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SERVICEMAN'S LOG
Fixing heaters – it’s a gas
Dave Thompson
I usually only repair electronic and mechanical devices, not gas
appliances. But when our heater started acting up in the middle of
winter, I thought I’d better look into it. It turned out to be an electrical
problem after all, so it was up my alley!
It’s almost the middle of winter here
in Christchurch, and as is usual for this
time of year, the weather is gloomy and
cold. Because of the ‘lockdown’, we are
spending a lot more time inside than
we usually would, and subsequently
spending a lot more on keeping the
house warm as well! Then again, as we
aren’t driving our cars that much, the
money saved and extra money spent
probably cancel out.
I know what you are thinking; LPG
isn’t the most efficient way to heat a
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home. I agree, but the 6.5kW Masport
gas stove (or fire, depending on where
you went to school) installed in our
lounge was already here when we
moved in. And given that we no longer
have a reticulated natural gas supply
in town, it is bottled gas or nothing.
We never actually intended to keep
this fire; we knew the people we purchased this house from and spent
many nights enjoying dinners here, but
because they didn’t use the fire much,
we thought it wasn’t much chop.
Australia’s electronics magazine
We planned to replace the gas fire
with a pellet fire (or stove, depending
on where you went to school). We’d
used a pellet fire in our old home for
the previous decade or so and we were
very happy with it. While some love
and some loathe pellet fires, for efficiency, they’re tough to beat.
The fuel is simply compressed
sawdust, which is cheap to make and
widely available, and emissions are
next-to-nothing. The ash pot only
needs emptying once every few weeks
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when the fire is used all day, every
day. Our old Canadian-made Evolution 2 pellet stove (which replaced a
log burner) could throw out around
10kW, but we only ever used it on the
lowest of five heat settings; otherwise,
we’d have melted!
Before we moved in, I purchased
an identical, almost-new Evolution 2
pellet fire salvaged from a quake-damaged home. It was a bargain, and all
we’d need to do was swap out the gas
fire with this one, although I’d have to
get resource consent and a registered
installer to do that work. I could do
it, of course; but I had to pay a professional to do it, to satisfy the insurance company.
But once we moved in, we discovered that the gas fire could produce
some decent heat (about 6.5kW worth),
so it wasn’t worthwhile to replace it.
That spare pellet fire is now taking up
valuable bench and power tool space
in my workshop, so if anyone is looking for a cheap, good-condition Evolution 2, drop me a line!
fires is the noise of the fan and auger
motor. On the low setting, the auger
runs for about three seconds twice per
minute; on high, more often. It isn’t
that loud, and we found after the first
few nights we no longer heard it, but
visitors would often ask what it was.
The fan noise is similar to a small
fan heater; not too intrusive but certainly audible. Many people think they
couldn’t put up with these noises, but
it really isn’t that intrusive, and we
soon got used to it.
Another downside is that a pellet
stove needs electricity, so it was initially rendered useless in the quakes,
when we had prolonged periods without mains power. However, I soon had
it rigged it up to our generator, so we
could at least keep warm if the power failed.
And that is pretty much it as far as
operation goes. Keeping it as dustfree inside as possible, and emptying
the ash pan once in a while is about
all that is required; plus a flue clean
every couple of years.
An introductory course on
pellet heaters
The problems begin
For those who don’t know what a
pellet stove is, or how they work, they
are actually very clever. Most work
similarly, regardless of make or model.
(Don’t worry, this is leading to a repair
story, I promise…)
The top part of the machine is a
hopper into which pellets are poured.
Pellets are available from supermarkets and hardware stores in 10, 15 or
20-kilo bags, with the largest bags being the hardest to carry, but also the
best value. Thankfully, since we usually ran our heater on low, it would
only burn through about 15kg of pellets each week.
A motorised auger system in the bottom of the pellet hopper periodically
feeds pellets into a burn pot, usually
within a sealed burn chamber in the
bottom half of the fire. You can generally see this burn pot through the glass
front door of the chamber, and this is
where the visible flames sprout from
as well, giving that cosy ‘fireplace’ effect. A blower fan spreads the hot air
outwards from the fire.
Once the fire is alight, the more pellets you feed in, the hotter it burns.
Drop in the pellets less-frequently, and
the heat output is reduced.
Besides having to feed the hungry
fire, the other main gripe with pellet
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As you’d expect, there are lots of
moving parts in a pellet heater, and
they need to be in good condition to
ensure they are operating effectively.
The first problem I had with our Evolution stove was a common one: a
failed igniter.
Usually, to get the fire going, you just
push a button. It starts the auger motor
and an internal fan. The auger drops
pellets into the burn pot. When they
have built up into a small pile, the igniter, which protrudes slightly into the
burn pot, glows red-hot and sets the
pellets burning. It’s helped along by
the calibrated airflow in the chamber.
When the chamber temperature
rises to a set level, the main blower
fan kicks in, and it’s away. This usually takes about 10 minutes or so, but
after a few years, it took increasingly
longer, and eventually failed to ignite
altogether.
This wasn’t as disastrous as you’d
think, because I could easily start the
fire by opening the door, manually igniting a small number of metho-soaked
pellets in the burn pot and then closing the door; the stove would then be
going almost instantly. However, this
took away some of the convenience,
so I looked into replacing that igniter.
I ended up getting the supplier to
send out their maintenance guy who
Australia’s electronics magazine
Items Covered This Month
•
•
•
•
Fixing a pellet heater
Upgrading a Labtech Q1590
frequency counter
Asus monitor repair
LG TV power board repair
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
replaced it, telling me that poor design meant that as long as the stove
was ‘on’, the igniter was powered
and glowing red hot. This makes little
sense, as once the thing was alight, it
didn’t need any other ignition source
and all this did was considerably
shorten the life of the igniter.
It went again after another two years
and that time I replaced it, at considerably less cost. When it failed again two
years after that, I left it as-is and simply used the metho starting method.
After about 10 years, the auger motor bearings failed, and that made a really nasty noise. Fortunately, they are
standard bearings and easily replaced,
but it goes to show that the more complex a system, the more breakdownprone it becomes.
All this influenced our decision not
to replace the Masport gas fire/stove.
For one, it is relatively cheap to run
(compared to electricity) and as we use
the gas for cooking as well, it makes
no real sense to replace it.
Even the fire is sick of the
lockdown
So it was a bit ironic that barely a
few weeks into the lockdown, the fire
would periodically go out. I never saw
it going out; I just noticed that while
the built-in fan was still running, there
was no fire on the fake logs. Re-lighting
it was also difficult.
At first, I thought that the 45kg bottle was empty and needed swapping
(I use a manual switching system, so
I know when one of the bottles needs
replacing). Usually, all I have to do is
open the tap on the fresh bottle and
flick the gas switch over, and all is
well. But this time, I could see the
go/no-go indicator in the gas line was
still showing green, so the tank wasn’t
empty after all.
August 2020 47
I went back inside and tried to ignite
the fire to no avail. To start it, I push
and turn the main gas valve to ‘light’
and hold it down while I press the
piezo igniter. Typically, it takes a few
strikes to light the pilot lamp, and after
about five seconds I can let up on the
valve and the pilot stays alight while
I hear gas enter the burn chamber, beneath the fake rocks. A few ‘WOOFS’
later and the thing is going.
We rarely have to turn this one up either, with level one or two sufficient to
warm our space. However, this time I
needed to keep the valve pressed much
longer, and even then the pilot barely
lit up. Once going, we needed to run
it on level five just to keep it alight.
Something was obviously wrong…
While I know a little about a lot of
things, I know next to nothing about
how gas fires work. But a quick internet search gave me all the information I needed, as well as an excellent
service manual for the appliance. At
least that allowed me to investigate
what could be wrong.
I know one thing though; messing
around with gas and fittings is something that absolutely should be left to
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the professionals. I can still clearly
recall sitting at my workshop desk a
few months back, and feeling/hearing
the massive bang as a house about four
kilometres from me literally blew to
bits because of a gas fire leak. Lesson
learned! Gas is not to be trifled with.
Editor’s note: as detailed in this column in the past, just because you get a
professional to do the job doesn’t necessarily mean that you will get a good
result. Our newly-built house had a
recurring gas leak (as did our neighbours, in the other half of the duplex).
That was despite it being checked and
approved by the relevant authorities!
The good news is that as there was
some electronics involved, I had a legitimate reason to at least have a poke
around.
These fires are actually very clever;
all gas fires must have a fail-safe system
that shuts off the flow if either the pilot
light goes out or the main gas valve is
opened without lighting the fire. This
stops the room filling up with gas and
suffocating anyone, or converting the
home into a bomb.
The gas-flow system is controlled
by a solenoid which is held open (and
Australia’s electronics magazine
thus allows gas to flow) only while a
flame heats a thermocouple (or thermopile). If the pilot flame goes out, the
thermocouple cools, its output voltage
drops and the solenoid closes, stopping the gas flow. It’s simple and highly
effective, as long as all the components
in the system are working.
So based on the symptoms, I could
at least start to troubleshoot this problem without having to take any gas
lines apart.
The first possibility was a blocked or
partially blocked gas line. If the blockage was further up the line, towards
the bottles and the fittings, I wouldn’t
be able to do anything without a gasfitter’s ticket.
However, we use the same system
for cooking, and our gas hob rings all
burned at full noise, so it was unlikely
to be a problem with the lines, at least
to the junction where the fire and gas
hob feeds split off – which is situated
handily right behind the heater.
That meant that it was unlikely
that the gas lines to the heater were
blocked. But we could have simply
had a blocked pilot light, and that assembly is readily accessible after removing the escutcheon and one glass
panel from the front of the heater.
Once exposed, I used a bent piece of
copper wire that just fit into the pilotlight jet to clear any potential blockage. It felt clear, and a quick puff with
one of my rubber-bulb circuit-board
dusters ensured that it was clear of
obstructions.
The pilot light on this fire has three
flame paths: one towards the bare-copper igniter wire, one to the thermocouple, positioned opposite the igniter
wire, and one into the main part of
the fire. I used a pipe-cleaner soaked
in white spirit to clean these out, and
as they came out remarkably clean,
that was likely not the fault.
I could hold the gas valve down
and turn the main gas input tap at
the back of the fire on and off, and
could hear a decent gas flow through
the system. So I doubted that it was
a flow problem.
The next thing to check was the thermocouple. These are a known consumable, and replacements are widely and
cheaply available. After removing the
rear access panel, I could see where
the thermocouple connected into the
main valve. This is a plumbing-type
fitting that is easily removed/undone
with an open-ended spanner.
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Once free, the copper tube-like
electric lead can be unfurled to bring
the connection out so I could get my
multimeter probes onto it. The tube is
grounded, while the internal wire is
the ‘hot’ lead (LOL!).
With the meter set to volts, I played
the flame of my small gas torch over
the thermocouple tip, where the pilot flame usually hits it. I measured
just on 9mV. According to the book,
I should read at least 15mV, so this
was a potential (haha!) problem; 9mV
may be barely enough to hold the solenoid in.
A replacement M9x1 thermocouple
was only $39 including delivery, so it
made sense to replace it and see what
happened. I tested the new one when
it arrived, and got a reading of 16mV.
Fitting it was as easy as loosening a
retaining nut and bolt, removing the
old one and threading the new one
in. I re-connected it to the main valve,
and the fire’s been going perfectly for a
month now, so I think that’s job done!
Labtech Q1590 frequency counter
upgrade
C. K., of Croydon, Vic, went a bit beyond the usual remit in this column of
making something that’s broken work
again. Instead, he took an older test instrument that was functional but a bit
inaccurate, and modernised it so that
it is super-accurate. As you can imagine, it took a bit of doing...
What can we do with test equipment, years old but still functional,
The interior view of the Q1590 frequency counter. There is an oscillator module
inside the centre metal enclosure.
that is well off the pace in regards to
accuracy and stability? This was my
dilemma when I tried to calibrate a
Labtech Q1590 multi-function counter.
I bought it probably in 1989, and it
has never failed me. But these days,
digital communication technology
requires extreme frequency accuracy.
Only a few Hertz out, and digital messages cannot be decoded.
I tried to calibrate the counter using
a GPS-disciplined source of 10MHz,
but the readout was about 150Hz
too low. Taking the case off revealed
an oscillator module inside a metal
case, with two trimcaps which can
be accessed through holes in the top
(shown above). One trimmer is for a
10MHz crystal, and the other is for a
3.906250MHz crystal, the purpose of
which is not clear to me.
As the readout was low, the 10MHz
oscillator frequency was too high. But
adjusting the trimmer still did not give
me a correct reading. Adding an 18pF
capacitor across it helped, but the adjustment was difficult and tended to
jump.
By replacing the trimmer capacitor
and the parallel fixed capacitor with
new ones, and with very careful adjustment, I could get to within about
3Hz. But I wasn’t satisfied with that.
Fig.1: the small circuit designed to utilise a cheap
TCXO found online as a replacement oscillator
module in the Q1590.
siliconchip.com.au
Australia’s electronics magazine
August 2020 49
The original oscillator module shown without the metal cover (left) and with the
oven and NPN transistor removed (right)
Also, on turning the counter on, the
reading started about 50Hz low and
after a couple of minutes overshot by
about 8Hz, then over several hours, it
gradually crept to within 3Hz.
Both crystals are wrapped in a piece
of copper that is heated by an NPN
power transistor (shown above). A
thermistor glued to the copper sheath
provides feedback so that it maintains
a more-or-less constant temperature.
But apparently, the temperature still
was not stable enough.
Since I hate to throw things out, I
decided to come up with an improved
oscillator design using a TCXO (Temperature Compensated Crystal Oscillator). These can be expensive, but I
found a 10MHz model on AliExpress
for less than $20. That seemed suspiciously cheap, but I decided to take a
punt anyway.
The 3.906250MHz crystal was a
problem – I couldn’t find a TCXO
at that frequency. So I decided to
use a DDS (Direct Digital Synthesis) chip like the Analog Devices
AD9850 (as described in the September 2017 issue; siliconchip.com.au/
Article/10805).
Modules using this chip are available cheaply on eBay and elsewhere,
but there was not enough space in the
Frequency Counter to fit such a module and associated micro.
Fortunately, I had a couple of the
bare chips in my stock of parts. Virtually any microcontroller can be used
to load the tuning word into this chip,
and as I have heaps of Atmel AVRs on
hand, I decided to use an ATtiny2313.
The circuit I came up with is shown
on the previous page. If it looks familiar, that might be because it’s quite
similar to my Circuit Notebook entry on pages 96-97 of January 2020
(siliconchip.com.au/Article/12231).
But that circuit used an Arduino and
an AD9850-based module, compared
to the more basic approach taken here.
There is a small problem in that
when the AD9850 has a 10MHz input
frequency, the 3.90625MHz we want
at the output is a bit too close to the
The fixed frequency counter with new oscillator module – the repair cost
totalled less than $50.
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Australia’s electronics magazine
siliconchip.com.au
The finished replacement module was
made using a custom PCB.
Nyquist frequency of 5MHz, resulting
in a very distorted output with many
spurs that could read as false edges. I
solved this with a tuned circuit that
cleans up the waveform, based on
transformer T1 plus one fixed and one
variable capacitor.
I managed to locate the original
counter schematic and discovered that
the 3.90625MHz crystal is driven by
one stage of a 74HC04 hex inverter, operating as an oscillator amplifier. So I
just had to remove the old crystal and
feed the output of the AD9850 chip
into pin 13 of the 74HC04.
All that the ATtiny2313 does is load
five bytes into the AD9850 to set up the
correct output frequency. The tuning
word is 0x64000000 (hex). Obviously,
there is some magic power-of-two relationship between the two frequencies
to get such a simple number (and this
hints at why a seemingly odd frequency was chosen).
Designing the PCB was a bit tricky,
as there is not much room available,
so I mostly used surface-mount components. Some resistors and capacitors are on the underside of the board.
It was fortunate that the pins connecting the oscillator board to the
motherboard were at 5.08mm (0.2in)
centres. I used socket strips on the
motherboard and matching pins on
the oscillator board so that it became
a plug-in module.
Once the custom PCB arrived, I
loaded the components and plugged
the module in (shown at left). Holding my breath, I connected the 10MHz
reference to the input. And up came
10000000 – spot on! I decided to leave
it running several hours, in which time
there was the rare jump to 10000001,
but only for one count period. I was
quite surprised and pleased that the
cheap TCXO is so accurate.
There is a sticky label on the oscillator which gives access to an adjustsiliconchip.com.au
ment, but I am rather glad that I did
not have to fiddle with that.
I still don’t know what the
3.96250MHz frequency is used for. I
believe it has to do with the 100MHz
to 1GHz range of the counter. Having
spent considerable time on this repair/
upgrade, I did not feel inclined to do
a full analysis of the original design.
Has the exercise been worth it? Not
if I count the (unpaid) hours I spent on
it. As I already had most of the components, I spent less than $50 in total.
But the satisfaction of extending the
life of an otherwise useless instrument
certainly made it worthwhile.
Asus monitor repair
Poor, innocent bugs are often unfairly targeted as the cause of electronics
misbehaving. But in the case of one
particular monitor, B. P., of Dundathu,
Qld, found the culprit to be of the reptilian variety instead...
We’ve been using an Asus computer
monitor in our camper as a TV, with
it connected to a personal video recorder (PVR). Recently, my wife told
me that the monitor was dead. I found
that she was right, so I had to take it
apart to see if it could be repaired. Often something that is totally dead is
easier to repair than something that
partly works; I was hoping that would
be the case here.
Opening the monitor up proved to
be quite tricky. Computer monitors, in
general, don’t seem to be built with repair in mind, as they are clipped and
Australia’s electronics magazine
not screwed together. So it’s often difficult to get them apart without damage.
The usual way of opening them is to
pull the front plastic surround away
from the screen carefully, making sure
not to damage the screen in the process. I’ve opened up quite a few monitors over time, but this one proved to
be a lot more difficult than most of the
others I’ve worked on. Still, I eventually got it open.
I then sat the monitor face-down on
a towel and lifted the back off. I could
then see why the monitor had stopped
working; there was a blown-up gecko
at the side of the metal housing. I could
see that the gecko had been burnt by
high voltage electricity. Despite that,
it had clearly crawled some distance
from where it had been zapped.
After removing the gecko, I proceeded to disconnect the cables necessary to turn the metal housing over
so I could access the circuit boards
on the other side. While doing this, I
found a dead cockroach in the corner
of the video board. I’ve previously had
a computer power supply blown up
by a roach, but this time, the culprit
was the gecko.
There was a considerable carbon deposit between the two tracks where the
gecko had come in contact. I’ve seen
other devices where tracks have been
shorted by some wildlife, but this is
the first time I’ve seen this carbon between the tracks. I would need to rectify this before I looked into what else
might have been destroyed.
August 2020 51
I started by scraping all the carbon
out of the burnt section of the PCB
until it was back to clean fibreglass.
This was to ensure that it would not
arc when voltage was applied. Next, I
touched up the corner of the blown-off
pad with solder, although this may not
have been entirely necessary.
I checked the fuse next, and it had
blown. That was potentially a good
sign, but it didn’t rule out damage to
other components.
I searched for a replacement fuse,
but as this fuse was a leaded type that
was soldered to the PCB, I was unable
to find a suitable replacement. I then
thought of fitting fuse clips, so that I
could use a regular fuse, but I didn’t
have any clips of a suitable size.
I wondered what junk circuit board
I might have that I could salvage some
smaller fuse clips from, and I located
an old CRT TV board that I hadn’t yet
stripped of components.
It had suitable clips and even a fuse
with the correct rating, so I removed
them from the board and considered
how I could fit them to the monitor
PCB.
Because the replacement fuse was
shorter than the original fuse, I decided
to re-use one of the original fuse pads
and fit the other clip to a section of
the PCB with no tracks. I drilled 1/16in holes for the clips, fitted them and
bent the pins over, then soldered the
first one to the pad.
It was then just a matter of soldering a wire from the pins on the other
clip to the original track. This would
save me effort in future if the fuse ever
blew again.
It’s always hit and miss replacing a
blown fuse, as it might just blow again
the instant that power is applied, or
perhaps it wouldn’t blow but something else would.
So before applying power, I decided
The dead gecko and the damage done
shown below.
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Australia’s electronics magazine
to make some further checks. I checked
the bridge rectifier, and it tested good.
I then checked across the power terminals and as there was no short circuit
apparent, I decided to apply power to
see what would happen. I plugged in
a power cable and turned the monitor
over, then pressed the power button
and the monitor came to life.
That was a good sign; it appears that
the fuse had done its job in protecting
the circuit from the killer gecko. I just
had to reassemble the monitor and put
it back into service. It has been working well since the repair and I’m hoping for no more wildlife invasions. Unfortunately, there are large openings in
the monitor for ventilation, so that is
still a possibility.
This was another successful repair
at no cost, which was a win-win situation. It saved the monitor from landfill and avoided us having to find a
replacement. It’s worth having a go at
repairing devices, but always remember that electricity kills, so proceed
with extreme care.
LG TV power board repair
R. S., of Fig Tree Pocket, Qld found
some damaged parts on a TV power
supply PCB and replaced them. But
it seems that the damage was more
widespread than he thought...
This LG TV power supply board had
a strange fault on the 5V standby supply. It uses a 3B0365 IC (IC500) with
an internal high-voltage FET, which
shorted out.
When this and the 1.2W currentsense resistor (which I found to be
open circuit) were replaced, the 5V
supply would still not power up.
The circuit (siliconchip.com.au/
link/ab3a and siliconchip.com.au/
link/ab3b) shows that the auxiliary supply generated for the 3B0365
comes from an extra winding on the
transformer. This also supplies two
other integrated circuits on the board,
via a transistor controlled by a powerup signal from the main board.
This transistor was shorted out, as
was the L6599 IC (IC100), so the auxiliary supply for the 3B0365 was being shunted, stopping it from working.
Once these additional faulty parts
were replaced, the board sprang to life.
What I am not sure about is whether
the L6599 failed first and damaged
the other components, or whether the
3B0365 failed first and caused the other problems.
SC
siliconchip.com.au
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