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SERVICEMAN'S LOG
The vacuum cleaner that didn’t suck
Dave Thompson
Anyone who works with particular tools or machines a lot gets to know
how they sound and feel, and so can quickly tell when they are not
working properly. A keen woodworker will know when his table-saw
blade is getting dull simply by the noise it makes when cutting.
An obvious sign of a dull blade is
that it takes a lot more effort than usual to push the wood through the saw,
or that the finish of the cut is not as
good as it should be. But a perceptive
craftsman will know well before that
just because of the different sound the
tool is making.
As a musician, I also tend to notice
melody and rhythm in almost everything. I know the regular rhythm of
our dishwasher when it’s working
correctly, and sometimes find myself
humming along to the harmonic-rich
tone our microwave oven emits when
it’s cooking. If these aren’t operating
correctly, I’ll know.
While this might appear sad or a little weird, it means I can often pick up
when something’s amiss just because
it doesn’t sound normal.
We rent our other house to shortterm tenants, and as I’m the one looking after it, I get to clean it from top
to bottom on average every couple
of days. It’s quite a time-consuming
process.
As a serviceman, I’m always looking for ways to improve how I do this
job, and that includes improving the
tools I use. If I can buy or make something to do things better, or quicker
and easier, I will.
pelled more dust back into the air than
they vacuumed up! While modern
designs and improved filter materials make new models more efficient,
a lot of those older machines don’t
make the cut.
These days a good vacuum cleaner needs to be lightweight, efficient,
clean, easy to manoeuvre and quick to
empty. But models that tick all these
boxes can be surprisingly expensive.
Recently, I started noticing that my
10-year-old Bissell PowerForce Turbo
bagless upright model sounded different and it took considerably more
effort to push around the floor. I also
found that I had to make more passes
to pick up visible debris.
When it was new, this cleaner glided
over all surfaces and just
about sucked the carpet
up with the dirt. While it is tempting
to just throw money at the problem
by buying the most expensive cleaner
on the market as a replacement, this
wouldn’t necessarily result in the best
tool for the job.
We recently traipsed around the
usual stores looking at the wide variety
of new vacuum cleaners and weren’t
that impressed by many of them, especially by some of the prices. The more
we looked, the less inclined I was to
buy new and the more convinced that
I could refurbish our existing hoover
and return it to rude health for far less
than the cost of a new one.
Fixing old faithful
This machine has done us well; the
only problem we had with it before
Vacuum cleaners
are my bag, baby
Aside from the usual aids such as
extendable dusters and good quality
cleaning cloths and agents, one essential appliance is a vacuum cleaner.
Not only does it keep the house free
from dust and dirt, but it also makes
it healthier.
It’s best to use a vacuum with a
HEPA-grade (High-Efficiency Particulate Air) filter or bags. Many vacuum
cleaners I’ve used over the years ex68
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Australia’s electronics magazine
siliconchip.com.au
Items Covered This Month
•
•
•
The suckless vacuum cleaner
An oven tripping the RCD
breaker
Fridge/freezer defrost repair
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
this recent loss of performance was a
blown ‘headlight’ and a broken plastic
height-adjustment assembly.
The latter is mounted under the
power foot. It alters the height of the
brush and air intake above the cleaning surface using a simple mechanical adjuster knob mounted on top of
the foot. The adjustment is meant to
be used when moving from plain to
carpeted floors.
However, I’ve never changed this setting. We have a mix of short-pile carpets
and vinyl floors, and the cleaner works
just as well on both with the knob set
half-way between the two extremes.
This only adds to the irony that the adjuster is the only part that has broken.
I don’t know how it broke; one day
I noticed one of the two 25mm plastic roller wheels that form part of the
adjuster had come away from its axle
mount. The whole assembly is pretty
flimsy, considering the strain it could
potentially be under if one was to lift
and drop the machine to the floor from
more than a few centimetres.
As is typical, the big-box store we
bought the cleaner from doesn’t sell
spare parts, fobbing us off instead to
a vacuum cleaner speciality store.
They didn’t carry parts for it either,
even though this model was widely
sold here. Nice one local stores, and
you wonder why people increasingly
buy online!
I ended up sourcing and buying the
part from Amazon; it only cost about
thirty bucks delivered, so I was grateful I didn’t have to junk the vacuum
for want of a cheap replacement part.
The headlight hadn’t worked for
about half the time we’ve owned the
machine and was dim and next-touseless anyway, which is why I never
bothered repairing it. It is one of those
‘features’ that seems great in theory,
but in practice, appears not very well
thought out.
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Actually, I think a headlight on
a vacuum cleaner is a brilliant idea
(LOL!). Not everywhere we want to
hoover is well-lit, and illuminating
that area can be very helpful. However,
this light is mounted on the base of the
moving handle assembly. So as soon
as I stomp on the pedal to release the
handle from its upright resting position, the whole thing tilts back and
lights up the walls instead.
This actually throws the area in
front of the foot into a contrast shadow.
It would have been better to mount
the lamp on the foot, which always
faces the same way and sits level on
the floor. It makes me wonder whether
Mr Bissell has ever used his own product; if he did, he would have seen in
a flash (pun intended!) how useless
this feature is.
The latest repair
This machine has done a lot of work
over the years, but as it wasn’t some
$99 special to begin with, I would
only consider junking it if I had no
other option.
I noticed that if I removed the hose
going from the cyclone to the power
head, it had good suction. But for
some reason, it just wasn’t ‘on song’
and picking up dirt the way it used to.
I usually either wash its filters in the
washing machine, as per the manufacturer’s recommendation, or simply
blow them clean with my compressor
and air gun. Overall performance is
usually restored after filter cleaning,
but lately, this hasn’t worked as well.
Because replacement filters also
aren’t available locally (noticing a
theme?), I once again hit the Interwebs. I found and purchased a twin
pack of replacement filters and a new
drive belt. It seemed sensible to replace the belt as a precautionary measure, even though I hadn’t checked it
for wear yet.
These parts came to around $50 delivered, a relatively cheap fix if it got
the performance back up to scratch. I’d
much prefer to buy this stuff locally
and support local stores, but if they
don’t bother stocking parts, I can’t.
Despite my servicing history, I have
scant vacuum servicing experience.
So I decided to take everything apart,
inspect all the parts and replace or repair whatever seemed worn or broken.
I would then reassemble the machine
in the hope that what I had done would
fix the problem. While this is a very
Australia’s electronics magazine
cowboy, shotgun approach, it does
usually work.
Dissecting the patient
The PowerForce is an easy machine
to work on; no lame anti-tamper or
purposely-obfuscated screws, just oldfashioned, easy-to-access meat and
three veg fasteners. I stripped this one
down to spare parts in about 10 minutes with one medium-sized Philips
screwdriver and a pair of pliers.
There really isn’t much to it; the
obvious things that could go wrong
are the motor, the filters, the drive belt
for the foot brush, and any bearings or
bushes that could wear out.
With the machine on the workbench, I took a good look at it. Most
of the hard work is done by a highrevving, low torque motor mounted
inside the body of the cleaner, near the
bottom of the tilting handle assembly.
This keeps the centre of gravity low.
Many new models have the motor assembly at the top of the handle, which
in my opinion makes swinging them
around more difficult and harder on
the arms.
Above the motor is the ‘dirt cup’,
the reservoir which collects the debris,
then a clear plastic cyclone separator
assembly sits on top of that. The dirtladen air is sucked from the bottom,
through the ‘foot’ intake, and enters
the cyclone at the top via a flexible
hose running up the side of the handle. There it swirls around due to
the cyclone design, and any dust and
debris (hopefully) drops into the dirt
cup beneath.
The remaining air exits through various filters, which trap pollen and other
pollutants, making the air (in theory
at least) cleaner than when it went in.
All components are easily removable;
the dirt bowl to be emptied and the
cyclone assembly to access three of
the five filters.
There is also a rotating brush in the
power foot. This belt-driven cylindrical brush spans the whole front part
of the foot, just before the air intake,
and runs all the time. But it only makes
contact with the floor when the machine’s handle is moved out of its upright resting position and the power
foot sinks to the floor. It’s a basic but
effective machine.
Repairing the motor
I learned as a boy playing in dad’s
workshop that running vacuum cleaner
March 2020 69
motors without load can lead to catastrophic failure, so I tested this one
using my non-Variac branded variac.
This allowed me to wind up the juice
and check the operation of the motor
assembly. Straight away, I could see a
lot of arcing around the brushes, which
also appeared quite worn down.
On closer inspection, I could see
the commutator had also been worn
smooth. While the motor itself might
be a common enough model, it appears to be built into an impeller and
duct assembly specifically designed to
fit this machine, so simply swapping
one from another type of cleaner isn’t
an easy option.
This motor also has a longer shaft
protruding from the rear for driving
the foot brush, so swapping out an
armature from another motor isn’t viable either.
Back in my aircraft engineering
days, I refurbished a lot of motors.
That typically meant replacing brushes and overhauling the commutator
section of the armature as part of the
process. Because many vacuum cleaner motors are similar, I hoped finding
replacement brushes wouldn’t be too
difficult.
I removed the clamps holding the
brush holders to the motor frame and
eased the brushes out. I took them to a
local appliance repair centre and asked
the guys there (who all have incredible
product knowledge) whether they had
anything like them in stock.
One guy came back with a few different types, which we compared on
the counter, and I bought a set that was
very close to the original’s dimensions.
While the carbon composition might
be different – ie, the brushes might
be harder or softer – I didn’t have the
luxury of choice so they’d have to do.
Back at the workshop, the new
brushes fit neatly into the brush holders, and while they were probably a little longer than the originals, there was
plenty of room in the holders.
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Silicon Chip
The commutator was trickier. It was
easy enough to get out, but I couldn’t
find any information online about the
depth of commutator undercut, or
even if there should be any in these
motors. However, I could see by the
unworn part of the commutator, where
the brushes hadn’t been contacting it,
that it was originally slightly larger
in diameter and that these segments
were undercut.
I’d have liked to have mounted the
armature in a lathe and skimmed it
flat, but there wasn’t a lot of meat left
in the copper, so I made do with handrubbing it with 180-grit wet and dry
sandpaper just to clean it up a little.
I broke off a piece of a junior-hacksaw blade and wrapped lots of tape
around one end to create a crude handle. I held the armature carefully in my
bench vice and used this make-shift
cutter to go around and ease out the
areas between the commutator’s copper sections, being very careful not to
slip and gouge any of the faces.
Once I’d gone right around, I then
cleaned up the copper again with
sandpaper to knock off any sharp
edges I’d created. Leaving them rough
would chew the brushes out very
quickly.
I reassembled the motor, checking the sealed bearings at each end of
the armature at the same time. They
seemed OK, and the armature spun
quietly and smoothly by hand. I powered it up and tested it; this time there
was minimal sparking and it sounded
great, so I considered that job done.
While it was all apart, I looked at
the headlight. The 12V, 11W bulb
had blown. I rummaged around my
bits boxes and found a 20W version;
bigger is better, right? The shiny tape
reflector behind the bulb had partially
peeled back; a few dabs of superglue
had that secured again.
Australia’s electronics magazine
The roller’s drive belt and bearings
were next. The new belt was smaller
and more pliable than the old one, so
it turns out that it did need to be replaced. I spun the roller in my fingers,
and the bearings ran smooth and quiet.
I also took the opportunity to remove
all the long hairs and threads that always seem to wrap themselves around
these brushes.
As I reassembled everything, I
cleaned anything that looked dirty,
removing years of built-up dust and
trapped hairs. I found the centres of
the main wheels had slogged out, so I
cut some small strips of Teflon sheet
and wrapped them around the axles
before putting the wheels back on.
I’ll eventually have to do something
more permanent, but that’s a repair
for another day.
I installed the new filters, plugged
the cleaner in and tried it out on the
workshop floor. The difference was
remarkable; not only does everything
run much more smoothly, it is quieter,
the suction more powerful and the
motor sounds like it used to, all for a
fraction of the cost of a new machine.
The only thing that left me baffled
was, despite having stripped down
and disassembled the whole machine,
even though this is the “Turbo” model,
I never actually located its turbocharger. How strange!
Oven tripping RCD
J. L., of Toowoomba, Qld, had a very
frustrating (and intermittent) problem
with his oven tripping an RCD. False
tripping of RCDs is unfortunately a
common problem, but in this case, the
cause turned out to be a bit unusual
and unexpected. This is
how he figured it out...
A couple of years
ago, our fairly new
wall-mounted oven
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started tripping the RCD on higher heat
settings, typically around 220°C. This
usually only occurred when the oven
reached that temperature, so I surmised that it was happening when the
element was switched off. The tripping
was only occasional, ie, “nuisance
tripping”, but it became more frequent
over a year or two.
I tried the usual approach: turn off
every appliance on that circuit, then
switch each one on in turn and see if
the RCD would trip. I started with the
usual suspects: fridges and dishwashers. The results were mixed. Every
time I thought I’d identified the culprit,
it would trip again without that appliance switched on, or even plugged in.
This was becoming very frustrating,
as each test required heating the oven
to a high temperature.
Eventually, it was decided that a
‘proper’ service agent had to be called.
In due course, he arrived and tested the
oven temperature, ramping it up slowly – which was precisely the condition
under which the RCD would not trip.
He determined that the oven should
be on a separate RCD and charged us
a $100 call out fee.
Since this did not seem very helpful, I tried another approach. The RCD
itself appeared to be the same model
but older, than another in the same
dwelling so I swapped them. But that
didn’t help. So I tediously repeated
the appliance removal tests.
In the meantime, I built the SILICON
CHIP Earth Leakage Tester (May 2015;
siliconchip.com.au/Article/8553) to
check the various appliances, and this
worked as expected. Some, such as
a dishwasher with ‘soft’ on, showed
leakage of the order of 1-2mA when
switched on at the wall but with the
appliance off. This is not enough to
trip a standard (30mA) RCD, even with
several such appliances in-circuit.
The next and most obvious culprit
was the oven element. I thought this
unlikely, but I know that elements can
lose their insulation over time (especially if liquid is spilled on them),
and can eventually trip the RCD. The
only solution then is to replace the
element.
I removed the oven element, measured the resistance to work out its
nominal power, and the dimensions
of the attachment plate. After a week
or two of unsuccessful searching, I
decided that we could ignore the element for now, since I could not find
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a replacement through the usual suppliers or even overseas, and that I
had no proof that this was actually
the problem.
So then I thought back to what had
changed since the oven used to work
normally. Then I suddenly realised
that the rangehood extractor fan over
the stove top had never been turned
off during my tests, since it has no
separate switch (I wish it did). It has
a pushbutton to turn on lights and a
fan, but I had the impression that this
was done via a controller board.
Then I remembered that shortly af
after the rangehood was installed, it was
repaired under warranty. And some
time after the repair (which I think involved replacing the main controller
board), the halogen lamps exploded
(thus ruining a meal). I had noticed
that these two lamps ran very, very
hot, and that did concern me. So the
halogens were replaced with LEDs,
which ran much cooler.
But that led to another observation:
a faint glow from the LEDs at night
time. I found this strange, but did not
get around to investigating it, and put
it down to stray capacitance or inductive coupling.
I removed the LEDs and replaced
them with another brand of LED, and
the faint glow also went. This initially
appeared to solve the oven tripping
problem, and it was put down to cheap
LED drivers. But alas, the problem
returned.
I then replaced the LEDs with halogens, and the problem disappeared.
But by now I was thoroughly perplexed. Removing the lights altogether
also stopped the oven tripping. Testing
the light fittings with a non-contact
tester revealed a curious and worrying scenario; there appeared to be
mains voltage at the socket with the
light turned off, but no voltage when
the lights were turned on.
A few days later, suddenly it
dawned on me that the mains wiring
was almost certainly reversed; Neutral
was being switched, rather than Active. That would explain the faint glow
of LEDs in the night, with perhaps a
few milliamps being inductively returned through Earth.
When time permitted, and after suitable safety precautions, I removed the
covers from the rangehood controller.
The controller is a small box about 90
x 60mm, located in the exhaust path,
visible when the grilles are removed.
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MARCH 2020
71
Upon opening the cover, my theory
was confirmed: Active (brown) was
wired to N (Neutral) on the PCB via
a screw connector, and Neutral (blue)
was wired to L (for Line, which I think
is the terminology used in the USA for
Active). This is precisely the opposite
of what it should be, and confirmed
my suspicions.
This should have been a quick fix,
and the end of the matter. However,
upon carefully unscrewing the PCBmounted connector, it seemed to be
quite loose. This worried me, given
that it was connected directly to the
mains. Perhaps excessive force had
been used in the previous repair to
tighten the screw, or perhaps it was a
cold solder joint, or both.
So the unit had to come out, which
entailed removing connections for the
mains, the motor, lights, and an IDC
connector for the switch panel.
I managed to resolder the connector easily enough. However, I was not
happy with the fuse arrangement. It
was one of those barrel-type fuses,
with a connector on the side and at
the end. The soldering on these was,
in my opinion, poor.
But worse, the exposed metal meant
that when the cover was replaced, the
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live parts on the fuseholder would
be close to the main board and
other terminals. That was
fixed by resoldering the
fuse connectors and applying heatshrink tubing
to both exposed
terminals.
Upon reinstallation, I noticed that the
push-on light
connector had
one wire connected by a copper
strand. This was
not visible before,
as it was shrouded in
plastic. I replaced this
with a PCB-mounting
screw-type connector,
as I thought it would be
much more robust. The
motor connector terminal
also had a dry solder joint,
like the mains connector.
In all, I had to take the
PCB out three times to fit
new sockets and resolder
dry joints. This was all complicated by one “recycled”
connector which would not accept a
wire. This sounds trivial, but remember that reinstalling the controller requires one to have their head in the
rangehood itself, bent over a stovetop,
and twisted around. The non-compliant connector was high up and difficult to access.
Also, some of the mains wires had
been tinned before being inserted into
the screw terminals. I don’t think this is
good practice, as it necessitates a tighter
turning of the screws to obtain a good
mechanical contact, and that could be
why the connector came adrift.
Furthermore, temperature and time
can make the solder flow, leading to a
loose connection. So I cut off the ends
and re-stripped those wires.
Eventually, all was reassembled and
checked, and everything worked perfectly, even with LED lights. Most importantly, the oven no longer tripped
the RCD. But I was unhappy to have
to do all this work when the board
supplied with the rangehood should
have been built to a better standard in
the first place. It came in what is supposedly an up-market kitchen fitting.
So I surmised that a small leakage
current was always flowing due to
the reversed polarity of the controlAustralia’s electronics magazine
ler. This reversal did not affect the
operation of the unit as such, but it
did mean that the external lamps were
always at mains potential. This in itself was not enough to trip the RCD,
but apparently, it was when combined
with the high current pulse at oven
switch-off.
It puzzled me why the unit was incorrectly wired. Perhaps the installer
did not know the difference between L
and N. Perhaps the installer did know,
but didn’t care because it worked anyhow. So beware of incorrectly wired
appliances and sockets – I have subsequently heard of people switching off
appliances, but not unplugging them,
and receiving a shock due to similar
wiring problems.
Fridge/freezer defrost repair
T. M. retired from the refrigeration
industry a few years ago and after 40
years working with commercial refrigeration equipment – he knows a thing
or two about fridges. He never liked
working on domestic units but faced
with warm beer, he had no choice but
to delve into such a repair. It was an
interesting experience, as he narrates...
I noticed the temperature in the
fridge side of our 10-year-old Whirlpool two-door fridge/freezer wasn’t
quite what it used to be. I had set the
temperature on the front keypad to
4°C but a measurement indicated that
it was actually 9°C!
I used a datalogger to check the temperature over the next couple of days
and it was gradually getting higher. But
the freezer seemed to be working fine,
maintaining around -16°C.
My first thought was that the motorised damper that allowed the cold air
from the freezer into the fridge was not
opening. This damper opens/closes to
allow cold air from the freezer section
into the fridge, maintaining the desired
temperature. But on inspection, the
damper was fully open but there was
minimal airflow into the fridge.
Air is channelled from the freezer by
a fan located above the finned evaporator, which also circulates air in the
freezer. I could hear the fan running
so this was not the culprit; it was evident that the evaporator was iced up
and after removing several panels, that
proved to be the case.
But this is a frost-free unit so that
should not happen. A frost-free system works by automatically defrosting
several times a day, thereby preventing
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ice buildup. The resulting meltwater
is channelled away into a tray in the
bottom of the fridge to be evaporated;
usually, the hot discharge piping from
the compressor passes through the tray
to accomplish this.
My next thought was that the defrost
element was faulty but a resistance
check gave a satisfactory reading for
a 750W element.
The next possibility was the defrost
thermostat (or “Klixon”) attached to
the evaporator. This has normallyopen contacts when warm, closing
when cold. It’s a mechanical safety device that terminates defrosting, should
the controlling defrost timer device
fail, thus preventing a mini Chernobyl!
This also tested good, however, I
was somewhat mystified by this encapsulated device as it had six wires
coming out of it; usually, only two are
required to perform the safety function. I identified the two wires that
were open when warm. So what were
the other four wires for?
These remaining wires were attached
to the fan and a multi-pin plug that
exited from the freezer compartment
and went down to the controller PCB.
I thought there might be a problem
with this board, as I expect the compressor and evaporator fan to switch
off for several minutes each time the
unit performs a defrost cycle and I was
not observing this. Nor could I measure
any voltage across the defrost element.
A fault with this control board
would be bad since it doesn’t lend it-
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self to component replacement due to
a heavy coating of resin.
I searched the web for information
relating to the control electronics
without success. A large local supplier of Whirlpool spares said that
replacement control PCBs were no
longer available. I finally located what
I thought was a replacement on a UK
website; it looked identical but had a
different part number and at a price
of £260 plus freight, I wasn’t about to
chance it being compatible.
I decided to modify the fridge instead to control the defrost cycle independently of the fridge electronics.
This could be done quite easily with
a mechanical defrost timer but I prefer
using a programmable controller that
gives me more options for controlling
the cycle instead of just on/off.
I have quite a collection of refrigeration parts in my workshop, including
a few such controllers.
The replacement seemed a simple
task. I would allow the fridge electronics to manage everything other
than defrosting. I would program the
controller set point to a very low (unachievable) temperature, then I would
connect a double-pole relay to the controller’s compressor output terminal.
This relay would remain energised at
all times except when defrosting.
The compressor and the evaporator
fan would be wired through the NO
contacts of that same relay and therefore the normal operation of the fridge
would be controlled by the fridge onboard electronics, which from time to
Australia’s electronics magazine
time would try to defrost it for a short
time with no result.
When my controller entered the
defrost state, it would open the relay,
thus halting the compressor and the
evaporator fan and enabling the inbuilt
controller defrost relay which was now
connected to the element via another
two-terminal defrost Klixon I fitted. The
original Klixon was left in place due to
the mysterious four additional wires;
the two wires originally connected to
the element were disconnected.
The added controller was mounted
on the back of the fridge in a position
that allowed the display to be easily
observed and the buttons accessed for
fine-tuning.
But when I fired up the fridge, nothing happened other than the display
showing the previous set points for
the fridge and freezer. It should have
entered the alarm mode due to the
high cabinet temperature. What was
going on?
It seemed that the fridge electronics
would not initialise after I had made
my changes. The only change I had
made from its perspective was disconnecting the defrost element from the
original Klixon, so I tried reconnected
it and the fridge fired up.
The control PCB likely performs a
diagnostic check at power-up and if
the defrost element is open-circuit,
it refuses to continue. But hang on a
minute, I thought, if it was correctly
sensing that the defrost element was
OK, how was it not able to drive it?
Anyway, I decided that the best
course was to try to trick the control
board into thinking that the defrost
coil was still connected, even when
it was not (so that the added control
board could drive it instead). I decided
to try connecting the coil of a 230V
AC-powered relay as a dummy load.
Eureka! The fridge powered up and
operated normally. I guess the control
PCB isn’t that fussy about the actual
resistance between those two wires,
as long as it isn’t very high; the relay
coil has a resistance of around 3.8kW
compared to the defrost coil at 80W.
But that was enough to fool it and so
I left this relay permanently wired up,
in the back of the fridge.
Everything is now working fine,
with my added controller managing
the defrost cycle as required. I made a
few adjustments over a couple of days
to optimise the defrost timing and it’s
now working normally.
SC
March 2020 73
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