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SERVICEMAN'S LOG
A shockingly cute new companion
Training pets, especially of the feline variety,
can be difficult. However, as is common
nowadays, there are likely close to a myriad
of ways to help. One method is via a “pet
training mat”, which emits a buzz and
‘small’ electric shock, with all the safety
you would typically expect from cheap
electronics sold online.
We recently got a new cat (or, perhaps more accurately, the cat got some
staff to look after it). This feline is as
cute as a button and therefore impossible to discipline properly.
While many cat owners allow their
pets to walk all over the kitchen benches and scratch the furniture, we don’t.
Footprints on work surfaces and shredded mattresses and armchairs may
well be part of the ‘joy’ of cat ownership, but we have always deterred our
furry housemates from this behaviour.
We’ve used several training methods over the years, the most technological of which was a slightly modified version of the Silicon Chip “NickOff” Bad Cat Deterrent (October 2012;
siliconchip.com.au/Article/502). We
found this worked for our cats at the
time.
However, they eventually got wise
to it and ended up blatantly ignoring
it. They would jump onto the cooktop and bench, to either drink out of
the sink (their expensive cascading
water fountain is obviously not good
enough!), or scavenge their share of
the roast we’d just eaten for dinner.
While we’d managed to train all our
cats, past and present, not to do this
with a combination of water squirting
bottles, sticky tapes, deterrent sprays
and electronics, the new addition did
and went where it liked. When the older cat saw this, his old habits started
creeping back in.
I’d long-since repurposed the NickOff for another project. But while I was
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browsing for parts to build another one
on AliExpress, I spotted a possible solution: electronic pet training mats.
These seem to be a hot product these
days, both on local and international
shopping sites. I was aware of such
devices, but in the past, I was put off
them because the one I saw was not
user-friendly and a bit too aggressive
in operation.
Admittedly, it was designed for a
medium-sized dog, but even on the
‘low’ setting it still delivered what I
considered a nasty shock, out of proportion to the ‘crime’ of the dog sitting
on the owner’s favourite chair. The
mat or sensor part of it was also rigid,
prickly to handle due to embedded
wires tracks and hard to clean.
I’ve never been a fan of giving electric shocks on purpose, having suffered a few ‘good ones’ over the years.
Because of this, I have some empathy and a natural aversion to deliberately shocking anyone (or anything). I
especially despise those ‘joke’ shockpens and cigarette lighters that were
all the rage at one point; I don’t think
lighting someone up deliberately is
funny at all. I can’t recall seeing anyone blitzed by one of those things rolling on the floor laughing. Mostly they
just look annoyed…
Anyway, I figured there must be
some better training mat options available these days, so I went online to
check. The modern versions are inexpensive and sized for different pets,
with adjustable shock levels and more
Australia’s electronics magazine
Maggie Thompson
Items Covered This Month
•
•
•
•
The cat in the mat
Hot water system repair
Yamaha CR-1020 restoration
Mitsubishi ABS pump repair
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
flexible, easier-to-manage sensor mats.
I found similar products for sale at
local pet shops, but at significantly
higher prices.
The pitfalls of buying online
I’m not a cheapskate, but I do object
to being gouged by local sellers. The
typical reason thrown about for exorbitant mark-up on just about everything
imported into New Zealand is “shipping costs”. That excuse may have
washed fifty years ago, when nobody
really knew the true cost of goods,
but these days everyone knows that it
doesn’t justify the prices many local
sellers try to charge.
So it is no wonder that buying from
overseas vendors is increasingly popular!
But there are challenges to ordering online. So many products look
very different when they arrive from
the often-doctored pictures on vendors’ sites.
The benefits of buying locally are obvious; stores typically have what you
want, have regular sizing and naming
conventions throughout product ranges, and you can always take something
back and (typically) get a refund or a
replacement if necessary. Sending anything, especially something of relatively
low value, back to an overseas vendor
is usually neither practical nor financially feasible.
In practice, I shop locally for some
items and use overseas vendors only
when this makes financial sense, or if
siliconchip.com.au
a job isn’t time-critical. I’ve made hundreds of online trades for all manner
of goods, generally from China and
the USA, and while I have had mostly
positive experiences, there have been
some hiccups.
I purchased several cameras from
China only to be disappointed. One, a
GoPro-style action camera, claimed to
be able to record video at 4K resolution
(3840x2160 pixels) and 60 frames per
second (fps). This is ostensibly backed
up by the words 4K emblazoned across
the front of the case.
But my attempts to record anything
with it higher than 720p (1280 x 720
pixels) and 25fps resulted in unusable
video. It’ll record at 4K, but only at
around 1fps. If a local retailer advertised and sold such a product, their
shop would be razed by a pitchforkand-torch-wielding mob. But online
vendors will happily hawk this and
similar products with the knowledge
that there’s little we can or will do
about it.
Another much more expensive action camera I bought online last year (I
was learning!) works much better, but
still had problems. It will record at 4K
and 60fps and has remote control via
app, Bluetooth and WiFi, among others. But the battery went flat overnight,
even when the camera was switched
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off. Having to
charge it for
hours before every use was a royal
pain in the lens cap.
When I looked into this, other buyers had the same problem, and a firmware update was apparently the answer. I eventually found and downloaded the firmware. The update resolved that issue, but it was a lot of
extra work when it really should have
worked properly in the first place.
As always, it comes down to “caveat
emptor”– buyer beware – particularly
with more significant purchases.
Bringing the felines back in line
Anyway, because of the relatively
low price of these training mats, and
with a lack of other ideas, we ended
up buying two small pet training mats
from AliExpress.
When they arrived a few weeks
later, the hazards of online shopping
were once again apparent. While the
mats were pretty much as advertised,
their construction is what one would
expect from such a cheap product.
Only one of them arrived in working
condition.
The mats are powered by three AA
cells; I hope they do not chew through
them too quickly, as that could get
expensive. If push comes to shove,
I’ll modify them to run on one of the
dozens of spare plugpack power supplies I have taking up drawer space
in my workshop. But before fretting
about that too much, I needed to fix
the broken one.
The mat’s controller is a sausageshaped plastic housing with a flattened
bottom that sits along one short edge
of the rectangular mat. It has a threecell battery holder with a removable
lid, and a single button on the top to
switch the power on and off when held
down. Short presses cycle through the
Servicing Stories Wanted
Do you have any good servicing stories that you would like to share in The Serviceman
column? If so, why not send those stories in to us?
We pay for all contributions published but please note that your material must
be original. Send your contribution by email to: editor<at>siliconchip.com.au
Please be sure to include your full name and address details.
Australia’s electronics magazine
October 2019 71
three shock settings: low, medium and
mad scientist. This is indicated by
three small LEDs.
There is also a built-in piezo buzzer
that chirps when the button is pressed
and quickly sounds multiple times if
the sensor pad detects anything. The
pad resembles a large, flexible-plastic
thin-film PCB with closely-interlocking printed silver tracks.
Briefly bridging the tracks results in
a warning alarm, but no shock; if contact is maintained for more than a few
seconds, a shock is delivered through
the tracks at the level selected. I’m too
chicken to put my hand on it, but I did
bridge the tracks with a short length of
hook-up wire and there was a frankly
unnerving amount of crackling and
popping at the connections, even on
the lowest setting.
There also appeared to be an undocumented feature; a vibration sensor
in the controller triggers the warning
beeps (but not the shock) when movement is detected. Even lightly bumping the bench sets it off.
the bottom of the controller. The two
moulded halves then came apart. The
electronics look surprisingly comprehensive and well-made, with a host of
SMDs and a couple of those blob-style
COB (chip-on-board) ICs on the board.
Cloth insulating tape covered some
of the components on the ‘hot’ end of
the board, and initially, I left that in
place. The circuitry was more complex
than I expected to find, and with PCB
component soldering looking good,
my expectations of an easy fix might
have been misplaced.
I found that the two HV output connections between the mat and the PCB
were just stripped-bare hook-up wires,
flattened out at the ends and clamped
onto ‘terminals’ on the mat between
the two halves of the case. A screw
through the centre of each terminal
ensured a solid
connection.
I don’t consider this to be a particularly elegant solution, but it’s probably
effective as long as the contacts are not
disturbed too many times by repeated
disassembly.
I wasn’t sure how rugged the sensor
tracks were. They appear to be made
from conductive silver paint, screenprinted onto the clear plastic mat;
scratching through a track at any point
would break its continuity. While one
of the PCB wire-to-pad connections
might have been where things had
failed, my gut feeling was that while
basic, the contacts should be OK.
To take the PCB out, I had to remove
a couple of small hold-down screws.
I also needed to release the positive battery terminal, which clips
Fixing the obvious fault
Disassembly of the faulty mat was
easy. Thankfully, there were no dumb
anti-tamper fasteners; just eight small,
cross-head PK screws to remove from
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Australia’s electronics magazine
siliconchip.com.au
into a moulding in the top half of the
controller and has a metal tongue that
extends down into the PCB cavity below, where it attaches to a solder pad
on the ‘input’ end of the board.
After removing the PCB screws, I
turned the unit over to see how that
positive battery terminal should be removed, and the PCB fell out onto the
workbench. I was reasonably sure the
battery terminal should be soldered in,
but a look under the magnifier revealed
no solder on it at all. There was a corresponding blob of solder on the PCB
though, with the shape of the tongue
embedded in it.
It looked like it had been pushed
into hot solder but had never been
physically connected.
Thinking that it might be designed
as a push-fit, for ease of assembly,
I opened the other working mat to
check. That mat’s positive terminal
was properly soldered in. I sat the
PCB back in the dead one, cleaned
the blobbed solder from the pad and
tinned and re-soldered the tongue. A
quick (and very careful!) check with
batteries fitted showed this resolved
the problem.
Reassembly was just as easy, though
I took care around those fragile-looking contacts. How the mat passed QA
checks (if any) is anyone’s guess, but
it’s a good example of why buying
online can be problematic. Someone
who isn’t afflicted with the Serviceman’s Curse would have probably just
binned the mat and taken the hit.
You’ll be pleased to know the cats
have come to no harm but very quickly
learned not to walk on the bench. They
now run off in every direction at the
mere sound of those warning beeps!
Hot water system repair
A. K., of Armidale, NSW, had a solar hot water system installed in 2010.
It worked well for years but recently
went on the fritz and he had to fix it...
Periodically, I check the various
temperature readings on the Solastat
controller, more out of interest than
any other reason. One sweltering day
last summer, I noticed that the solar
hot water controller was displaying
the fault code “SSd” instead of the
roof sensor temperature.
I checked the manual and “SSd”
stands for “Smart Shut Down”, where
the system idles in case of a shorted or
open sensor or cable wire. This fault
can also be displayed when the temsiliconchip.com.au
The Solastat temperature sensor, shown above, was repaired by replacing a
single NTC thermistor within it.
perature sensor is outside the specified
temperature range of -40°C to +150°C.
Upon further inspection, I found the
roof sensor or cable was open circuit.
Luckily for me, it was late afternoon
so the corrugated iron roof had time to
cool down from its peak temperature
on that 33°C day.
I went up onto the roof to remove the
sensor from its housing and noticed
that very little sealing compound had
been used. I decided to cut the sensor
from the cable, leaving 10mm exiting
the sensor. I probed these wire stubs
with my multimeter and found that
the sensor was open circuit.
The temperature sensor was potted
in a small steel case. I picked away at
the filling until I reached the sensor, a
small beaded glass device with no visible markings. The user’s manual didn’t
give any information as to its type.
I went onto the web and fortunately, Senztek (makers of Solastat controllers) have various manuals available for download from the website. I
found an installation guide with a table of NTC sensor resistance readings
at various temperatures. It specified a
value of 10kW at 25°C.
Further web searches revealed an
Australian site selling replacement
10m cable with roof sensor to suit
Solatstat controllers, including free
thermal paste and joiners. Tempting!
But fortunately, I already had some
10kW NTC thermistors which followed
the temperature curve of the original
sensor quite closely. The next day, I
removed all the filling from the old
sensor housing and replaced it with
my new NTC thermistor. I used hightemperature epoxy putty to hold it in
place and then re-soldered the sensor
to the controller cable, adding two layers of heatshrink tubing for weatherproofing.
Where the sensor cable exited the
corrugated iron roof was utterly devoid
of any sealant and as it was another
hot day, I decided to fix that later, in
the cool of the evening. So I dropped
down to my local electrical distributor
and purchased a cable gland.
Australia’s electronics magazine
Back on the roof that evening, I Installed the cable gland in the roof,
through which the sensor cable now
ran. I smothered the sensor’s metal
case with silicone-based thermal paste
and then slid the refurbished sensor
unit into place. Finally, I used some
neutral cure silicone sealant to secure
the unit into the solar heater housing
and prevent moisture ingress.
It has been nine months now since
the repair and my new sensor has not
missed a beat. The replacement NTC
thermistor sensor I used cost me $3
while a replacement cable with sensor would have cost $65 and that’s not
including labour. I figure it was a job
well done.
Yamaha CR-1020 receiver repair/
restoration
R. A., of Melbourne, Vic, decided to
restore a retro amplifier to its former
glory by fixing a few small faults which
had developed over its many years of
use. This is how he did it…
The Yamaha CR-1020 is a chunky
receiver from the late 70s. It’s powerful for its day at 80W per channel with 0.05% THD, both channels
driven. It incorporates an excellent
FM tuner. It originally cost $895, at
a time when a base Holden HZ sedan
started at $2150.
I snapped up this mint-condition
receiver in 2014 for $400. It has given
good service ever since. These now
sell in the USA for well over $1,000,
which prompted me to get to work
fixing mine.
It had a few minor niggles: none of
the lamps behind the fascia worked
and the back panel switch that couples the preamp/tuner to the power
amplifiers was scratchy. Working the
switch a few times helped, but I prefer
a permanent cure. Its timber case was
also damaged in transit, on a lower
front corner.
Opening it up, I found all five fascia lamps open-circuit. These “grain
of wheat” lamps are nominally
12V/60mA. Four are located behind
the three meters, connected in series/
October 2019 73
parallel and powered from a 19.23V
DC rail. The fifth is mounted on the
tuning dial pointer and runs from a
9.68V supply.
The reduced rail voltages were intended to prolong the life of the lamps.
The subtle glow also imparts an air of
sophistication to the unit.
Googling revealed that it is common
for these lamps to all fail, and that
plenty of replacements are available,
both LEDs and incandescent.
Oddly, all four lamps in a series-parallel circuit can fail; if one goes opencircuit, you would expect its parallel
lamp to then fail, disconnecting the
other two from the supply. But somehow, this does not happen.
I ordered some replacement incandescent lamps and then checked
the supply voltages. The 19.23V rail
(shown as 19.6V elsewhere in the circuit diagram), which also drives the
speaker protection relay, measured
just 13.5V.
I suspected a dud filter capacitor. My
DSO showed significant ripple on this
rail. Clipping two 100µF caps across
it drove the reading up to 17.5V (with
a low mains voltage of 227V), while a
2200µF cap increased it to 19.2V. So I
was pretty sure that the original filter
capacitor had failed.
While doing this testing, I also noticed that the speaker relay was pulling
in with a very soft click, but with the
larger capacitor added, the click was
restored to its normal, strong sound.
The replacement lamps arrived and
fitting the new meter lamps was fairly
straightforward. But the dial lamp was
more tricky. It uses a Heath Robinson
arrangement of articulated nylon arms
which keep the wiring from the dial
lamp out of the way as the pointer
tracks across the dial.
I undid the two Philips-head screws
that held the sliding assembly together,
gently pulled it half way open without
disturbing the dial cord, pulled out the
old lamp, inserted the new one and
put everything back together.
With a temporary capacitor in place
in the power supply, I powered the
unit up. The four meter lamps looked
good, but the dial lamp only glowed
dimly. It was only getting 4.3V due to
the higher current rating of the new
lamps (12V/70mA).
The dial lamp has a 180W dropping
resistor in series, while the four meter
lamps are fed from a low-impedance
source. I found that adding a 560W 1W
resistor across the 180W resistor gave
about 10V across the dial lamp and an
acceptable level of brightness.
I then turned my attention to the
low 19.23V/19.6V rail. There is an apparent oddity in the circuit diagram,
The internals of the Yamaha CR-1020 amplifier, with the power supply circuit diagram shown mispelled above. You can
find more details on this amp at http://www.mcqart.com/cr1020/ and http://sportsbil.com/yamaha/cr-1020-om.pdf
74
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Australia’s electronics magazine
siliconchip.com.au
in that this rail feeds into diode D1,
and you get 20.8V at its cathode. How
does this work?
It’s because there is so much ripple
on the 19.6V rail that its average voltage is much lower than its peak voltage. A 1000µF capacitor at D1’s cathode means that the voltage on that
side is much smoother and closer to
the peak voltage.
This was done on purpose, so that
the speaker protection relay drops out
fast when mains power is removed.
This avoids nasty speaker thumps as
the amplifier rails decay after switchoff. Diode D1 isolates the larger cap
from the 220µF unit and stops it from
prolonging the relay holding time.
I think that the high ripple current
the 220µF capacitor is subjected to by
this arrangement is the reason it failed.
So I replaced it with a more robust
330µF/50V unit.
Accessing the underside of the relevant PCB would have been a major
undertaking, so I removed the dud
capacitor and soldered the new one
across the wire-wrap stakes which
connect to the supply rail.
Next, I decided to fix the coupler
switch. Access to it proved basically
impossible, so I simply gave it a good
spray with isopropyl alcohol, which
appeared to do the job.
I fired the amp back up, and it all
worked as expected. With 237V AC
mains, the output of the diode bridge
was 19.0V DC, which is about right (the
original specs were for 240V mains).
The speaker relay pulled in firmly after
its three-second delay, with its subsequent release appearing to be simultaneous with mains power switch-off,
and no thumps were heard from the
speakers.
siliconchip.com.au
I then checked the quiescent current in the power amplifiers. Working
carefully, as a slipped prod can cause
mayhem, I compared the test point
voltages against the specification of
10mV±1mV. Both channels rose to
about 14mV, so I carefully adjusted
the trimpots to get 10.0mV.
With everything working well, I
turned my attention to repairing the
damaged veneered plywood sleeve. I
dripped water onto it over more than a
week, to get it to swell back out, then I
sanded it and applied ‘plastic wood’.
More sanding, then the application
of a dark stain and finally coats of Gilly’s dark restoring polish produced a
remarkably good result, as seen in the
photo of the restored unit below.
The quality and labour that went
into this receiver is a tribute to its
makers. The complicated electronics
(with 109 transistors) has worked well
for over 40 years, indicating a great design and execution.
The cadmium-plated chassis still
gleams like new. The newly-polished
timber sleeve still looks great, and the
sound is still excellent.
Mitsubishi Lancer ABS pump
motor repair
R. H., of North Sydney, NSW had
a frustrating experience where a professional repaired the ABS (anti-skid
brake) unit from his car twice, and it
quickly failed again both times. He
had to open it up to fix it properly
himself…
On taking my Lancer for a service,
the mechanic advised me that the ABS
light was on and a scan revealed error
code 116 (low voltage at the hydraulic
pump). A better description might be
“open circuit hydraulic pump motor”.
Australia’s electronics magazine
A new ABS unit would cost over
$3000 plus fitting. I then found out
about a business which fixed ABS
units. All I had to do was take the unit
out and then for $350, they would service it. After which, I had to re-install
it and bleed the brakes. All went well
after re-installation, with no ABS light
showing.
The trouble was, after about five
months, the light switched on again.
As the unit was still under warranty, I went through the same process
again. But after re-installing it, the
ABS light stayed on. A scan showed
the same error code 116, and it could
not be cleared, so I gave up for the
time being.
Shortly after that, I found a video
on YouTube showing how to fix this
ABS unit. It appears that quite a few
ABS units in various vehicles have the
same problem.
This time, I decided to do the whole
job myself. So out comes the ABS unit
once again, and following the steps
on YouTube, I managed to isolate the
motor from the valve body. I then put
an ohmmeter across the motor’s terminals and it showed an open-circuit
reading.
On taking the motor’s case off, I
found a brush hung up in its cage. It
had to be gently massaged with fine
sandpaper to give clearance between
the brush and cage, so that it could
move up and down easily. I gave the
same treatment to the other brush.
On re-assembling the motor and
applying power, the motor hummed
away – good! Next, I had to re-assemble
and re-install the ABS unit, then bleed
the brakes. The ABS light remained off;
wonderful! It has remained this way
for a couple of years now, touch wood.
I don’t understand how this problem
arises. Was the retaining spring behind
the brush too weak to keep it seated
on the commutator? What caused the
brush to lift off the commutator in the
first place?
Editor’s note: perhaps the car hit a
big pothole which lifted it off briefly,
and it got stuck.
One person on a web forum reported
that he hit his ABS unit with a hammer, with a block of wood between
the hammer and the valve body. It
sounds a bit Heath Robinson but in
hindsight, having observed the problem firsthand, it may just work; the
impact could re-seat the brush back
onto the commutator.
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October 2019 75
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