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Vintage Workbench
The
The Tektronix
Tektronix Type
Type 130
130 LC
LC Meter
Meter –– Part
Part 22
Restoration
Restoration
By Alan Hampel, B. Eng. (Electronics, Honours)
Last month, Alan Hampel described how the valve-based T-130 LC meter
worked. He also described how he purchased a non-working unit from
eBay (with “non-working” omitted from the description). Now he opens
it up and starts work on restoring it to its former glory.
I unwrapped the package from the
eBay seller and took the T-130 cabinet
sides off. It was covered inside and out
with cigarette smoke gunk. That’s not
uncommon in old laboratory instruments. Instead of the cabinet being an
attractive blue, it was a dull blue-grey.
The cause of the clunking noises
was immediately apparent – there was
no 6X4 in the rectifier socket, but a
1N2630 solid-state valve replacement
rectifier was loose amongst the works.
The 1N2630 was no doubt put in the
6X4 socket by a previous owner. But
it’s about four times as heavy as the
original valve, being solid epoxy and
not mostly vacuum. It also has a larger diameter, fouling the socket retaining screws and preventing the socket
fully gripping the pins; so it fell out.
A 1N2630 (left) was used instead of
the original 6X4 (right) as the rectifier.
Due to its larger diameter and weight,
it came loose from the socket in
transit, damaging one of the 6U8s.
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Silicon Chip
The loose 1N2630 smashed one of
the 6U8s and bent the plates of a trimmer capacitor. Annoying, but easily
fixed. I also noticed the meter clear
plastic casing was broken in one corner – the only corner not shown in the
eBay photos.
Preliminary evaluation
I carefully straightened out the bent
trimmer capacitor plates and performed a thorough search for glass
fragments within the instrument and
in the packaging. I only found two
tiny pieces jammed in out-of-the-way
spots, but not anywhere near enough
to account for the smashed 6U8. So
someone cleaned out almost all the
glass before shipping, without replacing the smashed valve. Interesting.
The front panel glass was cracked
along one edge. There was also grime
and dirt inside and outside the case.
Australia’s electronics magazine
I then removed all valves, carefully
noting which valves came from which
sockets. It’s a good idea to keep valves
separate, even if they are the same
type, especially if they are doublevalves like 6U8 triode-pentodes and
6BQ7 twin triodes.
Such valves, when faulty, have a
high probability of producing entirely different symptoms or no symptoms at all depending on which socket they are plugged into. Nor do you
want to allow circuit faults to cause
any more damage than has already
occurred.
The T-130 came from the USA, so
the next thing I did was to rewire the
power transformer twin primaries
for “234VAC” operation, and I also
changed the fuse to one half the original amperage.
The seller supplied a power cord,
with the correct US NEMA 3-pin female on the instrument end, and a
standard US 3-pin male plug on the
other end. That’s no good in Australia, and it was a very short cord too, so
I bought a longer NEMA power cord
on eBay and changed the male end to
an Australian 3-pin plug.
I then plugged the instrument into
a Variac and slowly wound it up
from 0V. Nothing dramatic happened
(no smoke released), but when I got
it up to 200V AC, I noticed that the
front panel pilot light was still not
lit. The lamp socket pins were bent
and shorting out the heater wiring.
More damage from the loose 1N2630,
most likely.
I lengthened the short circuit and
tried again with the full 230V AC
mains. The secondary voltages on the
power transformer were correct, so I
siliconchip.com.au
If you have a Tektronix instrument
with this AC mains connector on the
back, check the Earth pin. It may
show high resistance due to a loose
retaining nut.
plugged in a 6X4 taken from an old
radio, and the 0B2 regulator. I knew
the 6X4 was pretty weak, but the HT
drain in the T-130 should be a lot less
than a typical radio, and I needed to
quickly work out what was what before contacting the seller.
I now had 260V and 149.5V on the
HT rails, and 75V DC on the heater
wiring, so things were looking good.
As the 6U8 in the V30 socket had
been smashed, I plugged in a 6U8 taken from an ancient TV, checking that
the heater wiring was still at +75V in
case there was heater-cathode leakage.
It was still good, and my CRO showed
oscillation at about 140kHz.
Next, I plugged in V4, another 6U8,
functioning as the variable oscillator.
I was rewarded with weak oscillation
on the CRO at about 140kHz, varying
with the position of the front panel
COARSE ZERO control. The heaters
still measured +75V DC, so no major
faults were apparent.
I proceeded to replace the remaining valves one at a time, checking the
+75V rail each time, and was rewarded
with front panel meter deflection, varying with the COARSE ZERO control.
Now I knew there was nothing major
wrong, so I probably wouldn’t need
any parts made from unobtainium to
fix the set (eg, transformers or coils).
I therefore decided to proceed with a
full clean and restoration.
To conduct further tests, I connected a 415pF tuning capacitor to the
UNKNOWN socket, set the capacitor to minimum, and adjusted the
COARSE ZERO and FINE ZERO controls for a zero reading on the 0-300pF
range. Slowly turning the tuning capacitor towards maximum, I noticed
two things:
1) The meter reading increased
from zero up about 80pF indicated,
then slowly decreased back to zero at
about 120pF from the test capacitor! I
thought this might be a problem with
the Schmitt trigger circuit, perhaps
the 6U8 (V70).
2) As the tuning capacitor was
turned, there were violent swings of
the meter (and I do mean violent!) at
certain settings. The CRO showed this
was due to the Schmitt trigger breaking into RF oscillation.
Schmitt trigger circuits can sometimes oscillate if the valve is weak, or
a resistor has gone high, usually because the positive feedback is insufficient to produce a definite snap action,
but enough to oscillate with reactances
present in the circuit.
14 rules of restoration
I follow 14 rules when repairing or
restoring vintage professional electronics. I learnt these rules when I
was employed servicing professional electronics at the tail end of the
valve era. The rules maximise reliability and preserve resale value.
1) Never unsolder any component until, by deduction or in-circuit testing, you have proved that
it is faulty.
2) Never put back any part that
you unsoldered. Replace it with a
new one (or NOS/NIB if a new part
is unavailable).
3) Never replace non-electrolytic
capacitors just because they are old
and might be leaky. In professional
equipment, leakage is a lot less likely as higher grade parts are used,
voltages are lower, temperatures are
lower than in typical valve radios,
and circuits are more tolerant.
4) Never replace electrolytics just
because they are old. The long-life
types used in professional equipment are often perfectly good; there’s
no sense in sacrificing the factory
look if there’s nothing wrong with it.
5) Never swap valves of the same
type around in the chassis as a diagsiliconchip.com.au
nostic strategy or to fix a fault. Each
valve stays where it is unless and
until it is proved defective, at which
point it is replaced with a new valve
(these days, a NOS/NIB valve).
6) Clean and touch-up paint before addressing faults. Cleaning does
sometimes cause more faults, and a
nice clean instrument is a pleasure
to work on.
7) After cleaning, check every
single resistor for correct resistance
(without unsoldering it) and every
electrolytic in-circuit before proceeding with any diagnostic procedure. But don’t replace anything
found faulty yet.
8) Don’t rely on an overall functional check or rely on a check
against performance specifications.
Go through each stage with a scope
and verify that each stage works
precisely as it should. Replace parts
identified as out of specification as
you go through each stage.
9) Some brands of capacitor are
known to fail sooner or later. Replace
these after each stage is verified good
and the instrument meets and exceeds specifications. My T-130 did
not have any such components.
Australia’s electronics magazine
10) Every single time you replace
a component, do a comprehensive
set of checks to verify both that the
fault due to that component has been
cleared, and that no new symptoms
have appeared.
11) Where possible, replace resistors and capacitors with the same
original type, or if you cannot obtain
originals, use comparable components of the same vintage.
12) Clean and lubricate all
switches, pots, variable capacitors
and (later, during alignment/adjustment) presets. Don’t just apply contact cleaner/lubricant to switch wafers and pots, do variable capacitors
as well. Make sure you apply grease
to wafer switch clicker mechanisms.
13) Never touch calibration adjustments or presets until there is
nothing else left to do or check.
Mostly, you’ll find that an apparent
need for adjustment (beyond minor
touch-up) is in fact due to a faulty
component.
14) Do not modify to fix a fault.
Resist the temptation to modify
to improve performance. Reputable manufacturers knew what they
were doing.
July 2020 69
Tektronix component strips and soldering
Tektronix installed pig-tail type resistors, capacitors, and other small
parts on ceramic terminal strips (see
photo below).
These strips have a glazed finish;
they look nice and are rigid, which
helps stable circuit operation and
reduces vibration-induced failures.
They also have negligible leakage
and RF loss, and do not grow fungus
in high humidity climates like phenolic
tag strips can.
The strips also come in two different types, one that used nuts and bolts
on the underside for mounting and the
ones used here have snap-in fittings.
The former was used in earlier models and could help determine the age
of the meter.
Many people think these ceramic
strips are unique to Tektronix, but a
limited number of US manufacturers used them in tube-based military
equipment. The Japanese test equipment manufacturer Meguro used similar ceramic strips.
Tektronix made these strips by coating the moulded but unfired strips with
a paste of silver particles dispersed
in an organic grease, then wiping
the excess off. The wiping leaves the
Two of the ceramic terminal strips,
which many of the components mount
on. The notches in this strip are lined
with a silver alloy and the strip can
be mounted via snap-in fittings (as
shown) or bolt-on depending on type.
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Silicon Chip
paste neatly confined within notches
and slight depressions surrounding
each notch.
Upon firing, the grease evaporated,
leaving a microscopically thin coating
of silver in and around each notch,
bonded to the ceramic. They then
tinned each notch ready for soldering in the components.
The downside of these strips is that
silver readily dissolves in ordinary
tin/lead solder, and solder does not
stick to ceramic. Hence, using normal tin/lead solder will weaken the
silver-ceramic bond and will, sooner
or later, cause it to fail completely. In
the factory, Tektronix used a tin/lead
solder containing 3% silver, the 3%
being sufficient to stop its affinity for
more silver completely.
62% tin, 35% lead and 3% silver
solder used to be available from Tektronix under part number 251-514, but
they ceased selling it many years ago.
Its melting point is 188°C.
Note that this isn’t “silver solder”,
which is a British term for brazing alloy.
Nor is it modern lead-free electronic
grade solder, which contains silver but
has a significantly higher melting point
that can damage the ceramic strips.
Tektronix usually installed a small
roll of silver loaded solder inside their
oscilloscopes. They often did not include it in cheaper instruments. If you
have a Tektronix instrument that does
not have the little roll, it’s either because someone has swiped it, Tektronix never included it, or you have
an instrument originally supplied to
the military.
Fortunately, solder containing 62%
tin, 36% lead, and 2% silver is readily
available from RS Components (Cat
271-4172), along with element14 and
other distributors.
When working on Tektronix ceramic
strips, if you don’t have the supplied
roll, always use the modern 2% solder. Even 2% silver solder isn’t optimal, and you probably don’t know
the history of the device, so you must
assume the strips have already been
weakened. New strips do occasionally show up on eBay, but only occasionally.
Never place the soldering iron tip
within a notch and apply any force.
The ceramic easily cracks if you do.
Use a temperature-regulated chisel
tip 5-6 mm wide and apply it to the
side of the notch.
An example of the ceramic strips in place within the left-side of the chassis with
components soldered in. You can also see a warning about only using “silver
bearing” solder as tin-lead solder will eventually damage the silver alloy on the
strips. The T-130 did not come with this solder, so I turned a replica reel (shown
to the left of the note) and added 2% silver solder from RS Components. There is
more detail on these strips and the recommended solder in the panel above.
Australia’s electronics magazine
siliconchip.com.au
I also noticed that the zero setting
wandered about, and could not be
brought to an actual zero beat, so that
on the lowest range (3pF full scale),
the meter had over full-scale deflection regardless of the COARSE ZERO
control setting.
Contacting the seller
I sent a message to the seller via
eBay, informing him that the instrument was not operational, thus not
conforming to his description, and I
explained why.
He promptly wrote back, apologising, and offering to send me two replacement NOS/NIB (new old stock/
new in box) valves: a 6X4 and 6U8. I
accepted that, but pointed out that the
instrument uses five 6U8s and at least
one more was probably faulty.
The seller then arranged for a US
surplus valve dealer to courier one
6X4 and three 6U8s. They arrived two
days later. They were mil-spec valves
(W-suffix) too. I certainly couldn’t
complain about the after-sales service.
Making it pretty
Cleaning the cigarette smoke condensation off the cabinet was easy. I
removed all cabinet parts from the central chassis and washed them, along
with the front panel knobs. I did this in
the sink with dishwashing detergent.
I used a soft sponge to clean the
cabinet parts and a toothbrush for the
knobs. I then thoroughly rinsed everything with running water and then
Electrolube Saferinse, and dried the
parts off. Everything came up like new,
except for a few places where the paint
had been worn off over the years.
“Tek Blue” touch-up paint used
to be available from Tektronix under
part number 252-0092-02, but not any
more. Googling, I discovered that this
paint was made by the Chemtron Aerosol division of Rudd Company Seattle.
They no longer exist.
So instead, I bought the following
from Bunnings: White Knight Rust
Guard Quick Dry Advanced Enamel,
Neutral Tint Base 500mL Stain Finish, colour coordinates W 36.5 B 16.5
D 27 E 16.
This gives an excellent match.
500mL is far more than I could ever
use for touching up Tektronix instruments, but is the minimum they let me
buy. I used a cotton bud to apply the
paint where needed on the T-130 parts.
The UNKNOWN connector on the
siliconchip.com.au
Estimating the age of a T-130
This can be difficult, as the T-130 was
manufactured for 21 years, and there
are no date codes on any of the parts,
except the valves.
Of course, valve codes are useless, because you don’t know what
valves have been replaced during the
instrument’s life, and you don’t know
if any replaced valve was new, NOS,
or merely an old valve somebody had
on hand, good or otherwise.
You also can’t rely on the serial
number, at least not directly, as it is
not known how many were sold in any
given year, and that can vary widely. For an instrument like the T-130,
which filled a niche need for the first
time, there were probably brisk sales
in early years, and then just a trickle
each year, as new laboratories and
factories started up.
For oscilloscopes, Tektronix used a
few different coding schemes. These
encoded the factory which produced
the unit, country of origin, the revision
level, and in some cases the date of
manufacture. But it appears no coding scheme was used for the T-130,
and the serial numbers were purely
sequential.
In some cases, the serial number
for smaller Tektronix instruments was
sequential to the production line output, not to the instrument type.
For example, a production line may
have been making a batch of T-130s
and then changed over to making T123s (an oscilloscope preamplifier). If
the last T-130 in the batch was given
serial number 00226, the first T-123
would receive serial number 00227.
Thus, some smaller Tektronix instruments had large gaps in their serial number ranges. This likely applies
to the T-130, as the number sold would
not justify a dedicated production line.
Any Tektronix instrument with a serial number comprising a single letter
and two digits is a pre-production sample or a laboratory prototype. Once in
a while, these show up on eBay.
T-130 production started with serial
number 101. The T-130 got a major
facelift in 1958 (serial numbers 5000
and up) and a change in meter in 1965
(serial numbers 6168 and up).
If a T-130 has Sprague Black Beauty 160P capacitors (tubular capacitors
with red printing), it was made 1960
or later. If it has Sprague Bumble Bee
capacitors (colour-coded), it was probably made in 1960 or earlier.
Sprague “Bumble Bee”
capacitors (left) mean
the T-130 was likely
made pre 1960, while
“Black Beauty” 160P
caps (right) indicate
post 1960. The Bumble
Bee caps usually leak,
although leakage will
often not affect the
T-130’s operation.
front panel is an old-fashioned UHF
(SO-259) silver-plated socket, common
on test gear made before the 1960s. It
is much better than a BNC type in this
application – a BNC connector does
not have the mechanical strength to
support accessories typically used
with the T-130.
The connector was badly tarnished
and missing many of its ‘teeth’, so I
replaced it with a new one. Next, I reassembled the instrument using new
screws, because the old ones were all
corroded and unsightly. Shiny new
screws make all the difference – the
instrument now looked brand new –
on the outside, anyway.
Australia’s electronics magazine
As with many electronics manufacturers in the 1950s and ‘60s, Tektronix painted internal cabinet and chassis screws and adjustments with what
Tektronix staff called “Red Glyptal”.
Glyptal is a USA-based specialty paint
manufacturer. The original formulation is no longer available, at least in
small quantities.
Replicating Red Glyptal on the
screws and adjustments is a nice touch
in restoration. Many restorers use nail
varnish, but it’s far from ideal, in appearance or mechanical strength. A
close equivalent is “BLR Tamper Proof
Seal”, available from RS Components
(Cat 196-5245).
July 2020 71
Here is a page from the 1954 Tektronix catalog; when they started to produce the T-130 LC Meter.
Source: http://w140.com/tekwiki/wiki/Tektronix_Catalogs
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Silicon Chip
Australia’s electronics magazine
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Safety hazards
I plugged in the power cord and
checked the resistance from the Earth
pin of the Australian plug to the T-130
chassis. High Earth lead resistance is
a common fault in Tektronix instruments using a protruding NEMA 5-15
mains input connector. If you have
one, best check it. Mine had an opencircuit Earth.
As is typical, the nut that secures
the Earth pin to the connector backplate had worked loose. This is why
you shouldn’t use a mounting screw
for an Earth connection, which isn’t
permitted by most authorities. There
was tarnish on the Earth pin as well. I
cleaned the pin and tightened the nut,
using a drop of thread locker. I checked
again with an ohmmeter – no perceptible resistance – good.
There is another safety hazard in the
T-130. The range switch is a customassembled “Oak”-style three-wafer
switch. The rear-most wafer selects the
range setting capacitors and acts as the
power switch on the primary side of
the power transformer. So 230V AC is
within a millimetre of the range selection common.
That’s not very nice, Mr Moulton.
It’s an electric shock risk. One slip
of a probe and the switch is history.
And you can’t buy a replacement now.
I made a mental note never to probe
with a voltmeter or CRO around the
wafer while the T-130 is plugged in.
On the rear of the T-130 is the fuse, AC input and badge showing the voltage. A
desktop NC milling machine was used to make a 234V AC badge to replace the
117V AC version shown below.
Internal cleaning
An internal clean was needed to get
rid of accumulated cigarette smoke
residue and the general dirt that accumulates in all valve equipment
cooled by simple ventilation holes
in the cabinet.
First, I washed the chassis, components and terminal strips with Safewash citrus solvent, applying it with
a toothbrush and cotton buds.
Then, I went over it all again with
Saferinse to get rid of the Safewash,
and then again with isopropyl alcohol to remove the Saferinse. I was very
careful to avoid getting any Safewash
or Saferinse in the oscillator coils.
It is essential with old Tek equipment to thoroughly clean the terminal strips back to an uncontaminated
glazed ceramic surface.
If you don’t, the cigarette smoke
residue and general grime will in time
cause electrical leakage, if it hasn’t
already.
siliconchip.com.au
After cleaning, I took some photographs. Reviewing the photos, I realised the terminal strips still were not
completely clean. So I repeated the
whole process over again.
The T-130 was designed before highgrade polyester capacitors became
available, but almost all T-130s, including mine, were made with professional-grade Sprague “Black Beauty”
160P capacitors (black tubular capacitors with red printing).
These seldom show any leakage.
T-130s made before 160P production
started in 1960 have Sprague ”Bumble
Bee” (colour-coded) capacitors, which
usually do leak.
But quite a high leakage in the range
Australia’s electronics magazine
capacitors (C90-C94), say 5µA, will
only result in a slight change in FSD,
which can be adjusted out in calibration. 5µA leakage in a radio grid coupling capacitor would have a disastrous effect on audio quality.
The only other tubular capacitor
in the T-130 bypasses the 150V rail –
leakage short of a definite fault there
will have no effect.
Next month
Now that the T-130 was clean and
safe, I could get into the nitty-gritty of
figuring out what was wrong, fixing it,
and then adjusting it back to its original factory-spec condition. But that
will be in next month’s article.
July 2020 73
A brief history of direct-reading frequency meters
Digital frequency meters (counters) were
not widely used until integrated circuits
reduced the cost in the 1970s.
Imagine even a three-digit frequency
counter implemented with valves. You’d
need four twin valves for each decade
counter, four for each display latch, five
for each display decoder and eight more
for time-base division. Plus another three
for the power supply. That’s a total of 50
valves!
But there has always been a need in design laboratories to measure frequency,
and an analog meter of 1- 5% accuracy was
often good enough. So there have been
analog frequency meters for just about as
long as there has been electronics.
The earliest direct-reading frequency
meters were just an amplifier with enough
gain so that it is well over-driven, and the
output is almost a square wave. The output
is fed to a rectifier and moving-coil meter
circuit via a small capacitor, so that the
meter just gets a series of narrow pulses,
one pulse per input cycle.
Due to mechanical inertia, the meter responds to the average current, so its deflection is proportional to frequency. This
arrangement is shown in the upper circuit.
But this circuit has some serious disadvantages: if the input level is not sufficient to overdrive the amplifier, you get
a low reading. In fact, the reading always
depends on the input signal strength to
some extent. The calibration also depends
on not just the HT voltage and R1 and C1,
but also on the emission of V2, even when
V2 is completely overdriven.
Plus the contact potential of V3 causes
a continuous deflection even with no signal. The pulse-width set by C1 must be a
small fraction of the cycle time; otherwise,
C1 will not discharge adequately, and the
meter deflection will become excessive.
Howard Vollum, when a student at Reed
College in 1936, wrote a thesis, “A stable
beat frequency oscillator equipped with a
direct reading frequency meter.” The oscillator part was nothing remarkable, but
his frequency meter significantly advanced
the art. This is shown in the second circuit below.
Now V1 does not have to be overdriven.
It can be an ordinary low-µ triode as its
role is to provide a low-impedance drive
to the transformer; this lowers its cut-off
frequency.
The transformer provides push-pull
drive to V2 and V3. V2 and V3 are small
thyratrons and the circuit functions as a
bistable (flip-flop).
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Silicon Chip
Thyratrons (gas-filled triodes) function
something like an SCR in series with a zener
diode. If the grid is held sufficiently negative
(-10V), no current flows in the anode and
the grid. If the grid is taken less negative,
anode current flow starts and ionises the
gas. The anode current immediately rises
to the maximum possible in the circuit.
The anode-cathode voltage stays close
to 16V, regardless of what the anode current is. The grid is now more-or-less
shorted to the cathode due to its position
in the electron stream and proximity to
the cathode.
Assume V3 is conducting (on) and V2
is off. The cathode of V3 is at 74V and C1
is charged to 74V, positive on the right.
As soon as the left-hand end of the transformer goes sufficiently positive, V2 will
snap on. V2’s cathode rises immediately
to +74V, so the right-hand end of C1 must
rise to +148V, cutting off V3.
When the right-hand end of the transformer goes sufficiently positive, V3 turns
back on, forcing V2 off again. The circuit
flips back and forth at the input frequency,
as long as sufficient input level is present.
C2 and C3 communicate short pulses
to V4, which supplies two pulses to the
meter for each input cycle.
So the output pulse amplitude and width
is entirely independent of the input level.
If the level is insufficient to trigger either
thyratron, the action simply stops. As there
are two pulses per input cycle, the meter
pointer is a lot less
likely to shudder
with low (≲20Hz)
V1
input frequencies.
However, transformers were ex- INPUT
pensive, and Thyratrons cost more
than hard vacuum
triodes, yet were a
lot less reliable and
shorter-lived.
The next major advance came in 1941.
National Cash Register Co. filed a patent (inventor L. A. DeRosa) disclosing a precision
direct-reading frequency meter employing
a flip-flop circuit based on two pentodes,
triggered by an overdriven pentode amp.
The flip-flop ran at half the input signal
frequency, but two pentode monostable
circuits were triggered from each flip-flop
pentode. The meter then received one clean
and square monostable pulse for each input cycle. It was a little more accurate, a
lot more complex but not much more expensive than the Vollum circuit. It retained
the correct-or-nothing reading operation.
In 1951, Howard Vollum was now Tektronix chief engineer, and new engineer
Chris Moulton was designing the new ‘bistable’ configuration used in the T-130.
With the amplitude clamp circuit added by
Moulton, his circuit is a lot simpler than
the DeRosa method and just as accurate.
Most, if not all, subsequent designs for
audio direct-reading frequency meters are
derivatives of the Moulton and/or DeRosa
methods.
The Hewlett Packard 500B/C Frequency
Meter/Tachometer used a Schmitt trigger
followed by a monostable briefly turning
on (once per cycle), with a constant current source feeding the moving coil meter.
With a rectangular or on/off pulse instead
of a capacitor decay, the need to keep the
pulse width small compared to one cycle
SC
is removed.
+HT
V2
C1
V3
R1
_
+
+90V STABILISED
V1
V2
V3
R1
+148V
R2
-VE BIAS
+74V
INPUT
0V
+148V
C1
C2
R3
+74V
C3
V4
R4
R5
+
Australia’s electronics magazine
0V
_
+74V
R6
0V
R7
BACK BIAS 1.5V
+
_
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