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SERVICEMAN'S LOG
Giving an old companion its voice back
I’ve always been interested in loudspeakers.
Their electromechanical nature appeals
to me, as a good speaker needs to be both
mechanically and electrically sound, the
two parts working together in harmony. It
amazes me that despite modern technology
and improved materials, their basic
operation hasn’t changed in many decades.
Modern speakers tend to be more efficient, and usually offer a wider frequency range in a similar-sized cabinet compared to older speakers. But I
don’t think they necessarily sound as
good as older models.
Of course, this is open to argument.
There have been endless flame wars,
err, I mean discussions online as to
what is the best type of speaker. Some
quote specs to prove how much better their speakers are. But like many
others, I don’t care about the figures
as much as how the speakers actually
sound to me.
Money for nothing
I’ve spent a good deal of time in recording studios and high-end showrooms over the years listening to expensive drivers. They don’t always
sound as good to me as the numbers
suggest. While it could be that I’m just
an audio philistine, I know what I like.
Merely throwing money at speakers
with fancy-sounding European names
doesn’t guarantee pleasing results.
I’d also argue that the speaker is
merely one of the components in a
system; all the components need to be
up to scratch. Driving a $5000 set of
speakers from a cheap and nasty amplifier (or even an expensive one, if it’s
poorly designed) won’t do them any
favours. And running a rubbish set of
speakers from a $5000 reference amplifier is just a waste of money.
The fact is that all speakers are not
created equal, and the extensive range
of cabinets, enclosure materials, driv86
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er constructions/configurations and
crossover designs means there’s a lot
of room for experimentation.
Anyone who has kept up with hifi
magazines will be aware of the trends
and fads that have come and gone over
the years, with speakers made of everything from concrete tubes to metal
drums and even cardboard.
I recall back in the 70s, a family
friend showing off his expensive (and
admittedly cool-looking) electrostatic
speakers; the first I’d seen outside of
magazines.
When he fired them up though, I
wasn’t as blown away as I thought I
would be. They sounded good, but
I reckoned our middle-of-the-road
system at home sounded better. And
while our speakers didn’t look like a
couple of framed antique prints hanging on the wall, at least if I cranked
the volume, I could feel the sound as
well as hear it.
Editor’s note: electrostatic speakers
can give excellent mid-high definition but are famously lacking in bass,
with some having integrated magnetic woofers to try to overcome this
limitation.
However, home stereo systems are
not the only domain of quality drivers.
The live music and sound reinforcement worlds feature some serious,
high-wattage hardware. Whether it’s
an 18-inch bass driver designed for PA
systems or a 10, 12 or 15-inch instrument speaker, the type and quality of
driver used will profoundly affect the
resulting sound.
Australia’s electronics magazine
Dave Thompson
Items Covered This Month
•
•
•
•
Guitar speaker re-coning
Fixing an inverter arc welder
Panasonic AM/FM radio repair
Double wall oven repair
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
Let’s say I buy a generic 12-inch,
50W speaker from the local electronics store. It’s likely a lot cheaper than
buying a speaker designed specifically for instrument amplification, but it
will almost certainly not give me the
sound I’m looking for, and given the
punishing output of an overdriven
guitar amplifier, it may not last very
long either.
Listen to the music
Choosing the right speaker can
therefore be a bit of a mission. Only
the individual knows what sounds
good, and this knowledge is not always transferrable to somebody else.
Looking at catalogs doesn’t help much
either, with lots of purple prose being
used to describe speakers to potential
buyers.
It’s a bit like trying to describe colour to a blind person; for example, the
literature for guitar speakers throws
around terms like “crunch”, “throaty”,
“warmth”, “vintage”, “punch”, “expressiveness” and “chime”. But what
do these terms really mean? Half of
them sound more like terms you’d
expect to hear when wine tasting, not
shopping for a loudspeaker!
Most of the musicians I know simply go down to a music shop, plug in
their instrument and play various amp
and speaker combos until they find one
that sounds like what they are after.
I’ve only ever purchased one speaker from a catalog, and that was for
someone who specifically wanted it
to put into an existing cabinet. The
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result wasn’t to my taste, and certainly didn’t match what I interpreted the
catalog’s descriptive terms to mean,
but he was rapt with it, which is the
key point I guess.
This is why musicians become passionate about their gear. We’ve usually
spent years getting our sound, and we
don’t want to have to go through all
that drama again. Besides, this newfangled stuff generally doesn’t sound
as good. So losing an amp or speaker
can be like losing an old friend.
Having gear nicked by some chancer
at a gig, or damaged on-stage by a bandmate who has had one too many falling
into it can be tough to take. Losing a
‘vintage’ amp or speaker is even worse,
as these can literally be irreplaceable.
The sounds of silence
Recently, one of my speakers failed;
an ancient Celestion G12-65 (12-inch,
65W, 8W) used mainly for workshop
testing. I’m not sure why it popped,
but given it is at least 35 years old it
could have just thrown in the towel.
It worked the last time I used it, but
when I plugged it in the other day to
test a valve amplifier I’d repaired, there
was nobody home. I first thought I’d
messed up the amp repair, but on fursiliconchip.com.au
ther testing, I discovered the speaker’s
voice coil was open circuit.
I was despondent, as this speaker
has been with me through thick and
thin. While checking online and reeling at today’s prices for a replacement,
I came across some Celestion re-coning
kits and thought that this was a perfect solution.
Back in the day, proper re-coning
kits were hard to come by and expensive; now they’re a dime a dozen.
At $65 including shipping, it was a
lot cheaper than replacing the whole
speaker, which all things considered
is actually still in pretty good nick, the
blown voice coil aside.
The rub with replacing a voice coil
(pun intended!) is that to get to the
coil, everything has to come out of the
basket (the metal frame of the speaker).
And those parts are generally glued in
pretty well.
It might be possible to remove the
old cone and spider (the flexible, corrugated disc that covers and protects
the coil cavity) intact, using a razorblade or similar. But it simply isn’t
necessary as there is a new cone, spider and dust-cap (the bit in the centre
of most speakers) provided in the kit.
I can already hear the purists wailAustralia’s electronics magazine
ing about the fact this will no longer
be a vintage speaker. But I’m OK with
that; I’d rather have a newish working
speaker than a dead vintage one cluttering up the workshop.
When the kit arrived, I first tested
the new voice coil; I didn’t want to
go through replacing everything only
to fit a dud.
The old speaker had a nominal
impedance of 8W, and while the
replacement coil read only 6.3W on
my multimeter, that’s actually correct.
A multimeter measures the DC resistance only, not the complex reactance,
which depends on frequency.
September 2019 87
You probably wouldn’t get a correct
impedance measurement for a coil by
itself anyway, as there is a mechanical
component to the reactance as well as
the fact that the coil is inductive.
To measure the impedance of a driver, you need to use a specialised tester.
Or you can hook up a sinewave signal
generator to the input of an amplifier,
connect the driver to the amplifier via
a high-power fixed value resistor, then
measure the varying voltage across the
driver. Some basic calculations using
Ohm’s Law then give you the impedance at a given frequency.
Don’t fear the repair
Re-coning is often seen as a complicated process not worth doing, so
many people don’t even consider it.
But I’ve done it quite a few times over
the years and if I can do it successfully, so can anyone. I’m no magician!
Just a guy with some tools and a little
bit of knowledge, and I’m not afraid
to have a go.
I started the job at hand by preparing to remove the old cone. The spider
and voice coil are connected to the bottom of it, and the leads from the coil
are soldered to the terminal on the
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basket. So I first had to release those
wire connectors. I could have just cut
them off, but I wanted to get an idea
of their overall length, so I heated and
un-wrapped them instead.
I then used a hobby knife to cut
around the edge of the spider and removed enough of it to allow me to see
and mark the voice coil resting depth
in the magnet cavity with a sharpie;
I might need this approximate measurement later.
Next, I cut the cone away as close to
the basket as possible, leaving the gasket (the thick mounting material stuck
over and around the outside edge of
the cone) behind.
The whole assembly was then lifted
clear, and I noted the state of the voice
coil as it exited the magnet cavity; in
this case, it appeared undamaged. This
may seem an odd thing to do, but it
tells me whether I should check the
magnet aperture more closely for blobs
of melted wire or other debris.
With the cone clear, I quickly sealed
the open coil cavity using several
strips of masking tape. In a workshop
like mine, there are metal off-cuts and
dust everywhere, no matter how well
I clean it. Murphy’s Law dictates that
Australia’s electronics magazine
some of this will find its way into that
gap otherwise.
Given the size and strength of the
magnets on guitar speakers, which are
typically welded or otherwise permanently bonded to the basket, the potential for contamination is high. Removing anything magnetic that gets stuck
in there can be very difficult.
I know techs who don’t bother with
this masking-off ritual, especially if
they are going to re-cone the speaker
immediately, but I neglected to do this
on one of the first speakers I re-coned
and some foreign objects got in there.
It was a right-royal pain clearing them
out. For the sake of a minute or two of
time and a few strips of tape, I avoided
much potential misery.
I proceeded to strip the basket of the
remaining gasket, cone and spider material. It depends on how this has been
attached as to how much work it will
be to remove it. In this case, they used
some kind of cement. I used a hobby
knife and razor-scraper to very carefully cut the remains as close to the
basket rim as I could.
The possibility for slipping and
carving up one’s own hands at this
point is very high, and as I’d done exactly that a few times as a youngster
building model aircraft, I was particularly averse to having it happen now.
Nothing teaches sensible tool skills
better than the memory of a painful injury (and boy, do I have a few of those,
as regular readers will know)!
Even though I cut very close and
removed almost all of the remaining
bits, I couldn’t get it all with a knife.
While I could possibly have glued
the new bits onto this and had no further problems, it only takes a slight
amount of asymmetry at the wide edge
of the cone to stress it. That can result
in the voice coil rubbing on the side
of the magnet cavity or non-optimal
sound reproduction, even if the voice
coil does clear the sides.
It is well worth the extra effort to
clear the old glue and cone from the
basket completely. In such cases, I
break out my trusty rotary tool and use
it with a brass wire-wheel attachment
to clean up the rest. This tool is speedadjustable and perfect for the job, but
it does make a real mess, so I made
sure to do this job outside (see above
on sealing the magnet gap!).
A quick brush and vacuum afterwards had the basket completely free
of any debris. Compressed air can also
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be used, but I’m wary of blowing more
rubbish about, so prefer the vacuum
cleaner option.
Before going any further, I checked
that the basket was still reasonably flat
by sitting it face-down on a saw-bench
table. These speakers can get knocked
about a lot on tour, and over-worked
(and possibly over-enthusiastic) roadies can sometimes distort the basket
when securing the driver to a cabinet
using power screwdrivers.
A twisted basket can result in a
trickier set-up during the re-coning
process, and baskets that are out-ofround or too far gone usually need to
be replaced. This one was still fine,
despite its long history.
Meet the new cone,
same as the old cone
Speaker coning kits come in several
forms; some are pre-assembled, which
means the voice coil, spider and cone
are all glued together at the factory.
This makes the job considerably easier, as the new assembly can simply be
dropped into the basket, aligned and
glued down.
However, many kits come as separate components, and while this makes
things a little trickier, the process is
still relatively straightforward. My kit
came unassembled.
After double-checking there was
nothing loose that could foul things
up, I removed the masking tape covering the voice coil gap. Despite having
taken this measure, I decided to check
that the gap was clean by wrapping
some double-sided tape onto an old
ice-cream stick and inserting it into the
coil gap, probing it around inside the
cavity to pick up anything that might
have gotten in there.
The first tape came away slightly
grubby, so I repeated the process with
fresh tape a couple of times until it
came out completely clean.
I compared the new voice coil to the
old one, making sure they were the
same physical size; they were. I positioned the new coil into the gap, using the supplied Mylar shims packed
around the inside edge to centre everything properly over the magnet. I then
adjusted the coil to sit at roughly the
same height as the mark I’d made on
the old one; I’d fine-tune it later once
the spider and cone had been fitted.
I used a spare shim to check there
was enough clearance between the
outside of the coil and the magnet and
siliconchip.com.au
ensured the coil’s flat, tab-like connecting leads were positioned directly adjacent to the basket terminals, where
they’d eventually be connected.
I then dry-fitted the rest of the components; though my kit was unassembled, at least the cone and spider had
been pre-cut to the right size. Two
small holes for the voice coil connections hadn’t been made in the new
cone though, so after referring to the
old cone, I used a scriber to punch
new holes in the same locations on
the new one.
Satisfied everything fitted, I glued
the spider to the basket using the supplied adhesive, with the voice coil’s
tabs protruding through the centre of
the spider. After clearing excess glue,
I left it overnight to cure.
The next morning, I used epoxy resin to ring the centre of the spider, the
voice coil former and the rim of the
basket. I then set the cone into place
and gently twisted it side-to-side to
bed it into the glue. I also let this set
overnight.
The following day, I carefully slid
the plastic shims out and gently moved
the cone back and forth to check that
the voice coil was clear; all was well.
After soldering two lengths of the
supplied ‘tinsel’ wire to the voice coil
tabs, which now sat at the base of the
new cone, I fed them through the holes
I’d made in the cone and soldered them
to the basket terminals. Finally, I centred and glued the dust cap to the cone,
using some of the glue to run over the
short lengths of exposed tinsel wire.
I used the same glue to stick the
four-part, hard-cardboard gasket ring
around the top edge of the cone, and
the job was done.
I tested the speaker. It sounds as
good to my ears as it ever did. Quite
“crunchy”, “throaty” and “punchy” in
fact. I’d go as far as maybe even calling it “gravelly”!
Inverter welder repair
Don’t you hate it when you buy
something, check that it works and
then put it aside, and when you go to
use it again, it doesn’t work at all? Especially if it’s no longer under warranty! Well, that’s almost what happened
to B. P., with his wonderful new welder. He managed to get a replacement
unit but also got to keep the faulty one.
So of course, he had a go at fixing it...
I bought my first arc welder some 45
years ago. It was an Abel 110A AC unit
Australia’s electronics magazine
and over the years, I’ve done a lot of
welding with it. It’s massively heavy
with wheels and a handle to make
moving it easier. The transformer has
a copper secondary winding, which
was the standard back then, but is unheard of these days.
I’ve done very few repairs on this
unit during its life but I did replace the
electrode holder a long while back and
around five years ago, I replaced the
old dilapidated welding cables with
some 250A cables that were salvaged
from a defunct mobile diesel welder. I
still have this Abel welder and it still
works well after all this time.
Around five years ago, I bought a
smaller 100A AC arc welder from Aldi
when it was on special. This unit is
much smaller and considerably lighter than the Abel welder but it still has
a transformer, although it has an aluminium secondary. I’ve made a few
modifications and improvements to
this unit over time and it’s still working well today also.
This year, I decided to buy one of
the newer models of DC inverter welders. I chose a 250A unit, which was
the most powerful that was available
at the time. It weighs around 5kg and
is smaller than the 100A Aldi unit
while delivering 2.5 times the amperage. That just goes to show how fast
technology improves.
After the welder arrived, I unpacked
it and connected the cables and did
some test welds. I was impressed
with the high current and the ease of
striking the arc. I’ve only ever previously used AC arc welders and it’s a
lot harder to strike an arc with an AC
welder than a DC welder.
After the successful test, I put the
welder away, as I didn’t have an immediate need to do any welding. Around
six months later, I got the welder out
to do a small welding job but I was
amazed and disappointed to find that
it no longer worked. All I got was a
tiny spark which looked like it was
about 10A worth. I suspect this was
from the power source intended to initiate the arc. But where was the main
welding current?
Fortunately, the welder was still
under warranty, being less than 12
months old, so I contacted the seller,
who requested a video of the fault,
which I supplied. The seller then
promptly sent me an identical replacement welder but they didn’t want the
old welder back. With the high cost
September 2019 89
This photo shows the repaired arc welder PCB, with the problem diode circled.
All six diodes were re-soldered. Note the generally poor soldering quality. Many
of the SMD pads have lumpy-looking joints, indicating a lack of flux activation.
of repairs these days, it must have
been cheaper for them to just replace
the faulty unit with a new one, rather
than having it sent in for inspection
and possible repair.
As soon as the replacement welder
arrived, I tested it and confirmed that
it was working correctly and I put it
away. Then I contacted the seller again
and thanked them for their excellent
service and very fast replacement of
the defective welder.
The repair
Now that the original welder was officially scrapped, I could take it apart
and have a look at it. It would have
voided my warranty but the warranty
now applied to the new unit, so there
was no reason not to open up this nonworking welder to see if I could fix it.
I removed the eight screws securing
the top cover, lifted it off and put it
aside. I could now see the inner workings, which consisted of a couple of
circuit boards and a lot of aluminium
heat sinks. It still looked brand new
inside, which was not surprising, because it had barely been used.
The first thing I did was to remove
the main circuit board and inspect the
soldering on the back for any faulty
joints. On a previous occasion, my
gasless MIG welder had developed a
fault whereby the wire speed control
no longer worked and the wire ran at
full speed. It turned out to be noth90
Silicon Chip
ing more than dry joints on the PCB,
which was an easy fix, so I wondered
if a similar fault might be at work here.
But the PCB soldering was all good,
so I turned my attention to the component side of the board, where I looked
for any obvious signs of blown-up
components. I found nothing, so I took
a closer look with a magnifying glass,
but there was still nothing obvious.
I was beginning to think that this
fault was beyond my ability, due to
the obvious complexity of the circuitry
involved in the unit, when I noticed
something that was not quite right.
There were six of what appeared to be
surface-mount diodes next to a small
daughter-board and the middle diode
(D15) on the right-hand side just didn’t
look right.
This diode was sitting at an angle and one of its legs appeared to be
raised slightly above its solder pad. It
looked like a manufacturing defect,
where the component had not adhered
to the PCB and therefore was not soldered properly, but it must have been
initially touching the pad for the welder to have worked in the first place.
I was sceptical that this could be
the fault that had stopped the welder
from working, but I also wondered if
it might be the culprit.
As this was the only obvious thing I
could see at this time, I decided to resolder the leg of diode D15 and while
I was at it, I also re-soldered both ends
Australia’s electronics magazine
of all the diodes, as they all looked to
be lacking a good amount of solder at
their joints. This isn’t the first time
I’ve seen something like this (see the
photo of the repair).
I then connected the welder up
again and got out what I needed to
do a quick test, just in case it was
now working again. I wasn’t really
expecting it to work, as I didn’t think
that something as simple as this minor manufacturing defect could have
caused the failure. However, as I didn’t
know just how this circuit worked, it
was a possibility.
To my astonishment, the welder was
now working properly again. I was
amazed that just one bad solder joint
in this part of the circuit had been the
cause of the failure. I almost couldn’t
believe that I’d found the fault and
fixed it so easily. I’d been expecting to
find something major to be wrong with
the welder that would have either been
impossible to find or impossible to fix.
I put the welder back together and
put it away. Since then, I’ve used it
several times for small welding jobs
and it has been working faultlessly.
One of the great things I’ve discovered about it is that since it’s so much
easier to strike the arc, I can use old
welding rods that I’ve had stored for
some time. Over time, the flux absorbs
moisture, which causes difficulty in
striking an arc with an AC welder.
But not so with this one! It works with
rods that I reckon I’ve had for around
25 years.
Anyway, it just goes to show that it’s
worth having a look at a faulty device,
even if you only have limited experience with repairing these devices, as
sometimes the fault is easily found
and fixed.
Panasonic RF-P50 AM/FM radio fix
G. C., of Wellington, New Zealand
rescued a Panasonic RF-P50 AM/FM
radio from the rubbish bin. As is so
often the case in equipment that is
about to be discarded, the fault was a
simple one, easily fixed by someone
with some repair skills...
The Panasonic RF-P50 in question is
powered by two AA cells and it had a
very loud crackle in the audio output
when the volume control was operated. Also, the audio would “drop out”
entirely at some positions on the volume control, making the set virtually
unusable. I thought the fix would be
trivial: all I would have to do is dissiliconchip.com.au
mantle the plastic case and clean the
volume control pot.
The previous owner had taken the
set to an electronics repair shop (there
can’t be many of those left these days,
surely) and was told the repair was uneconomic (which it probably was!).
The set was given to me and I quickly had the case apart and cleaned the
volume control pot with a cotton bud
and some isopropyl alcohol.
After re-assembly, the set worked
fine for a day or two but then the
crackle and blank spots progressively
returned until again it was unusable.
Oh well, perhaps a further clean was
required, so I did so again.
However, the fault reappeared after
each clean and the radio was eventually put aside again as unusable. That
was a shame as it worked well, with a
clear, undistorted audio output for a
period after each clean.
Finally, after some time I had a
“lightbulb moment”; I thought maybe this perhaps this was the classic
case of a DC current flowing through
the volume control potentiometer.
That would likely be due to a faulty
(leaky) series capacitor or, lacking
such a capacitor, I could add one into
the circuit.
On a rainy afternoon and with little
else to do, I once again pulled open the
Panasonic radio’s case.
The set uses a 30-pin Sony CXA1619
FM-AM receiver IC centrally placed
on the PCB, so I googled the IC number and studied a number of typical
broadcast radio receiver circuits based
on that IC, one which showed a volume control connected via capacitors
between pin 24 (the detector output)
and pin 25 (the AF input).
Although the PCB was tightly
packed with small components, the
volume control arrangement could be
seen and the voltage divider circuit
easily discerned, but no capacitors
were located in this area of the PCB.
Maybe I was on the right track after all.
I had to figure out how to fit a small
capacitor in series with the volume
control pot. I thought about cutting
the very fine track, which was going
to be quite difficult if I was to avoid
damaging the PCB. Then I realised
that the top end of the voltage divider
was connected via a miniature 2.2kW
0.25W series resistor.
All that needed to be done was to cut
one leg of the resistor, lift that end of
the resistor off the board, remove the
siliconchip.com.au
remainder of the lead from the pad
and then solder a capacitor between
the pad and the remaining lead on the
end of that resistor. And that is what I
did. I added a 100nF Mylar capacitor
in this fashion, then re-fitted the AA
battery to test it out.
What a difference it made! Even
though the volume control pot had not
been cleaned this time, a few operations of the pot cleaned up its operation and it then gave perfect audio output. After re-assembly, this little radio
was restored to pride of place in the
household. It seems obvious now that
it was a design fault all along.
One has to wonder how many other
examples of this little radio have been
tossed into the rubbish bin because of
this annoying fault.
St George DEO-6
Double Wall Oven repair
R. L., of Oatley, NSW knew that he
would be on his own when it came to
fixing a 25-year-old appliance. He used
a methodical approach, and it paid off
in the end…
Approximately 25 years ago, when
we renovated our kitchen, we bought
a St George Double Wall oven, with
digital control. It performed flawlessly
until about two years ago. Since then,
occasionally while in use, it would
emit a beep and shut down. Resetting
the circuit breaker would restore its
operation. It would then work perfectly for several months until the same
thing would happen again.
It got to the point where the fault
would occur every other time that we
used it. My wife was not happy.
As I knew there would be no service support for a 25-year-old oven, I
would need to fix it or replace it. The
oven was in otherwise perfect condition and to replace it would probably
involve modification to the surrounding cupboards, so I decided to try to
fix it first.
I found a replacement controller on
eBay, except that it was for the single
oven model. But I decided to buy it and
become familiar with the circuit before
I disassembled my oven. The module
consists of two circuit boards. One is
a power supply/relay board, and the
other, a display/controller board.
From the connection diagram supplied with the oven, I figured out how
to connect the purchased module to
mains power and the other connections; it turns out that the single oven
module is identical to the dual oven
version, but with a few parts (eg, relays) missing. I plugged it in and
ran through all the functions, and it
worked fine.
So, the big moment came, and I disassembled my oven, removed the controller connections (about 30 wires)
and connected it to my bench set-up.
I applied power and went through all
the functions; it worked as expected.
I decided to heat it up a bit and tried
again; it still worked. So, I disconnected the module, got out my magnifying headset and carefully scanned the
boards looking for dry joints, as the
problem was obviously heat-sensitive.
I found a couple of suspect joints on
the digital board and re-soldered them,
but they were not drastic and unlikely
to be the cause of the fault.
I then checked the power supply
board. All was fine until I got to the filter capacitor joints. They looked very
strange. The capacitor looked perfectly
OK from the top, but I decided to remove it because of the strange-looking
solder joints.
And that was it; the 2200µF capacitor had leaked (and probably dried
out), but because it had been sealed
to the board, no electrolyte had spread
out from the base.
I checked the other three 1000µF
electrolytic filter capacitors in the supply circuit; they looked OK, but I replaced them all, as it was reasonable
to expect that they would be on the
way out as well.
I replaced the capacitors with
105°C-rated units, cleaned up the
board, reassembled the module and
installed it. The oven now runs like
new. I saved us the cost of a new oven
and my wife is happy.
SC
Servicing Stories Wanted
Do you have any good servicing stories that you would like to share in The Serviceman
column? If so, why not send those stories in to us?
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Australia’s electronics magazine
September 2019 91
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