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SERVICEMAN'S LOG
Well-designed thoughtlessness
A recurring theme for these columns as of recent
times is the prevalence of designers who, whether
intentional or not, put a lot of thought into not
thinking when designing devices.
People of a certain age may recall an
English sitcom named “The Fall and
Rise of Reginald Perrin”. I’m not talking about the insipid recent remake,
but the original show, which aired way
back in the mid-70s.
The premise of the show was the
hum-drum life of an ordinary, middleclass, middle-management worker and
his eventual descent into mid-life crisis. He wanted more, and ended up reinventing himself.
The show was satire, and an indictment of then-British society (and her
colonies). It took every opportunity to
skewer the class system, the unions,
the nationalising and de-nationalising
of various industries and much more.
One of several running gags involved
the trains, where because they always
ran late, Reginald was always late for
work. In the first series, he was always
11 minutes late. In series two, he was
always 17 minutes late and in series
three, 22 minutes late.
He always offered a different excuse
for his lack of punctuality, and these
excuses were increasingly outlandish,
such as: “seasonal manpower shortages, Clapham Junction”, or: “Seventeen minutes late, water seeping
through the cables at Effingham
Junction.”
Without spoiling it for anyone who wants to watch the
show (I recommend it, though it
isn’t everybody’s cup of tea), part of
the storyline involved a shop named
Grot. A sly dig at rampant consumerism, Grot’s stock was made up of
items that were purposely designed
to be bad or useless, such as salt and
pepper shakers with no holes in them,
non-stick glue, elastic tow-ropes and
square rugby balls.
I mention this, admittedly in a rather
long-winded lead-up, because recently
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I’ve been working on some items that
could have come from this shop!
Over the years I’ve regularly called
out what I see as lousy design, and I’ll
keep doing it, because it often seems the
person who designed the machine, appliance or manufacturing method has
no idea of how the appliance, machine
or manufacturing method will actually
be used in real life.
Examples include the light on my
vacuum cleaner that shines up the
wall, rather than on the floor, or the
lawnmower that doesn’t cut grass short
enough and has handles and levers that
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Dave Thompson
Items Covered This Month
•
•
•
Misanthropic designers
producing ill-considered designs
HP8595 spectrum analyser
repair
3A USB charger repair
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
protrude wider than the cutting track of
the mower, making it difficult to mow
right up against a wall.
Another example is the pickup selector switch on my Fender Telecaster; it
is almost impossible to actuate when in
the bridge pickup position because it is
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almost hard-up against the tone knob –
a design flaw that has persisted since
the late 50s. (For those pedants who
are preparing to flame me, like many
I flipped my Tele’s tone-plate around
for easier access, swapping the volume
and tone pots).
And don’t get me started on car engineering! Some cars have the battery
under the driver’s seat, so you have to
remove the seat to replace it. One gets
the impression that after the initial prototype rolled out, the engineers discovered that they had forgotten to include
a battery and so they had to scramble
to find a place to put it!
Many of the cars I drove as a youngster had steering-wheels that obstructed
the view of the instruments, and in one
car I test-drove, I had to sit at an awkward angle because the steering wheel
and pedals weren’t in line.
And the number of times I have
needed triple-jointed limbs or specially-made tools just to be able to access
nuts and bolts to disassemble machinery to get to faulty parts…
It’s a miracle that any of these designs get put into production with these
quirks. Indeed, there are web pages and
YouTube channels dedicated to this
subject: stair-wells heading into brick
walls, inward-opening toilet doors with
notches cut into them to fit around the
bowl or basin, water pipes right next to
electrical outlets; the list goes on.
Don’t get me wrong, these follies are
always good for a laugh, but usually, it
isn’t the people who have to deal with
them that are doing the laughing!
would have cost more than a new one
is worth, so it made sense to send the
faulty board (swapping the board fixed
the welder, so we know it is at fault).
The usual suspects are capacitors,
semiconductors or simply solder joints
gone bad, but working to resolve any of
these problems becomes a major mission due to the varnish coating. One
saving grace is that the customer supplied a circuit diagram for the board,
and while components on the PCB were
clearly marked, it always helps to have
a circuit diagram for troubleshooting.
When I encounter a coating like this,
the first thing I do is see if I can soften
it using solvents. None of the solvents
I have touched it. Next is cautiouslyapplied heat. While a proper heat gun
is ideal, I tend to use my desoldering
heat gun more these days, as it is easier
to control and aim.
I found an unpopulated corner of the
board and judiciously applied heat to
the area to see if I could make a dent (so
to speak) in the varnish. I couldn’t. It
didn’t even get softer; it just got hotter!
It turns out, though, that I could melt it
with my soldering iron, so that’s what
I did. Messy, but effective.
That partially solved one problem:
getting to the soldered connections
on the bottom of the board. But I still
had to deal with the component side.
Desoldering the leads below was one
thing; extracting the components was
another.
The first thing I did was to check the
soldering on the bottom of the board.
Though the varnish was thick, it was
Enter the culprit
Now we get to the meat of the matter. The other day, I received a faulty
PCB to fix, and the entire thing was
covered with a very thick layer of varnish, top and bottom, despite being a
single-sided board. Every component is
well-embedded into this coating, making parts incredibly difficult to desolder, let alone extract.
What genius thought this would be a
good idea? Obviously, it is designed to
be replaced rather than repaired, and
I’ve made my opinion on that subject
well known.
It must be evident to the manufacturer that end-users would want to repair faulty boards; they aren’t a cheap
replacement part, but a multi-hundreddollar investment. This one is from a
heavy-duty welder, which no longer
held its output. Shipping the welder
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mostly clear, so a visual inspection
was possible.
Like many such boards, there are
multiple, well-tinned heavy tracks for
the likes of Earth returns and power
supply paths. Welders generally boast
serious current-handling capabilities,
so the boards have to be up to supplying that current without sagging and
compromising the welds.
Where there is resistance, there is
heat, and as these boards would heat
up and cool down regularly, they will
expand and contract. This makes any
physical connection a potential weakness. As the resistance of a bad joint increases, so does current and heat, and
the cycle continues until something
eventually gives.
In many ways, it is better for the serviceman to get a board that has utterly
failed; at least the faults (or the consequences of the faults) are patently obvious. Intermittent or partial faults make
things more difficult, as does not having the ability to bench-test the board.
Several other satellite boards drive
this particular controller, and without
those, I can’t test the board at normal
operating levels. I can test each component though, and the overall physical integrity of the board, which is the
process I had to use.
There were some very large, heaped
solder joints which looked a bit dodgy
– this is typical of every high-current
power supply board. But I saw no obvious faults like overheated tracks, discolouration of the board or any other
visual clues to explain the failure.
I burned through the varnish over
several of the more dry-looking joints
and cranked up my heavy-duty soldering iron to reflow them, but overall the
board looked well-made, and the joints
generally were physically sound. So I
moved on to check the components.
Component checking
Six large capacitors dominate the
landscape of the board. I could measure them in-circuit using my Peak ESR
tester, but I prefer to do my component
testing off-board, just to be sure.
At least these caps were relatively
easy to remove because I could get
some purchase onto them. I did have
to first cut through the fillet of varnish
around the base of each one using a
razor blade; a task made more difficult
by the proximity of other components.
Still, I got them out, and though it
was hard to tell visually whether the
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goop coating the outside of some of
them was leakage or runs in the varnish itself, it proved to be the varnish.
All the caps measured very close to
their stated values, and the ESRs also
read very low.
So I moved onto the handful of smaller electrolytic capacitors and a dozen
or so high-voltage ceramic types; I removed them the same way, and they
all tested fine.
I also pulled a medium-sized transformer from the board and measured
it for resistance; the figures I took from
the primary and secondary corresponded roughly to the turns ratio supplied
on the schematic (no other specs supplied). But I was more interested in
shorts or open circuits, of which there
were none. A megger check also proved
there was no breakdown in the windings or insulation.
The board has three 24V 10A relays
mounted on it and these I tested by
clearing the varnish from their terminals on the track side of the board and
soldering test leads to their normallyopen contacts and coils. I downloaded
the data sheets and used my bench supply to raise and lower the voltage, testing each relay’s current draw and operation and drop out voltages.
I connected my multimeter’s buzzer
across the terminals; while not technically a perfect indicator of the electrical
condition of the contacts, my musical
ear can detect even subtle variations in
the frequency of the tone, which changes with resistance. Any deviation from
the closed-circuit tone (with the meter
leads shorted, for example) means there
is resistance in the circuit.
On these relays, the buzzer tone remained the same, indicating no significant changes in contact resistance.
Again, this is not a definitive test for
contact integrity, but adequate for my
purpose.
Semiconductors were my next target, and this board boasts many different types.
Here I had to cut some corners; while
the relay driver Mosfets and the large,
paired diodes in the voltage multiplier
section were relatively easy to remove
and test, the smaller DO-35-sized zeners and regular diodes were in almost
every case totally enclosed in varnish.
They would likely be impossible to remove without damage.
All I could do was clear the varnish
underneath (there was a lot of varnishclearing going on!) and measure them
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with my semiconductor tester. As this
automatically detects and takes into
account whether they are in-circuit or
not, I had to trust it was doing its job
correctly.
There was nothing suspicious in my
measurements with any of the diodes.
All the zeners measured as-rated, and
the other identical types all had very
similar breakdown voltages, which in
itself means nothing other than that no
individual component stood out as a
potential problem source.
Measurements of the three IRFZ24
Mosfets did show some discrepancies,
so even though not a smoking gun, I
decided to replace them. They are as
cheap as chips anyway (LOL!) and as
the TO-220 packages stand proud of
the board, they are easy (relatively!) to
remove and refit.
There is one small TO-92 type NPN
transistor, and because I broke one of its
legs removing it, I subbed in a BC549,
one of the suggested alternatives in my
transistor manual.
There were also sundry components,
such as a 4-pin DIP-style opto-isolator, which was buried in varnish and
bridged a physical channel cut into the
board. I could only resistance-test this
device, and it appeared to pass. There
are also several series-connected thermistors, used as inrush current limiters, and a chunky metal-oxide varistor
(MOV) used for surge protection; these
all tested fine.
Having replaced the only parts I
could find that could potentially be
causing faults, all I could do now was
to clean up where I’d been and re-coat
the places I’d dug into the varnish with
some standard polyurethane.
I doubt the board really needs it for
July 2020 63
electrical protection, given it’s all relatively low-voltage, and there would be
no stray coronas developing on pointy
solder joints. I’m assuming it is there
in case metal dust or welding swarf
might find their way into the cabinet
and potentially short out something
on the board.
In the end, I did as much as I could
without testing the board in the welder,
then sent it back to be reinstalled and
tested in-situ. Theoretically, checking
joints and testing individual components should resolve any problems,
but we all know there is more to it than
that, and it will only be dumb luck if
the board works when put back into
the machine.
More badly designed junk
Another potential Grot shop candidate is a USB3 hub I worked on recently. It had a problem that’s common
with many other modern devices. This
hub was relatively new, but the socket
inside had come away from the PCB,
rendering it useless.
The owner wondered whether it
could be repaired, not because it is a
particularly expensive device, but because it irks him (as it does me) to throw
something away that isn’t that old or
has had much use.
The problem with this, and other devices, is that it is designed to be small
and portable, but the cable that comes
with it is very heavy and not overly flexible, so the thing will never sit where it
is placed, and the stress and strain on
the socket is very high. The new USBC connectors might solve these issues,
but we shall see about that.
I’m sure this same problem affects all
of us; my phone, which is a few years
old now, is starting to show signs of
socket wear, mainly because many of
the OTG cables available now are quite
heavy gauge, and unless I am careful,
I can put a lot of strain on the charging socket. Editor’s note: this is one of
the benefits of wireless charging; while
slow and inefficient, it doesn’t wear the
USB connector!
I also purchased a Raspberry Pi 4 a
while ago, and this uses a USB-C connector for power and micro-HDMI for
video output. Both these cables are so
stiff that I just have the Pi sitting in midair, at whatever angle comes naturally
with the cables plugged in. To do otherwise would probably rip the sockets off.
Given that these sockets usually rely
on only a few tiny solder pads for adhe64
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sion, it’s no wonder they come adrift,
even with normal use.
Re-attaching the USB socket to the
hub wasn’t too taxing; the challenge
was getting the thing apart without
breaking the plastic clips they used
to hold it together instead of screws
(another Grot idea). I suggested the
owner let the repaired hub hang naturally on the cable and hope it doesn’t
break again.
I wonder if someone has upset the
designers of these devices, and they
are exacting their revenge on society by
designing shoddy, unserviceable products. If so, I wish they would take their
frustrations out in some other manner,
such as with a stress ball or a punching
bag. Do us servicemen a favour, please!
HP8595 spectrum analyser repair
A.L.S., of Turramurra, NSW has
been up to his usual hobby of buying
cheap test instruments from internet
sellers. And as is so often the case,
they turned out to need a bit of TLC
(by which we mean ‘serious repairs’)
to get them back into full working
condition...
You can buy a second-hand HewlettPackard HP8595E spectrum analyser
quite cheaply on the internet. These
devices can analyse signals from 9kHz
to 6.5GHz, but they are starting to age a
bit as they were new in the late 1980s.
Many now have little gremlins growing inside them.
The HP85xx series was very popular
25 years ago, because these instruments
are portable and easy to use. So there
are thousands of them for sale, and
many parts available on the internet.
The one I bought was a real find because it included several options, in-
cluding the HP-IB/parallel port interface for external control and printing.
It was this option which convinced me
to buy the instrument, so that I could
keep records of various traces.
Its specs are really impressive, and
it analyses an incredible array of RF
and modulated signals, including TV
signals. It also has an FFT function to
analyse harmonic distortion of AM/
FM audio signals.
On receiving the device from the
USA, I immediately tried out the print
function and connected up my “Print
Capture” device (parallel-to-USB
module). This allows me to download screen grabs, and has worked
tirelessly on all my test instruments
with parallel ports. But it refused to
work this time.
Another way I can obtain screen
grabs is via a GPIB-to-USB adaptor, but
that also failed to work. To my horror,
no matter how many combinations
and permutations I tried, I could not
get any screen grabs out of the device!
Of course, you can photograph the
trace on the screen easily, but the result is not as crisp and neat as a digital
hardcopy, because the signal moves a
bit and blurs.
An obvious clue as to why this was
not working was that the option “041”
was not listed on the setup screen.
But the other three options that were
supposedly installed according to the
seller were listed there. So my immediate thought was that the board was
installed, but not connected correctly,
so it was not being detected or used.
The instrument is relatively easy to
open up. I just had to unscrew four Allen-head bolts and four Philips-head
screws. The cover then slides off.
The HP-IB/parallel
port interface,
which is used for
external control
and printing, was a
welcome inclusion
with the spectrum
analyser.
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siliconchip.com.au
The first thing I noticed after opening it up was that there were some
missing screws, which suggested
someone had previously been inside
it. I feared that a dodgy board had been
fitted just so that the instrument could
be sold with more options.
However, once I got a chance to inspect it, I found that the GPIB board
looked pretty good. It was a bit dusty,
and I noticed that the multi-pin DIL
connector looked a tiny bit crooked. I
disconnected everything and applied
some contact cleaner to the plug and
socket. It was then that I noticed a bent
pin on the male header.
I wasn’t sure if I had bent it during
the disassembly, as the plug was very
stiff with age when I disconnected it (I
guess we all end up that way!).
Anyway, after cleaning the board
and connectors, I straightened the
pin and plugged it back together. It
snapped into place. On start-up, the
option “041” appeared, and I was finally able to obtain beautiful hard copies via both parallel and GPIB. Sadly,
though, that is not the end of the story!
The plot thickens
Some weeks later, I noticed that the
analyser amplitude readings seemed a
bit low. I connected its internal calibration signal up to the input and obtained a reading about 18dBm lower
than expected. So I ran the “cal amplitude” routine.
To do this, you need to connect a
BNC patch cable from the calibration
output directly to the input and then
press the “cal amplitude” soft-key. The
instrument should be warmed up for
at least 30 minutes before doing this. It
takes several minutes, and during this
time, you hear plenty of relays clicking in and out. However, in my case,
it stopped after a minute, and a message came up saying “Cal gain: Fail”.
The service manual explains that
this means the signal was too weak
and outside the specified minimum
level. Either the calibration signal was
poor, or there was an internal problem
with the analyser.
The manual suggests checking the
following parts of the circuit: A3 front
end, A7 analogue interface, A9 third
converter, A11 bandwidth filter, A12
amplitude control, A13 bandwidth filter and A14 log amplifier. That really
narrows things down – not (consider
that these assemblies total about half
of the instrument)!
siliconchip.com.au
A beautiful ‘hardcopy’ finally emerged after fixing the improperly connected
circuit board.
Hoping it was just the calibration
signal at fault, I hooked up a 1GHz
generator but found that the reading
was still 18dBm low, proving that the
problem was with the measurement
side of the instrument. I was hoping
it wasn’t a front-end problem, because
the attenuator is buried deep inside,
whereas the other boards are merely
plug-ins and changing them is an easy
job, if time-consuming.
I did some internet research and
discovered a great three-part YouTube
video about fixing an HP8590, which
is a similar device but with a 1.5GHz
maximum frequency. I highly recommend it if you enjoy repair stories. See:
https://youtu.be/kV4BOf3Oqk8
This inspired me to check out the
symptoms of my instrument, and I noticed that when I manually adjusted
Australia’s electronics magazine
the attenuation, I could get a correct
reading when it was set to -20dBm.
But the readings were all over the
place at other attenuation settings. I
also got obscure readings at different
frequencies; precisely the same symptom as in part three of those YouTube
videos.
Unfortunately, this meant that the
attenuator was the immediate suspect
and so it would be a significant repair.
Hunting around the internet, experts
reported that 90% of problems with
these instruments were the result of
poor or damaged attenuators, so I immediately looked around for a secondhand or reconditioned attenuator.
As luck would have it, I found somebody selling a brand new attenuator,
all sealed up in its original HP box, so
I made him an offer (which he didn’t
July 2020 65
The analyser’s ‘front end’ which processes the input signal via the attenuator.
The faulty attenuator (top right) was deep inside. It looks more like plumbing
than electronics!
refuse), and the part arrived in a few
days from Italy.
Now the fun and games began! The
YouTube guy, who calls himself “FeedbackLoop” (siliconchip.com.au/link/
ab3c), did not go into details of how to
extract the attenuator. I could not even
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find it after searching for some time!
The diagram in the manual is somewhat simplified, and the assembly (labelled A3) is just shown as a dotted
line. You cannot get to it from the side,
so the whole aluminium assembly has
to come out in one piece.
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Everything looks pretty simple until
you figure out how to extract it because
it’s a bit like a Rubik’s cube. You have
to start by loosening screws and then
gently shaking things to discover how
to extract the entire “box” containing
the attenuator.
For fear of boring readers, I won’t
describe the exact procedure here.
But if you find yourself in the same
boat as I was, you may wish to write
to Silicon Chip so your message can
be passed on to me. I will then reply
in excruciating detail.
I think the money I spent to obtain
a new attenuator just drove me on to
replace the suspect one, despite the
herculean task before me, because it
would be such a waste to have a beautiful new part and never use it. Sort of
like those blokes who buy an expensive car which then just sits in the garage, never being driven. What a waste!
You will see in the picture here that
the assembly looks somewhat like a
UHT dairy plant and is more about
plumbing than wiring, because of all
the semi-solid cables which require
disassembly. Caution is advised here,
because they must not be bent. I had to
work slowly and patiently to unthread
some of the wiring harnesses between
the semi-solid cables.
Finally, I managed to extract the culprit and replace it with the brand new
part, but it required the same amount
of patience to re-assemble everything.
Naturally, I made some mistakes and
had to do it all over again when I realised that I couldn’t re-fit one of the retaining screws because an aluminium
housing was blocking it. But finally,
it was done, and I checked it all thoroughly in case something was amiss.
Very cautiously, I switched it on,
hoping there would be no nasty noises. Amazingly, it all started fine, and
the measurements were almost exact
to within 0.5dBm. The frequencies
were also spot on!
After celebrating for the required
30-minute warm-up, I performed a
self-calibration, and the accuracy improved even more. I was really glad I
purchased the brand new attenuator
(at significant cost) because if it was a
second-hand ‘dud’, it would have been
a colossal waste of time and effort.
Now I have a really precise and importantly, working instrument. I intend to protect the attenuator by using
a DC-blocking device and an external
attenuator, in case a DC voltage might
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accidentally be applied. Any applied
DC will destroy it, as will RF signals
which exceed 1W or +30dbm.
3A USB charger repair
B. P., of Dundathu, Qld has had the
same simple fault fell multiple devices
in his possession. Is he cursed, or is
this a case of bad designs multiplying?
You be the judge...
When chatting with my mate via
Skype on a Samsung Galaxy S 10.5
Tablet, I found that its battery would
discharge even though the supplied 1A
USB charger was plugged in.
I ordered a 2A charger on eBay, but I
found that it was also unable to keep the
battery at 100%, so then I purchased a
3A charger. This one was finally able to
keep the battery charged at 100% while
using Skype. As I was quite happy with
it, I decided to get a spare, so I ordered
another identical one.
The original 3A charger worked well
for a couple of years, but recently I noticed that the battery was discharging
even while it was plugged in. I felt the
charger and it was cold, so it clearly
wasn’t working, as it was usually quite
warm when in use. Swapping it for the
spare charger got me back in business.
I decided to try to fix the failed unit.
It appeared that the two halves of the
case might be glued together, as is common with many chargers, so I clamped
it lightly in the vice with padding, to
see if it would crack open. It popped
apart and I found that it wasn’t glued,
but instead clipped together. This was
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good news, as it would be much easier
to reassemble it later.
I had a close look at the circuit board
and noticed blue corrosion build-up
on two of the 1N4007 diode leads, but
these diodes and the other diodes on
the board tested OK. I then noticed a
1W 0.5W resistor marked “F1” on the
circuit board, indicating that it was
used as a fuse. This resistor was connected between one of the mains wires
and the rest of the circuit and when I
tested it, it was open circuit.
I didn’t have any 1W 0.5W resistors
in my parts bin, only 1W types, but
I managed to salvage a similar resistor that tested OK from another dead
charger.
I reassembled the charger and tested
it, and it worked just fine. However,
after a few weeks of use, the charger
failed again. I wasn’t surprised when I
opened it up and found that the same
resistor was open circuit. I decided to
replace it with a 1W 1W type, and it
has been working reliably ever since.
Even though this 3A charger only
cost me about $5, it was an easy fix
which not only saved me $5 and the
wait for a new one, but that was one
less device going into landfill.
I had a similar problem with the
sensor light on our front verandah.
Its ‘fuse’ resistor failed several times,
so I ended up replacing it with two
higher-rated resistors in series. That
repair then lasted the life of the sensor, which eventually disintegrated
due to UV deterioration of the plastic.
I’ve also had mates bring me other
USB devices which had stopped working, and I was able to fix those by, you
guessed it, replacing a fusible resistor.
So this is a very common configuration in devices where a low voltage is
derived from the mains, and failures of
this part are a common occurrence. It’s
likely that the resistors are just barely
rated for their use in this configuration,
so it may be necessary to increase the
rating of the resistor to compensate for
the inadequacy of the original resistor
to cope with higher ambient temperatures and high mains voltages.
SC
The 3A USB charger PCB shown outside of its housing. F1 is
the 1W resistor shown sticking out at lower left.
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July 2020 67
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