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Vintage Radio
Velco
Velco 1937
1937 radio
radio chassis
chassis restoration
restoration
By Ken Kranz
Back in the 1960s, I rescued this 1937 Velco radio chassis from the tip.
I’m not sure what radio it came out of; it may have been a kit radio built
into a custom cabinet. The cabinet was long gone, but I reckoned that
one day, I could get the radio working again. Fast forward to 2019, and I
finally had the chance to do just that.
This chassis clearly was for a battery-powered radio, as it lacked a
mains transformer and rectifier. I
wasn’t sure which exact set it was
from. Velco made several ‘kit’ radios
so it could have been one of those.
I searched the internet to get some
information about the manufacturer,
Velco. Arthur J. Veall Pty Ltd (247249 Swanston Street Melbourne, 302
Chapel Street Prahran) manufactured
Velco-branded products from 1931 to
1955. From 1950, Velco Sound Systems Pty Ltd was at 65 Latrobe Street,
Melbourne.
siliconchip.com.au
Velco-branded products included
radios, signal generators, “set analysers”, volt-ohm meters, valve testers,
multimeters and tape recorders. Velco
manufactured a model 365B receiver
in 1937. Its specifications were:
Valves: 1C4, 1A6, 1C4, 1K6, 1D4
Intermediate Frequency: 175kHz
Wave bands: broadcast band only
Batteries: 2V (A) and 135V (B)
Speaker: permanent magnet
Case: timber
Valve markings on my set indicate the valve lineup to be 1C4 (RF
preamp), 1C6 (converter), 1C4 (first IF
amplifier), 1B5 (demodulator & audio
preamp) and 1D4 (audio output stage).
A 1K6 dual-diode pentode had been
fitted in the place of the 1B5, with the
pentode triode-connected.
This is very similar to, but not exactly the same as what’s specified for
the 365B. The 1A6 pentagrid converter
has the same pin connections as the
1C6 and very similar specifications.
So I think that this radio is a 365B
derivative.
Circuit details
Unfortunately, I could not locate a
83
Fig.1: the Velco 1937 radio circuit was traced from the original set and then modified. One modification was adding a set
of diodes to clamp the filament supplies and protect it from any high voltages during repair.
circuit diagram, so I had to create one
by tracing out the circuit. It is shown
in Fig.1. I drew the original version
of this diagram using LTspice, so I am
also able to simulate the operation of
the radio. The component designators are unlikely to match the original schematics, as I had to number
them myself.
Excellent SPICE models are available for all the common audio valves
and many RF valves, although it’s difficult to find models for pentagrid converters. You can download the files
for my circuit diagram/model from
siliconchip.com.au/Shop/6/5573 The
download package also includes many
handy valve models that could be used
to simulate other sets.
Looking at the circuit, there’s nothing really remarkable about this set.
It does have an RF gain stage built
around valve V1. The following mixer/oscillator is a conventional configuration, as are the IF transformers and
sole IF gain stage.
The two diodes in V4 are used to
demodulate the audio signal and to
derive an AGC control voltage, which
is used to vary the bias conditions of
the first three stages (V1-V3; RF amp,
converter and IF amp). The audio output stage (V5) is a very basic Class-A
configuration.
Fixing it up
The first thing I did after I got it on
my workbench was to take a good look
at it. I found that the tuning gang had
a bent shaft, presumably due to the
cramped nature of its storage location
for the last 50 plus years.
I removed the tuning capacitor and
placed the shaft in a vice. Quite some
force was required to make it almost
straight. I feared one extra adjustment
would break the shaft, so I stopped
there and refitted to the chassis with
new rubber mounting grommets, to replace the disintegrated originals.
A number of the paper caps tested
leaky, so I replaced all of them with
Shown here is the underside of the Velco radio chassis before it was repaired, with the finished set shown adjacent for
comparison. One of the biggest changes was the replacement of all the paper capacitors with newer film capacitors.
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Australia’s electronics magazine
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modern types. The back-bias resistor
was open-circuit; I was able to repair
it by removing one turn of its wire and
soldering that to its terminal.
I also found some badly damaged
wires and replaced them with 600Vrated black wires with silicone insulation.
I decided to add eight silicon diodes, two sets of four in series in an
inverse parallel arrangement across
the 2V filament supply. This was to
protect the radio against me accidentally connecting too high a voltage to
this supply.
The radio was initially designed to
drive a loudspeaker fitted with an im-
pedance matching transformer. So that
I could drive a modern 8W speaker instead, I decided to fit a 100V line transformer, connecting the 0.5W tap (20kW
impedance) between the anode of V5
(the 1D4 output pentode) and the B+
rail. I then connected my test speaker
across the 8W winding.
Testing the radio
I applied 2V to the filament supply
and measured the current drawn. It settled at around 700mA, which I thought
was a reasonable figure to power
the five valve heaters. I then slowly
ramped up the B+ supply to 135V DC
and measured a flow of about 10mA.
Australia’s electronics magazine
Some satisfactory noises were coming from the loudspeaker, so I fitted a
short aerial and found that all local
radio stations could be received with
good fidelity, in spite of Pimpala (ABC
891kHz) transmitting 50kW only 3km
from my location. I aligned the dial
pointer with the actual transmitted frequencies and left it tuned to 1323kHz
for some background music.
A few days later, the radio was playing away in the background when the
sound of silence hit me. The primary
winding on one of the IF transformers
had gone open circuit.
My friend Andy (VK5AAQ) advised
me that this was common on these
85
The coils for the replacement IF transformer was wound using a sewing
machine with 0.1mm copper wire (left). The coils were placed on a wooden
dowel, which is attached to the original mounting bracket as shown above.
sets, as they only switched off the filament supply; the constant B+ voltage
combined with moisture caused electrolytic corrosion, with this being a
typical result.
Rather than look for a replacement
175kHz IF transformer, I recalled that
back in the early days of radio, many
items were self-made. Inspired by B.
B. Babani’s Coil Design and Construction Manual (1960), I decided to repair
it with a home-made replacement coil.
A replacement IF transformer
The outer diameter of the coil former
was about 10mm. A sewing machine
bobbin is about 9mm; close enough for
me. I measured the wire diameter at
0.1mm. So I ordered a reel of 0.1mm
diameter enamelled copper wire and
some clear sewing machine bobbins.
I drilled a 1mm hole in the sidewall
of the bobbin for the start of the winding, then placed it on the semi-automatic coil winder of a sewing machine.
My daughter held a nylon rod with the
spool of 0.1mm wire so it could unspool freely, and the machine ¾ filled
the bobbin in no time.
The spooling speed is fully adjustable from a crawl to frightening. In
spite of the very low strength of the
0.1mm wire, we didn’t experience
any breakages.
I measured the inductance of the
good coil on the old IF transformer at
7.4mH using a TH2821B LCR meter,
and used a Fluke multimeter to determine that the DC resistance was 76W.
As both trimmer capacitors had similar
ranges (19-110pF), I decided to build
the IF transformer using two identical
7.4mH inductors.
I tested the freshly wound coil and
found it to be over four times the required value, so we transferred about
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Silicon Chip
half of the wire onto another bobbin.
I adjusted both coils by removing
turns until the required 7.4mH was
achieved. I found that the DC resistance and Q were very similar to those
of the original coils.
I cut the wires about 6mm from the
coil former and soldered flexible ribbon cable leads onto the coil ends. I
then covered the wire terminations in
some ten-second ultraviolet cure resin.
I then slid them onto a 6mm outer diameter wooden dowel, applied a generous amount of shellac to each end
and fitted the assembly to the original
mounting bracket. The wires were terminated as shown in the photos.
The moment of truth: I powered the
set on and turned the volume full up,
but it was very quiet. A quick adjustment of the IF trimmer capacitors gave
me lots of beautiful noise. I moved to
a blank spot on the dial and used the
trimmers to peak the noise at about ½
to ¾ compression. All the local stations came in loud and clear, including 5MU. An excellent result indeed.
Although the slideable coils would
allow adjustment of the coupling coefficient, the result was so pleasing that
I immediately coated the former with
shellac, including a small amount on
the coil. As one would expect, the set
stopped working. I did not re-tune the
IFs and simply let the set dry out for a
few days. At switch-on a few days later,
the radio was again playing 1323kHz;
most satisfactory.
I refitted the IF cover and that hardly
affecting the tuning. A quick re-tweak
and the set ran for about a week until
bench real estate required its movement back into storage.
Conclusion
All that’s left is to put the original
can back in place.
The repair of this set may offend
some restoration purists. The radio
was saved from landfill in the 1960s;
it now works and might be enjoyed
by somebody in the future. I saved all
the components I removed. It could
be reinstalled in a period cabinet by
someone with the skills and inclination to do so.
It still needs a replacement 2V dial
lamp (not shown on the circuit diagram). I might make a screw-in replacement using a white LED and resistor.
Some time in the future, I am hoping to find a diecast box that will locate over the large square hole, paint
it a similar colour, and build a power
supply into it so the set will run from
a 12V plug pack. The radio consumes
less than 3W, so I might even be able
to power it from a 1A USB port.
Velco references:
siliconchip.com.au/link/ab31
siliconchip.com.au/link/ab32
www.kevinchant.com/velco.html
SPICE references:
siliconchip.com.au/link/ab33
siliconchip.com.au/link/ab34
siliconchip.com.au/link/ab35
Plotting valve curves using LTspice:
https://youtu.be/VV3e_mNQ-dQ SC
Australia’s electronics magazine
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