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SERVICEMAN'S LOG
Samsunk – or the dishwasher that wouldn’t
Dave Thompson
I’ve owned many Samsung products over the years and no wonder; this
South Korean manufacturer has their fingers in many pies. They’ve been
around for years but more recently have become known as innovators
and leaders in the field of consumer electronics, especially phones,
tablets and TVs.
Like many other companies, they’ve
had the odd swing-and-a-miss, but in
general, they make quality products.
I was mindful of this when we renovated our house a few years ago and
decided on some shiny new Samsung
appliances for the kitchen. For the
dishwasher, we chose a Samsung Waterwall over appliances made by more
well-known brands that specialise in
kitchen appliances.
It certainly wasn’t the cheapest
option, but it looks the part with its
minimalist, brushed stainless-steel exterior and slick, futuristic blue multiLED display buried behind the door
panel and peeking through tiny, patterned holes laser-cut into the facia.
Very cool and just the thing for the
modern kitchen.
However, it is not without its problems. From day one, when the wash
program was set and the door closed,
the front display would often show
all 8s instead of the time remaining. A
light tap on the door beside
the display usual-
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ly got it back to normal. I suspected a
loose connection or dry joint perhaps.
We’d spent a long four months rebuilding and renovating the kitchen
while cooking on a gas range, having
dinner on crates and washing our dishes in a bucket. I wasn’t keen to tell the
wife that mere weeks after installing
the dishwasher, I’d have to pull it out
again and either get it repaired under
warranty or disassemble it and repair
it myself.
For the time being, we could live
with such a minor fault; after all, its
operation wasn’t adversely affected,
and the display glitch only manifested
itself roughly half the time anyway.
I did log the fault with the relatively
good online registration/warranty system and was advised by some virtual
assistant to take the dishwasher to an
accredited repair agent — advice that
I ignored because, well, that’s what
servicemen usually do when faults develop in their own gear. Besides, shoehorning a dishwasher into a 1997 MG to
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transport it to an appliance-repair guy
across town just isn’t feasible!
The dirty water thickens
That was two-and-a-half years ago,
and aside from that small fault, the
dishwasher performed flawlessly.
However (there’s always a however!),
a few months ago, I started noticing
that the bottom rack of dishes (usually
the most soiled in any dishwasher layout) were not being cleaned properly.
This would happen once every ten
or so washes, but over time it started
happening more often, until almost
every wash cycle ended up with dirty
dishes in the bottom tray.
I was actually becoming a bit annoyed. It’s a story all too familiar with
modern appliances, conveniently failing just outside of the two-year warranty period. I messaged the virtual
assistant on Samsung’s website and
May 2019 61
Items Covered This Month
•
•
•
•
The dishwasher that wouldn’t
RF interference at the end of
the rainbow
Marantz 1120 amp repair
Vacuum cleaner tripping RCD
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
received the same advice as before. I
don’t know how they expect people to
be dragging dishwashers all over town
but we still don’t have the capacity to
easily do that.
The other option was to have a technician come out and have a look at it.
Two things deterred me: one, the sheer
cost of the callout (I knew I should’ve
gone to appliance-repair school) and
two, the guys I rang up and talked to
had no experience with a Samsung
Waterwall dishwasher. Perhaps these
appliances were still a bit too new.
Desperately seeking solutions
My next stop was the good old interweb; somebody must have come
across this problem before!
And it seems they had; forums were
ablaze with the flaming posts of disgruntled Samsung Waterwall owners.
In fact, some posters were trying to
scrape up support for a class-action
type product recall, while others just
bemoaned Samsung and everything
connected with the company. Most
stated they’d never buy Samsung
again.
Crikey! I wish we’d seen
this before we bought the
thing, but then again,
these posts weren’t there
at the time (note to self:
must mend the time
machine, then go back
in time and choose a
different dishwasher. Also maybe do
something about that
Hitler guy).
It is worth noting that
forums tend to disproportionately magnify any
problems because they are
being viewed through the lens
of people whose first instinct
is to get online and vent their
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spleen. It’s as if they are on some kind
of modern-day crusade, using their
collective rage to try to take Samsung
down and thus salve their consumer
remorse for making a poor purchasing decision.
To put this into perspective, Samsung has sold hundreds of thousands
of our model of dishwasher alone, yet
20 people grumbling about it in a forum can make it look like this machine
is the worst thing ever made. Like I’ve
always said: the best thing about the
internet is that it gives people a voice;
the worst thing about the internet is
that it gives people a voice.
I did my usual research on the web,
first looking for similar problems and
solutions for my model of dishwasher.
When I found nothing but other people
griping without offering any clues to
the cause (or better still a fix), I cast my
net wider into other models, and used
broader and broader search terms, in
a quest for anything relevant.
Frustratingly, I found nothing constructive. I assumed at the time that
this was because of the relatively new
technology being used and the lack of
repair reports filtering through to endusers via the internet.
I couldn’t find any service manuals online, either. While there were
plenty of user manuals available for
download, they offered nothing but
the usual operating advice and a basic (ie, useless) troubleshooting guide.
What I needed was a full service manual. While I discovered a site advertising one for sale, it was too expensive.
Given time, free service manuals must
eventually appear online.
In the meantime, I played
around with the
dishwasher’s settings and enabled
some zone ‘turbo’ settings,
and this,
in conjunction with pre-rinsing the
dishes and trying different powders
and pellets, helped clean the bottom
rack a bit better.
Still, it rankled that I had to wash the
dishes before I put them in the dishwasher. After all, it was supposed to
be washing dishes for me — not the
other way around (you had one job,
dishwasher)! An actual fix or explanation of the cause of this problem
would be nice to have.
Now the dishwasher is
complaining too
So, that was the situation until a
new fault appeared just a few weeks
ago. This manifested as a grumbling
noise just after starting the wash cycle; usually. I noticed this immediately since its operation is normally
extremely quiet.
My first thought was perhaps a
pump bearing had failed, but I was
just guessing; I’d need more information on how it worked to be even in
the troubleshooting ballpark. But the
faults were likely related.
I went back to the web and once
again waded through the familiar
wasteland of the forums, though this
time, I started seeing a link to a YouTube video purporting to show a relatively simple fix for this very problem.
There was also more incidental information, so it appeared that between
now and when I first started looking,
a lot more people had experienced
similar problems and some valid repair information was finally starting
to appear. I also found a link to a free
service manual, which I immediately
downloaded. It was then off to YouTube to check out this ‘fix’ video.
The guy in the video, who appeared
to be American, described the exact
problem I was having and on a very
similar model.
This was fortuitous because there
are dozens of different models in the
Waterwall range (which is typical
given the different regional markets)
so it was a pleasant surprise that this
repair video appeared to apply to my
model as well.
Reinventing the (water)wheel
To explain the problem properly, I
have to also explain how this new-fangled Waterwall system works. In a typical dishwasher, rotating, freewheeling
booms with angled spray jets in the
top side are driven by water pressure
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siliconchip.com.au
and these spin beneath the dish racks
and the blasting, hot and soapy water
cleans then rinses the dishes.
There are usually two of these rotating arms, one for the bottom rack and
one for the top. It is a simple system,
and while there is obviously other
stuff going on (water heating, pumping, soap tray opening and drying cycles), that isn’t relevant here.
In the Waterwall system, there are
two horizontally-mounted ‘vanes’ sitting at opposite ends and spanning the
bottom of the washing chamber; one
is fixed at the far end, while the front
one is mobile and driven backwards
and forwards by a stepper motor.
The front vane is clipped to and
travels along a polished metal beam
running down the middle of the chamber floor, and has a sharp curve on the
edge, facing the rear vane. The fixed
back vane has a series of high-pressure
water outlets equally-spaced along its
length, pointing parallel to the floor
and aiming at the front vane’s curved
surface.
The idea is that water is blasted
from the rear vane into the front vane,
which creates the titular “water wall”
as that vane traverses the chamber and
this is what mainly cleans the bottom
rack of dishes. There is now a video
on YouTube showing this operation
using three different cameras mounted in the dishwasher, which explains
the process better than I can.
There are two other racks in the
dishwasher; one middle rack for cups
and glasses and a cutlery tray at the
very top, each with their own standard
rotating water jet
just like you’d
see on any other
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dishwasher. These traditional jets in
my dishwasher clean those upper trays
just fine; it is just the Waterwall system that is failing to clean the bottom
tray properly.
From my research, I discovered that
if I’d gone down the more well-trodden
route of having a technician come out,
he would likely have gone through the
Samsung-recommended protocols of
swapping out a couple of pump motors, a stepper motor and gearbox, a
sensor array and finally the main PCB,
all at our considerable cost.
This unsuccessful repair scenario
was a much-repeated story posted
in the various forums, and I have no
doubt this would have been the case
with us too. None of these ‘fixes’ would
have resolved our problem.
Finally figuring it out
From the video, I learned that the
noises I heard on cycle start were the
front vane moving along its usual travel path to check nothing was impeding
it before the wash cycle started.
Indeed, one of Samsung’s helpful
suggestions in their troubleshooting guide is to ensure that nothing is
protruding through the bottom of the
lower rack, as this can stop the vane
moving and cause possible damage.
The front vane on my dishwasher
was moving OK; it just didn’t know
when it hit the other end, so the poor
old motor kept spinning and the gears
kept slipping, causing the noise. The
vane eventually gives up trying to move
and just stops where it sits, explaining
the noise and the lack of cleaning.
So, what tells the vane to stop when
it gets to the end of its travel? Simple:
a magnet mounted on the vane hits a
sensor mounted beneath the floor of
the chamber, and this tells the motor
to reverse and send the vane back to
the start position. I proved this wasn’t
happening by opening and closing
the door just after and during the
start cycle, to check on the progress
of the vane.
Sure enough, it hit the end and the
motor kept on going if I shut the door
again. Obviously, this wasn’t doing
the motor or gearbox any good, so a
fix had to be implemented before we
could continue using the dishwasher.
All the sharp troubleshooters out
there will have already deduced
that there are two possible causes of this fault, the magnet and
the sensor.
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Fortunately, by this time I’d found
the service manual and could test the
sensor (and many other parts for the
system) by using codes from the book
to run the different components individually, without having to waste a lot
of time waiting for a cycle to complete.
Having this information was well
worth the hassle of finding the service manual.
By holding down certain buttons
and pressing others, I could initiate
the vane travel test, and by placing a
magnet near where the vane’s magnet
would sit, I could stop it from moving
any further. This proved the sensor
was working, and that the magnet is
the problem; however, I already knew
this because of the YouTube video.
The guy in that video explained
that the plastic-coated iron magnet attached to the vane gradually loses its
strength due to the constant heating
and cooling cycles.
His fix was to replace the magnet
with a much stronger rare-earth or
neodymium type. He simply took out
the old magnet, which is mounted in a
removable plastic housing, and glued
a whopping great rare earth one in its
place. His dishwasher then cycled
perfectly, and he sat back and basked
in the adoration of a grateful public.
In the end, a simple repair
I didn’t have a rare-earth magnet of
that size in stock, so I tried various solutions, such as removing some from an
old hard drive and cutting them down
to suit, but wasn’t overly successful.
I discovered that cutting these magnets with anything severely diminishes their strength. Putting two smaller
neodymium magnets together side by
side also didn’t work well, so I went
looking for alternatives.
Jaycar has some in various sizes, but
those few with magnetic strength mentioned were only rated at most N35,
which is probably not strong enough.
I hit my usual go-to hardware-stores’
websites and found that both places I
frequent had various magnets listed at
a reasonable cost.
I ended up with a packaged pair of
N42-rated ‘door’ magnets, just the right
size at 25 x 7mm and for the princely
sum of just $25. I figured I could use
one and have a spare for when the
problem inevitably returns.
Unlike the guy in the video, I kept
the original magnet holder and simply shaped it a little to accommodate
May 2019 63
the bigger magnet. I firmly tacked it
in place using some of the food-grade
silicone sealant that I had left over
from the kitchen reno and gave it a
good 24 hours before re-assembling
the holder to the vane and the vane
to the dishwasher.
After completely resetting the dishwasher by powering it off at the breaker and powering it up again, I ran a
test cycle using the magic codes. It
worked perfectly, without any nasty
noises and the bottom rack of dishes
are now cleaning correctly. The display still glitches now and then, but
$25 is an excellent repair bill, given it
could have been much, much higher.
Of course, the display is still a bit
flakey as that is an unrelated problem. But I’m so relieved to have clean
dishes again that I’m leaving that fix
for another time...
RF interference at the end of the
rainbow
D. P., of Faulconbridge, NSW went
on a bit of a wild goose chase to try to
track down the source of some strong
radio frequency interference. It took
some time but not only did he figure
out where it was coming from, he also
managed to shut the source down.
Here is how…
The Amateur Radio fraternity
maintains repeaters on various bands
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(mainly VHF and UHF). These repeaters are usually set up and maintained
by local amateur radio clubs and are for
the use of all licensed amateurs. The
idea is that one can get good communications from low-lying or other difficult locations by virtue of the prime
(radio) location of the repeater.
The repeaters have different input
and output frequencies and are located on the best high point that the club
can organise. For the higher bands, a
single antenna usually serves for both
the receive and transmit signals.
You may wonder how that is possible. The received signal is typically
tenths of a microwatt, while the transmitter output is usually 50W or more,
and the frequency separation between
the receive and transmit frequencies is
relatively small (600kHz, in the case
of VHF repeaters).
The secret is cavity resonators. They
have a very narrow passband, with
extremely high attenuation outside
of it. They can be connected in series
for even better filtering. Most VHF repeaters have three or more cavities,
providing a high degree of isolation
between the transmitter and receiver.
Other devices such as hybrid rings are
sometimes also used to enhance the
effect of the cavities.
A few years ago, I joined the repeater committee of my local club in the
Australia’s electronics magazine
Blue Mountains, west of Sydney. For
some time, the club’s VHF repeater had
been plagued by interference. The origin of the interference was unknown,
although it had been positively established that it was coming in on the antenna, and that nothing in the building
was causing it.
This had been established partly by
monitoring the repeater input frequency with various receivers at different
locations. The interference could be
heard well away from the repeater.
The interference consisted of bursts
of a nasty rasping noise and made the
repeater pretty much useless. The interfering signal was strong enough to
open the receiver squelch at regular
intervals, triggering the repeater, retransmitting the horrible noise. The
constant bursts of noise were so annoying that few people monitored the
repeater any more.
One of our club members had a job
as an engineer in one of the telecommunication companies. He became
interested in the interference problem and connected a VHF antenna to a
spectrum analyser at work. The interfering signal was plainly visible, and
one of our member’s colleagues said
he thought it was a pager signal, albeit
grossly distorted and “chopped up”.
Strangely, though, it was not on any
established pager frequency; it was
definitely in the VHF Amateur band.
Actually, it was centred adjacent to
our repeater input frequency with its
sidebands regularly intruding into our
repeater input passband. It was at these
times that the interference occurred.
I tried listening to the pager frequencies on a separate receiver while monitoring the repeater output but I was
initially confused because sometimes
the pager data seemed to be triggering
the repeater, sometimes not.
Telstra used three pager frequencies at the time. These same frequencies were transmitted simultaneously
from stations dotted around the country. Signals on one of these frequencies
were definitely unrelated to the interference, but the other two seemed to
both be contributing to it.
Eventually, by using two receivers,
we discovered that it was when both of
these frequencies were active simultaneously that the interference occurred.
So it seemed to be some kind of intermodulation effect, but where was it
occurring? It was not in our repeater,
since we had established that the insiliconchip.com.au
siliconchip.com.au
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May 2019 65
terfering signal could be heard many
kilometres from the repeater.
I started monitoring the repeater
input frequency in my car as I went
about my normal activities, to try to
get an idea of where the signal was
strongest. The interference could be
heard all over the place with varying
strength with no discernible pattern,
although I had the impression that elevation could have been a factor.
I obtained a list of pager station locations and tried approaching several of
these, however, the signal strength of
the transmitters up close was so high
that it swamped my receiver input and
made it impossible to make any meaningful observations.
I solved that problem by connecting several spare cavities between my
antenna and the receiver input, carefully tuned to the repeater frequency.
I could now get right next to a pager
station and maintain normal sensitivity of my receiver.
This approach eventually bore fruit
as I was confident that I was hearing
only the interfering signal, even when
close to a pager station. One day, my
travels took me further east than usual,
and I began to receive much stronger
signals than before as I moved towards
the coast. Eventually, as I topped a rise
to Bilgola Plateau, a flat area right near
the coast, the interference came roaring in at S9+.
At first, I thought something had
gone wrong with my gear, but it all
checked out. Maybe I was seeing the
actual interference! By inserting an
attenuator into the receiver input and
driving around a bit, I was able to establish that the signal was coming from
a tower on the edge of a public park
on the Plateau.
There was a hut next to the tower,
and the door was open. People were
working in there, so I approached
them, introduced myself, explained
what I was doing, and asked if they
could tell me anything about the pagers. They said no, they did mobile
phones, but they could give me a number for “the pager blokes”.
I asked them if I could have a look at
the pager gear. They showed me some
very impressive rack-mounted transmitters with large heatsinks. Apparently, they were quite high-powered
units. Connected to the transmitter
outputs were, guess what, cavity resonators! These were not the home-brew,
copper-pipe devices I was used to see66
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ing, but were nicely finished commercial units.
I called the number the mobile
phone guys had given me and spoke
to a very helpful technical officer who
listened patiently to my tale of woe. He
said he would send a technician out to
investigate the problem. When I suggested that the technician visit the repeater site to see the problem for himself, he agreed, and we arranged a time.
In due course, several members of
the repeater committee met the Telstra
technician, complete with his spectrum analyser, on site. After a coffee
break to help our new friend recover
from his long drive, we connected his
spectrum analyser in line with the repeater and antenna via a T-piece, after
assuring him that we had disabled the
transmitter!
Monitoring the repeater’s receiver
audio while watching the spectrum
analyser screen we could plainly see
and hear the interference. Our new
friend agreed that it was a pager signal,
and that it probably was an intermodulation product of two networks. He
said he would investigate the problem.
By the next morning, we were delighted to find that the interference had
gone; but it returned at a lower level
that afternoon.
Our friend phoned to explain what
he had discovered. He had found a
faulty cavity at the Bilgola site and
having no spares at that time, had
swapped it for a good one from the
Parramatta site.
His thinking was that Parramatta
would cause us less interference since
it was shadowed from our repeater by
the mountains to some degree. He had
ordered a new cavity.
He was right, the interference level
was lower, and by setting the repeater’s
squelch level higher, we were able to
stop it from triggering the repeater. This
was not ideal because it effectively reduced the sensitivity of the repeater,
but at least we didn’t have to listen to
the repeater triggering constantly. It
would do until the new cavity arrived.
I was curious as to why the pager
units, which were transmit-only devices, should have cavities connected to them. Our friend explained that
when several transmitters on similar
frequencies are feeding antennas nearby, the transmitted signals from each
antenna are induced into the adjacent
antennas.
With no cavity resonators, there
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would be nothing to stop these induced signals being fed back into the
power amplification (PA) stages of the
other transmitters. These PA stages are
highly non-linear (Class C), and when
the transmitter is triggered, a whole
spectrum of frequencies would be produced from the mixing of the transmitter output with the extra signals picked
up by its antenna.
This whole mess would then be
amplified and anything that could get
through the PA stage’s output circuit
would be transmitted. These ‘dirty’
signals would be induced into the adjacent antennas as before, in turn generating a mind-boggling array of new
modulation products.
The cavity on each transmitter prevents this by blocking the induced signals from reaching its transmitter and
rejecting any spurious outputs from
its transmitter.
A few weeks later, I received a call
from our Telstra friend to say that he
had installed the new cavity. I was able
to report to him that there was now absolutely no interference, and to thank
him profusely for his diligent attention
to our problem. Full marks to Telstra
and their staff!
Since then, a tone squelch system
has been installed in the repeater. A
sub-audible tone imposed on the user’s
audio is required to open the squelch,
Preventing the repeater from being
triggered by rogue signals. However,
this does not prevent legitimate traffic from being subject to interference
while the repeater is being used.
1970s Marantz 1120 amp repair
J. W., of Hillarys, WA did a mate
a favour a few years ago and fixed a
fault in his trusty Marantz amplifier.
Now something else has gone wrong
and so it’s back on the workbench for
some more surgery...
A few years ago, I repaired a friend’s
Marantz 1120 stereo amplifier (circa
1968). He rang last week to report another fault in the amplifier. I made a
house call to check it out and found
everything was working except for
the phono input. There was no sound
from the right channel. I disconnected
the myriad cables from the unit and
took the amp back to my workshop to
check it out.
I connected the phono input to an
iPod and wired up some speakers in
my workshop and found the fault was
still present – no output from the right
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channel speaker. I dug around in my
filing system and found the circuit diagram I used last time I fixed this amplifier, about six years ago.
The amplifier is built like a brick
outhouse with 2mm steel plate used
for the whole chassis and covers; not
a bit of plastic in sight. I removed the
nine screws holding the top cover in
place and opened it up. I then identified the phono/select board assembly
which sits vertically and plugs into
another PCB behind the front panel.
I connected my CRO (cathode ray
oscilloscope) to the two phono input
channels and I could see both waveforms from my iPod. This was difficult as the vertical phono board has
the input selector switch shaft running along the whole length. I then
identified the output terminals from
the phono preamplifier and connected up my CRO. The left channel was
OK but nothing was coming out of the
right section.
The circuit showed 6.8µF coupling
capacitors connecting the output
transistors to the selector switch, so I
hooked up scope up to the driven side
of the capacitors and found a good signal on both channels.
I then had to try to get the board free
enough to replace the faulty capacitor;
I did not want to remove it completely
as this involved desoldering about 10
wires. After removing the aluminium
front panel and another 10 screws, I
was able to move the board enough to
get to the capacitor.
Replacing the right channel coupling cap resulted in audio from both
speakers. I decided to replace the left
channel’s coupling cap as well, to be
on the safe side; after all, the amp is 50
years old! I wonder if a new amplifier
purchased today would last that long.
siliconchip.com.au
My friend had also told me that
the power-on indicator lamp was not
working, so I checked that and found
the globe (28V 40mA) was blown. I
searched in my container of small
globes and found a 6V 40 mA bulb
that looked like it came out of a telecom switchboard or equipment rack.
The amplifier circuit showed a 390W
2W resistor in series with the globe, so
after doing a bit of maths, I determined
that a 1kW 1.6W resistor should allow
me to use the 6V globe instead. I found
a 1kW 3W wirewound resistor about
the same physical size as the original
and mounted it on the opposite side of
the power PCB, to allow more air flow.
A bit of fiddling with the new globe
had it mounted correctly and working.
I left the amp running for a few hours
and found no sign of the replacement
resistor overheating. Since it was all
working, I put it back together, took it
to my friend’s house and connected
everything back up.
While I didn’t ask for any payment, I
was promised a bottle of scotch for my
efforts; that’s what you call a bonus!
Ducted vacuum repair
G. H., of Littlehampton, SA has had
problems with two different vacuum
systems and both of them involved
Earth leakage faults. He managed to
solve both...
Our house is about 20 years old.
It has a weatherproof double power
point on the back wall of the garage for
garden appliances. About a year ago,
plugging in and switching on the garden vacuum via the right-hand socket
caused it to trip the Earth leakage detector in our main circuit board.
Oddly, after resetting the RCD, it
worked fine. And I also found that using the left-hand socket never caused
Australia’s electronics magazine
the RCD to trip. The fault ended up
being a mass of spider webs embedded in the back of the power point. I
cleaned it out thoroughly and sealed
the gap in the wall around the power
point, to keep spiders out.
We also have a ducted vacuum
cleaner inside our house which has
worked well for many years. The main
unit is in the garage, so it produces
very little noise and no smell of musk.
Then, a few months ago, as my wife
pushed the cleaning hose into the wall
socket, all the power to our house went
off. The pipe has a metal ring which
connects two terminals inside the wall
socket, turning the unit on automatically. The switching is all done at low
voltage for safety.
I unplugged the motor unit in the
garage and checked the fuse box. The
RCD had tripped again, presumably
due to excessive Earth leakage. Resetting it restored power to the house.
I plugged the motor unit in and carefully switched on the power. The hose
must have been left in the wall socket,
so it sprang to life. We continued to use
it without any problem until the other
day, when the RCD tripped again. This
time, I restored the power but left the
motor unit unplugged.
I first measured the resistance
from the low-voltage switching wires
to Earth, Neutral and Active. I was
pleased to see that all readings were
open-circuit, so that part was safe. The
low-voltage supply comes from a 12V
transformer, which powers a relay to
switch the Active conductor.
But the resistance between the Neutral and Earth pins of the vacuum motor was less than I expected. I measured the resistance between the Earth
pin on the internal circuit board and
both the Active and Neutral connections again; it was too low.
I disconnected the motor from the
main board. Measuring the resistance
from the motor power wires to the
Earthed casing of the motor also gave
low resistance readings.
So I began dismantling the motor
carefully and measured as I proceeded. Eventually, I concluded that this
leakage was due to carbon deposits
which had come from the brushes. I
thoroughly cleaned the carbon brush
holders, then dried them before reassembly. All of the resistance readings
were open circuit, as they should be,
and since re-assembly, the vacuum has
not missed a beat.
SC
May 2019 67
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