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The Macintosh Classic II,
also called the Performa 200,
was released in 1991. With
computers of this age, corrosion
and time often take their toll. In
this case, the ever-present leaking
electros had caused some damage.
However, Bruce Rayne managed to
make this old “classic” run again.
I
was 10 or 11 years old when I received my first computer. It had an
8-bit, 3.5MHz CPU, 8KB of RAM and
used cassette tapes for data storage. After a couple of years, it was replaced
with a faster computer and ended up
in the bin. What reason could I possibly have to keep it when my new computer was so much faster?
Fast forward 35 years where CPU
speeds are measured in gigahertz,
RAM is measured in gigabytes and
hard drives are measured in terabytes,
you would think those old computers
would be long gone and worthless. But
there’s been an incredible nostalgic
resurgence in the popularity of these
old devices. I saw my exact model of
computer sell on eBay for nearly $300
a couple of months ago.
You might think that it’s only people my age and older that are collecting vintage computers, but you’d be
wrong. I’ve met teenagers who are
collecting 25-year-old computers,
fascinated by the role these devices
played in the evolution of the personal computer.
The more memorable and rare computers can sometimes go for quite obscene amounts of money. Apple’s very
first computer (the Apple I) is so rare,
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every single one known to be in existence is recorded in a registry, along
with its sale price. In October 2014,
one of these old Apples sold for over
US$900,000. Not bad for a computer
that sold for $666.66 back in 1976.
One of the main selling points of
any vintage computer is whether it
still functions, but many of the internal components have a limited lifespan, so the older the computer, the
greater the chance it will have a fault.
Among the most troublesome components are electrolytic capacitors. They
tend to leak electrolyte onto the PCBs,
corroding surrounding components.
Even when a working computer has
been tucked away in a dry cupboard
for years, it’s not uncommon for it to
fail when it’s finally pulled out and
switched on.
But even worse than a leaky capacitor is a leaky backup battery. These
were used to store settings and power
the clock when the computer was off
and can spew out corrosive chemicals
if left long enough, sometimes completely destroying the computer from
the inside out.
This has lead to a niche business
of restoring old computers to extend
their operational life. The commonly
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used term “recapping” refers to the replacement of old capacitors with new
ones. After recapping a few of my own
computers, I have recently started offering these services to others.
It’s not a very profitable business
model but I do get a great deal of joy
bringing these old computers back
to life.
I’m always on the lookout for potential bargains, so when I see a vintage computer for sale as “not working” or “untested” (which means the
same thing), I like to keep a close eye
on it. If the price is right, I snap it up.
The Classic II
My most recent purchase was an Apple Macintosh Classic II. For those not
familiar with this model, it followed
the release of the Macintosh Classic,
which was sold in 1990 as a sort of
modernised version of the original
compact Macintosh.
In one of many strange moves by Apple, the Macintosh Classic offered very
few improvements over the Macintosh
Plus, a model released four years earlier. Although it now had a built-in hard
drive and a slightly redesigned case,
it had the same four megabyte RAM
capacity, the same Motorola 68000
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Above: a close-up of the damage
caused by leaky capacitors.
Right: this version of the Macintosh
Classic II used a 3.6V ½-AA PRAM
lithium battery for CMOS backups,
which had luckily not leaked.
CPU and the same nine-inch monochrome screen.
The one thing it had going for it was
its low price tag, which made it very
popular with schools and home users.
As a result, over 1.2 million units were
sold, and there are still quite a few
Macintosh Classics floating around
these days.
A year later, Apple released the
more powerful Macintosh Classic II,
which looked almost identical to the
Macintosh Classic but it was more
closely based on the Macintosh SE/30,
a model released in 1989. The Classic II had a Motorola 68030 CPU running at 16MHz and the RAM was expandable to 10MB. It had one empty
slot for a ROM/FPU expansion card,
but in a strange twist, Apple never released one!
The Classic II was also a winner with
the education and home user market,
so they are also fairly easy to come by,
though finding one that still works can
be a challenge. Regardless of how well
a computer like this has been treated
or stored, chances are it won’t function
today without a few repairs.
The Classic II motherboard has between 13 and 16 SMD aluminium electrolytic capacitors (depending on the
model revision) as well as a ½-AA size
3.6V lithium backup battery. All early
compact Macs were held together with
Torx screws, and not many people had
matching screwdrivers. As a result,
very few owners ever opened them up
to replace the battery, so they’ve been
left there to leak and corrode.
The Classic II is comprised of three
main internal parts: the cathode ray
tube, the power supply board and the
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motherboard (referred to by Apple as
the analog and logic board respectively). There is also a cooling fan, a 40MB
SCSI hard drive and a 1.4MB floppy
drive crammed into the case, plus a
speaker mounted in the corner.
The power supply board provides
+5V, +12V and -12V DC outputs and
also hosts the controller for the CRT
display.
Starting the repair
I whipped out my trusty Torx driver and removed the four screws holding the back cover in place. Compact
Macintosh cases are sometimes a little
hard to open and require some gentle
persuasion, but this cover came off
with little effort. The corrosion from a
leaky battery often spreads to the metal
chassis in these Macs, but thankfully
the chassis of this one looked clean.
The next step was to inspect the
motherboard, which sits on metal rails,
so I unplugged the floppy cable, the
hard drive cable and the power connector and that allowed the motherboard to slide right out. To my relief,
I saw a completely intact backup battery. No leakage, no visible “battery
cancer”. The whole board looked pretty good to the naked eye.
It was the original revision of the
motherboard, with 13 SMD electrolytic capacitors (eight 10µF 16V, three
47µF 16V and two 1µF 50V), plus a little blue jumper wire snaking its way
across the board. This wire might look
like a user modification, but it actually
came like this from the factory. Later
revisions of this model didn’t have the
wire, so Apple obviously resolved this
design flaw.
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Each of the capacitors needed to be
removed and the pads cleaned.
Many of the ICs also needed to have
their pads cleaned.
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Some traces had also been damaged
by corrosion from the electrolyte. The
example shown above was fixed by
soldering copper wire from the nearby
via to the SMD IC shown below. This
was then cleaned with an ultrasonic
cleaner.
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I put the board under the microscope and could immediately see the
results of electrolyte leakage from the
capacitors. All of the surrounding
components had a caked-on yellow
crust, something I have seen many
times before. The whole board would
need a thorough clean.
The first thing to do was to get rid
of the old capacitors. I use a hot air rework station. Some people like to use
solder tweezers, and I’ve even seen
someone who likes to cut the tops of
the capacitors off, just leaving the pins,
then remove them carefully with a regular soldering iron, but I prefer hot air.
I use little flat pieces of steel as
shields, positioned carefully around
the capacitors, to minimise the amount
of hot air spilling onto other components. It’s 27 years since this computer was assembled, so I don’t want to
push my luck by blasting too much of
it with too much hot air.
Once the capacitors were off, it revealed large amounts of electrolyte
residue around the old pads, but it
looked far worse than it was. I started
to clean this up by adding a liberal
amount of a good quality gel flux, then
I added some new solder to the dirty
pads and gently moved the flat part of
my bevelled soldering iron tip around
the pad to melt any old, crusty solder.
This is definitely not a job for a conical tip; I prefer fine bevel or small chisel tip. Next, I grabbed some solder wick
and gently soaked up all of the solder
from the pads. Ever so gently, I rubbed
the pads with solder wick to clean off
any remaining residue. Finally, I used
a cotton bud soaked in isopropyl alcohol to clean off the excess flux, which
revealed a sparkling clean pad, ready
for the replacement capacitor.
There were some ugly looking solder joints on a nearby transistor, so I
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took the opportunity to remove it as
well, then cleaned the pads before reattaching it using fresh solder.
After removing one of the capacitors, I could see a break in one of the
nearby traces. The localised corrosion was so severe, it had eaten right
through the solder mask and trace, so
that would need to be repaired.
It took me a while to remove all 13
capacitors and clean the board up. I
was then ready to fit the replacements.
For many restoration purists, replacing the electrolytic capacitors with
tantalums may seem like vandalism,
but I have more interest in preventing
future capacitor leakage than I do in
preserving the exact look of the original motherboard.
I also like to remove the original
½-AA battery holder and replace it
with a 20mm button cell holder, as 3V
CR2032 batteries are much easier to
source, and the computers don’t seem
to mind the 0.6V difference between
the two battery types.
With all thirteen capacitors replaced, I turned my attention to the
broken trace. I followed it up to a
nearby via, then using a curved surgical scalpel, I gently scraped away
the solder mask, revealing fresh copper. I then applied some solder to the
copper and soldered some 0.2mm diameter enamelled copper wire to the
exposed copper.
I then ran the wire around to the
other end of the broken trace, which
was the pin of a surface mounted plastic-leaded chip carrier (PLCC) IC. I
scraped away at the trace coming out
from the destination pad (to increase
the solder area for the other end of the
wire) and trimmed the repair wire to
a more suitable length.
After repeating the same soldering
process to secure the other end of the
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wire, I used my multimeter to confirm
that the repair had restored continuity.
The only thing left was to give the
board a good clean. I’ve heard that
some people like to clean these old
boards with soap and a toothbrush,
while others like to resort to the household dishwasher but I wouldn’t recommend either approach. I use an ultrasonic cleaner filled with a diluted
detergent designed specifically for
PCB cleaning.
I dropped the board into the ultrasonic cleaner then gave it about
15 minutes on each side. Ultrasonic
cleaners do a great job of cleaning gunk
out of tiny crevices, while still being
quite gentle.
Once the cleaning was complete, I
dropped the board into a bath of isopropyl alcohol. This helps to wash
away any residual water and detergent,
and the low evaporation temperature
of the alcohol also speeds up the drying process. I use a small toaster oven
set to a very low temperature (around
60-70°C) for drying cleaned boards,
leaving the boards in the oven for about
60-90 minutes.
Once out of the oven, I gave it a quick
inspection while waiting for it to cool.
Almost all of the residual electrolyte
gunk was now gone, and the trace
repair had held together well. Even
though the repair looked solid, I still
applied several coats of UV-curing solder mask for extra protection. I usually
use a UV globe to cure the mask, but it
was a sunny day, so I left it in the sun
for a few minutes instead.
The repaired and cleaned motherboard shown above. Note the CMOS
battery and holder were replaced with a much more common CR2032.
The power supply board looked fine at a glance, but had large amounts of
electrolytic capacitor leakage on the underside (shown below).
Testing
I put the computer back together,
plugged in the mains power cord,
flicked the power switch and got nothing, not even a crackle or a pop. It was
completely dead. I grabbed my multimeter to see if I was getting any power
at all. The external floppy drive connector can be used to check the output
voltage, and I read just 2V on the 5V
pin, so the power supply board would
need some attention.
After discharging the EHT, I removed the power supply board and
gave it a quick once-over to see if there
were any obvious problems.
I didn’t find any burn marks, but
what I did find was a huge amount
of electrolyte leakage near a small
cluster of eight electrolytic capacitors. They all needed to be replaced.
This is a known failure point for these
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boards, so I keep a good supply of replacements.
I de-soldered the joints for all
eight capacitors and pulled them off
the board. This revealed the full extent of the leakage, with dirty brown
rings of liquid under each capacitor.
Cleaning the power supply board is a
little trickier than cleaning the motherboard, as it has a small speaker riveted to the surface.
Submerging a speaker in an ultrasonic cleaner wouldn’t be the smartest move, so I used a little isopropyl
alcohol and a toothbrush to get the
worst of the gunk off the board. Once
cleaned, I then soldered in the replacement capacitors.
Before reassembling the computer
for another test, I took a few moments
to inspect the solder joints. Some of
the components on the power supply
board are relatively large and bulky, so
the weight can sometimes cause cracks
in the joints over time. I found a few
ugly looking joints, so I removed the
old solder and replaced it with new
stuff, just to be thorough.
With fingers and toes crossed, I put
the Macintosh back together and powered it up. I got the familiar “ding”
sound of the Macintosh startup chime.
A couple of seconds later I heard more
“dings”, meaning I wasn’t quite finished yet. The computer was starting
but kept restarting itself in an endless loop.
Chances were this was being caused
by the voltage being a bit low
and I could probably fix this
with a minor adjustment.
My multimeter showed
about 4.5V on the 5V
power rail. Thankfully,
the power supply board is
equipped with a small potentiometer for minor voltage adjustments, so I gave it
a twiddle until the voltage
read exactly 5.0V.
The reboot loop stopped
and the Macintosh started
booting into an operating
system from the 27-year-old,
40-megabyte internal hard
drive. A quick glance at the
original owner’s files revealed that
this computer hadn’t been used in
nearly 20 years.
As I intended to sell this old Mac,
I went ahead with a few other housekeeping tasks, such as replacing one
of the cogs in the floppy drive eject
mechanism, as this is a well-known
weak point.
Don’t ask me why, but of the four
cogs in the mechanism, one of them
changes to the consistency of an aged
cheese when it gets old, while the others are unaffected.
Even though this one had not yet
failed, its disintegration was inevitable, so I saved the future owner
from any potential headaches. I also
gave the floppy drive heads a good
clean, then erased the internal hard
The black
potentiometer (PP1)
on the power supply
board provides
minor voltage
adjustments, and
was needed to adjust
the 5V rail.
The floppy drive
eject mechanism
in the old
Macintosh Classic
IIs had a habit of
deteriorating, as
seen by the yellowed
cog at far right.
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drive and installed a “fresh” operating system.
Even though a quick block test of the
hard drive came up clean, it’s a miracle that this drive still works, and it
could fail any day. Thankfully there
are modern replacements available,
such as the SCSI2SD adapter that allows the old SCSI hard drive to be replaced with a modern micro SD card.
Now that the Macintosh Classic II
works, what can you do with it? The
answer is quite simple: you can do anything you could do with it in 1991.
There are a large number of online resources with vintage software that can
be run on these old computers: word
processors, spreadsheets, graphics,
games, music etc. Thousands of old
applications that will run beautifully
on a computer of this vintage.
And that’s precisely what the collectors want to do. They want to relive
their past by playing old games from
their youth, writing a letter on Microsoft Word version 5.0, or composing a
musical masterpiece for playback on
the tinny, 55mm speaker. It’s all a bit
silly, but it’s also a lot of fun!
Extra Links
Schematic diagrams (the SE/30 is
close in specifications to the Classic
II) – siliconchip.com.au/link/aaqd
Developer notes – siliconchip.com.
au/link/aaqe
Service guide – siliconchip.com.
au/link/aaqf
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