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SERVICEMAN'S LOG
Treadmill trials over trails
Dave Thompson
Being stuck inside for a long time, we’ve found that we (try to) use things that
haven’t been touched in a while. Some of them have been sitting around for so
long that they no longer work properly. In the case of our treadmill, the repair
job provided more exercise than actually using it!
At the moment, I’m only allowed to
go out of my house to shop for essential supplies (though what constitutes
essential is open for debate) or to walk
or cycle for exercise. I have to say I’ve
never seen so many people out and
about; like us, they probably want to
get out of the house to stave off ‘cabin
fever’. It is sometimes so busy on the
footpaths it is challenging to maintain
the required 2m separation!
Combine this with increasinglygrubby autumnal weather and walking has become a lot less appealing.
Luckily, a few years ago we invested
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in a good quality treadmill. However,
like the vast majority of exercise equipment, after six months of solid use,
we used it less frequently, and it now
sits in the spare room gathering dust.
To be fair, the treadmill isn’t totally unused; the wife uses the arms to
hang washing on, and we store boxes
of who-knows-what on the mat! Given the current situation, though, it
seemed prudent to press it back into
service.
After a good clean, it looked brand
new, even though it is going on for 10
years old. That’s the great thing about
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equipment that typically doesn’t get
much use. At least it stays in good
condition! That said, we did do many
kilometres on this one back in the day,
though my motivation was more wanting to get my money’s worth out of it
rather than personal fitness!
This model is marketed under
the name ProRunner; a brand likely
dreamt up by the big-box company
that sells these treadmills. It wasn’t
inexpensive and is very well made,
rock-solid and almost to the level of
what you’d find in a fitness centre. It
has done everything we’d asked of it,
June 2020 61
so I considered it money well spent
at the time.
The treadmill stops running
To prep it for use, I vacuumed all
the dust off the frame and control
panel and wiped down the belt surface. I also broke out the long-necked
squeeze-bottle of silicone spray grease
that came with the machine and as per
the user manual, lubricated the deck
and the underside of the mat.
So far, so good; the machine was
running as smoothly as ever, and the
wife and I had several sessions over
the following days. Then, a few days
ago, as the wife was finishing her program and was in the cool-down phase,
it shut down unexpectedly. The control panel flashed on and off about
once a second, and each time it went
dark, a beep sounded from the builtin piezo buzzer.
Thinking it had simply ‘crashed’,
she hopped off and turned the main
switch off and on a few times, hoping this would reset it. There was no
change; all she got from it was the
rhythmic buzzing and blinking.
She called me in, but there was
little I could do. Full disclosure: I
know as much about treadmills as I
do about cardiothoracic surgery. That
is, nothing.
Well, I suppose that is not totally
true; I know there’s a motor and a
power supply in there, and likely some
electronic jiggery-pokery going on up
in the control panel and the two sections talk to each other, but that’s it.
I’ve never seen inside one or viewed
a circuit diagram.
Like any serviceman though, I considered it my sacred duty to get in
there and at least try to figure out what
was going on!
After a quick internet search, which
Items Covered This Month
•
•
•
•
Stuck in the house sans spare
semis
C-Bus home automation
system repair
Sharp R350Y microwave repair
A Japanese fridge in Russia
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
62
Silicon Chip
revealed little-to-no technical information about this make or model, I
learned that some machines have an
electronic reset somewhere. However,
I didn’t recall reading about this in the
user manual and a quick look over the
panel and around the motor housing
confirmed there was no breaker or
pin-hole, or any other obvious reset
mechanism.
Opening it up
There was nothing else for it but to
open it up and see what I could find.
Before doing that, however, I did my
due diligence and looked further on
the web. This proved frustrating; all
I could find were outdated ads from
the retailer or the odd expired listing
for similar units on auction sites. An
image search proved just as fruitless;
there are many, many types of treadmill and all look much the same.
So I had no choice but to break out
the tools, get the covers off and see
what I was dealing with.
I did learn there are several components to consider; down at deck level, there will be a motor and a driver
board for it. This sits (on our treadmill,
at least) in the lower front section of
the machine. Directly above that, in
between the arms, is the control panel.
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This is the part we mindlessly look
at when we are slogging through the
pre-set programs and it consists of a
couple of displays, one LCD and another LED, and few rows of membrane-style buttons (one row for preset speeds and one row for degrees of
incline).
Similar controls are also on the ends
of the support arms, with speed control on the right side and incline up
and down at left. There are also exposed metal contacts on each handle
that the user can hold onto, and the
machine will display their heart rate,
and from that, with speed and distance
figures, the controller will estimate
information like calories burned and
an estimated time of when my heart
will explode!
Nothing extraordinary there, but
relatively comprehensive compared to
some treadmills. The problem could
lie with the display/control panel up
at the top, or it could be the motor and
its associated driver down in the deck
housing. I started with the deck housing simply because I thought it more
likely to be something to do with the
motor and power supply.
The large, moulded-plastic housing
looked as if it would just pop off, but
was held up with something I couldn’t
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sink. I thought that this was where
the problem lay, because this part
does the lion’s share of the work, and
likely wears out first. Plus, I read a
few forum posts where ‘experts’ postulated that failed motor driver boards
are the cause of most powered treadmill failures.
The sticker on the motor states it is
rated for 90-180V DC. That’s some serious juice, and given it has to drive
the belt with someone weighing up
to 140kg standing on it, impressive
in itself.
My research on the web revealed
some generic circuit diagrams, but
nothing matched this setup.
However, it appears that most powered treadmills use very similar technology to control the motors, and given there are only three types of motor
typically used in treadmills, and two
of those types are relatively rare, I
could safely assume this controller is
a PWM type. The PCB assembly certainly looked very similar to images of
PWM boards I found online.
Taking the easy pickings
see. I could move the housing a little,
and unclipped it from two locations in
the very front, but something was holding it together further back. I couldn’t
see any screw holes, and went so far as
to lift the machine up so I could check
underneath for fasteners, but nothing
was visible.
A viscous problem
I assumed it to be just strong clips
holding it together, so I worked my fingertips in the gaps between the housings and applied increasing pressure,
expecting it to let go, but it stubbornly
refused to give. What a great start to my
treadmill adventure. I couldn’t even
figure out how to get it open!
After much huffing and puffing and
purple language, I eventually gave
it some real salt and pepper, and it
started letting go. One by one, six turret clips finally popped loose. When
I manoeuvred the housing away from
the deck, I could see what had been
holding it up: glue. Big, opaque blobs
of glue.
Great, it was going to be one of those
jobs. Someone, somewhere, must have
thought that clips alone just aren’t
good enough for our treadmills, let’s
smother everything with glue and
make it almost impossible to service!
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A quick look around the motor bay
proved my hypothesis; anything exposed or connected was slathered
with a generous dollop of the stuff.
And it isn’t like hot-melt glues and
silicones I’ve encountered before; in
some places, it is very hard and brittle
and breaks away, while in other areas
it rolls and stretches, making it very
difficult to remove.
I was loath to get my heat gun anywhere too close in case I damaged any
of the other parts, many of which are
plastic, so when I had to remove glue
from anything, I resorted to picking
away at it with my fingers.
I had to admire the motor and controller assembly. The DC motor might
be long and relatively small in diameter, but it is exceedingly torquey.
One end of the armature drives the
mat via a toothed belt and the other
end boasts a plastic, segmented sensor wheel.
What I assume to be an optical sensor straddles the wheel, looking much
like a disc-brake arrangement on a
bike. This sensor monitors the motor
speed and feeds data back to the control panel and/or motor driver.
The motor driver PCB is bolted to
the metal floor of the motor bay on a
solid, right-angled aluminium heatAustralia’s electronics magazine
As the motor can be tested using
a car battery or bench supply, that’s
where I started. I first had to pry the
glue off the connections, then wired
one of my workshop power supplies
directly to the motor.
I dialled in some current and then
gradually raised the voltage until the
motor started to spin. I got up to about
15V, and as the motor was humming
along nicely, I considered it to be serviceable.
Avoiding (for now) the glue-fest that
is the motor driver assembly, I took the
path of least resistance and removed
the upper control panel, which is only
held in with nine PK-type screws.
These are easily accessible from the
underside of the panel and once removed, the whole assembly lifts out
from the top.
And of course, because all the flying leads, sockets and plugs that connect the panel to the rest of the treadmill are dripping with glue, it took a
lot longer than it should. Once free,
though, I could at least take it to my
workbench, making it much easier to
work on.
I’d singled out the data cable from
the motor bay to the control panel
from the loom going up the tubular
frame and found it connected via a
four-pin plug. Two of the wires were
June 2020 63
black and red, so no prizes for guessing where to connect a power supply
for testing!
With 12V applied from my bench
supply, the panel lit up, and all the
familiar displays were working aside
from the main display cycling through
several errors codes (probably relating to the lack of sensor and data connections).
I wasn’t too bothered about what
these error codes meant… yet. For
now, all I needed to know was the display was working, so I reassembled it
temporarily back into the treadmill
and moved on.
Everything so far was pointing toward that motor control board. Removing it was as simple as taking out the
two machine screws holding the heatsink to the deck, and then, of course,
prying all the glue off everything connected to it.
On the bench, I began by removing
the single huge 500µF 450V electrolytic and testing it, simply because it was
the easiest potentially-suspect component to get at. It measured 0.05W ESR
and 490µF on my Peak ESR tester. So
no problem there.
I then removed the semiconductors
from the heatsink so I could more easily reach and test them. All are stacked
side-by-side and clamped to the heatsink with strips of metal and screws
and lashings of thermal grease. There
is a bridge rectifier in a SIL package,
a dual diode array in a TO-220 package and an IGBT in TO3P format, all
clearly identified.
The bridge rectifier tested fine, as
did the diode array, but I couldn’t test
the IGBT with my Peak semiconductor tester. So I had to use the diode
test function on my digital multimeter.
IGBTs are quirky things to test; with
the negative lead clipped to the emitter, and the positive lead on the collector, there should be nothing, until
a brief touch to the gate with the positive lead turns the transistor on. Then
a measurement can be made across
the collector/emitter junction. If the
gate and collector are then shorted
with a fingertip, the junction should
reset, and the meter measure open circuit again.
In this case, the only measurement
I could get on any pin combination,
with any lead polarity, turned out to
be the forward-bias of the fast-recovery diode. Also-called a ‘freewheeling diode’, according to the 18-page
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datasheet, it is connected internally
in ‘anti-parallel’ across the collector/
emitter junction and provides both
faster switching recovery and inductive reverse current protection.
A potential fix
At least now I knew what could be
wrong. After yet more internet searching, I found replacement IGBTs readily available from local suppliers and
AliExpress, with the usual crazy price
disparity.
I also found a vendor on AliExpress
selling replacement boards, identical to this one. Interestingly, they
were meant for Reebok-branded machines in the USA, so it seemed that
there was some badge engineering going on. They were asking a couple of
hundred dollars, which isn’t too bad
considering.
A dead IGBT might be just the tip of
the fault iceberg, and I could be wasting my time sourcing and replacing
it rather than just swapping out the
whole board, which given my lack of
treadmill servicing chops, might also
not be the problem!
But sourcing anything from overseas would take at least two weeks,
and while the IGBTs were available
locally, they cost six times as much as
the parts on AliExpress. But nothing
is being shipped until we are out of
level four lockdown, which will be at
least two weeks away, so we are hammered either way.
And by then we’ll likely be done
and dusted with lockdowns and can
get back to real walking, with the poor
old treadmill being relegated back
to hanging clothes and junk storage.
This is one of those rare cases where I
know what the problem is, but there’s
no straightforward way to resolve it.
It’s a disappointing end to the tale,
but fear not, I shall order a replacement part just as soon as I can and relate whether that did the trick. Fingers
crossed, it will.
Clipsal C-Bus home automation
system repair
About 18 months ago, D. S., of East
Melbourne, Vic purchased a house
with a fairly large Clipsal C-Bus installation controlling all of the lights,
blinds and sundry other things in the
house. It’s a good thing that he is a retired electronic engineer, as it wasn’t
long before the system started to malfunction...
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The home automation system in our
house includes multiple touch panels, many wallplate buttons, motion
sensors etc. When I saw how complex it was after moving in, I decided
to do some research on how the system worked, just in case something
went wrong.
All of the electrical devices to be
controlled are wired back to three
cabinets located next to the switchboard. The cabinets contain a mixture
of DIN-rail mounted main units: three
12-channel relay units and six 8-channel dimmer units.
The C-Bus system consists of an Ethernet-like pink cable that connects in
daisy-chain fashion to all of the control
inputs – switches, motion sensors and
touch panels. All of the input devices
are connected in parallel and are powered from the C-Bus.
Although the C-Bus cable looks like
an Ethernet cable and uses RJ45 connectors, it is not at all compatible with
Ethernet. It uses a single, duplicated
pair and the signalling is superimposed on the DC supply.
The C-Bus power (nominally 35V)
is supplied by some of the units; they
can optionally contain a 200mA power supply, at extra cost. The installer
works out the total power requirements of all the input devices, then
uses the required number of powered
units to meet that requirement, when
paralleled.
Up until recently, the system performed flawlessly, and my tinkering
has been limited to minor reprogramming of the touchscreens for new LED
lights. However, we came home one
rainy night to be greeted by darkness.
Cursory checks showed there was still
power to the house, but the C-Bus system was completely out of action.
A check in one of the cabinets containing the C-Bus main units showed
the C-Bus status lights were all off, indicating a problem with the bus itself.
Two of the 12-channel relay units were
chattering away with their lights blinking randomly. This should have been
a major clue but, you know...
I disconnected the C-Bus cable
from the top of one of the relay units
(which is also the connection to the
upper floor of the house). The chattering stopped, and the C-Bus status
lights flickered back on. So, my immediate thought was that there was possibly a short upstairs, perhaps caused
by the rain.
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One of the two 12-channel C-Bus relay units with its lids off.
I chopped an old Ethernet cable in
half and made up a test plug. With a
meter connected across the data wires,
I checked the C-Bus voltage with only
half the network running (34V) and
with the full house plugged in (10V).
The minimum acceptable voltage is
20V, so, it seemed my hunch could
be right.
However, a resistance check of the
upstairs section showed around 27kW,
which seemed reasonable. Was it
breaking down with voltage applied? I
tried connecting a 27kW resistor across
the bus to roughly simulate the additional DC power loading of the upstairs section, and the system continued to run OK. That eliminated the
Above: the power supply board had failed with two
‘dried-up’ electrolytic capacitors.
power supplies as the problem, or so
I thought.
Anyway, after a fruitless day fiddling with re-connecting parts of the
bus in the upper storey and finding that
the system just became less and less
reliable, I went back to have a closer
look at the power supplies.
The three relay units and two of the
dimmer units have an optional power supply, so I disconnected each one
and tried a 180W test load on them
individually.
Three of the units in the lower cabinet held up well, only dropping a few
volts under load. But the two 12-channel relay units that had initially been
chattering went berserk when the load
was connected, with lights flickering
out and relays clicking.
So, it seemed like the real problem
was that the power supplies in those
two units were faulty, leaving the input devices with only about 3/5 of their
total power requirements.
Looking online, the RRP of these
units is over $1500, so merely replacing them was an expensive option.
A manufacturer’s label showed they
were barely nine years old, so should
have life left in them. They were showing symptoms of dried-up electrolytic
capacitors (a fault which will be familiar to readers of this column!). So
a repair attempt seemed like a good
option to me.
Bench testing the repaired relay unit with a 180W load resistor. This time, the output voltage only dropped from 35V to
29V, as measured on the multimeter.
siliconchip.com.au
Australia’s electronics magazine
June 2020 65
The first challenge was extracting
them from the cabinet. Each unit was
connected to 24 power wires, power
wires for the unit itself plus two C-Bus
cables. Fortunately, there is a circuit
breaker at the end of the DIN rail that
cuts power to the entire unit and its
peripherals.
I wondered how I would keep track
of which wire went where, but the stiff
wires remained in correct alignment
even after they were disconnected
from the unit. Finally, the first unit
was out and on the bench.
The next challenge was opening the
case. The case is in two halves, split
vertically along the middle. There
are clips along the bottom of the case,
with three blue covers clipped on the
top that hold the two halves together.
The blue covers proved to be a real
battle. They slide into vertical channels and have lugs to hold them in
place. However, some genius at the factory had decided to add dobs of plastic glue to make these covers almost
unremovable. It took about an hour
of levering and battling with various
screwdrivers to finally crack the glue
before I could get the covers off, with
some battle scars to both the covers
and the case.
The innards are divided into three
boards: a large relay board, the C-Bus
controller board and a power supply
board. The power supply turned out
to be a simple switching supply with
three output rails.
Visual inspection didn’t show anything amiss, so I started by removing
and testing the mains filter capacitors,
which measured OK.
Next, I removed and tested the 22µF
63V filter capacitors on each of the output rails. The first, which was a little
raised off the board, measured 0nF.
For the second, my Fluke meter read
OL, which is not listed in the manual
as a valid measurement (no, it wasn’t
still charged, or shorted). Anyway, I
assumed this capacitor was bad. The
third capacitor measured OK.
So, it seemed that I had found the
problem. To be on the safe side, I also
removed and tested the three other
electrolytic capacitors on the boards,
but they all tested OK.
So, I ordered six Nichicon PW-series
105°C replacement capacitors (same as
the originals) for overnight delivery,
intending to replace all three capacitors in each unit, on the assumption
that if one lot was bad, the other lot
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Silicon Chip
would be too. Indeed, after battling
through the same difficulty getting
into the second unit, the same capacitor measured 0nF, while the other two
measured OK.
The following morning, the replacement parts arrived, and I soldered
them into the boards. With the units
hooked up on the bench, I used my
test cable and resistor to load them up.
This time, the output voltage only
dropped from 35V to 29V under load
with no relay chatter. I hoped there
weren’t any other hidden problems.
I re-installed the units into the cabinets, re-connected everything and
switched on with fingers crossed.
With some relief, I saw the lights
come back on, and everything was
back to normal.
The two units that failed are at
the top of the upper-most cabinet, so
probably had the highest heat loading. Nevertheless, there are three other units with power supplies which
may also need repair in the future.
I’ve ordered some additional capacitors, just in case.
Sharp R350Y microwave repair
R. S., of Fig Tree Pocket, Qld was not
happy with the price he was quoted for
a replacement module, so he decided
to fix that module instead. That’s often the only economical option these
days, as he explains...
The inverter in our Sharp R350Y
microwave failed. I looked for a replacement, but a new one costs more
than $300. There are some reconditioned ones on eBay for around $100.
I thought that was still too expensive
so I thought I’d have a look at it, to
see if it was repairable at the component level.
I found a copy of the service manual
online which contained the inverter
circuit diagram, reproduced here. The
control unit is shown as a black box.
I’m not sure why since the control ICs
consist of two LM339 quad comparators and one LM324 quad op amp; it’s
not exactly high tech.
The bridge rectifier tested OK. I applied power and checked the gate drive
signal to the IGBT Q110, and it looked
OK. I used a low-cost battery oscilloscope for this, as this circuit operates
at a high voltage relative to Earth. This
IGBT is a Toshiba GT40T321 rated at
1500V, 40A and is available on eBay
in pairs, at around $3 each.
The drive signal to the IGBT from
the control circuit is buffered by a pair
of complementary (NPN/PNP) transistors, not shown on this circuit because
it’s part of the control system.
To be safe, I replaced both gate drive
transistors, the IGBT and the 10W IGBT
gate series resistor. I also checked that
varistor VRS110 (TVR10102) between
collector and emitter of the IGBT was
still connected.
I found that a PCB track to one side
of the varistor had burned off the
board, so I repaired that. The other
varistor, VRS111, is not fitted to the
board, as indicated by brackets on the
circuit diagram.
I also checked for track damage on
the gate connection to the IGBT. It is
probably a good idea to leave the col-
The circuit diagram for the inverter section of the R350Y microwave, the text in
the diagram is so small it can’t be reproduced at a reasonable size, so check the
manual online: www.manualslib.com/manual/677215/Sharp-R-350y.html
Australia’s electronics magazine
siliconchip.com.au
lector of the IGBT disconnected until
you check that the gate drive looks
OK, with square wave pulses of about
15V peak.
It seemed all right, so I reassembled
the microwave, put a glass of water inside and heated it for a couple of minutes. The water started boiling, so that
had obviously fixed it.
You can find the manual for this
microwave at: www.manualslib.com/
manual/677215/Sharp-R-350y.html
Editor’s note: I paid less than $300 for
a brand new 1200W microwave with
inverter control. No wonder so many
appliances wind up at the tip when
replacement parts are so expensive.
Fridge repair from Russia
The “frost-free” fridge which had a broken thermostat.
J. L., of Orange, NSW was visiting
an Australian couple who live in the
far east of Russia and they happened
to mention that their son’s fridge was
not working properly. Being an old
fridge tech, he kindly offered to help...
My friends’ son was expecting the
first addition to his family, so a working fridge was a necessity in a Russian summer. Hence they were about
to buy him a new fridge. But I said I
would have a look at it first, to see if
I could save them the expense. Their
son only lived a few blocks away so
it was convenient enough and we
popped around.
The fridge was a very old Japanese
model which was powered using a
step-up transformer – apparently, the
fridge was made for the Japanese market but ended up in Russia, hence the
different voltage requirements. The
freezer compartment had some cooling, but the refrigerator compartment
had none. The fridge was a “frostfree” design.
A frost-free fridge has a fan which
circulates air through a hidden cooling coil and discharges the cooled air
into the freezer and refrigerator. Frost
forms out of sight on the cooling coil,
which is automatically defrosted several times each day, to keep the coil
clear of ice, allowing the air to circulate.
The defrosting process is initiated
by a defrost time switch, typically every six hours. The defrost timer stops
the compressor and initiates an electric heating element to melt the frost
off the cooling coil. Heating continues
until a small disc thermostat attached
to the cooling coil senses a temperature high enough to indicates all the
frost has been removed (typically
around 6°C).
The heating element then switches
off and the fridge sits idle until the
defrost timer runs out (typically after
30 minutes), allowing the compressor to start again, cooling the coil
back down.
I removed the back panel of the
freezer compartment to check the coil.
The coil was mostly clear of ice, indicating that the defrost system was
working but the build-up of ice at the
top of the coil suggested that the defrost thermostat was terminating the
defrost action before all the ice was
gone.
With a little ice left over after defrost, the ice accumulated more each
day and finally, the airflow became
blocked and the fridge could not cool
anymore.
I tried a non-traditional fix, relocating the defrost termination thermostat to a higher location on the cooling coil, but after a week it was clear
that the ice build-up problem was
fast returning.
Getting another defrost thermostat
proved impossible in the far east of
Russia – we just got that “idiot American” look from the servicemen to
whom we spoke. Even if they had a
thermostat to sell, I don’t think they
would have sold it to us on principle.
On the way home from searching
service stores, the father said he had
a couple of old fridges he was given
to support the family’s work with orphans, but the fridges had died because of city power supply problems.
Could one of these fridges have an
equivalent part that I needed?
After dismantling one old fridge, it
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Australia’s electronics magazine
turned out to be a frost-free style – the
style I needed – and so I went searching for the defrost termination thermostat. The fridge was a Russian-made
model but the principle of operation is
the same everywhere with old fridges,
so I removed the part and began testing
to see if it would do the job.
The test was to soak both thermostats in the freezer compartment of a
working fridge, to simulate normal
fridge conditions. I removed the thermostats to the kitchen table, to gradually warm up, and with an ohmmeter,
I was able to determine that the Russian part needed a higher temperature to open the circuit (and end the
defrost operation) than the original
thermostat.
The actual operating temperature
was not important but the fact that
it was a higher temperature than the
original thermostat was a definite plus.
The Russian defrost thermostat would
mean the defrost element would operate longer than previously and should
ensure all the ice is defrosted.
So I fitted the Russian part into the
old Japanese fridge. Fortunately, defrost termination thermostats are a
fairly standard design, a pre-set bimetal disc around the diameter of a
10¢ coin.
Fitting it was a breeze. I fired the
fridge up and it seemed to work fine
for the remaining week I was in Russia.
Two years later and the old Japanese
fridge has not missed a beat.
It’s a great feeling to have beaten the
odds with some thinking outside the
square to produce a lasting, good result
at no cost. I was the hero for a while
and “the fridge job” still gets trotted
out periodically to visitors!
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