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Vintage Radio
By Fred Lever
1930s “Vogue”
radio restomod
Sometimes our contributors simply
describe vintage radios. Other times
they fix them up or even restore them.
This goes way beyond that. It’s a
“restomod” – taking parts (or in this
case, a part) from an old radio and
putting newly built electronics inside,
either to improve it, or because the
original components are long gone.
While most of the radio is new, it was
built in the style of a 1930s radio.
I had shelves in my workshop made
from scrap materials. Some of the timber came from the cabinets of discarded radios and TV sets. One piece was
the front panel of an old 1930s style
radio. I remember that it had glass bottle valves, a circular tuning dial and a
very heavy loudspeaker. The workings
of the set went to the tip, and I used
the timber parts.
A couple of years ago, I was pulling
the shelves down in a workshop rearrangement, when out came the front
panel, complete with its brass escutcheon proclaiming it to be a “Vogue”!
It was in remarkably good condition
considering how it had been used. But
there were still quite a few scratches
on it, and the timber on one side was
soaked with motor oil.
Some web searches and forum posts
gave me information on “Vogue” radios but unfortunately, none of this information matched with what I had.
Based on what I remembered of the
chassis construction, it was a cut-price
radio, unlike the 5-8 valve, 3 or 4 knob
Vogue radios I found on the web.
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It had only two knobs: tuning and
volume. The power switch was in the
two-wire power cord which had a bayonet plug, which you connected to a
double adaptor in a ceiling lamp. I remember this because we used the radio for a short time but then scrapped
it when it failed.
That may seem amazing in this day
of vintage preservation, but back in the
1950s and 1960s, millions of radios
were scrapped as television came in.
I remember one large radio store in
town used to burn hundreds of radios at a time as they were traded in for
TVs and transistor radios!
History
While the restoration detailed below was in progress, I found out a little more about this set from a vintage
radio forum member. They identified
the escutcheon as part of a type of dial
assembly provided by Efco Mfg Co,
called the “Lion”.
The set may have been a low production private factory set or even a
kit set from one of the radio type parts
Australia’s electronics magazine
shops or retailers re-using the
name Vogue. I lean
towards the theory of this radio being
built from a kit, as I used to see kits
advertised in “Radio and Hobbies” using Australian-made parts. So my plan
to recycle parts from Aussie radios of
the period seemed like a good one.
Beginning the restoration
I cleaned the front panel up with
degreaser and water, then prised off
the ornaments and unscrewed the precious escutcheon and put them aside.
Then followed a few hours of sanding
back the veneer finish to remove some
of the horrors, giving a better view of
what was left. The veneer was badly
damaged but I decided to polish it anyway and use it as-is.
I achieved a reasonable state with
the front panel and the dimensions of
this gave me a starting point to build a
suitable chassis. Looking through my
junk box, I realised that I had a handful of RCA metal case valves and as
they were introduced in 1935, I desiliconchip.com.au
The circuit used for this Vogue radio is loosely based off the circuit used in the AWA Radiola Model 84, 193, 194 and 501,
all sold from 1939. You can find the Model 84 circuit diagram at www.radiomuseum.org/r/amalgamate_radiola_84.html
cided to make a classic 1930s superhet with five valves and drew up a
preliminary circuit.
Circuit description
It’s a superhet AM broadcast band
receiver. The aerial picks up radio signals and the tuned circuit of coil L1
and tuning capacitor G1 makes it selective for the tuned station frequency.
This signal is then fed to the control
grid of the 6K8G converter (V1).
V1 amplifies the signal and also mixes it with an oscillator signal which
tracks the station frequency with a
455kHz offset, set by inductor L2 and
the other half of the tuning gang, G2.
The output of V1 is a mixture of the
tuned and oscillator signals, which
produces a strong difference product at 455kHz. Coupling transformers IFT1 and IFT2 are resonant at this
intermediate frequency, so they pass
the signals at this frequency only and
rejecting the higher carrier and sumproduct frequencies.
IF amplifier valve V2, a 6K7M, amplifies this IF signal and its output is
fed into IFT2 which then couples to
a diode in V3, a 6Q7M dual diode/
triode. This, in combination with 80pF
filter capacitor C6, demodulates the
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audio and it is then fed to 1MW volume control pot P1.
The audio signal is also filtered to
remove the AC audio component by
2MW resistor R3 and 47nF capacitor C1
and the result used as the AGC control signal, which alters the DC bias
of the control grids of both V1 and
V2, reducing their gain when tuned
to stronger stations.
The audio signal from P1 is then fed
to the control grid of the triode in V3,
which acts as an audio preamplifier,
and the output is coupled from its anode to the control grid of audio amplifier valve V4, a 6V6GT, via a 10nF capacitor (C10). It’s configured as a ClassA amplifier and drives the primary of
the output transformer, which couples
the signal to a modern 8W loudspeaker.
V5, a 5Y3GT, is used to rectify the
output of the mains transformer PT,
to produce a 310V HT rail which then
passes through an LC filter to remove
ripple, before feeding the anodes of
the other valves. Each one receives a
different HT voltage as set by various
dropping resistors, to best suit that
particular valve and the way it is being used.
The mains transformer also has 5V
and 6V AC windings to drive the valve
heater filaments. Only V5 needs 5V;
The front panel of the Vogue radio
had torn mesh and was the only part
remaining of the set. The original radio
was likely sold as a kit set or small
production run. The emblem on the
cabinet depicts a muse (likely Erato)
playing a lyre and was manufactured
by Efco, based in Arncliffe.
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November 2019 99
the others have 6V heaters.
A trial chassis layout
I took a sheet of 0.7mm galvanised
steel I bought from Jaycar and tried
various layouts by arranging the parts
on a generously sized rectangle. From
this I determined that the chassis
would need to be about 355 x 230 x
50mm. I made sure to leave plenty of
room around the components, as the
cabinet would be pretty large anyway.
I planned to mount most of the
smaller parts on tag strips and wire
the set with coloured wires, with the
major components laid out neatly in
a rectangular grid. I wanted to use as
many period parts as possible.
The next step was to fold up the
chassis. I cut out the metal using a jigsaw and shears and folded it up using
a small press, plus a hammer and dolly in a vice. I ended up with one large
sheet and some smaller plates, which
I then pop riveted together.
I made up a box frame to carry the
side and top panels from timber flat
bars. The dimensions were to suit
the existing front panel, with enough
depth to accommodate the chassis. I
chose a 12in, 8W speaker from Jaycar,
mounted on a baffle board attached to
the main frame, as the front panel is
too brittle to take any screws or weight.
I made up the frame and did a trial
fit of the chassis, to locate the control
spindles and to make sure nothing
would be fouled. I made a board for
the speaker and clamped it in position,
to make sure that it would fit as well.
There were no major snags, so I was
then able to firm up a lot of details.
My woodworking skills are very
limited, so I assembled the cabinet
using butt joints with
The chassis
was made from
pieces of galvanised
steel, folded with a forming
press and held together with
rivets. It is about 355 x 230 x 50mm.
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The case was made
from plywood, while
the frame and speaker
baffle was made from
timber. The chassis
had the components
loosely placed on
top to help align the
location of the tuning
gang and dial.
plenty of glue. Once
the frame was squared
up, I clamped the front
panel to the frame and
glued it in place. It was
warped like a banana
and I had to clamp it
every 150mm or so, to
make it sit straight and
pull it onto the frame.
With that tacked on,
I then put in some more
flat bars for the chassis to sit on and glued
them in place. Finally,
I had a mounting place
for the chassis.
After mounting the
speaker and its frame,
I taped some gold coloured cloth on the
frame with the back
side of the cloth at the front, to give
a matte finish through the fretwork.
The side panels had to be bevelled
to mate with the front panel before
they could be fitted to the cabinet. Not
having the skill to produce a bevelled
edge, I did the next best thing and inserted a section of triangular timber
strip up against the front panel on each
side, thus presenting a taper for the
front panel and a flat face side panels
to butt up against.
I made a lid for the cabinet from
7mm plywood and added a centre
brace underneath,
in case heavy
items were placed
on top. I did not
want the plywood
to buckle inward.
With that glued
firmly in place, I then
cut the side sheets from
9mm plywood with my
trusty jig saw. I made
them a few millimetres
larger than necessary and
glued them into position.
Then I profiled the edges with
an angle grinder, to match the
Australia’s electronics magazine
frame, and smoothed the whole lot
using 120 grit, ready for finishing and
staining.
I then decided to test the gluing of
the frame and gave some of the rectangular bar sections a whack with a hammer. The bottom crossbar fell out, so
apparently, glue was not good enough
by itself! I added screws at each corner
to peg the joints. I threw a few more
screws in at the other main joints as
well, not wanting the cabinet to fall
apart later.
The next step was to paint the interior surfaces flat black. Once that dried,
I sanded the other faces (apart from the
front panel) using 400 grit sandpaper
and applied coats of cedar stain to pull
the shade of the white timber towards
the front panel shade.
I gave it several coats, sanding
again with 400 grit in between, until I achieved the shade I was looking
for and the ply flatted off without too
much wood fibre standing up. The
stain went darker upon drying so in
the end, I overshot a bit.
I then buffed the wood with oil and
then buffed a coat of silicone-based
car polish on top, giving an “antique”
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The sides and top were attached to the
case, with coats of cedar stain applied
to the outside.
The tuning gang was refurbished from an AWA radio. The drum it came with
was then drilled to form a circular hole that the spindle could travel across.
The spindle was cut from a metal rod.
look with a low-gloss finish showing all the scratches, bumps and fake
“wear” marks.
gang nicely. But I chose the inner circle to drive; thus, when I turned the
spindle clockwise the gang turned anti-clockwise!
I had to rework the brackets to raise
the gang for the spindle, to work on
the outside circle of the cut-out. But I
had removed most of the front face on
the outside so now the washers would
not grip reliably. I had to fit a rubber
grommet to the spindle as a tyre, which
drove against the inner surface of the
drum. It worked well and rotated the
drum in the same direction as the knob.
With the drive mechanism sorted, I
mounted the gang onto the chassis and
checked it in the cabinet and found I
had a space of about 20mm in front of
the drum to fit a dial. I would tackle
that later but at this stage, envisaged a
stationary card lit from behind with a
pointer mounted on the drum.
At this point, it would have been
easy to cut and re-drill the gang supports to get the dial drum outside diameter precisely in line with the escutcheon opening, but this point evaded me at the time.
Tuning mechanism
I now needed to think about the
tuning gang drive mechanism. The
front controls from the chassis have to
match the holes in the front panel, so
there were fixed centres to work from.
The proximity of the spindles indicated that the original dial drive was
probably a friction drive, direct onto
the tuning gang drum, so I decided to
mock up a drive and make sure that
it was possible.
I pop-riveted a temporary plate to
the front of the chassis, and after some
fiddling, I worked out what was possible and how to fit this into the space
available. I fitted a bush to the temporary plate and I then cut a short piece
of quarter-inch rod to form a spindle.
I cross-drilled the spindle for split
pins and slid a tension spring and
two washers onto the spindle so they
would grip a disc.
The tuning gang I used was from
a junked AWA chassis; the drum on
the gang was a nice size to make the
friction plate. I drilled the drum and
cut out a semicircular section for the
spindle washers to grip and drive the
gang through half a turn.
Here is where I made a stupid mistake. I set the whole thing up and fabricated brackets to hold the gang at
the height so that the spring-loaded
washers tightly gripped the flat face
of the drum cut-out and it drove the
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Chassis layout
I then turned my attention to assembling the chassis. I needed four tuned
coils. I had a junked model 84 AWA
set with the oscillator and IF coils and
after searching through my odd coil
box, I found an aerial coil that looked
promising. I needed the aerial coil
to cover 600-1700kHz, the oscillator
coil to about 950-2150kHz and the IF
coils would then be tuned to around
Australia’s electronics magazine
450-455kHz.
I tested all the coils using a signal
generator and a CRO, looking for a resonant peak when applying a varying
frequency signal. As I did this, I kept
in mind that the frequencies would be
somewhat reduced when built into the
set due to stray capacitances.
I added a 420pF padder to the oscillator coil and found that it would then
resonate from 960-2130kHz. The aerial coil resonated from 475-1550kHz,
again in the ballpark.
While IFT1 gave identical 400kHz
peaks on both windings, IFT2 was a
problem. One adjusting screw was
wound all the way out and jammed –
with the screwdriver slot broken off!
The good winding resonated at 405kHz
but the broken side was at 350kHz.
Freeing the adjusting screw just moved
the resonance down to 300kHz.
At some stage, the screw had been
wound right out in an effort to get near
the correct setting; the exposed thread
had a dab of red paint showing this
was a factory setting! The set probably
still worked but must have been down
on sensitivity.
I pulled the coil apart and removed
the peaking capacitor; it measured
120pF. Without this capacitor, the coil
resonated at 650kHz, so I judged the
coil was still usable. I fitted a 56pF
capacitor instead, and the coil then
resonated at 405kHz with its slug at
mid position, the same as the others.
The oscillator coil from the AWA set
was unshielded, but I wanted it in a
can, like the others. I fitted and tested
November 2019 101
The chassis was marked with the component layout and then holes were drilled for the valve sockets, power transformer
and IF transformers. After this, the chassis was coated with primer and painted blue.
it in a scrap square can to match the
aerial coil, which came from an unknown receiver. I planned to connect
the tuning gang fixed plates and the
converter grid cap above the chassis,
so drilled the cans for the coil grid
winding to come out the top.
The tuning gang already being located, I then marked up positions for
the coils, the valves and IF coils in the
front end of the set. I kept these parts
as a compact group on the left and
placed the detector and audio output
parts along the rear of the chassis. That
left the right side of the chassis for the
power supply parts.
I used the circuit diagram as a guide
and visualised the required layout.
The aerial and oscillator coils fit right
beside the tuning gang, to get the shortest connecting wires.
I positioned the aerial and Earth
connectors at the front, to avoid having
the aerial wire near the IF stages. I later
realised that I could have put the terminals on the back of the chassis and
routed the wires around to the front.
The valve sockets and the coils were
orientated for logical lead placement. I
drilled four holes for the two-bolt IFTs,
to give me several options later. You
have to think in three dimensions and
make sure that all securing bolts are
accessible and nothing hits anything
else. There are a few holes required for
wires to come from under the chassis
to above, eg, grid cap leads, dial lighting and gang connections.
It’s a bit like laying out a PCB. Some
of the resistors and capacitors will connect direct, point to point, but I placed
small pieces of tag board in strategic
locations to hold parts where the lead
length was not critical. I also added a
socket to the rear of the chassis for the
speaker leads.
The choke and power cord needed
holes too, as did the separate Earth
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Silicon Chip
screw on the right-hand side. I used
a Jaycar cord-grip gland to secure the
power cord. I drew the component
outlines with a Sharpie pen first, then
drilled all the holes once the pilot
marks were squared up.
Having drilled all the required
holes, I cleaned up the chassis, sprayed
it with etch primer and then blue Galmet hammer paint.
Speaker transformer
As the 6V6 audio output valve does
not have earth-shattering output power, I selected a Jaycar MM2002 (type
2215) 15W multi-tap power transformer to match it to the 8W speaker.
With a 230V AC primary and 15V AC
secondary, that gives a turns ratio of
15.3:1 (230 ÷ 15).
As the speaker is an 8W unit, the impedance seen by the valve will therefore be 1.88kW (8W × 15.32), which is
a bit low. If I used the 9V tap, the impedance would be 5.2kW which is a
bit more like it. A 6V6 in class A with
250V at the plate is specified for driving a minimum load of 5kW.
I wired a 6V6 and a 6Q7 together
on the bench to drive the transformer
and to test for the best of my valves to
use in the audio section. This lash-up
was powered from my trusty variable
power supply, which has 6V AC and
0-350V DC outputs.
The result was that the 6V6 gave
about 4W output with 250V DC at the
plate and the Jaycar transformer gave
identical results either interleaved or
air-gapped, which indicated there was
a surplus of iron and no DC offset saturation with either stacking.
I left the transformer air-gapped,
and on the final test, it was good for a
frequency response of 80Hz-5kHz at
4W using the 9V tap. The impedance
curve was fairly flat with a useful output from 2-16W, peaking at 6W. So it
would suit the 8W speaker nicely. The
output transformer started ringing at
The chassis at an early stage of assembly, with various sockets mounted, some
wiring done, and a fuse connected to the volume pot’s on/off switch.
Australia’s electronics magazine
siliconchip.com.au
The complete chassis is shown above. Note the stiff wire used as an Earth bar from the external Earth terminal at upper
left, terminating at the tag strip at lower right.
higher frequencies and at the clipping
power level. A capacitor across the primary reduced this tendency.
I did not employ any negative feedback in the circuit, to keep it simple
and keep the gain as high as possible.
I used 1930s parts in my tests and
found the only critical component
was the 6Q7 plate decoupling capacitor. Any leakage here would drive the
6V6 to maximum plate current (about
90mA) and choke off the audio. So a
low leakage capacitor is a must.
Chassis assembly
It was time to attach the basic bolton components such as sockets and tag
strips. RF components aside, I wanted
to mount them on tag strips. I drew up
a rough wiring diagram from the circuit diagram and pencilled in where
the parts could go.
From that, I arrived at the number of
tag strips needed and squeezed them
into the chassis as required, around
the valve sockets. These were washed
in methylated spirits and given a buff
up, then bolted to the chassis. Then
the transformers were given a black or
lacquer finish and also fitted.
I mounted the tuning gang and fitted the tuning coil and oscillator cans
in an orientation that gave the shortest grid and plate leads. That did not
work so well for the oscillator plate
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and grid leads, which can be seen running diagonally from the valve socket
straight to the coil.
The grid lead for the converter was
picked off the top of the tuning gang
fixed plate connection, and the oscillator coil was connected through the
can to the top of the gang. The IF cans
were mounted for shortest signal lead
length. I then fitted in the Earth bar
which runs from the external Earth
spring terminal, past the signal valve
sockets and terminates on a tag strip
with the HT divider components.
On its way, it picks up the shield
and cathode points of pins 1 and 8 for
each valve and provides a convenient
bar to wire bypass capacitors and signal ground points to.
I didn’t use the chassis itself for
any ground or B- connections; I prefer to run two wires to all points on
the circuit, keeping the signal B+ and
filament feeds separate. That is how I
make guitar amps, so I took the same
approach with this radio.
Mains cable and power-up
I fitted the mains cable and fuse and
completed the transformer primary
wiring. I used a bulkhead gland to
grip the power cord and attached the
Earth to a brass screw. That screw is
then wired to the single ground point
of the circuit, where the tuning gang
Australia’s electronics magazine
capacitors terminate.
I fitted a 2A mains fuse, then double-checked the power plug Earth pin
continuity to all chassis panels. Then
I powered up the transformer and
checked all the secondary voltages
and connections.
With all that satisfactory, I completed the filament wiring and plugged
in a set of dummy glass valves, and
checked that all the heaters lit up.
That also gave me the opportunity
to check the 5Y3 rectifier valve insulation and confirm B+ output at the filament, with the plates at about 450V
DC. With no smoke or flames, I then
proceeded to wire in the power supply components and the 6Q7 and 6V6
circuits, to test the audio section for
correct function and the smoothing DC
component’s suitability.
The volume control required shielded cable as the signal passes from the
rear of the chassis to the front and back
again. I probably should have mounted
the control on a bracket at the rear and
fitted a long extension shaft through a
front power switch.
Components and wiring for the audio and power supply were installed
but without the 6V6 and 6Q7 to start
with; just the 5Y3 rectifier. I powered
the set up via a Variac and monitored
the back-bias resistor voltage to give
me an idea of the current drawn. I
November 2019 103
watched the surge and forming current of the electrolytics, which was
around 100mA at first but dropped as
the capacitors formed.
After a minute or so, the current
dropped to a negligible level, so I slowly advanced the supply voltage to 230V
AC. The HT peaked at 450V DC with
little current flow, and nothing was
getting hot, so the forming action was
finished. The filament voltages were
normal, so I shut it down and plugged
in the 6Q7 and 6V6 valves.
The amplifier stages worked first
up, drawing a total of about 50mA, resulting in a back-bias voltage of -15V.
I injected an audio signal into the volume control and power tested with
a sinewave and a dummy load. The
6V6 gave an identical power output
as it did during my bench test, with a
similar frequency response.
Front-end testing
Working backwards, I continued by
wiring the detector and converter sections but only plugged in the 6K7. To
see how the IF transformers would react, I injected a 455kHz signal into the
plate pin of the 6K8 socket.
The signal got through to the 6K7,
and was then amplified, but IFT2 did
not seem right; there was no peaking
with slug adjustment, just a change in
amplitude.
This did not bode well, but I pressed
on, leaving the slugs set for an overall
peak at 455kHz. When the 6K8 was
plugged in, a stable oscillator signal
appeared at the 6K8 plate and this
could be adjusted over a range of 10002500kHz via the tuning knob. I checked
the DC voltages and they were more or
less as expected. There was -17V backbias with -2.5V at the tapping point for
the RF system. The HT was 280V DC
and 70V for the screen supply.
I injected a modulated RF signal
into the aerial circuit and was rewarded with a signal at the 6K8 plate
that included a strong 455kHz component, giving me a tuning range about
500-2000kHz which more than covered the AM broadcast band. So it
seemed that the basic tuning coil set
was suitable.
Substituting an external aerial for
the RF generator allowed me to tune
across the AM band and pick up the
spectrum of local Sydney stations from
2FC way past 2SM, and it was great to
hear actual radio stations!
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Troubleshooting
However, all was not well. The signal at the diodes of the 6Q7 was way
below expectations, and the volume
control needed to be at maximum to
get a reasonable output for the speaker – plus there was no AGC voltage.
There was indeed a problem with
IFT2. The only thing to do was to pull
it out and substitute another coil. I
found a Kingsley coil in my junk box
which was of a similar age and frequency range. I checked it for resonance and wired it in. Immediately,
I could peak the IF and had about a
volt of audio signal available at the
volume control.
Better still, I found I could slide
the Kingsley IFT can inside the faulty
AWA coil can, so from the outside,
both IFTs look the same.
But I still did not have any AGC
voltage, and the set was out of control,
with nasty distortion coming from the
detector and IF sections. I checked the
resistance of the AGC line to ground
and instead of megohms I found it to
be a varying low resistance of about
2kW. This was shunting the AGC voltage to ground.
This was caused by 2MW carbon
resistor R5 which had a resistance
which varied if I wiggled it! With that
replaced, I could get up to 20V off the
unloaded diode and once connected
back to the grid system, I saw between
1-10V depending on signal strength.
Interestingly, with the coil set working well, I could dispense with the
trimmers on the gang. The tracking of
the gang sections finished up giving
good enough matching so that trimming did not increase the signal level,
even at the top end of the scale; removing the trimmers simplified the build.
The signal was now as clean as you
could expect and with the IFTs all
peaked, the set was ‘lively’ with plenty
of background chatter off station with
low AGC, and an almost silent background when tuned in to a strong sta-
tion. However, there was a level of
hum and buzz that was not nice and
needed investigating.
The hum was mostly 50Hz, with
some buzz mixed in. I realised that I
had forgotten to Earth one side of the
heaters. Earthing pin 7 of V1-4 gave
better results than pin 2, and that
reduced the 50Hz level right down,
leaving the buzz to deal with. I noted
that the buzz varied with the volume
control setting, being almost non-existent at full volume and worse at half
volume.
This was because I had used a
switch pot to switch both mains and
millivolt-level audio signals. Placing
mains wiring anywhere near a highimpedance grid circuit is not a good
idea. The obvious thing to do would be
to get the mains wiring right away from
the audio wiring or shift the control
function to a less sensitive part of the
circuit, such as the output valve grid.
However, I persisted and found that
by re-dressing the mains wire around
the volume control and changing the
grounding point for the shielded cable,
I reduced the buzz to a minimum and
left it at that. In normal listening conditions, no hum or buzz can be heard.
DC voltage checks
I then decided to check the DC operating conditions of the valves. The
6V6 output valve was biased at -14V
and with 280V on the plate, was within specs. The 6Q7 generates its own
grid bias and amplified cleanly with
a gain around 15 times, with a plate
voltage of 80V.
The 6K7 and 6K8 were working OK
but with screen voltages a bit low, at
around 60V. I changed the divider
circuit to push the screen voltages to
90V, and the IF signal level increased
noticeably.
The set draws about 60mA with the
output valve accounting for most of
that, and after a couple of hours, nothing was overheating and the voltages
The faulty
AWA IFT2 was
replaced with
a Kingsley
coil which fit
perfectly inside
the AWA can.
However, this
did not fix the
lack of AGC
voltage.
Australia’s electronics magazine
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and currents were unchanged.
Tweaking the valve lineup
The valve lineup shown in the circuit diagram wasn’t finalised until
this stage, as I became a bit of a “valve
jockey”, substituting various compatible types to find the best combination.
I found that a particular metal 6Q7
had a bit more gain than the others.
The 6K7s all worked about the same,
so I picked the nicest-looking one.
The converter choice was interesting as I had many metal, glass GT and
G types to pick from. After a lot of to
and fro, I settled on a particular newold-stock 6K8G that worked quietly
with high gain and no sign of instability, as it is a shielded construction.
Not knowing a great deal about
converter design, I took the easy approach and merely selected the bestsounding valve.
Most of the capacitors I used are the
1960s mud-brown types. Low-value
capacitors are all original “Simplex”
mica moulded types. I didn’t use any
1930s or 40s wax or moulded paper capacitors as they are all quite leaky now.
The resistors are mostly carbon wire
end types plus a few wirewound. The
electrolytics are 1960s 600V TV plastic
types, hidden in some older “Ducon”
cardboard tubes.
Dial lighting and scale
The chassis was offered up to the
cabinet again and lined up, to check
the spindle length was correct to fit
knobs and to see what room there was
to fit the dial scale. It was then that I
discovered the gang spindle was not
in the centre of the dial escutcheon. I
missed by about 15mm
vertically for one reason or another, thus
making a direct 1:1 dial impossible.
The other choice I had to make
was between a fixed scale and moving pointer, or fixed pointer and moving scale. What then followed was a
series of trials, making up cardboard
dial scales. The best solution I came up
with was a porthole escutcheon with a
fixed pointer at top centre and a simple moving circular dial behind that,
bolted directly to the gang drum, with
the stations and frequencies marked on
it. In the end, I blanked off most of the
curve in the escutcheon with a plate,
leaving a wedge-shaped port with a
fixed centre pointer.
I then mounted a simple dial plate
off the gang drum. The dial plate was
then marked with stations and covered
with a plastic disc to keep it clean.
Working on the smaller radius of the
lower escutcheon opening reduces
the usable circumference and crowds
the station markers together, but that’s
what I am stuck with.
Next time, I will know better and
position the escutcheon to use a larger diameter for greatest scale length.
The remaining work concerned
mounting a dial light above the pointer
position, making up a speaker connecting lead, finalising the exact position
of the chassis in the frame, drilling the
chassis securing holes in the frame and
fitting a set of temporary knobs to operate the set. I will find a more suitable
pair at some stage.
It’s the old story; I have plenty of
knobs that look the part by themselves
but not two that look completely right
together.
Conclusion
The set is sensitive enough to pick
up local stations with a short lead on
the aerial terminal, but works much
better with a 10m outdoor aerial. The
6V6 gives adequate listening level for
room use. The tone of the finished radio
is slanted toward the bass end, mostly
due to the big speaker I used.
I did an audio frequency response
check from the RF modulated signal
generator and found it to be flat from
200Hz to 3kHz, with -3dB points at
110Hz and 6kHz. But the 15in speaker skews that towards the bass end.
The cabinet could do with a tweeter,
but enough is enough; this is 1935,
after all!
One of the last jobs was to level the
legs of the cabinet and drill the frame
for the hold-down chassis bolts. The
cabinet had warped over the couple of
weeks it took me to finish the chassis
and rocked diagonally by about 3mm.
I shortened the longer leg by about
2mm, then fitted some stick-on felt
feet – the cabinet finally stood square.
With the chassis pushed into final
position and the dial lined up, I pencilled through the chassis holes and
drilled the timber out double oversize,
then bolted the chassis in place with
3/16-in bolts.
The set now has the external appearance of a well-worn and faded
70-year-old cabinet, but it has a spick
and spiffy chassis inside with RCA
octal type valves, which were just
plausible in 1935. It’s as if some were
later replaced with glass types and the
capacitors were later replaced with
1960s models and re-wired with modern plastic cable.
The set sits in my little collection as
representing a 1930s radio and it was
fun to build, and learn a little more
about RF circuits and valves.
Extra details on this set can be read
in the forum post Fred Lever made at:
siliconchip.com.au/link/aapw
SC
The finished dial was drawn by hand
onto a piece of stiff paper.
siliconchip.com.au
Australia’s electronics magazine
November 2019 105
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