
still out, I turned the switch to operate the brush motor.
I found that by swivelling the head,
I could get the motor to run intermittently, so this indicated a broken wire
or loose connection. I then dismantled
the cleaning head by removing eight
more screws and checked the wires
and the motor but they were all OK.
I then unplugged the head from the
siliconchip.com.au
unit and I noticed that there had been
some arcing on the two connecting
pins, indicating a loose connection. I
needed to dismantle the main vacuum
cleaner body to find out more.
First I un-clipped the decorative
front panel and then undid six screws
to separate the body into the two
halves. I located the clip connectors
at the base of the body and tested the
fit of the pins, which were very loose.
After bending the clip connectors
to ensure that they had a firm grip on
the pins, I reassembled the main body
and refitted the handle assembly. Then
I reassembled the cleaning head and
the connector, making sure to turn the
connecting pins 90° so that the damaged area was no longer the section
that would make contact with the connecting clips.
With the unit now back together
again, it worked correctly, just like
new.
Smart kettle repair
R. S., of Hoppers Crossing, Vic,
makes problem-solving and repairing
various electronic items his hobby. His
neighbour is aware of this hobby and
decided to take advantage of his generosity with his time when the household kettle decided to go on the blink,
as follows...
My neighbour Phil and his wife
were having trouble with their kettle,
a “bells and whistles” type. The base is
used to control the final water temperature in five steps, from 70°C to 100°C.
As is typical for this type of kettle,
the base has a central metallic post,
about 2mm in diameter, with several
concentric rings around it. These fit
into slots in the base of the jug and
supply power to the heating element
along with feedback from the built-in
temperature sensor.
I noted that none of the pretty blue
LEDs in the base were illuminated
when power was applied but the GPO
seemed to be working correctly. The
base was held together using some
annoying tri-wing screws but luckily
I had a suitable bit in a Dick Smith
toolkit, so I managed to get it apart
without further drama.
Inside, I found two separate PCBs.
One is best described as the power supply and the other, the control board.
They are linked together by a five-way
flexible flat cable. The power supply
has a two-way flexible flat cable going
the main jug connector.
siliconchip.com.au
The power board was the main suspect, so I removed it and carefully
examined it. The circuit is simple; it
is the now-familiar capacitor/rectifier/filter/zener type of supply which
requires no transformer. The power
board also incorporates a 12V DC coil
relay to switch 230VAC to the kettle
element, plus a 78L05 5V regulator.
Both the 5V and 12V power rails are
fed to the control board as well, along
with control signals for the buzzer and
relay and a feed from the temperature
sensor.
I checked the diodes in the bridge
rectifier but they seemed OK. However, the zener diode which regulates
the 12V supply was surrounded by
some charring on the PCB. I carefully applied 230VAC to the board and
measured the voltage across the zener diode. It was only about 2V DC;
way too low.
So, I disconnected power and desoldered the zener diode from the
board. I measured the resistance across
it with my DMM and regardless of the
way I connected the probes, I got a
reading of just a few ohms. So it seems
like this component had shorted out,
possibly due to overheating, given the
charring I noted earlier.
I guess it was better that it went
short-circuit rather than open-circuit
as otherwise, the 78L05 could have
had a much higher-than-expected voltage applied to its input and that could
have fried it, and possibly other components too.
The only 1W zener I had handy was
rated at 11V. I figured that was close
enough that it should work, so I soldered it to the board and re-applied
230VAC. The 12V rail then came up (to
11V) and I could now measure 5V DC
from the output of the 78L05 regulator.
I powered it down, re-connected the
control board and once again applied
mains power. The pretty blue LEDs
began to flash and the buzzer beeped.
That was a good sign, so I decided
to pop down to my local Jaycar to get a
12V zener. I figured I would buy a 5W
type, seeing as the 1W zener originally
installed seemed to have burned out.
The pigtails of the 5W zener are larger in diameter than those of a 1W type;
I had to drill out the through-holes to
1.2mm. I mounted it about 7mm proud
of the PCB, to allow for better cooling
air circulation.
I could then finally re-assemble the
entire unit and return it to Phil’s wife,
Helen. She filled it with water and confirmed that it was back to normal. Now
I just need to get Phil to reimburse me
the $1.75 that I spent on replacement
components!
SC
At right is the base
of the smart kettle
with the yellow
power PCB before
any changes. Below
is the power board
after the blown zener
diode was replaced
(marked ZD1 on the
PCB). It was replaced
with a 12V 5W zener
(circled in red) that
had slightly larger
leads, so the holes
had to be enlarged.
Australia’s electronics magazine
January 2019 67
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