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SERVICEMAN'S LOG
When in doubt, swap it out
I’ve had a few cases recently where components
tested OK with the usual procedures, but they
were still far enough out of spec that they
fell over when put back into use. This can be
a very frustrating aspect of troubleshooting;
dud components can throw up all sorts of red
herrings, without having any really obvious
signs that they’re toast.
Servicemen are much like detectives, in that we are always looking
for evidence to explain why something
doesn’t work or isn’t performing as expected. The majority of the time, we
are familiar enough with the job we
are doing (whether from experience
or just dumb luck), so we don’t need
to overwork our ‘little grey cells’. But
there are times we need to think outside the box to fix a problem.
Most of the electronics repair jobs
that come through my workshop are too
mundane to mention. The most common ailment in many of these devices is
dodgy soldering. Regardless of whether it is the result of mass-production
quality control or the solder breaking
down over years of use, if any one of
those joints fails, things stop working.
This means that a simple clean-up
and re-solder may be all that is required to resolve a seemingly complex
problem. Anybody with a little soldering experience should not be afraid to
give this a try.
Coming a close second would have
to be faulty capacitors; leaking and
bulging electrolytics, and those which
have gone high-ESR due to the electrolyte drying up, have felled many a
gadget over the years. Computer motherboards are notorious for this, but any
device which operates at an elevated
temperature is at particular risk. Plastic film caps can also go bad, especially
those on the mains input side.
But back in the golden age of electronics, there was a whole other class
of electronic component failures. Often, fixing a device would require resiliconchip.com.au
placing parts that had ‘worn out’. In
the days of valves, this meant pulling
the tubes, plugging them into a tester
(which any workshop worth its salt
had on hand), and if the machine told
us the valve was ‘weak’ or ‘gassy’, we’d
simply replace it with a new one.
Over-reliance on such machines put
one at risk of being labelled a “valve
jockey”!
Valve replacement became such a
regular task that many corner shops
or local hardware stores would have
a tester in one corner, along with a
display stacked with commonly-used
tubes. Anyone could go to the store
with their suspect valves, plug them
into the tester and this would then
display the results on a traffic-light
style go/no-go meter.
Usually, there was also a
well-thumbed substitute
manual for those who
owned radios and TVs
using oddball valve
types, to help them
choose something
more common that
might work.
Australia’s electronics magazine
Dave Thompson
Items Covered This Month
•
•
•
The art of troubleshooting
Chromagen water heater repair
Multiple capacitor replacements
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
In cases where the tubes weren’t the
problem, it became a job for the serviceman. More than likely, some capacitors, inductors or resistors would
need replacing, typically failing due
to the high voltages and operating
temperatures valve gear could reach.
The point-to-point wiring commonly
used at the time meant it was a relatively straight-forward job to test and,
if necessary, replace old components.
February 2020 61
it did click in, it would soon let go
again. At one point, it chattered, engaging and quickly disengaging, so I
quickly powered it down. Something
was obviously wrong in there somewhere (that’s a really technical statement, I know).
Working on this type of amp is a
real pleasure. They are designed to
come apart easily, and everything inside is laid out so it can be worked
on. Everything is clearly identified
with part numbers, track outlines and
board designations all screen-printed
on the PCBs.
Wire-wrapped connections
When we transitioned to transistor circuits, PCB construction became commonplace, making troubleshooting more challenging. Circuit
boards enabled complex circuits to
be crammed into smaller areas, and
often these were not laid out logically
as tube gear often was, requiring more
attention to detail and an increasing
reliance on documentation.
A behemoth arrives on my
workbench
I recently had a large, 70s-era Pioneer transistor amplifier through the
workshop. Like many decent amps of
the time, this beast weighed a ton. Most
of this weight came from the massive
power transformer, although the heavy
steel chassis and polished walnut case
also contributed significantly.
Crucially, it also came with a comprehensive service manual and dinnertable-sized fold-out circuit diagram,
all of which makes working on these
older devices so much easier.
The amp’s main symptom was an
increasing trend for the anti-thump/
speaker connection relay not to kick
in, meaning zero sound output. If
the relay did engage, it would then
drop out at various times. Usually,
this points to either the relay itself
getting tired, or perhaps a related ca62
Silicon Chip
pacitor failing. So those components
were the obvious place to begin troubleshooting.
I first confirmed the fault before proceeding; while I did not doubt that
after 40 years, the amp’s owner knew
every little thing about it, there is nothing as informative to a trouble-shooter
as witnessing the actual fault in action. So when possible, this is what I
prefer to do.
I plugged the amp in and toggled
the seriously solid power switch to
on. I found the relay wouldn’t kick in
at all most of the time. The odd time
Australia’s electronics magazine
This amplifier also used the now
mostly forgotten technique of solderless wire-wrapping. Individual, colour-coded single-core wires are laid
out and then the ends are twisted a
dozen times or so around numbered
PCB pins, usually mounted on the edges of the boards, connecting the different sub-systems together.
This makes it relatively easy to logically track inputs and outputs and
also helps to relate everything to the
circuit diagram.
Admittedly, there are downsides
to this method of construction; over
time, vibration can wreak havoc with
this type of connection, though this
is not too much of an issue with a big
heavy amplifier (unless it is sitting on
a subwoofer!).
It also becomes a pain if we want
to remove or replace one of these
wrapped wires, because once it is
un-twisted from its post, it is almost
impossible to reattach it in the same
manner without a proper wire-wrapping tool.
Another potential problem is that
over time, dissimilar metal or galvanic corrosion between the wire and
post can cause even the most tightlywrapped wire to go high-resistance,
or fail altogether. In their defence, the
designers probably didn’t anticipate
their amps would still be in regular
use 40 years later!
Fortunately, the PCB pins are tinned
and thus readily soldered, so reconnecting the wires is easy. You just need
to trim off the old wrapped part of the
wire, strip about a centimetre of insulation and tin the core before twisting
it around the post a few times and then
sweating it all together.
Wrapping it the old way would retain the vintage vibe of the amp, but
siliconchip.com.au
two things prevented me from doing
this. One, I don’t have the wrapping
tools needed. And two, I’d need about
25mm of wire to wrap it back onto the
post, and while most of these wires
had some extra length, there wasn’t
enough spare for me to chop them
down and still have it run nicely in
the existing looms.
While the owner didn’t care about
that aspect of the repair, I did make
it a point to ask him, as some people
can be very finicky about such details.
Tracing the fault
I started by working backwards from
the speaker connectors. The next component in line was the anti-thump relay. Getting it out was as easy as desoldering the relevant wires from the
terminals at the bottom, and removing
a single mounting screw. The relay
cover and relay then lifted out through
the upper section of the amp.
Basic tests on the coil and contacts
using a multimeter and my benchtop
power supply proved the relay was
still very much alive and working correctly. This was fortunate; according
to my research, it was hard to get a direct replacement. I’d have needed to
substitute it with a relatively expensive type, with modifications to the relay’s cover, terminals and the chassis
to make it fit and work.
The next step was to check the relay
driver board. This, according to the circuit diagram, should have 24V present
on a couple of the output pins. While
I measured a voltage on those pins, it
was low and variable. I disconnected the relay coil wires and measured
again, with the same result.
There were about half a dozen electrolytic capacitors on this board; several of the larger caps had distorted
plastic jackets, a sure sign of excessive
heat and/or possible damage.
So the board would have to come
out, but there were 25 wire-wrapped
connections divided between the input and output sides of the board. I
therefore took several detailed photographs before removing it. I didn’t
want to have to rely on the circuit diagram to track every connection in and
out of that board if I didn’t have to!
The various satellite boards in the
amplifier are held in using white plastic ‘AT’ style standoffs, similar to those
used back in the day to attach motherboards to a computer case.
These have an expanding clip at the
siliconchip.com.au
end that pop into place once the board
is seated down. The PCBs have a 3mm
hole in each corner that fit onto the
clips. These simple fasteners work so
well in anchoring the PCBs, that they
can be a pain if you want to release
the board.
Many people use a pair of sidecutters or long-nose pliers to pinch
the expanded splines together, one
by one, so they can ease the board
up off the clips. I use an ancient pair
of Xcelite transverse end-cutter pliers that I poached from dad about 45
years ago.
While once probably sharp on the
cutting edges, they certainly aren’t
now. As they fit perfectly over the
clips, it’s really easy to pinch the
splines without fear of mangling them,
or worse still, accidentally chopping
one off flush with the board.
Finding more faulty
components
With the driver board out, I removed
and measured the suspect caps to work
out which ones might be failing. I use
one of those little Peak LCR40 meters
to test capacitors, resistors and inductors. I won it years ago in some competition or other, and it was such a useful device that I went out and bought
another one, just in case.
That one has never been out of the
box, except for me to take the battery
out for storage. I suppose I should
pass it on to someone who could get
some use out of it. Perhaps SILICON
CHIP can dream up some reason for a
giveaway…
Anyway, to test a component, I clip
the leads on, hit a button and read the
results. While they claim this machine
can be used in-circuit, I’ve found it
not as accurate as if the component is
tested off the board. In this case, half
the capacitors were well out of tolerance, with some obviously very leaky.
I replaced them all.
While the board was out, I also
tested the dozen or so transistors. For
these, I used my Peak Atlas semiconductor analyser. This is another extremely useful tool. Whether the component has a part number on it or not,
this tool will tell me what it is, the
pinouts and whether it is any good.
Obviously, it is better to have a type
number so I can refer to a data sheet for
specs, but in a pinch, when I haven’t
been able to identify some ancient TO92 or TO-18 package device due to age
Australia’s electronics magazine
FEBRUARY 2020
63
or deliberate part-number obfuscation,
it has saved me many times.
I removed each transistor and tested
them. I found two that gave “component not detected” on the Atlas, which
is always a bad sign. Fortunately, the
numbers were clearly visible, though
I also had the circuit diagram which
clearly stated which part went where.
I replaced these older NPN types with
a suitable (tested) substitute from my
parts bins.
Once that was done, I re-mounted
the board onto the standoffs, being
careful not to push it down below
the clips in case I needed to lift it out
again. I stripped, tinned, wrapped and
soldered the connection wires back
into place.
Something smells a bit off
When I powered it up to test it, the
relay didn’t click in at all, and I noted
the faint-but-familiar smell of some-
64
Silicon Chip
thing heating up. Old electronics getting hot have a distinct scent, and I am
very attuned to it.
After powering the amp down,
I broke out my laser thermometer
and aimed it around the relay driver board; nothing remarkable there.
I then shone it over the main power
supply board, which sits adjacent to
the relay driver board. I got some high
thermal readings from the heavier-duty components near the output of the
PSU board.
This PCB contained everything
necessary to provide the wide range
of voltages the amp needs. Its output
voltages range from ±3.5V to just over
50V. One of the four TO-220 heatsink-mounted output transistors and
some of its associated components
were heating up under load, so it was
clear that this board would also have
to come out.
More photos and wire-unwrapping
followed before I could remove the
power supply PCB. While that was disconnected, I measured the outputs of
the power transformer, just in case
something was wrong with it. All
AC outputs measured within a volt
of what the circuit diagram specified,
so the problem had to be somewhere
in this power supply board…
Once again, I worked through the
caps and smaller transistors associated with the suspect part of the supply. While some of the voltage outputs
were achieved using simple resistive
voltage-divider networks, the rest
was set out in clearly defined sections of the board, making troubleshooting a bit easier.
As I found several more dead capacitors, I replaced all of them on
the board. A few of the TO-92 driver
transistors were also suspect (and I
broke one getting it out for testing), so
I swapped them all out too.
I removed the output transistors
and tested them; one was significantly different in my
test results than the other three but still ‘passed’
according to my tester. I
substituted a similar spec
device from my parts bins
anyway.
One of the more timeconsuming parts of this
process is tracking down
all the different datasheets
for these old 2Sx series
(Japanese coding scheme)
Australia’s electronics magazine
components and finding equivalents.
Fortunately, I have Google and a good
supply of older transistors so I can
replace any dodgy components with
similar types.
I used new electrolytic capacitors,
but all the replacement transistors
were new, old stock (NOS) devices
around the same age as the originals.
There wasn’t that much else on this
power board; no complicated, mysterious, impossible-to-test proprietary ICs
or other unknown parts, just meat-andpotatoes analog components. Working on this type of hardware is such a
pleasure compared to the stuff manufacturers churn out for today’s throwaway culture.
All my effort pays off
I reconnected all the wiring and sat
the power supply board in-place, again
without clipping it home. This time
when I flicked the power switch, nothing happened, until a satisfying clunk
from the relay pulling in signalled that
the anti-thump was working.
On powering down, the relay
dropped instantly. I cycled it about a
hundred times over the next few hours;
the relay pulled in without fail every
time. A scan using my thermometer
over the boards revealed nothing was
getting warmer than ambient temperature.
I was very happy with the result.
But this story serves a cautionary tale
that just because any given tester says
a component is good doesn’t mean it
will work properly. My motto is: when
in doubt, swap it out!
Editor’s note: on a similar theme, I had
multiple people test the battery in my
wife’s car and tell me it was OK, but
we continued having problems with
certain 12V-powered accessories in the
vehicle. Running out of ideas, I decided to replace the battery on a hunch.
Out of the car, I charged it fully
and left it to sit overnight. The voltage dropped to 12.68V, when it should
have stayed above 12.9V. I suspect that
those battery testers only check how
much current can be drawn, which
will detect some faults but not others.
Now that I have a good battery in
there, I realise that it was faulty right
from the day she bought the car new.
We just weren’t familiar enough with
it at the time to notice the signs. For
example, we can now sit in the car
with the radio going for more than
two minutes without it shutting down!
siliconchip.com.au
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Programmed PIC32MX470F512H-120/PT
KIT INCLUDES:
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PCB
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20MHz low-profile crystal
Microcontroller (programmed with your choice) and IC socket
green SMD LED
3.3V low-dropout regulator
micro USB & microSD sockets
All capacitors (ceramic types supplied)
Right-angle tactile switch
10kΩ resistor and 100Ω trimpot
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Pin headers (male and female)
pin headers and shorting block
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Specialised components for MICROMITE BACKPACK projects published in SILICON CHIP
Parking Assistant
Black/clear/blue UB5 lid & ultrasonic sensor: siliconchip.com.au/Shop/7/3338
Boat Computer
VK2828U7G5LF GPS module with antenna and cable:
siliconchip.com.au/Shop/7/3362
$7.50
$25.00
Super Clock
VK2828U7G5LF GPS module with antenna and cable:
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DS3231 real-time clock (RTC) with mounting hardware:
siliconchip.com.au/Shop/7/3491
DS3231+ rechargeable LIR2032 cell: siliconchip.com.au/Shop/7/3519
Energy Meter
DS3231 real-time clock (RTC) with mounting hardware:
siliconchip.com.au/Shop/7/3491
DS3231 + rechargeable LIR2032 cell siliconchip.com.au/Shop/7/3519
ACS718 20A isolated current monitor IC: siliconchip.com.au/Shop/7/4022
Main PCB [04116061 RevI]: siliconchip.com.au/Shop/8/4043
Matte black UB1 lid: siliconchip.com.au/Shop/19/3538
$25.00
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Voltage/Current Reference
Short form kit:
All parts including PCB, but not including the BackPack module, case,
power supply, PCB pins and wire siliconchip.com.au/Shop/20/3987
Matte black or blue UB1 lid: SC4084/SC4193
Main PCB [04110161] as separate item: siliconchip.com.au/Shop/8/3988
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DDS Signal Generator
AD9833 DDS module: siliconchip.com.au/Shop/7/4205
$25.00
Deluxe eFuse
IPP80P03P4L04 P-channel Mosfet (2 rqd): siliconchip.com.au/Shop/7/4318
LT1490ACN8 op amp (2 rqd): siliconchip.com.au/Shop/7/4319
BUK7909-75AIE N-channel SenseFET (2 rqd): siliconchip.com.au/Shop/7/4317
Main PCB [18106171] siliconchip.com.au/Shop/8/4370
Matte black UB1 lid: siliconchip.com.au/Shop/19/4316
$4.00
$7.50
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Radio IF Alignment
AD9833 DDS: siliconchip.com.au/Shop/7/4205
$25.00
Altimeter/Weather Station
DHT22/AM2302 temp. & humidity sensor: siliconchip.com.au/Shop/7/4150
$7.50
1A/500mA Li-ion/LiPo charger board: siliconchip.com.au/Shop/7/4308
$15.00
GY-68 pressure/altitude/temperature sensor: siliconchip.com.au/Shop/7/4343 $5.00
5V 0.8W 160mA solar panel: siliconchip.com.au/Shop/7/4339
$4.00
Tariff Super Clock
VK2828U7G5LF GPS module with antenna and cable:
siliconchip.com.au/Shop/7/3362
DS3231 real-time clock (RTC) with mounting hardware:
siliconchip.com.au/Shop/7/3491
$25.00
$5.00
GPS-synched Frequency Reference
Short form kit:
All SMD parts and PCB. Not including BackPack module, case, power supply, GPS
module, connectors and a few through-hole parts:
siliconchip.com.au/Shop/20/4762
$80.00
VK2828U7G5LF GPS module with antenna and cable:
siliconchip.com.au/Shop/7/3362
$25.00
Main PCB [04107181] as a separate item: siliconchip.com.au/Shop/8/4728
$7.50
FOR MORE DETAILS ON ANY OF THESE BACKPACK PROJECTS OR COMPONENTS,
LOG ONTO SILICONCHIP.COM.AU/SHOP AND SEARCH FOR THE ITEM OF INTEREST
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Australia’s electronics magazine
February 2020 65
Previously, I thought that this behaviour was simply due to an over-cautious low battery cutout setting.
Chromagen water heater repair
R. W., of Mount Eliza, Vic noticed a
problem with his Chromagen gas/solar
water heater. As in past cases of similar faults, the repair was simple once
the faulty part had been tracked down.
Here is what happened...
How do you know if a solar hot water system is working correctly? I was
checking it by seeing if the pump was
working and testing the temperature of
the return pipe with my hand, to see if
it was hotter than the supply pipe to
the roof. Because the return pipe was
hotter, it appeared that it was working
correctly. But I was wrong,
One night, I was by the hot water
tank and noticed that the pump was
still running even though there was no
sun. The supply and return pipes were
at the same temperature. This meant
that it was pumping the hot water from
the tank and dissipating heat energy
into the air. No wonder the gas bill
was high! I set out to determine the
reason for this.
There is a temperature sensor that
is mounted on the solar panels on the
roof, and a second temperature sensor
at the bottom of the hot water tank. A
Kanitti Solar Controller mounted on
the tank controls the mains-powered
water pump.
When the solar panel sensor temperature is at least 4°C above the tank
temperature, it switches on the water pump. The pump is switched off
when the solar panel sensor temperature is less than 1°C above the tank
temperature.
The temperature sensors are connected to the controller via RCA plugs
and sockets. I disconnected the sensors and used a multimeter to measure their resistances. The solar panel
sensor read 392W while the tank sensor read just under 10kW.
I e-mailed Kanitti requesting a service manual or a circuit for the solar controller, so I could determine
whether these readings were correct.
Even though it was midnight, within
10 minutes, I got a reply indicating that
I should not try to service the controller as it could be dangerous. They also
told me that the problem is more likely
to be the temperature sensors and indicated that the sensors are 10kW NTC
thermistors.
66
Silicon Chip
This indicated that the solar panel
sensor resistance reading was wrong,
because 392W for a 10kW NTC thermistor corresponds to a temperature
of about 120°C! The problem could
be either in the sensor itself or in the
extension cable. I got up onto the roof
and disconnected the sensor, then
measured the resistance across the cable wires, which was very high. So it
must be a faulty sensor.
I ordered a new sensor from Chromagen for $64 plus $20 postage and received it the next day. I then searched
the Chromagen website and found a
manual that included (on pages 36
and 37) a test procedure for the controller and temperature sensors. Before replacing the sensor, I turned off
the main water tap and mains power
to the controller.
I carefully got up on the roof to swap
in the new sensor. The connection to
the extension cable is under the roof
tiles, so I had to slide up a roof tile to
gain access. I then disconnected the
old sensor and connected the new one.
I tied the connectors together to stop
them from coming apart, then slid the
roof tile back into place.
The installation procedure also
shows how to purge any air that might
get into the system.
But I used a simpler procedure; I
partly screwed in the temperature sensor and turned on the mains water tap.
The water pressure allowed the air to
escape. When water started to escape
too, I completely screwed in the sensor to finish the job.
Back at the solar controller, I used
my multimeter to re-check the sensor
resistance. I measured 13.46kW, which
equates to 14°C. The tank sensor measured 11.53kW, which corresponds to
17°C. So these readings now seemed
sensible. So I plugged them back in
and switched on mains power to the
controller.
As the temperature difference was
less than the 4°C required to activate
the pump, I had to wait for the solar
panel temperature to rise before the water pump would turn on. Which it did,
indicating that it was working correctly.
When reading the manual on how to
purge any air that gets into the system,
I noticed a section that indicates that
the water flow rate should be 0.75L/
min for a single solar panel and 1.75L/
min for two-panel systems. On checking the flow rate, I found that it was
well over 3L/min.
Australia’s electronics magazine
The water pump has a switch to select between three different speeds. It
was set at the highest speed. Setting
the switch to the lowest speed caused
the flow meter to indicate a flow rate of
3L/min. I then rotated a screw above
the flow meter to make the final adjustment, setting the flow rate to 1.75L/
min as we have two solar panels.
From now on, I will check that the
water pump is not working at night
when there is no sun. Only Harry
Hindsight knows how long the system
was not working correctly. He should
have told me earlier!
Multiple capacitor replacements
R. E., of Townsville, Qld appears to
be cursed because pretty much every
motor in his house has failed lately,
and in some cases, more than once!
Luckily, he is now pretty adept at fixing them…
Some time ago, our clothes drier
started acting up. My wife complained
that it sometimes rotated and sometimes did not.
After a lifetime of repairing electromechanical devices for the government, none of which I could throw
away, I am reluctant to throw out an
appliance without attempting a repair first.
So I carried the drier outside to the
patio area where I had more room to
work. This is as close to using laundry equipment as I am allowed, since
the time I tried to wash a red T-shirt
with some white socks and ended up
with pink socks.
Getting access to the inside of the
drier required removing the rear panel,
which provides support for the drier
drum and some rigidity for the entire
structure, as it has no framework. So
as soon as the rear was removed, the
drum basically fell out, being held in
only by the drive belt around the motor pulley.
There is very little inside a drier,
apart from the motor, pulley, belt and
drum, and the front-mounted control board. I removed the drum and
drive belt from the motor, then powered up the drier and selected “dry”.
The motor did not turn at all. No surprise there.
A large white motor capacitor was
quite visible, and as it had a real possibility of affecting the motor operation,
I bought a replacement from a local
electrical supplier for $15, installed
it and tried the unit again. The motor
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now ran without fail. I then re-fitted
the drum, pulley and rear panel, and
re-installed the drier in the laundry for
my wife to further test it in use.
It operated successfully for several
years until my wife rushed into the
lounge room one day to tell me that the
laundry was filling with black smoke
coming from the drier.
I knew that it couldn’t be from burning lint, as my wife religiously cleans
the lint filter before each use. Flicking off the laundry circuit breaker, I
figured that this time the drier was
surely finished, and took it outside to
air out and cool down, as well as air
out the laundry itself. The next day I
took it apart again.
Amazingly, everything looked fine
inside, with no fire damage or even
soot visible. But it was evident that
the motor capacitor had ruptured and
split, and was obviously the source of
the thick black smoke. Replacing it yet
again returned the drier to service, and
it has been running for another couple
of years since with no problem.
So, when our pool pump motor became intermittent a year or so later,
my suspicion naturally fell on any capacitor attached to the motor, if there
was one. Removing the terminal cover
showed just such a motor capacitor.
Replacing it with an identical unit
restored the pool pump to normal
action; an expensive pump replacement avoided. The replacement capacitor cost less than $20, whereas a
new pump would have been anywhere
from $350-600 depending on the quality and power, so I was pleased with
the result.
A few years later when it failed
again, I found that the replacement capacitor had failed similarly to that of
the clothes drier, catching fire and even
melting the plastic electrical connection cover, making it very clear where
the problem lay. But like the drier, a
new capacitor once again returned it
to operation.
More recently I had a problem with
my electric garage door opener, which
became intermittent, sometimes opening, sometimes not. When it wouldn’t
open, it instead emitted a buzzing
noise. Fortunately, it is possible to
open the door mechanically by pulling a latch on the mechanism that disconnects the door itself from the chain
driven shuttle, but it is hardly an ideal
long-term solution.
Not feeling particularly optimistic,
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I removed the cover over the drive
mechanism mounted to the ceiling of
the garage, to see if there was an obvious problem. One of the first things
that I saw was the large white motor
capacitor. Due to my previous experiences, I decided to look no further
and immediately started looking for
a replacement.
It was impossible for me to purchase
an exact match, as no 12.5µF capacitor was available at our local electrical
supplier, but I found one 12µF capacitor in their spares collection, which I
had no doubt would be suitable.
For some reason, it is considerably smaller than the original, with a
correspondingly smaller slot for the
metal mounting screw frame to slide
into. So it does not fit as well as the
original, and it now sits off to one side
of the mounting hole. But that isn’t a
real problem.
The garage door opener’s operation
returned to normal as soon as I fitted
the new capacitor, with no hesitation
by the motor. It now seems to run quieter as well, possibly due to re-tightened cover screws etc.
I have since found a wide selection
of motor capacitors at, of all places, a
local plumbing supplier, but will leave
the current capacitor in place while it
continues to function.
Capacitors in our current ceiling
fans have also caused me some problems, noticeably slowing their operation. I found the motor capacitor in the
cap under the fan where a light could
be attached. It was a small, flat black
1.5µF unit.
I found a replacement part at our local spares store, Solex, and have now
replaced all the capacitors in the ceiling fans, as many of them were showing signs of slowing down. This is
something I never recall needing to do
in the past with cheaper ceiling fans.
Repairing so many household items
by simply replacing the motor capacitor makes me wonder what people do
if they are not capable of doing such
work. Do they call in repairmen who
offer an economical repair on-site, or
do they end up having to buy expensive new appliances?
After all, if you saw thick black
smoke pouring out of a clothes drier,
would you expect it to be so easy to
repair?
SC
Servicing Stories Wanted
Do you have any good servicing stories that you would like to share in The Serviceman
column? If so, why not send those stories in to us?
We pay for all contributions published but please note that your material must
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Please be sure to include your full name and address details.
Australia’s electronics magazine
February 2020 67
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