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SERVICEMAN'S LOG
When things go wrong – really wrong
Dave Thompson
Sometimes a job comes along which seems like it’ll be
straightforward, but really isn’t. This can happen even if that
job is well within your field of expertise. Here’s one story where
everything and anything seemed to go wrong.
If you’ve read my previous columns,
you will know that I started out servicing planes for Air New Zealand and
then later, moved on to computer repair, which mainly involves swapping
modules and fiddling with software.
While I have repaired plenty of other
electronics, especially audio gear (as
I’m a bit of a muso), I’m still essentially an amateur serviceman in fields
outside of those two.
While I have repaired (and sometimes failed to repair) everything from
an abacus to a Zimmer frame, my main
focus for the past 25 years has been
computers, with the odd curly job
fired my way.
As something of a keen amateur, I am not shackled too
tightly to the conventions
(and regulations) that real
servicemen are legally
and technically required
to abide by.
That’s not to say I’m
a cowboy; far from it.
With all the work I do,
I always strive to adhere to the relevant
standards and codes of
practice.
After all, they have
typically been put in
place to ensure safety
and integrity. Before
doing anything unfamiliar, I do my best to
research the task ahead.
For example, I
wouldn’t just decide
one day to re-wire my
house. I could probably
do it successfully, but I
wouldn’t take the risk.
All the re-wiring work
I’ve done has been under the supervision of a
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qualified electrician who has then inspected and signed off on it.
It would be madness just to pile in
and do this type of work without some
oversight by a professional, yet plenty
of DIYers do. In many cases, no harm
ensues, but if it all goes wrong, the
house burns down, and maybe someone along with it; an outcome I find
unthinkable.
But sometimes a job comes along
where despite being well qualified for
it, it all goes wrong anyway. I think we
have all had
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those jobs where, in retrospect, they
seemed doomed from the start; no matter how hard you try to dig yourself
out of the hole you’re in, the hole just
keeps getting deeper!
While these jobs are thankfully few
and far between (for me at least!), I’ve
had a few over the years, and the following tale is one of those cases.
This happened many years ago
and did more to educate me on obtuse points of consumer law, and just
how far some companies will go, than
anything before or since. I’ll set the
scene, and you can decide
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Items Covered This Month
•
•
•
•
The trials and tribulations of
fine print
Sony 8FC-100W digital clock
radio repair
Daikin aircon repair
USB flash drive repair
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
whether or not the chips should have
fallen the way they did.
It all started so innocently
It began when I received an urgent
call from a client who ran a high-profile car sales yard in town. I’d been
looking after their office computers
for a year, after taking over that task
from the retired tech who’d set up
their offices. Due to their importance
as a client, I always tried to do any
servicing or maintenance as promptly
as possible.
They had half a dozen sales staff, a
receptionist and the owners on-site, all
of whom had their own desktop-style
workstation. These were all networked
together in a semi-typical ‘star’ configuration, where each computer runs
its own version of Windows and grabs
important business files via mapped
drives from a designated central server machine.
This server should ideally be a purpose-designed unit with redundant
power supplies, RAID-configured, hotswappable hard drives and a dedicated
server operating system such as Linux
or Windows Small Business Server.
But in the real world, such machines
can be pretty expensive to buy and
maintain, so many small businesses
just use a standard PC in a server role
instead. This car yard was no different; their server was one of the owner’s
machines, set up with the necessary
drive and file shares.
This made some sense, as it was the
most powerful computer in the office.
As such, all the scanning, printing,
photo-processing and faxing jobs were
done on or through this machine over
the network.
This type of configuration usually
works well and as long as nothing
particularly challenging happens, and
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backups are being kept, disaster recovery isn’t too much of a problem, even
if the server goes down. The backedup data can simply be copied to and
shared on any of the other machines,
networked machines’ mapped drives
adjusted and life goes on.
On that fateful morning, I got a call
that the owner’s machine wouldn’t
start and they were dead in the water.
Could I come and take a look?
Fortunately, they were only a few
blocks from my then-workshop, and
they were visibly relieved when I
turned up within around ten minutes.
As it was still early, there weren’t many
tyre-kickers around, and thankfully
there wasn’t much for the staff to do
but sit around drinking coffee and talking cars (or rubbish!), so I had some
breathing space.
As described over the phone, the
machine wouldn’t fire up at all, and
it looked for all intents and purposes
to be completely dead.
In situations like this, I usually take
the machine back to my workshop
where I can properly troubleshoot it,
and that’s what I did.
On the bench, it appeared Christchurch’s notoriously rubbish postquake power supply had claimed
another victim. The power supply
was dead and so was the motherboard, as I discovered when I tried a
Australia’s electronics magazine
known-good power supply in place
of the old one.
I’d been advising these guys since
they became my client to get a UPS
(uninterruptible power supply) but as
everything had been fine – until now –
they (like many others) assumed their
office was the exception rather than the
rule. At least the hard drive appeared
to be OK, so no data had been lost.
I called and told them the bad news;
they’d need a new computer. I also
talked them into a UPS. In the meantime, they could think about insurance claims, but I suggested that I’d
better build a new box straight away
to get them going. They were fine
with this, so I proceeded to strip the
old box down; we could at least reuse the case.
As I pulled it apart, I noticed a PCI
expansion card that had a parallel
port-style plug on the riser. It certainly
looked like a typical parallel port, and
this is what their large office printer/
scanner/copier/fax had been connected to. As many modern motherboards
don’t sport a parallel port, I assumed
at the time that it was a simple expansion card to allow them to connect this
large printer/copier.
Replacing the motherboard, CPU
and RAM was unremarkable and only
took a few hours. I also replaced the
hard drive; if the machine had gotten
January 2020 63
a power spike bad enough to fry the
motherboard, it could have done some
subtle damage to the drive too. Copying their data back and regenerating the
shares was easy; the problems started
when I took the machine back and reconnected their printer.
With the vast majority of printers,
installing them is a breeze. As long as
you know the make and model number, drivers and utilities that support
the printer are usually downloadable
from the manufacturer’s web site. But
I couldn’t find any mention of this
printer at all on their site, and Windows didn’t pick it up as it does with
many other printers.
When I pressed the business owner
for details on the printer, he informed
me that it was a leased machine and
not to worry too much about it as
they’d get a technician from the lease
company to come out to re-install it.
Frankly, this was a relief, as I was out
of ideas as to how to get this thing
working.
I tidied up the rest of what I could
and they were back up and running
that afternoon, bar the printer. As the
manufacturer is one of the biggest
names in printers, scanners, cameras and other consumer electronics, I
had no doubt their guy would have
the car yard up and selling old clunkers to the unsuspecting public before too long.
The plot starts to curdle
And that’s where things stood until the following morning, when I got
another call from the car yard. Apparently, there was a problem with me
messing with the printer, and the technician was getting all prickly about it
and berating the owner, threatening
all manner of ramifications.
Technically, the car yard leased the
printer; it was owned by the manufacturer, and the lease agreement states
that nobody can touch the printer
but the company’s representatives.
That’s all fine, but apparently (and
unbeknownst to me), they considered the expansion card to be part of
the printer!
This put the car yard owner in
breach of his lease terms, and the
manufacturer’s reps were now throwing shade on both of us because of it.
I advised the owner that if he’d told
me that the machine was leased, I
wouldn’t have touched the thing with
a barge pole, yet he didn’t, so I did.
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As I hadn’t yet been paid for the job,
this caused me some stress, as did the
vague threats made via the car yard
owner from the printer people about
my legal liability. That day certainly turned out very differently than I
thought it would!
And things just kept getting better;
that afternoon, with the lease technician spending hours on-site trying to
get the printer going with no luck, the
car yard owner again called to tell me
that the technician had taken the expansion card out of the machine and
had supposedly found it physically
damaged. Apparently, this explained
why the printer wasn’t working.
As I had been the one to swap it out,
they reckoned that I must have caused
the damage, and therefore was liable
for both the card and any time this
other guy spent trying to get it going.
I’ve installed more expansion cards
than most blokes have had meat pies,
so I thought it very unlikely that I’d
done any damage to it, especially without realising it.
When I asked what sort of damage
they found, I was told that there was
an obvious mark on it, where it looked
like a screwdriver had slipped and had
gouged a track on the board. According to the tech, this was why the card
wasn’t working and the printer not operational. I certainly don’t remember
doing anything of the sort.
When I asked how much the card
was to replace I almost fell over; they
quoted $4,500, and reckoned I was
fortunate as this would be for a second-hand card; new ones were double that price!
It turns out the printer was a deprecated model, and new cards were
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no longer available. Also, as this one
was the only card left and had to be
imported from Australia, I would be
liable for freight charges, a temporary
printer rental for the time it would take
to get the card as well as the technician’s fees to install it.
All this certainly got me riled up;
for a start, how could a PCI parallel
port expansion card possibly cost that
much, no matter how special it is? It
would be cheaper if it was made out
of pure platinum! And I’m pretty sure
I didn’t stab this one with a screwdriver; if it was damaged, how do I know
it wasn’t the other guy taking it out
who did it?
I called the lease company and
asked to be put in touch with someone who could clear this up. I ended
up talking to the New Zealand manager and he was as toxic as they come,
threatening me with legal action. Dealing with them was thoroughly unpleasant, and my feeling is they went
out of their way to make things difficult. I felt like I needed a shower after
hanging up the phone.
I wasn’t about to roll over, so I asked
to see the damaged card myself and
to at least have the right of repair. A
cut track isn’t insurmountable, and if
I couldn’t fix it, perhaps I could find
someone else to do it. I was confident
the card could be totally rebuilt for
way less than four-and-a-half large!
They reluctantly agreed and told me
I could pick it up from the car yard the
following day. I arrived to find the staff
passing it around the office, trying to
spot the supposed damage. I couldn’t
see anything on it either, no matter
how closely I looked (and I looked
very closely!).
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When I mentioned potential damage due to static, the yard owner commented that a courier had delivered it
just as it was. There was no packaging,
static or otherwise, with just a courier
sticker protecting it.
At this point, I realised that repair
was not going to be feasible, and was
reasonably sure the lease company had deliberately sent it like this.
When I raised this point with them
later, they confirmed it by stating that
after talking with their legal team (!)
the card was considered unserviceable as soon as I’d removed it and as
such, they wouldn’t accept a repaired
card anyway.
They threatened to recover the money from me or the car yard, as we had
jointly violated the terms of their lease.
Nice people, and I’ll certainly never
buy one of their products, no matter
how good they are supposed to be.
The owner goes to bat for me
When all seemed lost, I found an
ally in the car yard owner. He was
more than happy with my service record and was appalled at how he and
I were being treated and bullied by
these people.
After wading through the original
documentation for the printer lease,
he discovered that under the terms of
the contract, the printer should have
been regularly upgraded.
Their printer had been due for that
upgrade almost 18 months before all
this happened. The leasing company
had neglected to do this, essentially dumping this older model on the
car yard.
When the owner confronted them
with this information, they immediately started back-pedalling and apologising and offered to install the very
latest machine with free upgrades and
anything else they could chuck in to
sweeten the deal.
The yard owner also stipulated that
they also drop any claims against me
and this they did, claiming that they
had been talking about it and had already decided to upgrade the printer
due to the cost and hassles of getting
that second-hand PCI card for such an
old machine.
While that part still didn’t ring true,
I was past caring and was hugely relieved. That sort of money is a major
deal to a micro-business like mine,
and I didn’t appreciate all the drama
associated with it either.
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While all this was all going down,
I’d spent much of my time panicking,
studying points of law and even discussing it with a lawyer friend of mine,
who fortunately hates corporate bullying and was happy to offer his advice
for nothing.
If push came to shove, I might well
have been liable for those costs, especially if the lease company and car
yard had both turned their guns on me;
even though I’d only done as instructed, and had no way of knowing that I
was doing anything wrong.
Thankfully it all worked out, but
you can be sure that these days, I check
the lease status of similar hardware before I got anywhere near it.
Sony 8FC-100 flip-card clock
radio repair
J. W., of Hillarys, WA is a regular
contributor to Serviceman’s Log. This
time, he repaired a clock radio which
is as much electro-mechanical as it is
electronic…
A friend rang and asked if I could
have a look at his broken clock radio. I
told him that I would see what I could
do. When he dropped it off, I was a bit
nonplussed as it was much older than
I thought. It’s the type of mechanical
clock which has the numbers on cards
which flip over under the control of a
synchronous motor and set of gears,
using the mains frequency as a time
reference.
I looked up the model number on
the ‘net and found a service manual
printed in 1972, so the clock is about
45 years old.
I took it out to the workshop and
powered it up. The radio worked, but
the clock did nothing. So I took off the
back cover and found that the radio
module was behind the clock section,
so I would have to remove the radio
Australia’s electronics magazine
to get to the clock mechanics. The radio PCB had several wires soldered
to different tracks. I took a photo in
case one or more broke off during the
repair process.
With the radio removed, I took out
a few more screws and removed the
clock module entirely. I could see
a small motor with the rotor visible
through a section of the case that was
cut out. The rotor had some green and
white tape stuck on it, so when the motor was spinning, it would be visible
through the front cover as an indication that it was running.
I tried to turn the rotor by hand; it
moved, but a small piece of dried-up
tape fell out. Maybe this was causing the low-power motor to stall. I
plugged the clock back in, and the
motor started to spin, with the clock
now functioning.
Even though some of the tape had
fallen off, the rest still seemed to be
stuck on well, so I decided to leave it
alone, and not tempt fate by trying to
dismantle the mechanism any further.
The time and alarm are set using concentric shafts that protrude
through the case. These connect to a
system of gears. A microswitch riding on an adjustable cam activates
the alarm, so that it triggers at the correct time. It’s quite a complicated mechanical device when compared to the
all-electronic models that followed in
later years.
I put everything back together in reverse order, although it was difficult to
determine the exact placement as the
radio PCB obscured the clock module
when trying to get them both back in
the case. After some frustration, I had it
all back together and powered it up as
a final check. To my disappointment,
the radio no longer worked.
So off with the rear panel again. I
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eventually found a black wire which
had broken off the PCB; it was lucky
that I had taken that photo earlier so I
knew where to solder it back on again.
Now it all worked well, and after
leaving it running for a few days, I
returned it to my friend. In fact, it belonged to his wife, and she was happy to have her ‘antique’ clock running again.
Daikin Air Conditioner repair
M. B., of Parramatta, NSW made two
discoveries when his aircon failed.
Firstly, sometimes you have to fix
something yourself when even the experts give up, and secondly, parts may
test OK, but they can still be faulty.
Here is the story of how he tracked
down and fixed the fault...
A couple of weeks ago, thankfully
as the weather was starting to get a bit
cooler, my wife pointed out that our
air conditioner was pumping out room
temperature air.
I repair cancer treatment machines
for a crust and am reasonably confident
about my abilities to fix most things
around the home, but I’ve never tackled an air conditioner. So I rang the
company who had installed it. The
serviceman duly turned up, checked
the refrigerant levels and found they
were OK.
After removing the top cover of the
outdoor unit, he found that several error LEDs were lit. He said that given
the age of the unit, it was unlikely that
replacement PCBs were still available,
and if they were, would probably be
very expensive and possibly close to
the cost of a new unit.
I wasn’t surprised to hear this, so
I asked the serviceman to get back to
me about a quote for a replacement
and got on with my day.
After a few days, I hadn’t heard back
from them, so I decided to check eBay
for replacement boards. All three PCBs
(Controller, Active Module and Power
Filter) were still available and at a reasonable price, nowhere near the $3000
that a replacement unit would cost.
I found to my surprise that I could
get the boards directly from Daikin at
roughly the same price as those listed on eBay. They would even take the
boards back that I didn’t use and didn’t
charge a restocking fee, which was a
pleasant surprise.
So I decided to try my hand at becoming an air conditioner mechanic.
I bought all three from Daikin’s Warsiliconchip.com.au
wick Farm (Sydney) warehouse for a
total of $640. I wasn’t sure which PCB
I needed; I would simply return the
others once I’d figured that out.
I was pleasantly surprised to find a
free installation manual via a Google
search. YouTube also had a couple of
repair videos that, while not covering
my exact symptoms, were at least for
my specific model and gave me a bit
more familiarity with it. So, emboldened, I lifted the lid and started to investigate.
The YouTube video mainly talked
about the boards failing due to corrosion. Even though these boards are
covered by a protective lacquer, 10
years exposed to the elements would
no doubt test it.
My controller PCB didn’t look too
bad compared to the ones in the videos, but was still covered in insect
debris and dirt, and the lacquer was
starting to perish in parts.
The other two PCBs didn’t look too
bad, so I dusted them down and removed the controller PCB to give it a
thorough clean. I reinstalled it, crossed
my fingers and powered it back on. It
still didn’t work.
I eventually figured out what all
three boards do. The Controller PCB
hosts the microcontroller, IGBTs and
bridge rectifier. The “Active Module”
is a Mosfet-based Power Factor Correction (PFC) device with an external
inductor. The Filter PCB filters the incoming mains and the PFC-corrected
DC output of the Active Module.
There are five LEDs on the Power
Filter board, one green and four red.
The green LED is a ‘heartbeat’ to indicate that the microcontroller is active while the other four show error
codes. Since the heartbeat LED was
flashing, I suspected that the controller PCB was OK. The first two error
LEDs were flashing, and according
to the manual, this meant that one of
the three thermistors on the aircon
was faulty.
The manual gave a method to test
the three thermistors, which attach to
the controller board via a single plug.
It even gave a graph of the resistance
vs temperature for these thermistors.
So, armed with three glasses of
water of various temperatures and a
temperature probe connected to my
multimeter, I checked all three thermistors on the loom. Removing the
loom wasn’t too difficult. After plotting each, it seemed that they were all
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January 2020 67
within cooee of what I’d expect, judging by the graph.
I was still sure that most of the controller PCB was working, but now had
some doubt about the thermistor interface. The part of the PCB dealing with
the thermistors could be faulty. But not
having new thermistors to hand, no
proper circuit diagram, and since they
tested OK, I decided to bite the bullet
and swap in a new controller board.
This was relatively easy. The only
tricky part was needing to apply some
thermal paste to the bridge rectifier and
IGBT module heatsinks.
So, with bated breath, I switched
the circuit breaker back on. Nothing!
Well not exactly nothing; the indoor
unit ran for a couple of minutes before the whole thing shut down again.
I checked the error LEDs again, and
they were flashing in an identical pattern to before.
After thoroughly reading the manual
again, I discovered that in the indoor
unit remote control could give more
detail as to the cause of the fault. It indicated that the faulty thermistor was
on the outdoor unit heat exchanger.
This checks the temperature of the
outdoor radiator.
I was still puzzled by this, as all the
thermistors had tested OK. I hadn’t
purchased the thermistors on my first
trip to Warwick Farm, as I couldn’t
think of any reason why they would
go bad. So I headed down to Warwick
Farm again, to return the Active Module and the Power Filter PCB, and to
pick up a thermistor set.
To get to the condenser thermistor,
most of the panels had to be taken off.
I took plenty of photos to make sure
I could put everything back together
in the right place. But when I went to
turn the unit back on again, it wouldn’t
start at all!
I thought I must have messed up
when I re-connected the mains wiring.
Thankfully, the manual has a diagram
of the mains connection, and I discovered that I’d swapped the incoming
and outgoing wires because the 1.5mm
cable to the indoor unit and the incoming 2.5mm gauge wiring looked much
the same in my photos.
Anyway, having fixed that, I crossed
my fingers and powered it up. The A/C
fired up straight away, with no error
LEDs lid, and cool air came out of the
indoor unit! Success!
I’m still puzzled as to how the thermistors had become faulty and why
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they passed my tests but were still bad
enough to cause a controller fault. This
is something I have not come across before in my field. I would like to know
how the microcontroller determines
that a thermistor is faulty. It must expect a very specific change in resistance during the start-up procedure.
I ended up spending a total of $550,
which is a lot less than a new aircon
unit would have cost. I might be able
to get some of that back by selling my
still-working original controller board
on eBay.
USB flash drive repair
D. M., of Toorak, Vic had some pictures on a faulty USB drive that he
didn’t want to lose. It’s often (but not
always) possible to recover files from
flash drives. Luckily, he was able to
do it...
I had an old USB flash drive that
stopped working about ten years ago.
It contained some pictures I wanted
to keep, but which I never backed up.
This flash drive is a folding type;
I did some research and discovered
that these often fail due to broken internal wiring, which means it should
be fixable. So I kept the drive, hoping
that one day I could recover the data.
To start the recovery process, I first
had to carefully remove the plastic
housing without damaging the enclosed circuit board. I used a ‘spudger’
tool which is like a plastic screwdriver
with a wide wedge, to separate closely
joined surfaces that are pressure-fitted
or adhered together.
Having exposed the circuit board,
I established with a multimeter that
the drive had failed due to a break in
the flexible circuit board that formed
the fold-out connector. So I had to join
a new set of wires directly to the circuit board to bypass the damage. To
do this, I had to work out which PCB
pads were the connections GND, Vcc,
D+ and D-.
Getting GND and Vcc mixed up
would likely be fatal to the device, but
if you get D+ and D− swapped, it will
typically still be detected as a USB device, but it will not work.
The usual colouring scheme for USB
1.1 or 2 is GND (black or blue), Vcc or
+5V (red or orange), D+ (green) and D(white or gold). Note that the device
was a four-wire USB 1.1/2 device, not
USB 3 which uses more wires. There
is usually no indication on the circuit
board as to which pin is which, so refAustralia’s electronics magazine
The circuit board of the recovered
USB drive. The connector with the
defective flexible circuit board has
been held down with tape to expose
the solder pads, so that wires can be
soldered to them for data recovery.
erence needs to be made to the original connector.
To make the connection, I cut an
old USB cable in half and kept the end
with the Type-A plug. I then stripped
the four exposed wires and soldered
them to the pads on the memory stick
circuit board, after having determined,
based on the original cable, which end
was GND.
I first tried an old drive for practice
soldering the very small wires. I then
moved onto the recovery target. Once
the wires were soldered correctly, I
connected the drive to a computer.
It detected a USB device, but I could
not access it, so I swapped the D+
and D- wires. I then plugged it back
in, and it worked immediately, so I
copied its contents to the computer.
I was delighted to have gotten my
photos back.
The pinout of a USB Type-A
connector. The white area (top) is the
cavity while the dark area (bottom)
is solid material. Pin 1 is Vcc or +5V,
2 is D-, 3 is D+ and 4 is GND. Doublecheck and triple-check that you get
the corrections right, referring to the
old connector, as it may be hard to
figure out the connections from the
SC
circuit board alone.
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