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SERVICEMAN'S LOG
A shed full of tools
By Dave Thompson
I love tools, and I’m not ashamed to admit it. Ever since I was old enough
to understand what was going on, I enjoyed going through dad’s array of
tools and admiring their form and build quality. I learned early on that
having the right tool for the job (and the skills to use it) meant you could
accomplish pretty much anything.
Dad also instilled in me the benefits
of tool quality. By the time I joined the
airline as a wet-behind-the-ears apprentice, I already had what I thought was
a decent tool kit, but it was nothing
compared to the tools they issued to us.
I got most of my tools during the
first six months, but others came my
way over the following years, usually when posted to a new section that
required more specialised tools. For
example, the instrument workshops
used a vastly different toolset than the
radio/radar shop or when working on
‘the line’ on the airport apron, turning
aircraft around.
All were the best money could buy
at the time, and probably still are. So
even though we were paying for our
tools by way of a small amount taken
from paycheques over the following
years, they seemed like a gift from
God at the time.
Thirty-six of us started at the airport on the same day, all ‘engineering
apprentices’, so we were issued the
same set of basic tools. After three or
so months of common training, both
practical and academic, six of us split
off from the pack and began our own
curriculum, learning more avionicsspecific stuff.
So I had a lot of tools I never ended
up using on an actual aircraft, but rest
assured they’ve all been put to good
use anyway! I still have the vast majority of these tools 40 years on.
You’d think that having mainly imperial sockets and spanners would
be a hindrance (the majority of aircraft I worked on were British or
American). But the fact I
grew up driving
mostly British cars meant that I still
used them regularly.
Only the finest for me, please
One of the downsides is that this
made me somewhat of a tool snob;
I scoff at the cheap socket
sets and spanners
for sale at
Items Covered This Month
•
•
•
•
•
•
The toolshed
The intermittent audio analyser
RF interference, part deux
LED lamp repair
LED motion lamp modification
Induction cooktop repair
*Dave Thompson runs PC Anytime
in Christchurch, NZ.
Website: www.pcanytime.co.nz
Email: dave<at>pcanytime.co.nz
46
Silicon Chip
Australia’s electronics magazine
siliconchip.com.au
the local motoring shops. After all,
buying cheap tools can actually cost
more in the long run, not only from
having to replace those tools when
they wear out (soon!), but in lost productivity as well.
How many of us have purchased a
set of screwdrivers only to twist the
handle off the first time we used them?
Or stripped the Phillips heads round
trying to undo a stubborn screw? They
can be just a complete waste of money.
Almost all the screwdrivers, spanners, hammers and sockets I own were
issued by the airline or purchased
years ago, and because I avoid using them for purposes they weren’t
designed for, they are still as good
as new.
I once purchased an expensive,
high-quality set of screwdrivers as a
gift for a family member, thinking they
would appreciate it. When visiting a
few months later, I was horrified to see
all the drivers bent out of shape; he’d
been levering his car engine out with
them – or at least, trying to! I guess
there’s no helping some people.
Dad also gave me some of his tools
when he no longer needed them. I
don’t do a lot of machining, but if I ever
take it up, I will never have to buy any
reamers, cutters, clamps, vices or dial
gauges. And I have enough drill bits
of various sizes to use each one once
and then throw it away!
I also inherited an excellent engineer’s benchtop drill press, to which
dad had made some modifications.
Most drill presses of this type suffer
from at least some float in the quill assembly (the part of the machine with
the spinning chuck which goes up and
down). As a general rule, the cheaper
the drill press, the more play it has
and therefore, the less accurate it is.
My own expensive pedestal-mounted drill press, which I used to make
everything from project chassis to furniture and guitars has minimal play in
the quill, but it’s still a lot compared
to dad’s.
Everything else, such as the nozzles,
combustion chambers and fuel tubes
had to be fabricated. I recall him experimenting with various materials
and custom-made tools, with varying
degrees of success.
Due to the size of some of the parts,
he faced many challenges, and soon
discovered that some of his tools were
not up to the job.
He fashioned the fuel tubes for his
engines from specially-made 1mm
brass tubing. He had to drill a series of
tiny holes at exact increments around
these tubes; using a large drill press
to do this job was far from ideal. He
even had to make a chuck to hold the
tiny drill bits.
He soon found out that even the
minimal play in the quill on this machine prevented him from accurately
forming the holes. So he machined a
whole new quill assembly and mounted it in high-spec bearings. With a
dial indicator stuck to the bed, even
if I lean on the chuck in any direction
with the quill at its lowest extended
reach, I can barely get the indicator
pointer to budge.
It was therefore a ‘no-brainer’ to
make this my primary drill press.
Even though I don’t do anything that
requires such high precision, it is good
to know I have it.
I also inherited all the tiny drills
dad used, and though I’ll likely never
use them, I have them just in case (the
tool-owner’s mantra!).
This sums up my tool philosophy:
buy (or otherwise obtain) the best
quality tools you can afford,
and they will likely never
let you down.
Disaster strikes
However, after moving dad’s drillpress from our old place to my current
workshop, it just wouldn’t go. There
is nothing worse than needing a tool,
and it doesn’t work (or isn’t sharp).
I knew it had power because the
built-in lamp turned on when the light
switch was toggled. So there was either a fault in the motor circuit, or the
motor had failed.
While used ¼ and 1/3 horsepower
motors are a dime a dozen on local
auction sites and can be (relatively)
inexpensive, anything new or rated
above that starts incurring a hefty premium. I don’t think the ½ horsepower
motor mounted at the top rear of the
drill press is the original; I have vague
memories of dad telling me he’d upgraded it.
Even though the mounting system
allowed for various sizes of motors to
be fitted, I’d like to stick with the larger
motor if possible.
But before ordering a replacement,
I had to determine what was going on
with this one. I had to work on the
drill press in-situ; it took two of us to
heft it into its current position on the
workbench. However, I could lie it
down by myself if necessary.
Desperately seeking solutions
The first thing I did was to ensure
that the chuck, the three pulleys and
two belts in the drivetrain were moving freely. This was simply a matter
of turning everything by hand and
Dad’s special tool requirements
As I’ve previously written, dad
made small-scale gas turbine engines
for model aircraft. This was long before
you could just go out and buy one. He
had to build most of the components
from scratch, but he used a modified
car turbocharger housing and its bearings and impellors as the basis of the
engine.
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Australia’s electronics magazine
May 2020 47
judging the amount of pressure required to move it.
If something had jammed the mechanism, I imagine that the motor would
sit there and try to turn, or complain
loudly, but I would be remiss if I started tearing into the guts of the machine
without at least checking for freedom
of movement first. It all turned easily
and smoothly, so that wasn’t it.
The next thing I looked for was
a popped thermal switch or circuit
breaker. Many motors, especially of
this rating or higher, have one of these
safety cut-out devices built-in. This
push-to-reset type switch is usually
found on the end of the motor housing, near the terminal block, or in some
cases near where the power cables enter the motor.
These are either a simple circuit
breaker, which will open if too much
current is drawn, or a thermal-magnetic type device. They essentially do
the same thing; cut power to the motor should a fault arise or if the motor
is stalled or overloaded.
I pushed the breaker button on my
motor. Even though it didn’t feel as
though it had popped, I tried switching on the motor again anyway in the
vain hope of that being the problem.
No such luck; it was not a simple
breaker activation.
I then removed the motor’s flat
metal terminal block cover, exposing the power connections underneath. Everything looked fine, with
no loose wires or wayward terminals.
I plugged it in and measured the voltage with my multimeter anyway, just
to rule out something in the power
plug and lead.
Many a device has been stripped
down to spare parts, only to discover the problem was a broken or loose
mains plug wire. I would never do
something as silly as that, though! No,
I wouldn’t waste hours and hours disassembling and reassembling a device
with a simple fault that I should have
looked for before starting, all the time
cursing my own stupidity… Ahem,
now, where was I?
All measured as expected at the motor terminals, so I unplugged it again
while I probed further.
The next step was to check the motor start capacitor. I’ve had several of
these fail over the years, but as they
are generally reliable devices, I didn’t
give it much chance that this would
be the problem either.
I disconnected the terminals coming
from it, made sure it was discharged
(using a discharging wand – not a
screwdriver!) and used my multimeter to make sure it wasn’t obviously
shorted or open circuit.
For the sake of thoroughness, I also
used my capacitance meter to check
the value, and it was within about 13%
of the stated value on the case (25µF).
So it wasn’t going to be the cause of
the problem either.
The fault could also be in the centrifugal switch inside the motor, but I
left that option for last resorts, as fixing that would involve removing the
motor and stripping it down.
Safety first!
Instead, my next step was to check
the switch assembly at the front-right
side of the machine. My old drill press
has a simple on/off toggle switch on
the front of the tower, though it does
have one of those red plastic switch
guards on it, like you get on military
equipment or aircraft. The idea is that
in a panic, it can be simply hit with
a flick of the hand and switched off.
Dad’s machine has a much better
NVR (No Volt Release) style switch
with separate on and off buttons, along
48
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Australia’s electronics magazine
with a paddle-off arrangement. I don’t
think this is original equipment, as
the switch housing appeared to have
been enlarged to accommodate the
bigger NVR switch’s footprint, so I’m
guessing dad retrofitted that version
at some stage.
NVR switches are ideal for machinery because when the tool is plugged
in, no matter the on/off switch’s position when it was turned off, the machine will not start until the “on” button is deliberately pushed.
You can imagine the potential for
carnage if, for example, a bench saw
was left switched on and was simply
turned off at the wall, then someone
comes along and turns the wall switch
back on (or plugs it in) without checking the switch status, and the thing
starts up. NVR switches prevent that
from happening.
A further safety accessory on some
NVR switches is a wide plastic paddle
that hinges at one end of the switch
housing and rests above the “off”
switch. This means that if you need the
machine to stop, you can just bang on
the paddle. Because it is much larger
and far more visible than the actual off
button, it is much easier to find and
requires less physical accuracy to shut
everything down in an emergency.
Therefore, I consider an NVR switch
a worthwhile upgrade to any machine
(and clearly, so did my dad).
Four screws held this switch’s
mounting panel to the body of the
drill press. Immediately after pulling
the panel away, I could see a problem;
one of the wires was hanging literally
by a thread. Unfortunately, the thread
was not a conductive strand of wire,
but a piece of the fabric wire insulation
trapped under the terminal.
This almost certainly accounted for
the lack of motor power, and explained
why the lamp, which is switched separately, still worked.
The problem I had now is that these
wires were very short and I had almost
nothing spare with which to re-terminate the wire. I traced the wire back
through the body of the drill press to
where it connected to the motor, and
noted that it was part of a bundle that
shared an insulation sleeve. Pulling
a single wire through wasn’t a problem, but putting one back through
could be.
I ended up soldering a new length
of wire to the existing one and simply
pulled it all through until the old one
siliconchip.com.au
was out, and I had two new ends in
place, ready for the terminals.
After connecting the terminals to
their respective lugs, I plugged in
the mains cable and with no belts
engaged, tested the motor. It spun up
and ran smoothly. Reassembly was
a doddle, and the machine is ready
for another 30 years of no-doubt reliable service.
The (intermittent) return of the
UPL audio analyser
A. L. S., of Turramurra, NSW, ran
into an odd problem in an expensive
piece of test equipment. And unfortunately, it was one of those dreaded
intermittent faults. Luckily, he managed to fix it, and saved thousands of
dollars in the process...
I purchased a second-hand Rohde &
Schwarz UPL DC-110kHz audio analyser a few years ago, at a fraction of
its original price (which is in the tens
of thousands).
In the June 2018 issue (pages 62-63;
siliconchip.com.au/Article/11104), I
described the problems that I had with
it due to its CR2032 memory back-up
battery going flat and the difficulty in
finding and replacing that cell. After
that, it worked really well, until recently, a new and rather strange problem emerged.
Now and again, this device would
start up as usual, pass the self-test and
revert to its previous test setup. But
the image on the screen was inverted!
The image was beautifully bright, with
accurate measurements displayed, but
you would have to stand on your head
in front of a mirror to read it! Eventually, if left to warm up, the display
would come good.
This analyser was a real find because
it had eight factory options, including
low-distortion generators, jitter and interface tests and mobile phone acoustic testing analysis. Its specs are really
impressive, and it analyses an incredible array of audio signals, including
digital audio signals.
As you would expect for this type
of fault, it grew worse over time, and
the screen would sometimes invert unexpectedly. It became annoying when
setting up audio tests because I had to
wait some time for it to warm up before I could use it.
Looking in the “basic” UPL operating manual, which is 462 pages, I could
find nothing concerning this fault. I
couldn’t even find a service manual on
siliconchip.com.au
the internet, which was discouraging.
But because of its relative youth and
its complexity, I decided to approach
Rohde & Schwarz again for repair.
I rang them first to see if it was repairable in Sydney because they are
very close to my home, but they said
that this was not possible. They would
have to send it off to Germany to get
a quote, and this would cost approximately $1400, with no guarantee that it
could be fixed. To make matters worse,
I was told that this instrument was no
longer supported, and parts may not
be available.
I’m not complaining though; I understand that they are just trying to
cover their costs. This is one of the
most complex instruments I have
ever used.
Anyway, I wasn’t going to spend that
much money just for a quote, so I soldiered on despite this fault, until one
day it dawned on me to see whether
printing the screen when it was inverted would show the same fault.
As it happens, the instrument has
a parallel output port. I have a device
called “Print Capture” which I connected to a small laptop on top of the
instrument, to save screen dumps.
I figured if it still printed screenshots correctly when the display was
mirrored, that might give me a clue as
to the origin of the fault. So, I waited
for the fault to appear, then quickly
pressed the hardcopy button. Unfortunately, during the two-minute download, the fault disappeared. So I had
to wait again for the fault and do it
all over again. Finally, the hardcopy
printed, with a perfect image!
That meant that the fault was down-
stream of the CPU and must be between the mainboard and the screen.
I then had another idea – to connect a screen to the VGA port on the
instrument. If that worked, perhaps
I would not have to worry about the
screen inverting on me in the middle of a test.
All I could find in the workshop
at that time was a small Panasonic
television with a VGA input, so I set
that up. When the fault eventually
re-appeared, I fired up the monitor
and got a perfect image on the screen.
This meant that at least I could use
the instrument without interruption,
but it was a bit unwieldy because the
TV was big and difficult to mount.
These symptoms confirmed that the
fault was not on the mainboard nor the
CPU and must be isolated downstream
to the display screen and its associated circuitry.
I then developed a plan to remove
the front panel assembly, so I could
take out the suspect screen and get
the part number from it. I would then
buy a new screen and replace it, and
hopefully, that would fix it. If the fault
still existed, I would then need to trace
the fault back to the PCB which fed
the display.
This seemed like a good plan, but
it did not go smoothly. For a start, the
front panel was an integral part of
the chassis, and I had to undo lots of
screws to remove it.
Then I found that there was a brittle ribbon connector that I was very
reluctant to remove, meaning that I
could not completely remove the front
assembly without doing some permanent damage.
The UPL audio analyser initially displayed the screen inverted when turned on,
but would return to normal after ‘warming’ up.
Australia’s electronics magazine
May 2020 49
Thirdly, Rohde & Schwarz had
thoughtfully removed the part number
from the back of the screen, so I could
not buy a new one with confidence.
So rather than cause any permanent
damage to an instrument which was
working well, I decided to backtrack
and put it all back together, and just
resigned myself to using it with an external monitor.
In doing so, I noticed that one of
the connectors I had to plug back in
was sticky, so I pushed it home, and
it clicked in beautifully with the retainer clips. But then I remembered
that one of those clips was only halfway engaged when I disconnected it.
Putting it all back together was tricky
because there was an Earthing spring
shaped like a hairclip. I cleaned this
to make sure it would make good contact, but it had to be held in place while
some screws were inserted. Each time I
tried to do this, the screws were flung
out all over the floor. But I persevered
and eventually got it all back together.
This is such a delicate, complex
and expensive instrument and I was
very nervous about powering it back
up, but it came up OK, with a normal screen. And it has never inverted
since! A miracle?
This left me a bit puzzled. Was the
fault due to that connector not being
locked in properly? Or perhaps cleaning the Earth spring helped? All I know
is that I am happy to have it working
correctly again.
In retrospect, I realised that this
problem sometimes occurred when
there was some vibration in the workshop. I also remember it happening
when some of the buttons on the front
panel were pressed. So I suspect that
the Earthing comb had tarnished and
was occasionally losing contact and
upsetting the display.
RF interference at the end of the
rainbow, part deux
Regular readers of “The Serviceman’s Log” may recall the story from D.
P., of Faulconbridge, NSW in the May
2019 issue (p64). It was about a pager
signal that was producing interference
on amateur radio VHF frequencies in
the Blue Mountains, NSW. They managed to track down the source and get
it fixed. Now he’s at it again...
Encouraged by our success with
the pager interference problem, Blue
Mountains Amateur Radio Club members decided to tackle another interfer50
Silicon Chip
ing signal which had been bothering
us for quite some time. This interference was again on the amateur VHF
(2m) band.
It no longer triggered our repeater
since the repeater had been fitted with
a tone squelch system, but it did disrupt its operation while it was actually
in use. It also interfered with simplex
operations, and with the reception of
other repeaters on the band.
The interference took the form of a
strong carrier modulated with a noisy,
randomly varying and hum-infested
audio tone. There was no discernible
pattern to the signal, and the modulation seemed to be a mixture of AM and
FM. The signal drifted up and down
the VHF Amateur band, sometimes
disappearing for hours at a time, only
to return later.
Monitoring the signal with a generalcoverage VHF receiver, we found that
during the times it was absent from the
amateur band, it had merely drifted
into other bands, potentially causing
problems for other services. As far as
we could tell, the signal was present
24/7, moving around the VHF spectrum seemingly at random.
Various services in the Mountains
use VHF communications, including
aircraft working on rescues and bush
fires, and the Rural Fire Service and the
National Parks and Wildlife Service,
during bush fires and search-and-rescue operations. This signal could potentially interfere with these activities.
This interference could be heard
over a wide area, with widely varying signal strength, giving no clue to
its location. Attempts to triangulate
the source had produced inconsistent results, with bearings that did not
intersect.
The technique I had used with the
pager interference, of monitoring the
signal in my car while going about my
normal activities, was impractical in
this case because a second operator
would have been needed to keep the
receiver tracking the interfering signal
as it drifted in frequency.
Our first thought was that the culprit could be a ‘dirty’ switch mode
power supply (SMPS), but it was detectable over a much larger area than
could be accounted for by a single device. Could it be an SMPS propagating
over a wide area by being conducted
over mains power lines? That seemed
a bit unlikely.
Another idea was that this could be
Australia’s electronics magazine
something to do with the railways. The
Blue Mountains are crisscrossed by
“traction feeders”: large three-phase
power lines which feed rectifiers, situated in sub-stations in various locations throughout the Blue Mountains,
to provide 1500V DC for trains. This
is an extensive, heavy-duty network, a
legacy of the days when electric goods
trains operated on the Mountains.
Electric locomotives were abandoned some years ago in this area in
favour of diesel-driven locomotives. A
bad idea, it seems to me! The electric
locomotives, when travelling down
the Mountains, used regenerative braking, which put enormous amounts of
power back into the network.
It was said that a good proportion of
Sydney’s passenger network could be
run by the regenerative power from a
goods train with a full load as it drove
slowly down the Mountains.
Anyway, our club was keenly involved in “fox hunting”, so many of
us were kitted out with mobile yagis,
receivers with input attenuators, “sniffers” (small hand-held receivers which
are used in the final stages of locating
the “fox”) and various other bits and
pieces.
I should point out that in the Amateur Radio fraternity, “fox hunting”
refers to the activity of searching for
hidden transmitters. It does not typically involve horses, packs of dogs,
pink coats or hunting horns!
Without any better ideas, we decided to have another crack at triangulating the signal. We thought that the previous inconsistent results could have
been due to propagation changing as
the signal frequency drifted, because
of probable multi-path phenomena, so
we decided to try taking bearings only
when the signal was around a particular frequency and only from the highest locations we could find.
Several cold and lonely vigils were
spent on top of wind-swept mountains, waiting for the signal to drift
into range; a bit like fishing, I suppose!
We began to get more consistent
results. At least the bearings now intersected, but the intersection was in
rugged bushland, well away from developed areas.
We were somewhat doubtful that
this was correct, but we had been
quite careful and had repeated the
triangulation several times, so maybe
it was right.
The topographic map showed a
siliconchip.com.au
pumping station near our target area.
This seemed like an unlikely source,
but we decided to investigate further.
We drove towards the target area as
a small group, monitoring the interfering signal as we went. We found ourselves on a road that passed through a
group of houses, and beyond the last
house, headed into the bush, towards
the area indicated by our triangulation. The signal here was very strong,
and the direction indicated by our
equipment was straight ahead along
the road.
We noted a heavy-duty three-phase
power line and a large diameter water
pipe running alongside the road, so it
looked like we were on the right track.
Eventually, we arrived at the pumping station.
As luck would have it, there were
vehicles parked outside, and people
were working in the building. The
interfering signal was now extremely
strong. It had to be coming from the
pumping station.
We approached the people working
in the building and spoke to their supervisor. He seemed quite suspicious
of us and our gear, and asked us if were
ghost hunters or UFO enthusiasts! We
told him that we were not nearly as
exotic as that, just ham radio operators trying to track down some radio
interference.
When we let him hear the interfering
signal and demonstrated our directional antenna, he seemed quite interested
and became less suspicious; friendly,
even. He invited us into the building
and gave us permission to look around.
Using a sniffer, we established
that the signal was incredibly strong
around a box mounted high on a wall
in the building.
The box had no visible label or
markings, had a power lead and what
appeared to be a telephone cable going
into it, and a coax cable which disappeared into the ceiling. It seemed odd
that it was mounted in such an inaccessible position.
There was a great deal of RF emanating from the box, possibly due to
a bad coax shield connection, or even
something as simple as a loose coax
connector. But we were not in a position to touch anything, and had to
content ourselves with speculation.
Our new friend and his crew (who
by now had also become quite interested in what we were doing) said they
had no idea what the box was, and that
siliconchip.com.au
as far as they could remember, it had
always been there.
We demonstrated to them that a
strong interfering signal was coming
from it, and pointed out that whatever
was in there was probably malfunctioning and not doing its intended job.
We asked him if he would turn its
power off temporarily to confirm that
it was the source of the interference.
This he did, whereupon the interference immediately stopped.
Apparently, we had done a good
enough job of convincing him that
we were not insane and that we knew
what we were talking about.
He declared that he was going to
leave it turned off until he could find
out what it was, who was responsible
for it, and get some maintenance done
on it! The interference has never returned. What was in the box remains
a mystery.
LED lamp repair
L. B., of Mittagong, NSW got fed
up with modern globes which don’t
last anywhere near as long as they
are supposed to. Having had two fail
in quick succession, he decided to
open them up and take matters into
his own hands...
The life expectancy of mains-powered LED lamps can be far less than
stated on the packaging. Some time
ago I purchased four Mirabella lamps
from the supermarket at half price and
they worked just fine for a while. I used
them ‘base up’ in lamps in my work-
shop, and after about five months the
first one failed – it started flickering
when switched on and then went dark.
I swapped it for another and put the
failed one aside until I had time to explore why it had failed so soon. Then a
little while later, the second one failed
in a different light fitting. I decided it
was time to open them up and see what
was going on. I was able to cut off the
diffuser housing quite easily using a
hobby knife, by slicing through the
silicone attaching it to the base.
Under the diffuser I found one LED
array, held to a heatsink using two
screws. I marked the circuit board with
which wire connected where and then
unsoldered them.
Removing the two screws allowed
the removal of the circuit board. The
heatsink was a press fit into the internal metal body and when removed, it
exposed the power supply board, encapsulated in more silicone.
Carefully removing the silicone with
the hobby knife and pliers then desoldering the wires from the bayonet
base allowed me to remove the power
supply board.
Removing the remaining silicone
from the base exposed two slots on the
sides of the base for locating the circuit
board. Both power supply boards had
an off-board 10W resistor which had
desoldered itself, hence the failure of
the lamps. The area where it used to
be soldered to the board was burnt in
both cases, apparently due to a lot of
heat being produced.
Right: the power supply board for the LED lamp, with an external 10W resistor
shown in black below.
Australia’s electronics magazine
May 2020 51
I assume that the heat from the resistor (encapsulated in the silicone) did
its dastardly deed on the connection to
the circuit board. Or maybe the original solder joint was not good, resulting in high resistance and therefore
heating of the joint.
I reattached the resistor to the board
after cleaning away some of the solder resist and applied a much larger
amount of solder. Refitting the circuit
board without the silicone encapsulation seems to have fixed the problem as
neither of these LEDs has failed again,
after being in service for longer than
they were when they failed. Anyway,
I guess time will tell.
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plied but the replacement then failed
after a few weeks. I claimed another refund under warranty, but heard
nothing back.
As I seemed to have little to lose,
I disassembled one cooktop, which
seemed to be well made, and hence
possibly worth repairing. I identified
a blown 12A fuse and a short-circuit
IGBT, type H201353, rated at 1350V
and 20A.
My experience is that the failure of
a main power supply component often causes failure of several other components but as the new IGBT and fuse
were inexpensive, I decided to try replacing both and see what happened.
I decided to up-rate the IGBT using
an IHW30N135R3, rated at 1350V and
30A. Somewhat to my surprise, this
fixed the fault entirely.
Heartened by this success, I then
disassembled the other failed cooker
and found a blown 12A fuse, a faulty
IGBT and a short-circuit bridge rectifier. I replaced the bridge rectifier with
a higher rated unit, a GBJ2510 rated at
1000V, 25A. The fuse and IGBT were
also replaced, as before, and again this
fixed the fault.
I had three subsequent failures but
new IGBTs fixed these faults. For the
latest replacement, I used the highest
rated TO-247 “TrenchStop N-Channel”
IGBT that I could find, an Infineon
IHW30N160R2, rated at 1600V, 60A.
Touch wood, but they have not failed
since.
In the Baumatic unit, the bridge
rectifier and IGBT are mounted on a
heatsink on the main circuit board.
The unit is easily disassembled; plugs
and sockets interconnect the individual boards. Replacing the rectifier and
IGBT only required basic soldering
and de-soldering skills but of course,
as with any mains-powered device,
caution is needed.
As an IGBT failure does not seem
to take out other components, and the
devices are not that expensive, it is
generally worthwhile for reasonably
experienced and cautious people to
have a go at fixing similar units.
The designers could perhaps have
used more robust semiconductors. It is
asking a lot of a relatively small TO-247
component, even in so-called “resonant
switching mode”, to deliver 2000W.
There may be other faults in the design. This model of Baumatic portable
cooktop does not seem to be available
now, except as a clearance item.
SC
Australia’s electronics magazine
siliconchip.com.au
LED motion light modification
G. P., of North Rocks, NSW didn’t fix
something that was broken, but rather,
modified the circuit because it didn’t
do exactly what he wanted. While not
strictly servicing, it does show that you
can alter some commercial devices to
provide the exact functions that you
require...
Our double-level unit has a dark
staircase passage. As the light switches
for this area are located away from the
staircase, we purchased some motionactivated battery-powered LED lights.
They work well but due to the long
minimum light on-time, the three AA
cells in each do not last long. So I decided to investigate whether I could
shorten that on-time.
I took one unit off the wall and
opened it. I found that it uses a
BISS001 IC (“Micro Power PIR Motion Detector”). I used Google to find
and download its data sheet.
This was very helpful. I discovered
that the time duration (Tx) during
which the output pin (Vo) remains
high after triggering depends on the
RC circuit (R10 and C6) connected to
pin 3 (Tx = 24576 × R10 × C6). I compared this to the unit, and found that
R4 and C2 corresponded to the R10
and C6 described in the data sheet.
I timed the minimum on-cycle at
approximately 33 seconds, but we required 15-20s. On the board, R4 was
150kW, so I determined that I should
roughly halve its value by replacing it
with a 68kW resistor.
But after replacing this resistor, I
found that the on-time was only a
few seconds shorter. After testing a
few different resistor values, I found
that a 62kW resistor gave an on-time
of about 19 seconds. That was good
enough. Perhaps there is a leakage
path in the circuit which can alter the
time constant.
Induction cooktop repair
R. S., of Moruya, NSW, has become
something of an expert on the workings
of induction cookers after performing
several repairs on these finicky devices. But he seems to have figured out
how to solve the reliability problems
he’s encountered, as explained below...
Induction cookers work by converting 50Hz mains power to a higher frequency, typically 20-40kHz, and applying that to a flat coil of heavy wire
which sits under the glass “hotplate”
of the cooktop.
The ferromagnetic pan (only this
type will work) then acts as the secondary of a transformer, being heated
by the combination of eddy currents
and magnetic hysteresis losses.
Current to the coil and thus heat is
controlled by an IGBT (insulated gate
bipolar transistor). The IGBT control
circuitry incorporates a timer function
and temperature control and also prevents operation if there is no suitable
pan on the cooktop. An excellent description of the operation of this type
of circuit is at: siliconchip.com.au/
link/ab13
I bought my first portable induction cooktop in early 2016 but it failed
dramatically and noisily when first
switched on, taking out the switchboard circuit breaker. I returned it for
a refund.
Later in 2016, I was given a Baumatic BHI100 portable cooktop which
worked very well for nearly a year before failing in a similar manner to the
other one. I claimed a replacement under warranty and this was duly sup-
Servicing Stories Wanted
52
Silicon Chip
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